Similar Documents at Salem |
---|
Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARLR-N99-0448, Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With LR-N99-0449, Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With LR-N99-0415, Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 9909131999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 LR-N99-0416, Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With LR-N99-0380, Monthly Operating Rept for July 1999 for Salem,Unit 2.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With LR-N99-0379, Monthly Operating Rept for July 1999 for Salem,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With LR-N99-0325, Monthly Operating Rept for June 1999 for Salem,Unit 2.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With LR-N99-0324, Monthly Operating Rept for June 1999 for Salem,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With LR-N99-0275, Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With LR-N99-0278, Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With LR-N99-0226, Monthly Operating Rept for Apr 1999 for Salem Unit 2.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With LR-N99-0225, Monthly Operating Rept for Apr 1999 for Salem Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 LR-N99-0177, Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With LR-N99-0176, Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With LR-N99-0114, Monthly Operating Rept for Feb 1999 for Salem Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With LR-N99-0115, Monthly Operating Rept for Feb 1999 for Salem Unit 2.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With LR-N99-0081, Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With1999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With LR-N99-0080, Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With1999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With LR-N99-0007, Monthly Operating Rept for Dec 1998 for Salem Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With LR-N99-0008, Monthly Operating Rept for Dec 1998 for Salem Unit 2.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With LR-N98-0571, Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With LR-N98-0572, Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With LR-N98-0540, Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with LR-N98-0541, Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with LR-N98-0479, Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With LR-N98-0478, Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With LR-N98-0435, Monthly Operating Rept for Aug 1998 for Salem Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With LR-N98-0436, Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With LR-N98-0392, Monthly Operating Rept for July 1998 for Salem,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1 LR-N98-0393, Monthly Operating Rept for July 1998 for Salem,Unit 21998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2 LR-N98-0334, Monthly Operating Rept for June 1998 for Salem,Unit 21998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2 LR-N98-0333, Monthly Operating Rept for June 1998 for Salem,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1 LR-N98-0293, Monthly Operating Rept for May 1998 for Salem Unit 21998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2 LR-N98-0292, Monthly Operating Rept for May 1998 for Salem Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1 LR-N98-0244, Monthly Operating Rept for Apr 1998 for Salem Unit 21998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2 LR-N98-0243, Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1 LR-N98-0192, Monthly Operating Rept for Mar 1998 for Salem,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1 LR-N98-0193, Monthly Operating Rept for Mar 1998 for Salem Unit 21998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2 LR-N98-0133, Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 21998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2 LR-N98-0132, Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 11998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1 ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2 ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1 ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1 ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2 LR-N970795, Monthly Operating Rept for Nov 1997 for Salem,Unit 21997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2 LR-N970794, Monthly Operating Rept for Nov 1997 for Salem,Unit 11997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1 LR-N970753, Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ LR-N970752, Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ LR-N970682, Monthly Operating Rept for Sept 1997 for Salem,Unit 21997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARLR-N99-0448, Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With LR-N99-0449, Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20212B7221999-09-14014 September 1999 Safety Evaluation Supporting Amends 224 & 205 to Licenses DPR-70 & DPR-75,respectively LR-N99-0415, Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 9909131999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 LR-N99-0416, Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 05000272/LER-1999-006-02, :on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With1999-08-26026 August 1999
- on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With
ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO 9) Second Interval,Second Period, First Outage (96RF) LR-N99-0380, Monthly Operating Rept for July 1999 for Salem,Unit 2.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With LR-N99-0379, Monthly Operating Rept for July 1999 for Salem,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 05000311/LER-1999-008, :on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With1999-07-28028 July 1999
- on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With
ML20210B7371999-07-21021 July 1999 Safety Evaluation Supporting Amends 223 & 204 to Licenses DPR-70 & DPR-75,respectively ML18107A4411999-07-0909 July 1999 SER Denying Licensee 980730 & 990222 Requests to Revise TS 3/4.7.6, Control Room Emergency Air Conditioning Sys, & Associated Bases to Change Acceptable Criteria for Control Room Emergency Air Conditioning System 05000311/LER-1999-007, :on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With1999-07-0606 July 1999
- on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With
