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{{#Wiki_filter:December 15, 2006Mr. William LevisSenior Vice President & Chief Nuclear Officer PSEG Nuclear LLC - N09 Post Office Box 236 Hancocks Bridge, NJ 08038
{{#Wiki_filter:December 15, 2006 Mr. William Levis Senior Vice President & Chief Nuclear Officer PSEG Nuclear LLC - N09 Post Office Box 236 Hancocks Bridge, NJ 08038


==SUBJECT:==
==SUBJECT:==
HOPE CREEK GENERATING STATION - FINAL ACCIDENT SEQUENCEPRECURSOR ANALYSIS OF OCTOBER 10, 2004, OPERATIONAL EVENT
HOPE CREEK GENERATING STATION - FINAL ACCIDENT SEQUENCE PRECURSOR ANALYSIS OF OCTOBER 10, 2004, OPERATIONAL EVENT


==Dear Mr. Levis:==
==Dear Mr. Levis:==


The enclosure provides the final results of the Accident Sequence Precursor (ASP) analysis ofan event which occurred at the Hope Creek Generating Station (Hope Creek) as documented in Licensee Event Report 354/04-010. The subject event occurred on October 10, 2004, when a pipe failure occurred in a moisture separator reheater drain line, leading to a manual reactor scram and plant cooldown. The ASP analysis calculated a mean conditional core damage probability of 3.4 x 10
The enclosure provides the final results of the Accident Sequence Precursor (ASP) analysis of an event which occurred at the Hope Creek Generating Station (Hope Creek) as documented in Licensee Event Report 354/04-010. The subject event occurred on October 10, 2004, when a pipe failure occurred in a moisture separator reheater drain line, leading to a manual reactor scram and plant cooldown. The ASP analysis calculated a mean conditional core damage probability of 3.4 x 10-6.
-6.The Nuclear Regulatory Commission (NRC) established the ASP Program in 1979 in responseto the Risk Assessment Review Group Report (see NUREG/CR-0400, dated September 1978).
The Nuclear Regulatory Commission (NRC) established the ASP Program in 1979 in response to the Risk Assessment Review Group Report (see NUREG/CR-0400, dated September 1978).
The ASP Program systematically evaluates U.S. nuclear power plant operating experience to identify, document, and rank the operating events that were most likely to have led to inadequate core cooling and severe core damage (precursors), accounting for the likelihood of additional failures.The ASP Program has the following objectives:
The ASP Program systematically evaluates U.S. nuclear power plant operating experience to identify, document, and rank the operating events that were most likely to have led to inadequate core cooling and severe core damage (precursors), accounting for the likelihood of additional failures.
The ASP Program has the following objectives:
* Provide a measure for trending nuclear power plant core damage risk.
* Provide a partial check on dominant core damage scenarios predicted by probabilistic risk assessments (PRAs).
* Provide feedback to regulatory activities.
* Evaluate the adequacy of NRC programs.
The NRC also uses the ASP Program to monitor performance against the safety goal established in the agency's Strategic Plan (see NUREG-1100, Vol. 21, dated February 2005).
For more information about the ASP program, see the annual ASP program report at http://www.nrc.gov/reading-rm/doc-collections/commission/secys/2005/secy2005-0192/2005-01 92scy.pdf.


*Provide a measure for trending nuclear power plant core damage risk.
W. Levis                                       The enclosure is provided for your information and no response is requested. If you have any questions about the analyses, please contact me at (301) 415-1321 or at snb@nrc.gov.
*Provide a partial check on dominant core damage scenarios predicted by probabilisticrisk assessments (PRAs).*Provide feedback to regulatory activities.
Sincerely,
*Evaluate the adequacy of NRC programs.The NRC also uses the ASP Program to monitor performance against the safety goalestablished in the agency's Strategic Plan (see NUREG-1100, Vol. 21, dated February 2005). For more information about the ASP program, see the annual ASP program report athttp://www.nrc.gov/reading-rm/doc-collections/commission/secys/2005/secy2005-0192/2005-0192scy.pdf.
                                            /RA/
W. Levis-2-The enclosure is provided for your information and no response is requested. If you have anyquestions about the analyses, please contact me at (301) 415-1321 or at snb@nrc.gov.Sincerely,/RA/Stewart N. Bailey, Senior Project ManagerPlant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor RegulationDocket No. 50-354
Stewart N. Bailey, Senior Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-354


