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| number = ML061000598
| number = ML061000598
| issue date = 12/20/2005
| issue date = 12/20/2005
| title = E-mail from D. Croulet of Entergy to J. Noggle of Usnrc, Regarding H-3 Sources IPEC-RL-Comments-1
| title = E-mail from D. Croulet of Entergy to J. Noggle of USNRC, Regarding H-3 Sources IPEC-RL-Comments-1
| author name = Croulet D
| author name = Croulet D
| author affiliation = Entergy Nuclear Operations, Inc
| author affiliation = Entergy Nuclear Operations, Inc
| addressee name = Noggle J D
| addressee name = Noggle J
| addressee affiliation = NRC/RGN-I/DRS
| addressee affiliation = NRC/RGN-I/DRS
| docket = 05000247, 05000286
| docket = 05000247, 05000286
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:}}
{{#Wiki_filter:James Noggle - FW: H-3 sources iPECRL Comments 1.xls                                                              _Page1JJ From:                "Croulet, Donald" <dcroule@entergy.com>
To:                  "'James Noggle"' <JDN~nrc.gov>
Date:                12/20/05 3:30PM
 
==Subject:==
FW: H-3 sources IPEC_RL_Comments_1.xls Jim, At todays Spent Fuel Pool status meeting I inquired about our plans to verify that the Unit 1 south curtain drain was unblocked and functioning and also the Unit 2 containment footer drain system and segregation of its outfall for sampling at manhole 5. I was told that a feasibility study is in progress to determine robotics entry points.
From: Croulet, Donald Sent: Tuesday, December 20, 2005 9:46 AM To: 'James Noggle'
 
==Subject:==
FW: H-3 sources IPECRLComments_1.xls Jim, This is the last list I have. I will confirm with Bill Axelson. We will send you an updated version as changes occur to this list.
From: Lavera, Ron Sent: Tl ursday, December 08, 2005 5:47 PM To: Solanto, Robert; Bob Evers; Christopher English; David Smith; Don Leach; Don Mayer; Donald Croulet; Dragos Nuta; Gary Hinrichs; Hank Santis; James Peters; Joe Kulaga; John Skonieczny; Kathy McMullin; Kenneth Morin; Michael Durfee; Michael Rutkoske; Paul Deeds; Richard Colville; Richard Drake; Flon Lavera; Ronald Sachatello; T. R. Jones
 
==Subject:==
H-3 sources IPEC_RLComments_1.xIs To all This is the known past leakage list that Dennis Quinn and I have compiled, so far. Please let me know about any addtions/deletions/changes.
Thanks Ron
            <<H-3 sources IPEC RL-Comments-1.xls>>
 
Js Nogge - FW: H-3 sourcesIPEC RL Comments 1.xls                                                                      Pag1 From:              "Croulet, Donald" <dcroule&#xa9;entergy.com>
To:                "'James Noggle"' <JDN~nrc.gov>
Date:              12/20/05 9:46AM
 
==Subject:==
FW: H-3 sources IPECRLComments_1.xls Jim, This is the last list I have. I will confirm with Bill Axelson. We will send you an updated version as changes occur to this list.
From: Lavera, Ron Sent: Thursday, December 08, 2005 5:47 PM To: Solanto, Robert; Bob Evers; Christopher English; David Smith; Don Leach; Don Mayer; Donald Croulet; Dragos Nuta; Gary Hinrichs; Hank Santis; James Peters; Joe Kulaga; John Skonieczny; Kathy McMulli,; Kenneth Morin; Michael Durfee; Michael Rutkoske; Paul Deeds; Richard Colville; Richard Drake; Ron Lavera; Ronald Sachatello; T. R. Jones
 
==Subject:==
H-3 sources IPEC_RLComments_1 .xls To all This is tne known past leakage list that Dennis Quinn and I have compiled, so far. Please let me knovi about any addtions/deletions/changes.
Thanks Ron
        <<H-3 sources IPEC_RL_Comments_1.xls>>
 