05000272/LER-1999-005-02, :on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With1999-07-0202 July 1999
- on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With
05000311/LER-1999-006, :on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With1999-07-0101 July 1999
- on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With
05000311/LER-1999-002, :on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With1999-07-0101 July 1999
- on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With
ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO 10) Second Interval,Second Period,Second Outage (99RF) LR-N99-0324, Monthly Operating Rept for June 1999 for Salem,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept LR-N99-0325, Monthly Operating Rept for June 1999 for Salem,Unit 2.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With ML18107A3931999-06-23023 June 1999 Safety Evaluation Supporting Licensee Response to GL 95-07 ML18107A4161999-06-23023 June 1999 Safety Evaluation Accepting Licensee Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions 05000272/LER-1999-004-02, :on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With1999-06-17017 June 1999
- on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With
ML18107A3751999-06-15015 June 1999 Safety Evaluation Accepting Licensee Request for Approval of Proposed Changes to Nuclear Business Unit EP for Hope Creek & Salem Generating Stations,Iaw 10CFR50.54(q) 05000272/LER-1999-003-02, :on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With1999-06-0909 June 1999
- on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With
05000311/LER-1999-005-01, :on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With1999-06-0202 June 1999
- on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With
ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 LR-N99-0278, Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With LR-N99-0275, Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With ML18107A3111999-05-21021 May 1999 SER Accepting GL-88-20,suppl 4, IPEEEs for Severe Accident Vulnerabilities, for Plant,Units 1 & 2 05000272/LER-1999-002-02, :on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With1999-05-12012 May 1999
- on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With
05000311/LER-1999-004-01, :on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With1999-05-10010 May 1999
- on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With
05000311/LER-1999-003-01, :on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With1999-05-0404 May 1999
- on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With
ML20206H2631999-05-0404 May 1999 Safety Evaluation Supporting Amend 222 to License DPR-70 05000311/LER-1999-002-01, :on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With1999-05-0303 May 1999
- on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With
ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 LR-N99-0225, Monthly Operating Rept for Apr 1999 for Salem Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 LR-N99-0226, Monthly Operating Rept for Apr 1999 for Salem Unit 2.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With ML20206B4761999-04-26026 April 1999 Safety Evaluation Supporting Amends 220 & 202 to Licenses DPR-70 & DPR-75,respectively 05000311/LER-1999-001-03, :on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With1999-04-23023 April 1999
- on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With
ML18107A1791999-04-15015 April 1999 Safety Evaluation Supporting Changes to QA Program in That QA Program Continues to Meet Requirements of App B to 10CFR50 ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11 ML18107A1601999-04-0707 April 1999 Safety Evaluation Accepting Request for Exemption from Update Requirements of 10CFR50.71(e)(4) ML18106B1461999-04-0101 April 1999 SER Accepting Util Proposed Request to Use 1992 Edition of ASME Boiler & Pressure Vessel Code,Section Xi,Article, IWA-4500,for Potential Repair of Feedwater Nozzles for Salem Nuclear Generating Station,Unit 2 LR-N99-0176, Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With LR-N99-0177, Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 05000272/LER-1999-001-02, :on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with1999-03-29029 March 1999
- on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with
05000272/LER-1999-001-01, :on 990228,reactor Scram Resulted in Turbine Trip.Caused by Personnel Error.Revised Lesson Plans to Explicitly Demonstrate Manner in Which Valve Functions. with1999-03-29029 March 1999
- on 990228,reactor Scram Resulted in Turbine Trip.Caused by Personnel Error.Revised Lesson Plans to Explicitly Demonstrate Manner in Which Valve Functions. with
1999-09-30
[Table view] |
Text
~I.
L e
OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn: Document Control Desk MONTHLY OPERA TING REPORT SALEM UNIT NO. 1 DOCKET NO. 50-272 Gentlemen:
LR-N98-0243 May 15, 1998 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original Monthly Operating report for April 1998 is attached.
/rbk Enclosures C
Mr. H. J. Miller Sincerely, A. C. Bakken Ill General Manager -
Salem Operations Regional Administrator USNRC, Region 1 475 Allendale Road
_ _Kin~ ()f f)r~~~i~, J=>~ -~ ~9~6
~ __ _
9805260057 980430 PDR ADOCK 05000272 R
PDR The power is in your hands.
I le~ Zif 95-2168 REV. 6/94
Reporting Period: April 1998 DOCKET NO.: 50-272 UNIT: Salem 1 DA TE: 5/15/98 COMPLETED BY: R. Knieriem TELEPHONE: (609) 339-1782 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) 1115 Maximum Dependable Capacity (MWe-Net) 1106 Month Year-to-date Cumulative No. of hours reactor was critical 559 559 104940 No. of hours generator was on line (service 318 318 100707 hours)
Unit reserve shutdown hours 0
0 0
Net Electrical Energy (MWH) 181900 181900 100318443 UNIT SHUTDOWNS NO.
DATE TYPE F=FORCED S=SCHEDULED 1
4/1/98 F
4/17/98 (1) Reason A - Equipment Failure (Explain)
B - Maintenance or Test C - Refueling D - Regulatory Restriction DURATION (HOURS) 401 E - Operator Training/License Examination F -Administrative G - Operational Error (Explain)
H-Other Summary:
REASON METHOD OF (1)
SHUTTING DOWN THE REACTOR (2)
F,C 4
(2) Method 1 - Manual 2 - Manual Trip/Scram 3 -Automatic Trip/Scram 4 - Continuation 5 - Other (Explain)
CORRECTIVE ACTION/COMMENT Steam Generator Replacement and Refueling Outage Salem Unit 1 was synchronized to the electric power grid at 1743 on April 20. The unit was operating at approximately 19% reactor power at the time of synchronization.