==Enclosure:==
==Enclosure:==
Final ASP Analysiscc w/encl:  See next page


ML063390090OFFICELPL1-2/PMLPL1-2/LALPL1-2/BCNAMESBaileyCRaynorHChernoffDATE12/31/0612/13/0612/15/06 Hope Creek Generating Station cc:
Final ASP Analysis cc w/encl: See next page
Mr. Dennis WinchesterVice President - Nuclear Assessments PSEG Nuclear P.O. Box 236 Hancocks Bridge, NJ  08038Mr. George P. BarnesSite Vice President - Hope Creek PSEG Nuclear P.O. Box 236 Hancocks Bridge, NJ 08038Mr. George H. GellrichPlant Support Manager PSEG Nuclear P.O. Box 236 Hancocks Bridge, NJ 08038Mr. Michael J. MassaroPlant Manager - Hope Creek PSEG Nuclear P.O. Box 236 Hancocks Bridge, NJ 08038Mr. James MallonManager - Licensing 200 Exelon Way - KSA 3-E Kennett Square, PA 19348Jeffrie J. Keenan, EsquirePSEG Nuclear - N21 P.O. Box 236 Hancocks Bridge, NJ  08038Mr. Michael JesseManager - Regulatory Assurance P.O. Box 236 Hancocks Bridge, NJ 08038Township ClerkLower Alloways Creek Township Municipal Building, P.O. Box 157 Hancocks Bridge, NJ  08038Mr. Paul Bauldauf, P.E., Asst. DirectorRadiation Protection Programs NJ Department of Environmental Protection and Energy


CN 415 Trenton, NJ 08625-0415Mr. Brian BeamBoard of Public Utilities 2 Gateway Center, Tenth Floor Newark, NJ 07102Regional Administrator, Region IU.S. Nuclear Regulatory Commission
ML063390090 OFFICE LPL1-2/PM            LPL1-2/LA            LPL1-2/BC NAME SBailey                CRaynor              HChernoff DATE      12/31/06          12/13/06            12/15/06 Hope Creek Generating Station cc:
Mr. Dennis Winchester                Mr. Paul Bauldauf, P.E., Asst. Director Vice President - Nuclear Assessments Radiation Protection Programs PSEG Nuclear                        NJ Department of Environmental P.O. Box 236                          Protection and Energy Hancocks Bridge, NJ 08038            CN 415 Trenton, NJ 08625-0415 Mr. George P. Barnes Site Vice President - Hope Creek    Mr. Brian Beam PSEG Nuclear                        Board of Public Utilities P.O. Box 236                        2 Gateway Center, Tenth Floor Hancocks Bridge, NJ 08038            Newark, NJ 07102 Mr. George H. Gellrich              Regional Administrator, Region I Plant Support Manager                U.S. Nuclear Regulatory Commission PSEG Nuclear                        475 Allendale Road P.O. Box 236                        King of Prussia, PA 19406 Hancocks Bridge, NJ 08038 Senior Resident Inspector Mr. Michael J. Massaro              Hope Creek Generating Station Plant Manager - Hope Creek          U.S. Nuclear Regulatory Commission PSEG Nuclear                        Drawer 0509 P.O. Box 236                        Hancocks Bridge, NJ 08038 Hancocks Bridge, NJ 08038 Mr. James Mallon Manager - Licensing 200 Exelon Way - KSA 3-E Kennett Square, PA 19348 Jeffrie J. Keenan, Esquire PSEG Nuclear - N21 P.O. Box 236 Hancocks Bridge, NJ 08038 Mr. Michael Jesse Manager - Regulatory Assurance P.O. Box 236 Hancocks Bridge, NJ 08038 Township Clerk Lower Alloways Creek Township Municipal Building, P.O. Box 157 Hancocks Bridge, NJ 08038