Potential Volume      H-3  H-3 total      for.
U2 FSP          3.OOE+05 2.80E-02 3.18E+01 high            1990-1992, 2005 2000 leak from wall from skimmer U3 FSP          3.OOE+05 3.40E-02 3.86E+01 High            pump leak onto concrete Noticed in 1990-1994 time frame. Initial leakage not contained/collected. On going leakage. Containment process U1 West Pool      1.OOE+05 4.OOE-04  1.51 E-01 High          implemented.
leakage not contained/collected. On U1 Other Pools                        0.00E+00 High            going leakage. Containment process Anecdotal information that it over flowed to the ground on several U2 RWST          3.50E+05 1.68E-01 2.23E+02                occasions in the past No known significant leakage to the U3 RWST          3.50E+05 4.64E-02 6.15E+01                ground.
Anecdotal information that the area was U2 CVCS Tanks                        0.OOE+00                flooded in the past Anecdotal information that the area was U2 Waste Tanks                        0.00E+00                flooded in the past Anecdotal information that the area was flooded by Waste Collection Tank U2 MOB                            0.OOE+00 Med            water, in the past Overflows of 31 Waste Tank into tank A  pit
                                                                . containing 31 WHUT, and 31-33
    .Ve-    -. m T-nnL  -LC                                            pitccotIng IMe d 31r-  WHUT+
III IL4LHTS I-n', andl l 70' UL4c1a31,-3 y V's
        .                                                    I.
 
                                                ._                                    31 WHUT tank area flooded. 32 & 33 U3 Waste Tanks                              _.O0E+00                  Tank areas never flooded.
Potential for Tritium contamination of U2 SFP 1990 - 1992 Leak [a]                  1.83E+04 2.OOE-02  1.39E+0O High  soil.
U2 RWST Overflow (year?)                                        0.OOE+00      _ (
U2 PAB Sump                    =          1.OOE-01 0.OOE+00 Med    Sump is not lined with stainless steel.
Floor was flooded to significant depth in U2 15 Ft. PAB                                        0.OOE+00 Med    late 1970's early 1980's U3 PAB Sump                          =        =    0.OOE+00 U3 to U2 underground waste line -                                                      Leaked in 1980s; it was abandoned in abandoned                                          0.OOE+00        place Known Contamination near the GT U3 to U2 Blowdown Transfer Line                                                High  between units.
U2 Resin Spill in alleyway next to                                                    Resin spill with relative small volume of FSB                                        0.OOE+00 low    water.
%J.J-  I IJWJI I  WV ILI I  LIAVI I IAUJ PD;7u-trench from PAB spilling into area                                                    Known leakage in the 1977-1985 time below cable tunnel                                        0.OOE+00 High  frame.
Known leakage in the 1977-1985 time U3- area between VC, FSB, PAB,                                                      frame. Extends to building curtain aka Pigeon Pit, unknown leakage                      _              0.OOE+00        drains and storm sewer system.
a- assume 25 gallons/day x 2 years
              = 18,300 gallons                              _0.E+00L
 
south of U3 Command Post, had Cs 137, Co-60, others. Removed in -
1980 and stored on hill past met 1
tower                                  O.OOE+Oo High U2 Blowdown (Past) atmospheric                                            Known operation for years, with primary release                                O.OOE+O0            to secondary leaks.
U2 Blowdown (current) atmospheric                                          Known operation for years, with primary release                      5.OOE-07 O.OOE+00            to secondary leaks.
Contamination of secondary plant -
U2 SG Tube Leak Feb 2000                          O.OOE+00            drains U3 SG Tube Leak Oct 1989          =.OOE+00                            Contamination of secondary plant U3 Operation of Main Steam supply                                          Auxilary steam system drains go to to Auxilary Steam system.                5.OOE-07 O.OOE+Oo High        plant drains and storm drain system.
Anecdotal information that the area U2 PAB 15' Overflow/Pump to                                            flooded or was pumpted into the transformer yard                    1.OOE-01 O.OOE+Oo High        transformer yard, in the past On going - Also during years operating IP-2 Transformer Yard - Turbine hall                                        with known primary to secondary condensate drainage                                        High    leakage.
U3 RWST base of Hill contaminated Water stream                                          High    Source may have been IP-1 leakage IP-3 41' PAB Auxilary Condensate sump pump discharge was aligned to lP-3 41' PAB Sump Pump                                                storm drain system in late 1970's to Dishcharge to storm drain                                    Low      early 1980's. Since locked closed.
9                9          9        9
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Latest revision as of 07:15, 23 March 2020

