05000440/FIN-2008003-02: Difference between revisions

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| CCA = N/A for ROP
| CCA = N/A for ROP
| INPO aspect =  
| INPO aspect =  
| description = The inspectors identified a finding of very low safety significance for the failure of licensee personnel to adhere to corrective action program procedures. Specifically, during inspection of the linear velocity transducer connector for the 'A' flow control valve actuator, the connector was found in a degraded state, and personnel applied tape to the connector. Licensee personnel did not initiate a condition report to address this condition or to assess operability, and the connector later failed causing reactor flow and power oscillations. The licensee entered the issue of failure to adhere to corrective action program procedures into their corrective action program. This finding has a cross-cutting aspect in the area of Problem Identification and Resolution because the organization failed to properly identify issues related to nuclear safety P.1(a). This finding was considered more than minor because it was associated with the equipment performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective of limiting the likelihood of events that upset plant stability. The finding was determined through a Significance Determination Process analysis to be of very low safety significance because no mitigation equipment or functions were affected. No violation of NRC requirements occurred. (Section 4OA2
| description = The inspectors identified a finding of very low safety significance for the failure of licensee personnel to adhere to corrective action program procedures. Specifically, during inspection of the linear velocity transducer connector for the \'A\' flow control valve actuator, the connector was found in a degraded state, and personnel applied tape to the connector. Licensee personnel did not initiate a condition report to address this condition or to assess operability, and the connector later failed causing reactor flow and power oscillations. The licensee entered the issue of failure to adhere to corrective action program procedures into their corrective action program. This finding has a cross-cutting aspect in the area of Problem Identification and Resolution because the organization failed to properly identify issues related to nuclear safety P.1(a). This finding was considered more than minor because it was associated with the equipment performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective of limiting the likelihood of events that upset plant stability. The finding was determined through a Significance Determination Process analysis to be of very low safety significance because no mitigation equipment or functions were affected. No violation of NRC requirements occurred. (Section 4OA2


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Latest revision as of 20:35, 20 February 2018

02
Site: Perry FirstEnergy icon.png
Report IR 05000440/2008003 Section 4OA2
Date counted Jun 30, 2008 (2008Q2)
Type: Finding: Green
cornerstone Initiating Events
Identified by: NRC identified
Inspection Procedure: IP 71152
Inspectors (proximate) M Wilk
M Phalen
G Wright
M Franke
R Leidy
T Taylor
J Cameron
R Murray
INPO aspect
'