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{{#Wiki_filter:. .(7 77)LICENSEE EVENT REPORT
{{#Wiki_filter:. .
'*CONTROL BLOCK:
(7 77)
lllll(PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 0 l t l l 0 l H l D l B l S l 1 l@l 0 0 l-l 0 l0 lN lP lF l-0 3 l@l4 l1 l1 l1 l1 l@l ll@7 8 9 LICENSs ? CODE 14 lb LICENSE NUMBER 2b 26 LICENSE TYPE JO 57 CAT 68 CON'T"$RCl l L lgl 0 5l0l-l4l3l 4l 6 @l 1 l 1 0 l 9 l 7 l 9 l@
LICENSEE EVENT REPORT
l l 1 l 2 l 1 l 7 l 9 @
* CONTROL BLOCK:                                                                 (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) l l    l    l  l l7 0 l t8 l 9l 0 l H l D l B l S l 114l@llb0                  0 l-l 0 l0       lN lP lF l-LICENSE NUMBER 0     32bl@l4 26 l1LICENSE l1 l1TYPE l1JOl@l57 CAT  l 68 l@
" 0 1 S 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l On 11/9/79 at 1400 hours during the review of NRC I6E Bulletin 79-21 response, it was (lis-o 2'covered that our steam generator low level trip setpoints to Steam and Feedwater Rup- l o 3[ure Control System Channels 1 and 2 were less conservative than the limits of T.S.
LICENSs ? CODE CON'T 0 1 8
o 3.3.2.2.This finding is being reported in accordance with T.S. 6.9.1.8.h.
                    "$RCl S
A Mode 3 l o sl restraint was placed on the unit until new values were determined and adjustments lo el made.A safety analysis is being made and will be forwarded as a revision.
l L lgl 0 5l0l-l4l3l 4l 6 @l 169 l 1EVENT      68 0 l 9 l 7 l 9 l@ l l 1REPORT DATE          74        75 l 2 l 1 l 7 l 980 @
l0 7l(NP-32-79-12) lo a 80 7 8 9 DE CODE SB E COMPONENT CODE SUSCOdE SU DE N S Tl R Ul@ g@ g @
DATE 7                             60             61         DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2      l On 11/9/79 at 1400 hours during the review of NRC I6E Bulletin 79-21 response, it was (lis-o 3          covered that our steam generator low level trip setpoints to Steam and Feedwater Rup- l o   [         ure Control System Channels 1 and 2 were less conservative than the limits of T.S.
l C l H l@ y@ l A l@ lI o 9 7 8 9 to 11 12 13 18 19 20 ,_SEQUENTIAL OCCURRENCE REPORT REVISION LE R/RO EVENT YE AR REPORT NO.
o   s        3.3.2.2.               This finding is being reported in accordance with T.S. 6.9.1.8.h.                                                     A Mode 3 l o e        l restraint was placed on the unit until new values were determined and adjustments                                                                         l 0  7    l made.         A safety analysis is being made and will be forwarded as a revision.                                                                         l o  a      l(NP-32-79-12)                                                                                                                                             l 80 7       8 9 DE         CODE       SB       E             COMPONENT CODE                   SUSCOdE           SU     DE o 9                            l C l H l@ y@ l A l@ lI                               N      S    Tl R Ul@ g@ g @
CODE TYPE N O.b Rjll9 ll1l5lyl0l1lgl_l0ln E 21 22 23 24 26 27 28 29 30 31 32 AKEN A O ON PL NT MT HOURS 22 SB IT D FOR b B.SUPPLIE MANUFACTURER IF{g{bgl Zlg 0 l1 0 lT] glNl@dhlC 16 l5 10 l@
18          19              20 7       8                         9         to       11           12           13
33 34 3 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lil0llThe cause of the occurrence was an error in the analysis used in determining the i i steam. generator low level bistable setpoints.
                                ,_                                      SEQUENTIAL                        OCCURRENCE           REPORT                   REVISION LE R/RO       EVENT YE AR                         REPORT NO.                             CODE               TYPE                         N O.
The analysis failed to take into 3 7l account the actual pressures and temperatures as seet by the steam generator during ll operation. On 11/17/79, the adjustments were made and ST 5031.14 was successfully l3 3li i4 l l performed. The restraint was lifted.
b Rj n      E l    l9 l 23 l1 24 l5l26 y
7 8 9 80 A S% POWER OTHE't STATUS ISCO RY DISCOVERY DESCRIPTION 79-21l115l W h 10 l0 0 lhl NAllD l@lNRCInspectionReport ACTIVITY CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE
27 l0l1l 28       29 g30 l_
[Z} h (Z j g l NA llNA 1 6 7 8 9 , 10 _11 44 45 80 PERSONNEL EXPOSURES l0@ l 0 lhl Z lhl DESCRIPTION lNUMBER TYPE NA 1 7'' 'PE RSONNE L INJURtES NUM DESCRIPTION 10 I EERl0l@l NAli a 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DE SCRIPTION NA j zOp') J 7 (Zjgl1 9 7 8 9 _10 80[N_jhl NA el 911 '2 7 0 y lllllil;illj ISSUE DESCRIPTION 2 O 7 8 9 10 68 69 80 5 419-259-5000, Ext. 235 Dan Trautman o-" VR 79-163 NAME OF PREPARER PHONE:  
31 l0l 32 21        22 AKEN A       O             ON PL NT       MT                     HOURS 22           SB IT D         FOR b     B.     SUPPLIE           MANUFACTURER IF 33
~.., TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-79-12 DATE OF EVENT:
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November 9, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
{bg l Zlg 3              36            37 0 l1 0 lT 40
Steam Generator low level trip setpoints found to- [he less conservative than assumed.
                                                                                                        ] g 41 lNl@
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lil0llThe cause of the occurrence was an error in the analysis used in determining the i i         steam. generator low level bistable setpoints.                                         The analysis failed to take into 3 7      l account the actual pressures and temperatures as seet by the steam generator during                                                                         l 3 3      l operation. On 11/17/79, the adjustments were made and ST 5031.14 was successfully                                                                         l li i4 l l performed. The restraint was lifted.
7       8 9                                                                                                                                                             80 A S             % POWER                     OTHE't STATUS               ISCO RY                             DISCOVERY DESCRIPTION l115l W h 10 l0 0 lhl NA                                                          l    lD l@lNRCInspectionReport 79-21 ACTIVITY CO TENT RELE ASED OF RELE ASE                     AMOUNT OF ACTIVITY                                                     LOCATION OF RELEASE 1 6 8
[Z} h (Z j g l NA 9 ,
l            lNA 7                          10 _          11                                    44             45                                                                     80 PERSONNEL EXPOSURES NUMBER                TYPE 1 7      l0 @ l 0 lhl Z lhl DESCRIPTION           NA                                                                                                                   l PE RSONNE L INJURtES NUM                   DESCRIPTION NA 7
i a 8 9 10 I EERl0l@l   11         12 l
80 LOSS OF OR DAMAGE TO FACILITY TYPE       DE SCRIPTION 1 9      (Zjgl          NA                                                                                                               j zOp       ') J 7 7       8 9 _          10                                                                                                                                              80 ISSUE      DESCRIPTION 2 O      [N_jhl NA                                                                             el 911 '2 7 0 y                             ll      lllil;i        llj 7       8 9             10                                                                                                               68 69                           80 5 Dan Trautman              -                                          419-259-5000, Ext. 235               o VR 79-163               NAME OF PREPARER                                                                                 PHONE:
 