475 Allendale Road King of Prussia, PA  19406Senior Resident InspectorHope Creek Generating Station U.S. Nuclear Regulatory Commission Drawer 0509 Hancocks Bridge, NJ  08038
==SUMMARY==
OF FINAL ACCIDENT SEQUENCE PRECURSOR ANALYSIS PIPE FAILURE AND SCRAM ON OCTOBER 10, 2004 HOPE CREEK GENERATING STATION PSEG NUCLEAR LLC Manual reactor scram due to moisture separator reheater drain line failure at Hope Creek (October 2004). This event is documented in Licensee Event Report LER 354/04-010, dated December 9, 2004.
The Region I office of the Nuclear Regulatory Commission conducted a Special Inspection and issued Inspection Report (IR) 05000354/2004013 on February 4, 2005. A Notice of Violation was issued for this event under EA-05-001 on February 28, 2005.
Event summary. On October 10, 2004, at 17:39 hours, a pipe failure occurred in a moisture separator reheater drain line of the Hope Creek Nuclear Generating Station. A power reduction to 80-percent power was initiated at 17:59 hours due to reports of a steam leak in the turbine building. At 18:14 hours, the reactor recirculation pumps were reduced to minimum speed and the reactor was manually scrammed. Operators initially began to reduce the reactor pressure vessel (RPV) pressure using the turbine bypass valves to allow for use of the condensate and feedwater pumps for RPV makeup. Due to the continued degradation of condenser vacuum, the reactor feedwater pumps all tripped. At this point, RPV makeup and pressure control was provided by manually initiating the high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) systems. At 18:17 hours, the control room supervisor directed the reactor operator to close the turbine bypass valves. As the bypass valves closed, RPV level decreased causing an isolation signal.
With the RCIC system injecting into the RPV and water levels trending upwards, HPCI injection was terminated. Condenser vacuum continued to degrade and operators manually closed the main steam isolation valves (MSIVs) and main steam line drain valves prior to automatic closure on low condenser vacuum. Following MSIV closure, HPCI was placed in the pressure control mode. While placing HPCI in the pressure control mode, operators were initially unable to open the HPCI full-flow test line motor-operated valve. At 18:31 hours, the A and B residual heat removal trains were placed in the suppression pool cooling mode. At 18:46 hours, RPV level dropped and the RPV Level 3 scram setpoint was again actuated. RCIC flow was manually increased to restore water levels above the RPV Level 3 scram setpoint. Following this, at approximately 18:50 hours, the feedwater system was restarted (with flow being provided by the condensate pumps) with the startup feedwater level control valve set in the automatic mode.
At 20:48 hours, the operators commenced a plant cooldown using HPCI, RCIC, and safety/relief valves (SRVs). This effort was complicated by repeated trips of the HPCI barometric vacuum pump, a non-safety support system which maintains a slight vacuum on the HPCI steam discharge line. This led operators to secure the HPCI system and rely on a combination of SRVs and RCIC to maintain RPV level and depressurize the system. At approximately 22:03 hours, the Level 3 setpoint was again reset and feedwater startup level Enclosure


