ML20202F857: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot insert)
 
(StriderTol Bot change)
 
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:}}
{{#Wiki_filter:__
OPERATING DATA REPORT Docket No. 50-311 Date    June 10,1986 Completed by                                                    Telephone    935-6000 Pell White                                Extension    4451 Operating Status
: 1. Unit Name                              Salem No. 2
: 2.                                                              Notes Reporting Period                        May 1986
: 3. Licensed Thermal Power (MWt)                    3411
: 4. Nameplate Rating (Gross MWe)                    TITU
: 5. Design Electrical Rating (Net MWe)              TTTI
: 6. Maximum Dependable Capacity (Gross MWe)TTTT
: 7. Maximum Dependable Capacity (Net MWe) 1106
: 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
: 9. Power Level to Which Restricted, if any (Net MWe)                      N/A
: 10. Reasons for Restrictions, if any                                        N/A This Month      Year to Date      Cumulative
: 11. Hours in Reporting Period                    744                3623            40608
: 12. No. of Hrs. Reactor was Critical              713.4            3128.0          23453.8
: 13. Reactor Reserve Shutdown Hrs.                    0                0            3533.6
: 14. Hours Generator On-Line                      700.0            3087.7                    -
: 15. Unit Reserve Shutdown Hours                      0
                                                                                      - 17624.5 0                  0
: 16. Gross Thermal Energy Generated (MWH)                            2324078
: 17. Gross Elec. Energy Generated                                  10233464          69979162 (MWH)                            750850
: 18. Net Elec. Energy Generated (MWH)                              3363200          22939680 718914          3219044          21753888
: 19. Unit Service Factor                            94.1              85.2
: 20. Unit Availability Factor                        94.1              85.2 55.7    I
: 21. Unit Capacity Factor                                                                55.7 (using MDC Net)                          87.4
: 22. Unit Capacity Factor                                              80.3              48.4 (using DER Net)                          86.7
: 23. Unit Forced Outage Rate                                            79.7              48.0 l
5.9              12.3              34.7
: 24. Shutdowns        scheduled REFUELING 9-20-86 over  next  6 months    (type, date  and  duration  of each)  ,
: 25. If shutdown at end of Report Period, Estimated Date of Startup l
N/A
: 26. Units in Test Status (Prior to Commercial Operation) :
Forecast        Achieved Initial Criticality            6/30/80        8/2/80 I:.itial Electricity            9/1/80          6/3/81 8-1-7.R2                        Commercial Operation            9/24/80        10/13/81 8607130247 DR          860531 ADOCK 05000311 PDR.                                TEM
 
AVERAGE DAILY UNIT POWER LEVEL Docket No.      50-311 Unit Name    Salem # 2 Date June 10,1986 Completed by      Pell White                            Telephone    609-935-6000 Extension 4451 Month        May 1986 Day Average Daily Power Level                    Day Average Daily Power Level (MWe-NET)                                      (MWe-NET) 1          930                                    17        1057 a
2              0                                  18        1064
:      3              0                                19          1060 4          771                                  20          1065 i
j      5          1059                                  21          1054
[
]
6          1067                                  22          1050 1
7          1065                                  23          899 i
8          1081                                  24          1026
;      9          1075                                  25          1049 j      10          1058                                  26          1048
!    11          999                                  27          1032 j      12          1068                                  28          1052 1
j      13          1057                                  29          1052 14          1065                                  30          1047 15          1065                                  31          1014 4
16          1071 Pg. 8.1-7 R1 i
>                                                                                                      \
b                                                                                                      l i
4 1
l
 