E-mail from D. Croulet of Entergy to J. Noggle of USNRC, Regarding H-3 Sources IPEC-RL-Comments-1
ML061000598
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 12/20/2005
From: Croulet D
Entergy Nuclear Operations
To: Noggle J
Division of Reactor Safety I
References
FOIA/PA-2006-0081
Download: ML061000598 (10)


Text

James Noggle - FW: H-3 sources iPECRL Comments 1.xls _Page1JJ From: "Croulet, Donald" <dcroule@entergy.com>

To: "'James Noggle"' <JDN~nrc.gov>

Date: 12/20/05 3:30PM

Subject:

FW: H-3 sources IPEC_RL_Comments_1.xls Jim, At todays Spent Fuel Pool status meeting I inquired about our plans to verify that the Unit 1 south curtain drain was unblocked and functioning and also the Unit 2 containment footer drain system and segregation of its outfall for sampling at manhole 5. I was told that a feasibility study is in progress to determine robotics entry points.

From: Croulet, Donald Sent: Tuesday, December 20, 2005 9:46 AM To: 'James Noggle'

Subject:

FW: H-3 sources IPECRLComments_1.xls Jim, This is the last list I have. I will confirm with Bill Axelson. We will send you an updated version as changes occur to this list.

From: Lavera, Ron Sent: Tl ursday, December 08, 2005 5:47 PM To: Solanto, Robert; Bob Evers; Christopher English; David Smith; Don Leach; Don Mayer; Donald Croulet; Dragos Nuta; Gary Hinrichs; Hank Santis; James Peters; Joe Kulaga; John Skonieczny; Kathy McMullin; Kenneth Morin; Michael Durfee; Michael Rutkoske; Paul Deeds; Richard Colville; Richard Drake; Flon Lavera; Ronald Sachatello; T. R. Jones

Subject:

H-3 sources IPEC_RLComments_1.xIs To all This is the known past leakage list that Dennis Quinn and I have compiled, so far. Please let me know about any addtions/deletions/changes.

Thanks Ron

<<H-3 sources IPEC RL-Comments-1.xls>>

Js Nogge - FW: H-3 sourcesIPEC RL Comments 1.xls Pag1 From: "Croulet, Donald" <dcroule©entergy.com>

To: "'James Noggle"' <JDN~nrc.gov>

Date: 12/20/05 9:46AM

Subject:

FW: H-3 sources IPECRLComments_1.xls Jim, This is the last list I have. I will confirm with Bill Axelson. We will send you an updated version as changes occur to this list.

From: Lavera, Ron Sent: Thursday, December 08, 2005 5:47 PM To: Solanto, Robert; Bob Evers; Christopher English; David Smith; Don Leach; Don Mayer; Donald Croulet; Dragos Nuta; Gary Hinrichs; Hank Santis; James Peters; Joe Kulaga; John Skonieczny; Kathy McMulli,; Kenneth Morin; Michael Durfee; Michael Rutkoske; Paul Deeds; Richard Colville; Richard Drake; Ron Lavera; Ronald Sachatello; T. R. Jones

Subject:

H-3 sources IPEC_RLComments_1 .xls To all This is tne known past leakage list that Dennis Quinn and I have compiled, so far. Please let me knovi about any addtions/deletions/changes.

Thanks Ron

<<H-3 sources IPEC_RL_Comments_1.xls>>

Potential Volume H-3 H-3 total for.