==SUMMARY==
control valve setpoint raised from 25 inches to 35 inches (with flow being provided by the condensate pumps). The plant reached cold shutdown conditions at 05:09 hours on October 12, 2004.
OF FINAL ACCIDENT SEQUENCE PRECURSOR ANALYSISPIPE FAILURE AND SCRAM ON OCTOBER 10, 2004HOPE CREEK GENERATING STATIONPSEG NUCLEAR LLCManual reactor scram due to moisture separator reheater drain line failure at Hope Creek(October 2004). This event is documented in Licensee Event Report LER 354/04-010, datedDecember 9, 2004.The Region I office of the Nuclear Regulatory Commission conducted a Special Inspection andissued Inspection Report (IR) 05000354/2004013 on February 4, 2005. A Notice of Violation was issued for this event under EA-05-001 on February 28, 2005. Event summary. On October 10, 2004, at 17:39 hours, a pipe failure occurred in a moistureseparator reheater drain line of the Hope Creek Nuclear Generating Station. A power reduction to 80-percent power was initiated at 17:59 hours due to reports of a steam leak in the turbine building. At 18:14 hours, the reactor recirculation pumps were reduced to minimum speed and the reactor was manually scrammed. Operators initially began to reduce the reactor pressure vessel (RPV) pressure using the turbine bypass valves to allow for use of the condensate and feedwater pumps for RPV makeup. Due to the continued degradation of condenser vacuum, the reactor feedwater pumps all tripped. At this point, RPV makeup and pressure control was provided by manually initiating the high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) systems. At 18:17 hours, the control room supervisor directed the reactor operator to close the turbine bypass valves. As the bypass valves closed, RPV level decreased causing an isolation signal.With the RCIC system injecting into the RPV and water levels trending upwards, HPCI injectionwas terminated. Condenser vacuum continued to degrade and operators manually closed the main steam isolation valves (MSIVs) and main steam line drain valves prior to automatic closure on low condenser vacuum. Following MSIV closure, HPCI was placed in the pressure control mode. While placing HPCI in the pressure control mode, operators were initially unable to open the HPCI full-flow test line motor-operated valve. At 18:31 hours, the A and B residual heat removal trains were placed in the suppression pool cooling mode. At 18:46 hours, RPV level dropped and the RPV Level 3 scram setpoint was again actuated. RCIC flow was manually increased to restore water levels above the RPV Level 3 scram setpoint. Following this, at approximately 18:50 hours, the feedwater system was restarted (with flow being provided by the condensate pumps) with the startup feedwater level control valve set in the automatic mode.At 20:48 hours, the operators commenced a plant cooldown using HPCI, RCIC, andsafety/relief valves (SRVs). This effort was complicated by repeated trips of the HPCI barometric vacuum pump, a non-safety support system which maintains a slight vacuum on the HPCI steam discharge line. This led operators to secure the HPCI system and rely on a combination of SRVs and RCIC to maintain RPV level and depressurize the system. At approximately 22:03 hours, the Level 3 setpoint was again reset and feedwater startup levelEnclosure  control valve setpoint raised from 25 inches to 35 inches (with flow being provided by thecondensate pumps). The plant reached cold shutdown conditions at 05:09 hours on October 12, 2004.Results. This initiating event resulted in a conditional core damage probability (CCDP) of3.4x10-6. An uncertainty analysis for this operating condition resulted in a mean CCDP of3.4x10-6 with 5% and 95% uncertainty bounds of 4.7x10
Results. This initiating event resulted in a conditional core damage probability (CCDP) of 3.4x10-6. An uncertainty analysis for this operating condition resulted in a mean CCDP of 3.4x10-6 with 5% and 95% uncertainty bounds of 4.7x10-8 and 1.2x10-5, respectively.
-8 and 1.2x10
SDP/ASP comparison. The result of the Significance Determination Process (SDP) analysis was a White finding. The White finding was based on a SDP Phase 3 assessment assuming an unavailability of 25 days and an estimated increase in core damage frequency (CDF) of 1.8x10-6 for internal events. Since the SDP did a CDF calculation and the Accident Sequence Precursor (ASP) analysis did an initiating event assessment (i.e., calculated the CCDP), the two analytic results are not numerically comparable. The analytic assumptions and dominant risk contributors are similar in the two analyses.
-5, respectively.SDP/ASP comparison. The result of the Significance Determination Process (SDP) analysiswas a White finding. The White finding was based on a SDP Phase 3 assessment assuming an unavailability of 25 days and an estimated increase in core damage frequency (CDF) of1.8x10-6 for internal events. Since the SDP did a CDF calculation and the AccidentSequence Precursor (ASP) analysis did an initiating event assessment (i.e., calculated the CCDP), the two analytic results are not numerically comparable. The analytic assumptions and dominant risk contributors are similar in the two analyses.The ASP analysis can be found in the Agencywide Documents Access and ManagementSystem at Accession number ML062710037. If you have any questions about the analysis, please contact Gary DeMoss (301-415-6225).}}
The ASP analysis can be found in the Agencywide Documents Access and Management System at Accession number ML062710037. If you have any questions about the analysis, please contact Gary DeMoss (301-415-6225).}}