UNIT SHUTDOWN AND POWER REDUCTIONS                  Docket No.      50-311 REPORT MONTH MAY 1986                            Unit Name      Salem No.2        .
Date            June 10,1986 Completed by            Pell White                                                            Telephone      609-935-6000 Extension      4451              .
Method of Duration            Shutting  License                              Cause and Corrective No.            Date    Type    Hours  Reason      Down    Event    System    Component                  Action to 1                2        Reactor  Report  Code 4    Code 5              Prevent Recurrence Other Nuclear Reactor -
268            0501    F      5.2        A          5        -
SF    VESSEL            Problems Misc.
Other Nuclear Reactor 270            0502    F      44.0        A          1        -
SF    VESSEL            Problems Misc.
Loss of Vacuum /High 320            0523    F      12.4        A          5        -
HC    HTEXCH            Back Pressure Feedwater Pump Drive 348            0531    F      2.1        A          5        -
CH    PUMPXX            Lube Oil System 1                          2 Reason                                  3 Method                  4 Exhibit G          S Exhibit 1 F: Forced                    A-Equipment Failure-explain              1-Manual                  Instructions        Salem as S: Scheduled                B-Maintenance or Test                    2-Manual Scram.          for Prepara-        Source C-Refueling                              3-Automatic Scram, tion of Data D-Regulatory Restriction                4-Continuation of        Entry Sheets E-Operator Training & Licensing Exam      Previous Outage        for Licensee F-Administrative                        5-Load Reduction          Event Report G-Operational Error-explain              9-Other                  (LER) File H-Other-explain                                                    (NUREG 0161)
 
MAJOR PLANT MODIFICATIONS                    DOCKET NO.:      50-311 REPORT MONTH MAY 1986                        UNIT NAME:        Salem 2 DATE:    June 10, 1986 COMPLETED BY:      J. Ronafalvy TELEPHONE:      609/339-4455
                  *DCR NO.                PRINCIPAL SYSTEM          SUBJECT I
2EC-1501              Diesel Generators          Install control circuit transfer switches on the engine and generator control panels of each diesel generator to enable an operator to start the diesel generators under postulated fire and blackout conditions.
2EC-1566              Chilled Water System      Install a 10 PSIG regief valve at the chilled water expansion tank.
2EC-1785              Safe Guards Emergency    Install new Lamda Power                      !
Controls                  Supplies new Potter                          ;
Brumfield relays in 2B SEC,                  j 2A SEC and 2C SEC.                            l 2EC-1970              Containment Personnel    Install caps and valving 1
Hatch                    at personnel hatch -
El. 100 & 130, 2EC-2000              Main Reheat & Turbine    Replace turbine first stage Bypass                    impulse pressure pressure transmitters PA-0195 and PA-0216 and mount so as to reduce vibration.
2SC-1168              Reactor Coolant System    Change reactor coolant flow transmitter from Fisher Porter model # 10B2496PB to new model and type specified                  ;
by Engineering.
i Design Change Request i
 
MAJOR PLANT MODIFICATIONS                        DOCKET NO:    50-311 REPORT MONTH - MAY 1986                        UNIT NAME:    SALEM 2 DATE:    MAY 10, 1986 COMPLETED BY:    J. RONAFALVY TELEPHONE:  (609)339-4455
            *DCR              SAFsTY EVALUATION 10 CFR 50.59 2EC-1501            This design change improves the plant safety by making vital power available much sooner during ce.rtain postulated fire plus blackout conditions.
Failure of the control transfer switch may cause the ' associated diesel to fail to start during a safeguards actuation. This failure is considered to be within the realm of the single failure criteria. This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.
2EC-1566            This design change does not jeopardize the pressure retaining boundary nor impact the operation or basic design criteria of the Chilled Water System. This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.
2EC-1785              This design change replaced existing components with ones manufactured by a different vendor.
The replacement components have been seismically qualified to IEEE 344 which is to the same or higher stress levels as the original equipment.
This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.
2EC-1970 All  realistic failure modes have been considered but are not applicable.
1 This design change meets GDC 56 requirements and complies with safety Guide #11. The additional equipment meets the design criteria of seismic I and nuclear class II. This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.
Design Change Request 1
 
.i
                      ~ UNIT 2 MAJOR PLANT MODIFICATIONS (contd) i                      REPORT MONTH - MAY 1986
                                *DCR          SAFETY EVALUATION 10 CFR 50.59 l
2EC-2000              The existing transmitters malfunction. The replacement ones are of better design. There is no functional change in the system or component.
This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.
2SC-1168                All potential, realistic failure modes have been considered but are not applicable. Regulatory requirements do nce apply. The replacement transmitters do not modify the function of the system. The original transmitters are considered obsolete by the manufacturer. This modification does not alter any plant process or discharge.
Therefore, no unreviewed safety or environmental questions are involved.
l l
I Design Change Request
 
