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CC*i* T lojil 8
CC*i* T lojil 8
y' T lL Q ]O l5 [0 l- l0 l3 l4Gl6 gl0 l1 l0 [7 l8 l0 @l0l8l0l4l8l1lg b3        EVENT CATE          74      M        9EPORT DATE          sJ 7                                    60            61                000<E T '.W/3 Ea fvENT DESCRIPTION AND PROBABLE CONSEQUENCES h (T,2i l On January 7,1980 at 2115 hours Control Rod 5-11 absolute position indication (API)                                                                                                        l g j was declared inoperable due to fluctuating siFnals which caused numerous " asymmetric                                                                                                          l
y' T lL Q ]O l5 [0 l- l0 l3 l4Gl6 gl0 l1 l0 [7 l8 l0 @l0l8l0l4l8l1lg b3        EVENT CATE          74      M        9EPORT DATE          sJ 7                                    60            61                000<E T '.W/3 Ea fvENT DESCRIPTION AND PROBABLE CONSEQUENCES h (T,2i l On January 7,1980 at 2115 hours Control Rod 5-11 absolute position indication (API)                                                                                                        l g j was declared inoperable due to fluctuating siFnals which caused numerous " asymmetric                                                                                                          l
[aj:il rod" alarms. This placed the unit in the action statement of T.S. 3.1.3.3 which re-                                                                                                          l
[aj:il rod" alarms. This placed the unit in the action statement of T.S. 3.1.3.3 which re-                                                                                                          l jo;3;        [ quired the position of the control rod to be verified by actuating one of its zone lc p ;1 referenca indicators. The rod was verified at its 100% withdrawn position, and the                                                                                                          ;
                                                                                                                                                                                                          ;
g o ); l l position indication placed in asymmetric bypass. There was no danger to the public or; ia la I Lstati n Personnel. The ' control rod never deviated from its intended position.                                                                                (hr-JJ-OU-U/)            sc 7        6 g SYSTENt                CAUSE              CAUSE                                                        CO* 9P.          VA LV E CODE                  CCCE          SUBOODE                    COWonENT CODE                      SUSCCOE            SUSCODE Lt.L9J                                lI I E lh [D_j@ [z_J @ lI l Ni SITlRlUl@ [E_jh (2.jh          1J                              is          is                20 3        C                            9          IG              II                12 OCCURRENCE          REPORT                      REVISION SEQUENTI A L
jo;3;        [ quired the position of the control rod to be verified by actuating one of its zone lc p ;1 referenca indicators. The rod was verified at its 100% withdrawn position, and the                                                                                                          ;
g o ); l l position indication placed in asymmetric bypass. There was no danger to the public or;
                                                                                                                                                                                                          ;
ia la I Lstati n Personnel. The ' control rod never deviated from its intended position.                                                                                (hr-JJ-OU-U/)            sc 7        6 g SYSTENt                CAUSE              CAUSE                                                        CO* 9P.          VA LV E CODE                  CCCE          SUBOODE                    COWonENT CODE                      SUSCCOE            SUSCODE Lt.L9J                                lI I E lh [D_j@ [z_J @ lI l Ni SITlRlUl@ [E_jh (2.jh          1J                              is          is                20 3        C                            9          IG              II                12 OCCURRENCE          REPORT                      REVISION SEQUENTI A L
                                             ._ EVENT YE AR                                      REPORT NO.                              CODE              TYPE                          N O.
                                             ._ EVENT YE AR                                      REPORT NO.                              CODE              TYPE                          N O.
1                @ ,"te  gi,5  n a0 I        8I el                  1-1                1 01 01 4l                l/]            le l3 l              lX l              [-j        [LJ 22 21          22            23                24              2t;      27            23      23          30              31 ATTACHVENT        NPP D.4        PR1*.'E COvP.          CO*.9FON E N T ACTION FUTUp!                        EFFECT              SHtJTDO'?!N                                                                                            MANUFACTLeia TAKFd ACitOte                      CN PLMAT                SYLTNGO                    MOURS              SUBMITTED      FORMbu8.          SUPPLt *!'i 1                [*j@ d @ lz l(h J3            34                    Ju Wh 36                3l1 0l dl 0 l
1                @ ,"te  gi,5  n a0 I        8I el                  1-1                1 01 01 4l                l/]            le l3 l              lX l              [-j        [LJ 22 21          22            23                24              2t;      27            23      23          30              31 ATTACHVENT        NPP D.4        PR1*.'E COvP.          CO*.9FON E N T ACTION FUTUp!                        EFFECT              SHtJTDO'?!N                                                                                            MANUFACTLeia TAKFd ACitOte                      CN PLMAT                SYLTNGO                    MOURS              SUBMITTED      FORMbu8.          SUPPLt *!'i 1                [*j@ d @ lz l(h J3            34                    Ju Wh 36                3l1 0l dl 0 l
Line 38: Line 34:
48              42 lN 43 l@      l9[ll5lojg 44                47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h                                                                                                                                      A.
48              42 lN 43 l@      l9[ll5lojg 44                47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h                                                                                                                                      A.
The apparent cause has been determined to be defective API reed switch assemblies.
The apparent cause has been determined to be defective API reed switch assemblies.
   , U]0] I                                                                                                                                                                                                  I
   , U]0] I                                                                                                                                                                                                  I ml major contributing cause to ihis failure is the excessive temperatures to which the
                                                                                                                                                                                                            ;
ml major contributing cause to ihis failure is the excessive temperatures to which the
         ,,33; l            assemblies and their cables were subjocted due to a procedure deficiency
         ,,33; l            assemblies and their cables were subjocted due to a procedure deficiency
* Under FCR g gl                  79-413, a new "RC4" API system with built-in channel redundancy and high temperature l t
* Under FCR g gl                  79-413, a new "RC4" API system with built-in channel redundancy and high temperature l t