      ~
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-79-12 DATE OF EVENT:     November 9, 1979 FACILITY:   Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:     Steam Generator low level trip setpoints found to
  - [he less conservative than assumed.
Conditions Prior to Occurrence: The unit was in Mode 5, with Power (MWT) = 0, and Load (Gross MWE) = 0.
Conditions Prior to Occurrence: The unit was in Mode 5, with Power (MWT) = 0, and Load (Gross MWE) = 0.
Description of Occurrence: On November 9, 1979 at 1400 hours, during the review of NRC I&E Bulletin 79-21 response, it was discovered that our steam generator low level trip setpoints to Stcam and Feedwater Rupture Control System (SFRCS)
Description of Occurrence: On November 9, 1979 at 1400 hours, during the review of NRC I&E Bulletin 79-21 response, it was discovered that our steam generator low level trip setpoints to Stcam and Feedwater Rupture Control System (SFRCS)
Channels 1 and 2 were less conservative than the limits of Technical Specification 3.3.2.2.The steam generator low level bistable trip setpoint was 23 inches + 2 inches.However, the re-evaluation of the method used to determine the setpoints based on actual versus indicated level found that the actual level would be~less conservative than the minimum 20 inches of water above C u Jower tube sheet as required by Technical Specifications.
Channels 1 and 2 were less conservative than the limits of Technical Specification 3.3.2.2. The steam generator low level bistable trip setpoint was 23 inches + 2 inches. However, the re-evaluation of the method used to determine the setpoints based on actual versus indicated level found that the actual level would be~less conservative than the minimum 20 inches of water above C u Jower tube sheet as required by Technical Specifications.
As a result, a Made 3 restraint was placed on the unit until new values could be determined and adjustments to the bistable trip setpoint made.
As a result, a Made 3 restraint was placed on the unit until new values could be determined and adjustments to the bistable trip setpoint made. This occurrence is being reported in accordance with Technical Specification 6.9.1.8.h which re-quires prompt notification with a followup report within two weeks for an error in analysis, which would have permitted reactor operation in a manner less conser-vative than assumed.
This occurrence is being reported in accordance with Technical Specification 6.9.1.8.h which re-quires prompt notification with a followup report within two weeks for an error in analysis, which would have permitted reactor operation in a manner less conser-vative than assumed.
Designation of Apparent Cause of Occurrence:     The apparent cause of the occurrence was found to be an error in the analysis used in determining the steam generator low level bistable setpoints.     The analysis failed to take into account the actual pressures and temperatures as seen by the steam generator during 7eration and in transients.
Designation of Apparent Cause of Occurrence:
The apparent cause of the occurrence was found to be an error in the analysis used in determining the steam generator low level bistable setpoints.
The analysis failed to take into account the actual pressures and temperatures as seen by the steam generator during 7eration and in transients.
Analysis of Occurrence: A safety analysis is being performed and will be forwarded as a revision.
Analysis of Occurrence: A safety analysis is being performed and will be forwarded as a revision.
Corrective Action:
Corrective Action: On November 17, 1979, new steam generator low level bistable trip setpoints were established and adjustments were made. All four channels were proven operable by performance of ST 5031.14, "SFRCS Monthly Surveillance Test". The mode restraint relating this event was removed as of 1755 hours on November 19, 1979.
On November 17, 1979, new steam generator low level bistable trip setpoints were established and adjustments were made. All four channels were proven operable by performance of ST 5031.14, "SFRCS Monthly Surveillance Test".
Failure Data:     There have been no previous similar occurrences.
The mode restraint relating this event was removed as of 1755 hours on November 19, 1979.
Failure Data:
There have been no previous similar occurrences.
LER #79-105 1398 278}}
LER #79-105 1398 278}}