_____..__m___.._________.___.__..m.___..________,____..________.__.______                                  _                . . _ _      __. _ . _ _ . _ _ _ _ . . - _ . _ . _ . . _ _ _ _ . . _ .
PSE&G SALEM GENERATING STATION SAFETY RELATED WORK ORDER LOG SALEM UNIT 2 WO NO                                              UNIT      EQUIPMENT IDENTIFICATION                                                                                                  .
                                                                                                                                                                                                                +
8604251090 2    21 CHILLER CONDENSER FAILURE DESCRIPTION:    21 CHILLER CONDENSER IIAS A TUBE LEAK.
CORRECTIVE ACTION:      REPLACED DEFECTIVE CONDENSER TUBE, PRESSURE TESTED                                                          ;
SYSTEM. REPLACED FILTER, DRYERS AND OIL.
8605020580 2    RTD ORIFICE i
FAILURE DESCRIPTION:  22 RCP COLD LEG BYPASS RTD ORIFICE IS BLOWING AND LEAKING ONTO FLOOR.
CORRECTIVE ACTION:    REPLACED GASKET IN FLANGES.
8605121173 2    21 SW PUMP AUTO CONTROL                                                                                                                              ,
FAILURE DESCRIPTION:    21 SERVICE WATER PUMP WILL NOT STAY IN THE AUTO CONTROL MODE.
CORRECTIVE ACTION:      INSTALLED NEW OPERATE RESET RELAY IN BAILEY CABINET RC-116.
                                                                          -r
                                                                                                              - - _ _ _ _ v        ,_s4                            _                              m1-
 
I SALEM UNIT 2 9
WO NO      UNIT  EQUIPMENT IDENTIFICATION 8605121513 2  26 SW PUMP FAILURE DESCRIPTION:  PUMP HAS EXCESSIVE PACKING LEAKAGE.
CORRECTIVE ACTION:    REPACKED PUMP.                                                l 1                                                                                                      -
! 8605140500 2  21 SW STRAINER FAILURE DESCRIPTION:  STRAINER HAS A SEVERE PACKING LEAK.
CORRECTIVE ACTION:    REPLACED PACKING.
l 8605150882 l            2  REACTOR VESSFL FLANGE LEAKOFF INDICATOR
\
!                FAILURE DESCRIPTION:  BEZEL INDICATION HAS FAILED HIGH, VERIFIED VESSEL LEAKOFF WITH COMPUTER POINT.
CORRECTIVE ACTION:    FOUND LOWER LEVEL AMP 2TM-401 FAILED HIGH. REPLACED S/N E092 WITH S/N E040. CALIBRATED TO AS LEFT VALUES OF TABLE 20.0 PAGE 5 OF 2IC-2.10.047.
RETURNED CHANNEL TO SERVICE. TEMPERATURE INDICATION WAS 87 DEGREES F.
ci i
i r---    -,- ,. _
 
l                                                                                                                                                                                                                            . .    .
SALEM UNIT 2            .
WO NO                                                                              UNIT  EQUIPMENT IDENTIFICATION 8605190019 2 ACCUMULATOR LEVEL CHANNEL FAILURE DESCRIPTION:                                            #24 ACCUMULATOR CHANNEL 2 LEVEL HI-LO ALARM IS ILLUMINATED.              NO APPARENT LEVEL PROBLEM.
CORRECTIVE ACTION:                                              REPLACED PC BOARD IN RELAY RACK #112 AND TESTED OKAY.
8605200073                                                                                                                                                                                                                            f 2 CHARGING FLOW ORIFICE                                                                                                                        l FAILURE DESCRIPTION:                                            NO CLOSED INDICATION.                                                        ,
CORRECTIVE ACTION-                                              REALIGNED LIMIT SWITCH ACTUATING hRM AND                                    I TIGHTENED.              TI'GHTENED LIMIT SWITCH BRACKET.
!                                                                                                                                                          CONTROL STROKED AND VERIFIED LIMITS.
 