Latest revision as of 22:51, 13 March 2020

Final Accident Sequence Precursor Analysis of October 10, 2004 Operational Event
ML063390090
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 12/15/2006
From: Stewart Bailey
NRC/NRR/ADRO/DORL/LPLI-2
To: Levis W
Public Service Enterprise Group
Bailey S N,NRR/DLPM,415-1321
References
Download: ML063390090 (6)


Text

December 15, 2006 Mr. William Levis Senior Vice President & Chief Nuclear Officer PSEG Nuclear LLC - N09 Post Office Box 236 Hancocks Bridge, NJ 08038

SUBJECT:

HOPE CREEK GENERATING STATION - FINAL ACCIDENT SEQUENCE PRECURSOR ANALYSIS OF OCTOBER 10, 2004, OPERATIONAL EVENT

Dear Mr. Levis:

The enclosure provides the final results of the Accident Sequence Precursor (ASP) analysis of an event which occurred at the Hope Creek Generating Station (Hope Creek) as documented in Licensee Event Report 354/04-010. The subject event occurred on October 10, 2004, when a pipe failure occurred in a moisture separator reheater drain line, leading to a manual reactor scram and plant cooldown. The ASP analysis calculated a mean conditional core damage probability of 3.4 x 10-6.

The Nuclear Regulatory Commission (NRC) established the ASP Program in 1979 in response to the Risk Assessment Review Group Report (see NUREG/CR-0400, dated September 1978).

The ASP Program systematically evaluates U.S. nuclear power plant operating experience to identify, document, and rank the operating events that were most likely to have led to inadequate core cooling and severe core damage (precursors), accounting for the likelihood of additional failures.

The ASP Program has the following objectives:

  • Provide a measure for trending nuclear power plant core damage risk.
  • Provide feedback to regulatory activities.
  • Evaluate the adequacy of NRC programs.

The NRC also uses the ASP Program to monitor performance against the safety goal established in the agency's Strategic Plan (see NUREG-1100, Vol. 21, dated February 2005).

For more information about the ASP program, see the annual ASP program report at http://www.nrc.gov/reading-rm/doc-collections/commission/secys/2005/secy2005-0192/2005-01 92scy.pdf.

W. Levis The enclosure is provided for your information and no response is requested. If you have any questions about the analyses, please contact me at (301) 415-1321 or at snb@nrc.gov.

Sincerely,

/RA/

Stewart N. Bailey, Senior Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-354

Enclosure:

Final ASP Analysis cc w/encl: See next page

ML063390090 OFFICE LPL1-2/PM LPL1-2/LA LPL1-2/BC NAME SBailey CRaynor HChernoff DATE 12/31/06 12/13/06 12/15/06 Hope Creek Generating Station cc:

Mr. Dennis Winchester Mr. Paul Bauldauf, P.E., Asst. Director Vice President - Nuclear Assessments Radiation Protection Programs PSEG Nuclear NJ Department of Environmental P.O. Box 236 Protection and Energy Hancocks Bridge, NJ 08038 CN 415 Trenton, NJ 08625-0415 Mr. George P. Barnes Site Vice President - Hope Creek Mr. Brian Beam PSEG Nuclear Board of Public Utilities P.O. Box 236 2 Gateway Center, Tenth Floor Hancocks Bridge, NJ 08038 Newark, NJ 07102 Mr. George H. Gellrich Regional Administrator, Region I Plant Support Manager U.S. Nuclear Regulatory Commission PSEG Nuclear 475 Allendale Road P.O. Box 236 King of Prussia, PA 19406 Hancocks Bridge, NJ 08038 Senior Resident Inspector Mr. Michael J. Massaro Hope Creek Generating Station Plant Manager - Hope Creek U.S. Nuclear Regulatory Commission PSEG Nuclear Drawer 0509 P.O. Box 236 Hancocks Bridge, NJ 08038 Hancocks Bridge, NJ 08038 Mr. James Mallon Manager - Licensing 200 Exelon Way - KSA 3-E Kennett Square, PA 19348 Jeffrie J. Keenan, Esquire PSEG Nuclear - N21 P.O. Box 236 Hancocks Bridge, NJ 08038 Mr. Michael Jesse Manager - Regulatory Assurance P.O. Box 236 Hancocks Bridge, NJ 08038 Township Clerk Lower Alloways Creek Township Municipal Building, P.O. Box 157 Hancocks Bridge, NJ 08038

SUMMARY

OF FINAL ACCIDENT SEQUENCE PRECURSOR ANALYSIS PIPE FAILURE AND SCRAM ON OCTOBER 10, 2004 HOPE CREEK GENERATING STATION PSEG NUCLEAR LLC Manual reactor scram due to moisture separator reheater drain line failure at Hope Creek (October 2004). This event is documented in Licensee Event Report LER 354/04-010, dated December 9, 2004.