U2 FSP 3.OOE+05 2.80E-02 3.18E+01 high 1990-1992, 2005 2000 leak from wall from skimmer U3 FSP 3.OOE+05 3.40E-02 3.86E+01 High pump leak onto concrete Noticed in 1990-1994 time frame. Initial leakage not contained/collected. On going leakage. Containment process U1 West Pool 1.OOE+05 4.OOE-04 1.51 E-01 High implemented.

leakage not contained/collected. On U1 Other Pools 0.00E+00 High going leakage. Containment process Anecdotal information that it over flowed to the ground on several U2 RWST 3.50E+05 1.68E-01 2.23E+02 occasions in the past No known significant leakage to the U3 RWST 3.50E+05 4.64E-02 6.15E+01 ground.

Anecdotal information that the area was U2 CVCS Tanks 0.OOE+00 flooded in the past Anecdotal information that the area was U2 Waste Tanks 0.00E+00 flooded in the past Anecdotal information that the area was flooded by Waste Collection Tank U2 MOB 0.OOE+00 Med water, in the past Overflows of 31 Waste Tank into tank A pit

. containing 31 WHUT, and 31-33

.Ve- -. m T-nnL -LC pitccotIng IMe d 31r- WHUT+

III IL4LHTS I-n', andl l 70' UL4c1a31,-3 y V's

. I.

._ 31 WHUT tank area flooded. 32 & 33 U3 Waste Tanks _.O0E+00 Tank areas never flooded.

Potential for Tritium contamination of U2 SFP 1990 - 1992 Leak [a] 1.83E+04 2.OOE-02 1.39E+0O High soil.

U2 RWST Overflow (year?) 0.OOE+00 _ (

U2 PAB Sump = 1.OOE-01 0.OOE+00 Med Sump is not lined with stainless steel.

Floor was flooded to significant depth in U2 15 Ft. PAB 0.OOE+00 Med late 1970's early 1980's U3 PAB Sump = = 0.OOE+00 U3 to U2 underground waste line - Leaked in 1980s; it was abandoned in abandoned 0.OOE+00 place Known Contamination near the GT U3 to U2 Blowdown Transfer Line High between units.

U2 Resin Spill in alleyway next to Resin spill with relative small volume of FSB 0.OOE+00 low water.

%J.J- I IJWJI I WV ILI I LIAVI I IAUJ PD;7u-trench from PAB spilling into area Known leakage in the 1977-1985 time below cable tunnel 0.OOE+00 High frame.

Known leakage in the 1977-1985 time U3- area between VC, FSB, PAB, frame. Extends to building curtain aka Pigeon Pit, unknown leakage _ 0.OOE+00 drains and storm sewer system.

a- assume 25 gallons/day x 2 years

= 18,300 gallons _0.E+00L

south of U3 Command Post, had Cs 137, Co-60, others. Removed in -

1980 and stored on hill past met 1

tower O.OOE+Oo High U2 Blowdown (Past) atmospheric Known operation for years, with primary release O.OOE+O0 to secondary leaks.

U2 Blowdown (current) atmospheric Known operation for years, with primary release 5.OOE-07 O.OOE+00 to secondary leaks.

Contamination of secondary plant -

U2 SG Tube Leak Feb 2000 O.OOE+00 drains U3 SG Tube Leak Oct 1989 =.OOE+00 Contamination of secondary plant U3 Operation of Main Steam supply Auxilary steam system drains go to to Auxilary Steam system. 5.OOE-07 O.OOE+Oo High plant drains and storm drain system.

Anecdotal information that the area U2 PAB 15' Overflow/Pump to flooded or was pumpted into the transformer yard 1.OOE-01 O.OOE+Oo High transformer yard, in the past On going - Also during years operating IP-2 Transformer Yard - Turbine hall with known primary to secondary condensate drainage High leakage.

U3 RWST base of Hill contaminated Water stream High Source may have been IP-1 leakage IP-3 41' PAB Auxilary Condensate sump pump discharge was aligned to lP-3 41' PAB Sump Pump storm drain system in late 1970's to Dishcharge to storm drain Low early 1980's. Since locked closed.

9 9 9 9

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Unit- Site 2

3 tI 1

1 I-r 2

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