SALEM GENERATING STATION MONTHLY OPERATING
 
==SUMMARY==
- UNIT NO. 2 MAY 1986 SALEM UNIT NO. 2 The Unit began the period operating at full power.        On May 2, 1986 at 1717 hours, a controlled shutdown was initiated to perform
,          environmental equipment qualification inspections in the Containment.
As the Unit was taken off the line, on May 3, 1986 at 0332 hours, a Reactor Trip with Safety Injection occurred due to "High Steam Line Flow With Low Tave" which was apparently caused by a steam flow spike when the Generator output breakers were opened. On May 3, 1986 at 2231 hours, the Turbine was latched and power ascension to full power operations was initiated. Unit power was reduced to 65% on May 11, 4
1986 at 0220 hours due to limited system load demand. The Unit was returned to full power the same day at 0642 hours.        During the period from May 23, 1986 to May 25, 1986 minor load reductions were required due to high river grasses and debris causing Circulating Water System problems. On May 31, 1986 at 2200 hours a load reduction to 61% was commenced in order to remove #21 SGFP from service for replacement of the governor.        On June 1, 1986 at 1515 hours, work on #21 SGFP was completed and the Unit was returned to 100% power where it remained for the rest of the period.
I 1
l l
1
 
e REFUELING INFORMATION DOCKET NO.:      50-311 COMPLETED BY:      J. Ronafalvy              UNIT NAME:      Salem 2 DATE:  June 10, 1986 TELEPHONE:      609/935-6000 EXTENSION:      4455
{                  Month    May 1986 i
: 1. Refueling information has changed from last month:
;                                        YES              NO    X
: 2. Scheduled date for next refueling:          September 20, 1986 1
: 3. Scheduled date for restart following refueling: November 19, 1986 l
: 4. A)  Will Technical Specification changes or other license amendments be required?                                              .
YES            NO                                          '
Not determined to date B)  Has the reload fuel design been reviewed by the Station Operating Review Committee?
i YES              NO      X If no, when is it scheduled?        August 1986
: 5. Scheduled data (s) for submitting proposed licensing action:
August 1986 if required j                  6. Important licensing considerations associated with refueling:
NONE I
i j                  7. Number of Fuel Assemblies
;                      A)    Incore
  '                                                                                            193 B)    In Spent Fuel Storage                                            140 i
: 8. Present licensed spent fuel storage capacity:                          1170 Future spent fuel storage capacity:                                    1170
: 9. Date-of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity:                                            March 2003 8-1-7.R4 l                                                                                                  )
 
J O PSEG Putsc Service Electnc and Gas Company P O Box E Hancocks Brutge, New Jersey 08038 Salem Generating Station June 10, 1986 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, DC            20555
 
==Dear Sir:==
 
MONTHLY OPERATING REPORT SALEM NO. 2 DOCKET NO. 50-311 In compliance with Section 6.9, Reporting Requirements for the Salem Technical Specification, 10 copies of the following monthly operating reports for the month of Ma) 1986 are being sent to you.
Average Daily Unit Power Level                                  I Operating Data Report Unit Shutdowns and Power Reductions                            )
i Major Plant Modification Safety Related Work Orders                                      I operating Summary Refueling Information Sincerely yours,                          !
J. M. Zupko, Jr.
General Manager - Salem Operations          )
JRtal cc:      Dr. Thomas E. Murley Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA            19406 Director, Office of Management                                                        i U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555                                                                    l Enclosures                                                                                      1 8-1-7.R4                                                                                        1
[b1 The Energy People kg n v u nvm u}}

Latest revision as of 19:49, 1 January 2021

Monthly Operating Rept for May 1986
ML20202F857
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/31/1986
From: Ronafalvy J, White P, Zupko J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
NUDOCS 8607150247
Download: ML20202F857 (12)


Text

__

OPERATING DATA REPORT Docket No. 50-311 Date June 10,1986 Completed by Telephone 935-6000 Pell White Extension 4451 Operating Status

1. Unit Name Salem No. 2
2. Notes Reporting Period May 1986
3. Licensed Thermal Power (MWt) 3411
4. Nameplate Rating (Gross MWe) TITU
5. Design Electrical Rating (Net MWe) TTTI
6. Maximum Dependable Capacity (Gross MWe)TTTT
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
9. Power Level to Which Restricted, if any (Net MWe) N/A
10. Reasons for Restrictions, if any N/A This Month Year to Date Cumulative
11. Hours in Reporting Period 744 3623 40608
12. No. of Hrs. Reactor was Critical 713.4 3128.0 23453.8
13. Reactor Reserve Shutdown Hrs. 0 0 3533.6
14. Hours Generator On-Line 700.0 3087.7 -
15. Unit Reserve Shutdown Hours 0