Latest revision as of 05:15, 2 February 2020

LER 79-105/01T-0:on 791109,steam Generator Low Level Trip Setpoints to Steam & Feedwater Rupture Control Sys Channels 1 & 2 Found Less Conservative than Tech Specs.Caused by Error in Analysis to Determine Low Level Bistable Setpoints
ML19210D641
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 11/21/1979
From: Trautman D
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19210D631 List:
References
LER-79-105-01T, LER-79-105-1T, NUDOCS 7911270418
Download: ML19210D641 (2)


Text

. .

(7 77)

LICENSEE EVENT REPORT

  • CONTROL BLOCK: (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) l l l l l l7 0 l t8 l 9l 0 l H l D l B l S l 114l@llb0 0 l-l 0 l0 lN lP lF l-LICENSE NUMBER 0 32bl@l4 26 l1LICENSE l1 l1TYPE l1JOl@l57 CAT l 68 l@

LICENSs ? CODE CON'T 0 1 8

"$RCl S

l L lgl 0 5l0l-l4l3l 4l 6 @l 169 l 1EVENT 68 0 l 9 l 7 l 9 l@ l l 1REPORT DATE 74 75 l 2 l 1 l 7 l 980 @

DATE 7 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l On 11/9/79 at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> during the review of NRC I6E Bulletin 79-21 response, it was (lis-o 3 covered that our steam generator low level trip setpoints to Steam and Feedwater Rup- l o [ ure Control System Channels 1 and 2 were less conservative than the limits of T.S.