The Region I office of the Nuclear Regulatory Commission conducted a Special Inspection and issued Inspection Report (IR) 05000354/2004013 on February 4, 2005. A Notice of Violation was issued for this event under EA-05-001 on February 28, 2005.

Event summary. On October 10, 2004, at 17:39 hours, a pipe failure occurred in a moisture separator reheater drain line of the Hope Creek Nuclear Generating Station. A power reduction to 80-percent power was initiated at 17:59 hours due to reports of a steam leak in the turbine building. At 18:14 hours, the reactor recirculation pumps were reduced to minimum speed and the reactor was manually scrammed. Operators initially began to reduce the reactor pressure vessel (RPV) pressure using the turbine bypass valves to allow for use of the condensate and feedwater pumps for RPV makeup. Due to the continued degradation of condenser vacuum, the reactor feedwater pumps all tripped. At this point, RPV makeup and pressure control was provided by manually initiating the high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) systems. At 18:17 hours, the control room supervisor directed the reactor operator to close the turbine bypass valves. As the bypass valves closed, RPV level decreased causing an isolation signal.

With the RCIC system injecting into the RPV and water levels trending upwards, HPCI injection was terminated. Condenser vacuum continued to degrade and operators manually closed the main steam isolation valves (MSIVs) and main steam line drain valves prior to automatic closure on low condenser vacuum. Following MSIV closure, HPCI was placed in the pressure control mode. While placing HPCI in the pressure control mode, operators were initially unable to open the HPCI full-flow test line motor-operated valve. At 18:31 hours, the A and B residual heat removal trains were placed in the suppression pool cooling mode. At 18:46 hours, RPV level dropped and the RPV Level 3 scram setpoint was again actuated. RCIC flow was manually increased to restore water levels above the RPV Level 3 scram setpoint. Following this, at approximately 18:50 hours, the feedwater system was restarted (with flow being provided by the condensate pumps) with the startup feedwater level control valve set in the automatic mode.

At 20:48 hours, the operators commenced a plant cooldown using HPCI, RCIC, and safety/relief valves (SRVs). This effort was complicated by repeated trips of the HPCI barometric vacuum pump, a non-safety support system which maintains a slight vacuum on the HPCI steam discharge line. This led operators to secure the HPCI system and rely on a combination of SRVs and RCIC to maintain RPV level and depressurize the system. At approximately 22:03 hours, the Level 3 setpoint was again reset and feedwater startup level Enclosure

control valve setpoint raised from 25 inches to 35 inches (with flow being provided by the condensate pumps). The plant reached cold shutdown conditions at 05:09 hours on October 12, 2004.

Results. This initiating event resulted in a conditional core damage probability (CCDP) of 3.4x10-6. An uncertainty analysis for this operating condition resulted in a mean CCDP of 3.4x10-6 with 5% and 95% uncertainty bounds of 4.7x10-8 and 1.2x10-5, respectively.

SDP/ASP comparison. The result of the Significance Determination Process (SDP) analysis was a White finding. The White finding was based on a SDP Phase 3 assessment assuming an unavailability of 25 days and an estimated increase in core damage frequency (CDF) of 1.8x10-6 for internal events. Since the SDP did a CDF calculation and the Accident Sequence Precursor (ASP) analysis did an initiating event assessment (i.e., calculated the CCDP), the two analytic results are not numerically comparable. The analytic assumptions and dominant risk contributors are similar in the two analyses.

The ASP analysis can be found in the Agencywide Documents Access and Management System at Accession number ML062710037. If you have any questions about the analysis, please contact Gary DeMoss (301-415-6225).