- 17624.5 0 0

16. Gross Thermal Energy Generated (MWH) 2324078
17. Gross Elec. Energy Generated 10233464 69979162 (MWH) 750850
18. Net Elec. Energy Generated (MWH) 3363200 22939680 718914 3219044 21753888
19. Unit Service Factor 94.1 85.2
20. Unit Availability Factor 94.1 85.2 55.7 I
21. Unit Capacity Factor 55.7 (using MDC Net) 87.4
22. Unit Capacity Factor 80.3 48.4 (using DER Net) 86.7
23. Unit Forced Outage Rate 79.7 48.0 l

5.9 12.3 34.7

24. Shutdowns scheduled REFUELING 9-20-86 over next 6 months (type, date and duration of each) ,
25. If shutdown at end of Report Period, Estimated Date of Startup l

N/A

26. Units in Test Status (Prior to Commercial Operation) :

Forecast Achieved Initial Criticality 6/30/80 8/2/80 I:.itial Electricity 9/1/80 6/3/81 8-1-7.R2 Commercial Operation 9/24/80 10/13/81 8607130247 DR 860531 ADOCK 05000311 PDR. TEM

AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-311 Unit Name Salem # 2 Date June 10,1986 Completed by Pell White Telephone 609-935-6000 Extension 4451 Month May 1986 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 930 17 1057 a

2 0 18 1064

3 0 19 1060 4 771 20 1065 i

j 5 1059 21 1054

[

]

6 1067 22 1050 1

7 1065 23 899 i

8 1081 24 1026

9 1075 25 1049 j 10 1058 26 1048

! 11 999 27 1032 j 12 1068 28 1052 1

j 13 1057 29 1052 14 1065 30 1047 15 1065 31 1014 4

16 1071 Pg. 8.1-7 R1 i

> \

b l i

4 1

l

UNIT SHUTDOWN AND POWER REDUCTIONS Docket No. 50-311 REPORT MONTH MAY 1986 Unit Name Salem No.2 .

Date June 10,1986 Completed by Pell White Telephone 609-935-6000 Extension 4451 .

Method of Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to 1 2 Reactor Report Code 4 Code 5 Prevent Recurrence Other Nuclear Reactor -

268 0501 F 5.2 A 5 -

SF VESSEL Problems Misc.

Other Nuclear Reactor 270 0502 F 44.0 A 1 -

SF VESSEL Problems Misc.

Loss of Vacuum /High 320 0523 F 12.4 A 5 -

HC HTEXCH Back Pressure Feedwater Pump Drive 348 0531 F 2.1 A 5 -

CH PUMPXX Lube Oil System 1 2 Reason 3 Method 4 Exhibit G S Exhibit 1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salem as S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- Source C-Refueling 3-Automatic Scram, tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

MAJOR PLANT MODIFICATIONS DOCKET NO.: 50-311 REPORT MONTH MAY 1986 UNIT NAME: Salem 2 DATE: June 10, 1986 COMPLETED BY: J. Ronafalvy TELEPHONE: 609/339-4455

  • DCR NO. PRINCIPAL SYSTEM SUBJECT I

2EC-1501 Diesel Generators Install control circuit transfer switches on the engine and generator control panels of each diesel generator to enable an operator to start the diesel generators under postulated fire and blackout conditions.

2EC-1566 Chilled Water System Install a 10 PSIG regief valve at the chilled water expansion tank.

2EC-1785 Safe Guards Emergency Install new Lamda Power  !

Controls Supplies new Potter  ;

Brumfield relays in 2B SEC, j 2A SEC and 2C SEC. l 2EC-1970 Containment Personnel Install caps and valving 1

Hatch at personnel hatch -

El. 100 & 130, 2EC-2000 Main Reheat & Turbine Replace turbine first stage Bypass impulse pressure pressure transmitters PA-0195 and PA-0216 and mount so as to reduce vibration.

2SC-1168 Reactor Coolant System Change reactor coolant flow transmitter from Fisher Porter model # 10B2496PB to new model and type specified  ;

by Engineering.

i Design Change Request i

MAJOR PLANT MODIFICATIONS DOCKET NO: 50-311 REPORT MONTH - MAY 1986 UNIT NAME: SALEM 2 DATE: MAY 10, 1986 COMPLETED BY: J. RONAFALVY TELEPHONE: (609)339-4455

  • DCR SAFsTY EVALUATION 10 CFR 50.59 2EC-1501 This design change improves the plant safety by making vital power available much sooner during ce.rtain postulated fire plus blackout conditions.