o s 3.3.2.2. This finding is being reported in accordance with T.S. 6.9.1.8.h. A Mode 3 l o e l restraint was placed on the unit until new values were determined and adjustments l 0 7 l made. A safety analysis is being made and will be forwarded as a revision. l o a l(NP-32-79-12) l 80 7 8 9 DE CODE SB E COMPONENT CODE SUSCOdE SU DE o 9 l C l H l@ y@ l A l@ lI N S Tl R Ul@ g@ g @

18 19 20 7 8 9 to 11 12 13

,_ SEQUENTIAL OCCURRENCE REPORT REVISION LE R/RO EVENT YE AR REPORT NO. CODE TYPE N O.

b Rj n E l l9 l 23 l1 24 l5l26 y

27 l0l1l 28 29 g30 l_

31 l0l 32 21 22 AKEN A O ON PL NT MT HOURS 22 SB IT D FOR b B. SUPPLIE MANUFACTURER IF 33

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{bg l Zlg 3 36 37 0 l1 0 lT 40

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42 dh 43 lC 44 16 l5 1047l@

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lil0llThe cause of the occurrence was an error in the analysis used in determining the i i steam. generator low level bistable setpoints. The analysis failed to take into 3 7 l account the actual pressures and temperatures as seet by the steam generator during l 3 3 l operation. On 11/17/79, the adjustments were made and ST 5031.14 was successfully l li i4 l l performed. The restraint was lifted.

7 8 9 80 A S  % POWER OTHE't STATUS ISCO RY DISCOVERY DESCRIPTION l115l W h 10 l0 0 lhl NA l lD l@lNRCInspectionReport 79-21 ACTIVITY CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 1 6 8

[Z} h (Z j g l NA 9 ,

l lNA 7 10 _ 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE 1 7 l0 @ l 0 lhl Z lhl DESCRIPTION NA l PE RSONNE L INJURtES NUM DESCRIPTION NA 7

i a 8 9 10 I EERl0l@l 11 12 l

80 LOSS OF OR DAMAGE TO FACILITY TYPE DE SCRIPTION 1 9 (Zjgl NA j zOp ') J 7 7 8 9 _ 10 80 ISSUE DESCRIPTION 2 O [N_jhl NA el 911 '2 7 0 y ll lllil;i llj 7 8 9 10 68 69 80 5 Dan Trautman - 419-259-5000, Ext. 235 o VR 79-163 NAME OF PREPARER PHONE:

~

TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-79-12 DATE OF EVENT: November 9, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Steam Generator low level trip setpoints found to

- [he less conservative than assumed.

Conditions Prior to Occurrence: The unit was in Mode 5, with Power (MWT) = 0, and Load (Gross MWE) = 0.

Description of Occurrence: On November 9, 1979 at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />, during the review of NRC I&E Bulletin 79-21 response, it was discovered that our steam generator low level trip setpoints to Stcam and Feedwater Rupture Control System (SFRCS)

Channels 1 and 2 were less conservative than the limits of Technical Specification 3.3.2.2. The steam generator low level bistable trip setpoint was 23 inches + 2 inches. However, the re-evaluation of the method used to determine the setpoints based on actual versus indicated level found that the actual level would be~less conservative than the minimum 20 inches of water above C u Jower tube sheet as required by Technical Specifications.

As a result, a Made 3 restraint was placed on the unit until new values could be determined and adjustments to the bistable trip setpoint made. This occurrence is being reported in accordance with Technical Specification 6.9.1.8.h which re-quires prompt notification with a followup report within two weeks for an error in analysis, which would have permitted reactor operation in a manner less conser-vative than assumed.

Designation of Apparent Cause of Occurrence: The apparent cause of the occurrence was found to be an error in the analysis used in determining the steam generator low level bistable setpoints. The analysis failed to take into account the actual pressures and temperatures as seen by the steam generator during 7eration and in transients.

Analysis of Occurrence: A safety analysis is being performed and will be forwarded as a revision.

Corrective Action: On November 17, 1979, new steam generator low level bistable trip setpoints were established and adjustments were made. All four channels were proven operable by performance of ST 5031.14, "SFRCS Monthly Surveillance Test". The mode restraint relating this event was removed as of 1755 hours0.0203 days <br />0.488 hours <br />0.0029 weeks <br />6.677775e-4 months <br /> on November 19, 1979.

Failure Data: There have been no previous similar occurrences.

LER #79-105 1398 278