Latest revision as of 11:22, 17 February 2020

LER 80-004/03X-1:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals,Causing Numerous Asymmetric Rod Alarms.Apparently Caused by Defective Reed Switch Assemblies
ML20010B503
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 08/04/1981
From: Werner J
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17275B377 List:
References
LER-80-004-03X, LER-80-4-3X, NUDOCS 8108170115
Download: ML20010B503 (2)


Text

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  • 41",7 7)

> LICENSEE EVENT REPORT CO'4THOL PLOCK: l 1

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(PLEASE PRINT oR TYPE alt REQUIRED INFORMATtoN) o i l Ol 11l Dl Bl Sl 1l@l0 l0 l- l0 l0 lN lP lFl-l0l3[gl4l1l1l1l1l@l 23 ;6 LsCLNsE TYPE JO l

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CC*i* T lojil 8

y' T lL Q ]O l5 [0 l- l0 l3 l4Gl6 gl0 l1 l0 [7 l8 l0 @l0l8l0l4l8l1lg b3 EVENT CATE 74 M 9EPORT DATE sJ 7 60 61 000<E T '.W/3 Ea fvENT DESCRIPTION AND PROBABLE CONSEQUENCES h (T,2i l On January 7,1980 at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br /> Control Rod 5-11 absolute position indication (API) l g j was declared inoperable due to fluctuating siFnals which caused numerous " asymmetric l

[aj:il rod" alarms. This placed the unit in the action statement of T.S. 3.1.3.3 which re- l jo;3; [ quired the position of the control rod to be verified by actuating one of its zone lc p ;1 referenca indicators. The rod was verified at its 100% withdrawn position, and the  ;

g o ); l l position indication placed in asymmetric bypass. There was no danger to the public or; ia la I Lstati n Personnel. The ' control rod never deviated from its intended position. (hr-JJ-OU-U/) sc 7 6 g SYSTENt CAUSE CAUSE CO* 9P. VA LV E CODE CCCE SUBOODE COWonENT CODE SUSCCOE SUSCODE Lt.L9J lI I E lh [D_j@ [z_J @ lI l Ni SITlRlUl@ [E_jh (2.jh 1J is is 20 3 C 9 IG II 12 OCCURRENCE REPORT REVISION SEQUENTI A L

._ EVENT YE AR REPORT NO. CODE TYPE N O.

1 @ ,"te gi,5 n a0 I 8I el 1-1 1 01 01 4l l/] le l3 l lX l [-j [LJ 22 21 22 23 24 2t; 27 23 23 30 31 ATTACHVENT NPP D.4 PR1*.'E COvP. CO*.9FON E N T ACTION FUTUp! EFFECT SHtJTDO'?!N MANUFACTLeia TAKFd ACitOte CN PLMAT SYLTNGO MOURS SUBMITTED FORMbu8. SUPPLt *!'i 1 [*j@ d @ lz l(h J3 34 Ju Wh 36 3l1 0l dl 0 l

_40 W@ lYl@

48 42 lN 43 l@ l9[ll5lojg 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h A.

The apparent cause has been determined to be defective API reed switch assemblies.

, U]0] I I ml major contributing cause to ihis failure is the excessive temperatures to which the

,,33; l assemblies and their cables were subjocted due to a procedure deficiency

  • Under FCR g gl 79-413, a new "RC4" API system with built-in channel redundancy and high temperature l t

i yl API cables was installed. 80 l

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PDR ADOCK 05000346 419-259-5000, Ext. 231 ,

. John Werner inON E: $

.DVR E S PDR l- A

TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEME'NTAL INFORMATION FOR LER NP-33-80-07 DATE OF EVENT: January 7, 1980 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Control Rod 5-11 Absolute Position Indication (API) fluctuations Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 637, and Load (Gross MRE) = 212.

Description of Occurrence: On January 7,1980, at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br /> Control Rod 5-11 API was declared inoperable due to fluctuating signals which caused numerous " asymmetric rod" alarms. All API channels are required to be operable and capable of determining control rod position within + 6.5% in Modes 1 and 2. This placed the unit in the action statement of Technical Specification 3.1.3.3 which required the position of the control rod to be verified by actuating one of its zone reference indicators. The rod position was verified at its 100% withdrawn position, and the rod position indication '

was placed in asymmetric bypass.

Designation of Apparent Cause of Occurrence: After several months of collecting data on Contro. Rod 5-11, the apparent cause has been determined to be defective API reed switch assemblies. A major contributing cause to this failure is the excessive tempera-tures to which the assemblies and their cables were subjected. This occured during 1 several months of operation in which the head assembly cooling fans were not in operation due to a deficient procedure which allowed restsrt following the 1978 outage without reconnecting the cooling fan power cables. The Reactor Vessel Closure Head Removal and Replacement Procedure, SP 1504.01, was corrected.

Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The control rod never deviated from its intended position, only the API was faulty.

Corrective Action: During the last shutdown in December, 1979, and with vendor assistance, a test connection under Facility Change Request 79-424 was placed be-I l tween the position indication (PI) assembly and its associated cabling to monitor the various voltages at that point. This was done as a corrective action to the same type of occurrence reported under Licensee Event Report NP-33-79-141.

Under Facility Change Request 79-413 a new "R4C" API system was installed. This 1 system features built-in channel redundancy and high temperature API cables.

Failure Data: There have been previous failures of control rod API's. Control Rod 5-ll's current symptoms were previously reported in Licensee Event Eeport NP-33-79-141.

l l

l LER 180-004

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