Failure of the control transfer switch may cause the ' associated diesel to fail to start during a safeguards actuation. This failure is considered to be within the realm of the single failure criteria. This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.

2EC-1566 This design change does not jeopardize the pressure retaining boundary nor impact the operation or basic design criteria of the Chilled Water System. This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.

2EC-1785 This design change replaced existing components with ones manufactured by a different vendor.

The replacement components have been seismically qualified to IEEE 344 which is to the same or higher stress levels as the original equipment.

This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.

2EC-1970 All realistic failure modes have been considered but are not applicable.

1 This design change meets GDC 56 requirements and complies with safety Guide #11. The additional equipment meets the design criteria of seismic I and nuclear class II. This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.

Design Change Request 1

.i

~ UNIT 2 MAJOR PLANT MODIFICATIONS (contd) i REPORT MONTH - MAY 1986

2EC-2000 The existing transmitters malfunction. The replacement ones are of better design. There is no functional change in the system or component.

This modification does not alter any plant process or discharge. Therefore, no unreviewed safety or environmental questions are involved.

2SC-1168 All potential, realistic failure modes have been considered but are not applicable. Regulatory requirements do nce apply. The replacement transmitters do not modify the function of the system. The original transmitters are considered obsolete by the manufacturer. This modification does not alter any plant process or discharge.

Therefore, no unreviewed safety or environmental questions are involved.

l l

I Design Change Request

_____..__m___.._________.___.__..m.___..________,____..________.__.______ _ . . _ _ __. _ . _ _ . _ _ _ _ . . - _ . _ . _ . . _ _ _ _ . . _ .

PSE&G SALEM GENERATING STATION SAFETY RELATED WORK ORDER LOG SALEM UNIT 2 WO NO UNIT EQUIPMENT IDENTIFICATION .

+

8604251090 2 21 CHILLER CONDENSER FAILURE DESCRIPTION: 21 CHILLER CONDENSER IIAS A TUBE LEAK.

CORRECTIVE ACTION: REPLACED DEFECTIVE CONDENSER TUBE, PRESSURE TESTED  ;

SYSTEM. REPLACED FILTER, DRYERS AND OIL.

8605020580 2 RTD ORIFICE i

FAILURE DESCRIPTION: 22 RCP COLD LEG BYPASS RTD ORIFICE IS BLOWING AND LEAKING ONTO FLOOR.

CORRECTIVE ACTION: REPLACED GASKET IN FLANGES.

8605121173 2 21 SW PUMP AUTO CONTROL ,

FAILURE DESCRIPTION: 21 SERVICE WATER PUMP WILL NOT STAY IN THE AUTO CONTROL MODE.

CORRECTIVE ACTION: INSTALLED NEW OPERATE RESET RELAY IN BAILEY CABINET RC-116.

-r

- - _ _ _ _ v ,_s4 _ m1-

I SALEM UNIT 2 9

WO NO UNIT EQUIPMENT IDENTIFICATION 8605121513 2 26 SW PUMP FAILURE DESCRIPTION: PUMP HAS EXCESSIVE PACKING LEAKAGE.

CORRECTIVE ACTION: REPACKED PUMP. l 1 -

! 8605140500 2 21 SW STRAINER FAILURE DESCRIPTION: STRAINER HAS A SEVERE PACKING LEAK.

CORRECTIVE ACTION: REPLACED PACKING.

l 8605150882 l 2 REACTOR VESSFL FLANGE LEAKOFF INDICATOR

\

! FAILURE DESCRIPTION: BEZEL INDICATION HAS FAILED HIGH, VERIFIED VESSEL LEAKOFF WITH COMPUTER POINT.

CORRECTIVE ACTION: FOUND LOWER LEVEL AMP 2TM-401 FAILED HIGH. REPLACED S/N E092 WITH S/N E040. CALIBRATED TO AS LEFT VALUES OF TABLE 20.0 PAGE 5 OF 2IC-2.10.047.

RETURNED CHANNEL TO SERVICE. TEMPERATURE INDICATION WAS 87 DEGREES F.

ci i

i r--- -,- ,. _

l . . .