Operators successfully conducted integrated testing and continued to increase power.
DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 5715798 COMPLETED BY: R. B. Knieriem TELEPHONE: (609) 339-1782 At the end of the month, reactor power was at approximately 90%. Following NRG concurrence, reactor power will be increased to 100%.
DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 5715798 COMPLETED BY: R. 8. Knieriem TELEPHONE: (609) 339-1782
SUMMARY
OF CHANGES, TESTS, AND EXPERIMENTS FOR THE SALEM UNIT 1 GENERATING STATION MONTH: APRIL 1998 The following items completed during April 1998 have been evaluated to determine:
- 1.
If the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased; or
- 2.
If a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created; or
- 3.
If the margin of safety as defined in the basis for any technical specification is reduced.
The 1 OCFR50.59 Safety Evaluations showed that these items did not create a new safety hazard to the plant; nor did they affect the safe shutdown of the reactor. These items did not change the plant effluent releases and did not alter the existing environmental impact. The 1 OCFR50.59 Safety Evaluations determined that no unreviewed safety or environmental questions are involved.
Design Changes - Summary of Safety Evaluations 1 EC-3301, Pkg. 1, Salem Unit 1 Steam Generator Slowdown Piping And Valve Modification This design change modified Salem Unit 1 Steam Generator Blowdown system piping and components to improve system reliability. The changes included the replacement of components with upgraded designs, improvements to component accessibility, and piping material upgrades.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3342, Pkg. 1, Circulating Water Bearing Lubrication/Screen Wash Setpoints And System Changes This modification implemented changes to the Circulating Water system to improve system reliability and performance. The changes included recalibration of system pressures and flows, changes to the Lubrication pump and Screen Wash pump controls for strainer backwash, replacement of the Lubrication Water
and Screen Wash strainer pressure gauges, and replacement of control valves
, with manual valves to simplify the system.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3345, Pkg. 1, Turbine Run back/Steam Generator Feed Pump (SGFP)
Control Circuit Modification This modification installed circuitry to provide an automatic run back of the Main Turbine in the event of a SGFP trip. The runback circuitry will also open the Condensate Polishing Bypass valves and the Feedwater Heater Bypass valve.
These actions will occur above a turbine power level of 60%-70% without operator intervention, to prevent a reactor trip.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3353, Pkg. 1, Small bore Piping Replacement This design change replaced carbon steel piping and valves in the Main Steam, Steam Generating, Condensate, and Feedwater systems with components manufactured from upgraded materials to reduce erosion/corrosion induced failures.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3370, Pkg. 1, Moisture Separator Heater Tube Bundle Replacement This modification removed and replaced the low pressure tube bundles on three Salem Unit 1 Moisture Separator Reheaters. The new tube bundles are manufactured from stainless steel and replaced the existing copper-nickel alloy tubes. The existing copper-nickel tubes were replaced to address their contribution to corrosion pitting of steam generator tubes.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction
_J
of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3388. Pkg. 1, Steam Generator Feed Pump (SGFP) Recirculation System Upgrade This modification implemented changes to the SGFP Recirculation Control valve design and system configuration to address erosion/corrosion concerns in the SGFP Recirculation piping. The change will also reduce Feedwater system flow transients during startup caused by instabilities in the existing valves while operating in the automatic mode.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3441, Pkg. 1, Automatic Temperature Control For The Air Side And Hydrogen Side Seal Oil Coolers This design change provided automatic temperature control for the Air Side Seal Oil cooler and Hydrogen Side Seal Oil coolers through the installation of an air-operated, fail as-is, temperature control valve in each of the Turbine Auxiliary Cooling system discharge lines from these components.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3458, Pkg. 1, Doric Temperature Monitor Replacement This modification replaced the existing Doric Temperature monitoring system, which remotely monitors the temperatures of numerous secondary, non-safety-related system parameters, with a more reliable and up-to-date system.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3481, Pkg. 1, Moisture Separator Reheater Drain And Vent System Modifications This design change modified and upgraded the Moisture Separator Reheater bleed steam coil drain and Main Steam coil drain system to improve system performance. The change involved increasing drain line piping sizes, drain piping rerouting, control valve replacement, and resizing of drain orifices.