SALEM UNIT 2 .

WO NO UNIT EQUIPMENT IDENTIFICATION 8605190019 2 ACCUMULATOR LEVEL CHANNEL FAILURE DESCRIPTION: #24 ACCUMULATOR CHANNEL 2 LEVEL HI-LO ALARM IS ILLUMINATED. NO APPARENT LEVEL PROBLEM.

CORRECTIVE ACTION: REPLACED PC BOARD IN RELAY RACK #112 AND TESTED OKAY.

8605200073 f 2 CHARGING FLOW ORIFICE l FAILURE DESCRIPTION: NO CLOSED INDICATION. ,

CORRECTIVE ACTION- REALIGNED LIMIT SWITCH ACTUATING hRM AND I TIGHTENED. TI'GHTENED LIMIT SWITCH BRACKET.

! CONTROL STROKED AND VERIFIED LIMITS.

SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

- UNIT NO. 2 MAY 1986 SALEM UNIT NO. 2 The Unit began the period operating at full power. On May 2, 1986 at 1717 hours0.0199 days <br />0.477 hours <br />0.00284 weeks <br />6.533185e-4 months <br />, a controlled shutdown was initiated to perform

, environmental equipment qualification inspections in the Containment.

As the Unit was taken off the line, on May 3, 1986 at 0332 hours0.00384 days <br />0.0922 hours <br />5.489418e-4 weeks <br />1.26326e-4 months <br />, a Reactor Trip with Safety Injection occurred due to "High Steam Line Flow With Low Tave" which was apparently caused by a steam flow spike when the Generator output breakers were opened. On May 3, 1986 at 2231 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.488955e-4 months <br />, the Turbine was latched and power ascension to full power operations was initiated. Unit power was reduced to 65% on May 11, 4

1986 at 0220 hours0.00255 days <br />0.0611 hours <br />3.637566e-4 weeks <br />8.371e-5 months <br /> due to limited system load demand. The Unit was returned to full power the same day at 0642 hours0.00743 days <br />0.178 hours <br />0.00106 weeks <br />2.44281e-4 months <br />. During the period from May 23, 1986 to May 25, 1986 minor load reductions were required due to high river grasses and debris causing Circulating Water System problems. On May 31, 1986 at 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> a load reduction to 61% was commenced in order to remove #21 SGFP from service for replacement of the governor. On June 1, 1986 at 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br />, work on #21 SGFP was completed and the Unit was returned to 100% power where it remained for the rest of the period.

I 1

l l

1

e REFUELING INFORMATION DOCKET NO.: 50-311 COMPLETED BY: J. Ronafalvy UNIT NAME: Salem 2 DATE: June 10, 1986 TELEPHONE: 609/935-6000 EXTENSION: 4455

{ Month May 1986 i

1. Refueling information has changed from last month:
YES NO X
2. Scheduled date for next refueling: September 20, 1986 1
3. Scheduled date for restart following refueling: November 19, 1986 l
4. A) Will Technical Specification changes or other license amendments be required? .

YES NO '

Not determined to date B) Has the reload fuel design been reviewed by the Station Operating Review Committee?

i YES NO X If no, when is it scheduled? August 1986

5. Scheduled data (s) for submitting proposed licensing action:

August 1986 if required j 6. Important licensing considerations associated with refueling:

NONE I

i j 7. Number of Fuel Assemblies

A) Incore

' 193 B) In Spent Fuel Storage 140 i

8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170
9. Date-of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity: March 2003 8-1-7.R4 l )

J O PSEG Putsc Service Electnc and Gas Company P O Box E Hancocks Brutge, New Jersey 08038 Salem Generating Station June 10, 1986 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 2 DOCKET NO. 50-311 In compliance with Section 6.9, Reporting Requirements for the Salem Technical Specification, 10 copies of the following monthly operating reports for the month of Ma) 1986 are being sent to you.

Average Daily Unit Power Level I Operating Data Report Unit Shutdowns and Power Reductions )

i Major Plant Modification Safety Related Work Orders I operating Summary Refueling Information Sincerely yours,  !

J. M. Zupko, Jr.

General Manager - Salem Operations )

JRtal cc: Dr. Thomas E. Murley Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Director, Office of Management i U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 l Enclosures 1 8-1-7.R4 1

[b1 The Energy People kg n v u nvm u