1 This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3505, Pkg. 10, Work Control Center Air Conditioning System This modification provided an independent non-safety related roof-top air conditioning system to provide heating, cooling, and ventilation for the Salem Unit 1 and Unit 2 Common Work Control Center and the Field Senior Reactor Operator Office area.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1EC-3523, Replacement Of Westinghouse-Hagan/7100 Reactor Protection And Control System With NUS Modules This design change replaced Westinghouse-Hagann100, Class 1 E isolator, summator, comparator, resistance temperature detector low level amplifier, and power supply modules in the Reactor Control and Protection system with equivalent modules manufactured by NUS.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3537, Pkg. 1, Circulating Water System Controls Modification This design change modified the Circulating Water pump starting circuitry to remove the pump start vacuum interlock. This interlock was removed after it was determined that starting a Circulating Water pump with a vacuum present in the condenser water box could produce pressures that exceed the water box design values.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3576, Pkg. 1, Bleed Steam/Heater Drain Control Valve (11 HD9, 12 HD9, 13HD9) Replacement This design change replaced the existing 1 O", carbon steel, Fisher Model 100 control valves with 12" Copes-Vulcan D600 control valves. The new valves are designed to minimize flashing and erosion and to provide more precise control.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3631, Pkg. 2, Moisture Separator Reheater (MSR) Drain Piping This design change increased the capacity of the pumped drain system by replacing drain control valves and the impeller in the 11 Bleed Steam Coil Drain Tank pump. This capacity increase was necessary to accommodate modifications that replaced the MSR tube bundles and the gravity drain lines from the 12E and 13E Bleed Steam Reheat Coils to the 11 Bleed Steam Coil Drain tank.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3650, 4KV Group Bus G.E. Magne-blast Breaker Replacements This design change replaced the 2000A infeed breakers and the 1200A load breakers for all 4160V Group bus applications on Salem Unit 1. Specifically, the existing G. E.
Magne-blast air circuit breakers were replaced with Siemens manufactured vacuum circuit breakers, within the existing switchgear cubicles.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1 EC-3652, Pkg. 1, Moisture Separator Reheater (MSR) Control Logic Upgrades This design change replaced the existing Bailey 820 control system with a more up-to-date Programmable Logic Controller (PLC) based system.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
1EC-3668, Pkg. 14, Protection For Service Water Accumulator Tanks And Associated Equipment This modification installed a gated security barrier in the area of the Service Water Accumulator vessel enclosure and a tornado missile barrier on the roof of the Auxiliary Building. The barrier was installed to provide protection for the vessels and their associated equipment.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
Minor Modification, S97-142, Pkg. 1, Upgrade Of Circulating Water Emergency Backup Line Pressure Reducing Valve (1SC13)
This modification installs.a Fisher Model 4160K Pneumatic Pressure Controller that utilizes an isolation diaphragm seal connected to the process piping being monitored. This modification was implemented to prevent intrusion of silt, impurities, and other debris into the reducing valve internals that in the past have impacted the reliability of the valve and resulted in unnecessary valve maintenance.
This design change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
Temporary Modifications - Summary of Safety Evaluations Installation Of A Mechanical Gag On 11CC6, 11 Component Cooling Water (CCW) Heat Exchanger Isolation Valve This temporary modification installed a mechanical gag on valve 11 CC6 to hold the valve in the open position. The valve is a manually operated gate valve and serves as the inlet isolation valve for the 11 CCW heat exchanger. The gag was installed to hold the valve in the open position until plant conditions permit repair of a damaged valve shaft.
This temporary modification does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this temporary modification does not involve an Unreviewed Safety Question.
Procedures - Summary of Safety Evaluations There were no changes in this category implemented during April 1998.
UFSAR Change Notices - Summary of Safety Evaluations There were no changes in this category implemented during April 1998.
Deficiency Reports - Summary of Safety Evaluations Deficiency Report, 12TB10 Pipe Nipple And Cap Repair This repair replaced a damaged pipe nipple and cap welded into the turbine bypass pipe with a tapered metal plug. The tapered plug was seal welded directly to the main pipe to serve as an equivalent pressure boundary to the damaged pipe and nipple.
This repair does not negatively impact any accident response; nor does it
" increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this repair does not involve an Unreviewed Safety Question.
Other - Summary of Safety Evaluations Change To Salem Unit 1 Technical Specification Bases 3/4.9.1, Refueling Operations, Boron Concentration This change to the Bases for Technical Specification 3/4.9.1 provided clarification of the Technical Specification requirements for sampling of the Salem Unit 1 Refueling Canal.
This change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.
Change To Salem Unit 1 Technical Specification Bases 2.2.1, Safety Limits And Limiting Safety System Settings This change to Technical Specification Bases 2.2.1 revised the description of Negative Flux Rate Trip (NFRT) to make the Bases consistent with the Salem Updated Final Safety Analysis Report. This change was required because of the implementation of an updated Westinghouse rod drop methodology in which the NFRT is no longer credited with protecting against minimum Departure From Nucleate Boiling Ratio (DNBR) concerns.
This change does not negatively impact any accident response; nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.