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See also: [[see also:Press Release-I-14-039]]


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{{#Wiki_filter:No: I-14-039 October 21, 2014 CONTACT: Diane Screnci, 610-337-5330                       Neil Sheehan
{{#Wiki_filter:No: I-14-039                                                                         October 21, 2014
, 610-337-5331     NRC Issues 'White' Inspection Finding for Millstone 3 Nuclear Plant; Level of Oversight to be Increased The Nuclear Regulatory Commission will increase its level of oversight at the Millstone Unit 3 nuclear power plant following the finalization of a "white" (low to moderate safety significance) inspection finding for the Waterford, Conn., facility. The finding, which involves a violation of NRC requirements, is based on the plant owner's failure to promptly identify and correct repetitive problems involving a pump that is part of a reactor safety system.
CONTACT: Diane Screnci, 610-337-5330
Specifically, NRC inspectors determined that from May 2013 through February 2014, Millstone Unit 3's turbine
              Neil Sheehan, 610-337-5331
-driven auxiliary feedwater pump was operated improperly due to the installation of an incorrect bearing. This manifested itself in two cases of oscillations, or unexpected fluctuations, in reactor coolant flow from the pump and three trips, or shutdowns, of the pump because of overspeeding.
          NRC Issues White Inspection Finding for Millstone 3 Nuclear Plant;
The auxiliary, or back
                                Level of Oversight to be Increased
-up, feedwater system is one of several that can be used to help cool down the reactor following a shutdown by pumping water into the secondary side of the plant's steam generators. The steam generators are essentially large heat exchangers that convert heat produced by the reactor into steam, which in turn is used to spin the plant's turbine and generate electricity.
      The Nuclear Regulatory Commission will increase its level of oversight at the Millstone Unit 3
Although Dominion Nuclear Connecticut Inc., the plant's owner and operator, has taken action to repair the pump and has completed a root
nuclear power plant following the finalization of a white (low to moderate safety significance)
-cause evaluation, the NRC is taking enforcement action because of the length of time it took for the issue to be addressed.
inspection finding for the Waterford, Conn., facility. The finding, which involves a violation of NRC
"Our inspectors have carefully documented multiple problems involving this pump that occurred over the course of many months," Acting NRC Region I Administrator David Lew said. "What concerns the NRC is that despite repeated efforts to repair this important component, the problems persisted and called into the question the pump's past reliability."
requirements, is based on the plant owners failure to promptly identify and correct repetitive problems
Under the NRC's Reactor Oversight Process, inspection findings are classified by color based on their safety significance. The colors range from "green," for a very low safety issue, to "white,"
involving a pump that is part of a reactor safety system.
"yellow" or "red," which connotes high safety significance. Because this finding has been finalized as "white," Millstone Unit 3 will move from the Licensee Response Column of the NRC's Action Matrix to the Regulatory Response Column and be subject to additional inspections by the agency.
      Specifically, NRC inspectors determined that from May 2013 through February 2014, Millstone
Unit 3s turbine-driven auxiliary feedwater pump was operated improperly due to the installation of an
incorrect bearing. This manifested itself in two cases of oscillations, or unexpected fluctuations, in
reactor coolant flow from the pump and three trips, or shutdowns, of the pump because of
overspeeding.
      The auxiliary, or back-up, feedwater system is one of several that can be used to help cool down
the reactor following a shutdown by pumping water into the secondary side of the plants steam
generators. The steam generators are essentially large heat exchangers that convert heat produced by
the reactor into steam, which in turn is used to spin the plants turbine and generate electricity.
      Although Dominion Nuclear Connecticut Inc., the plants owner and operator, has taken action to
repair the pump and has completed a root-cause evaluation, the NRC is taking enforcement action
because of the length of time it took for the issue to be addressed.
      Our inspectors have carefully documented multiple problems involving this pump that occurred
over the course of many months, Acting NRC Region I Administrator David Lew said. What
concerns the NRC is that despite repeated efforts to repair this important component, the problems
persisted and called into the question the pumps past reliability.
      Under the NRCs Reactor Oversight Process, inspection findings are classified by color based on
their safety significance. The colors range from green, for a very low safety issue, to white,
yellow or red, which connotes high safety significance. Because this finding has been finalized as
white, Millstone Unit 3 will move from the Licensee Response Column of the NRCs Action Matrix
to the Regulatory Response Column and be subject to additional inspections by the agency.


Page l 2 The NRC conducted a Special Inspection at Millstone Unit 3 in February and May in response to the problems involving the auxiliary feedwater pump. Among the areas that were reviewed during the inspection were Dominion's responses to the issues, including the adequacy and completeness of testing on the pump and a root
      The NRC conducted a Special Inspection at Millstone Unit 3 in February and May in response to
-cause evaluation of the problems.
the problems involving the auxiliary feedwater pump. Among the areas that were reviewed during the
On Sept. 15, 2014, the NRC initiated an additional Special Inspection at Millstone Unit 3 in response to further unrelated problems with the pump. This action occurred after the pump failed quarterly surveillance tests in July and September. That Special Inspection is still in progress, and the results will be detailed in an inspection report to be issued within 45 days of its completion.}}
inspection were Dominions responses to the issues, including the adequacy and completeness of
testing on the pump and a root-cause evaluation of the problems.
      On Sept. 15, 2014, the NRC initiated an additional Special Inspection at Millstone Unit 3 in
response to further unrelated problems with the pump. This action occurred after the pump failed
quarterly surveillance tests in July and September. That Special Inspection is still in progress, and the
results will be detailed in an inspection report to be issued within 45 days of its completion.
                                                  Page l 2
}}

Latest revision as of 03:47, 5 December 2019

Press Release-I-14-039: NRC Issues 'White' Inspection Finding for Millstone 3 Nuclear Plant; Level of Oversight to Be Increased
ML14294A590
Person / Time
Site: Millstone Dominion icon.png
Issue date: 10/21/2014
From:
Office of Public Affairs Region I
To:
References
Press Release-I-14-039
Download: ML14294A590 (2)


See also: see also:Press Release-I-14-039

Text

No: I-14-039 October 21, 2014

CONTACT: Diane Screnci, 610-337-5330

Neil Sheehan, 610-337-5331

NRC Issues White Inspection Finding for Millstone 3 Nuclear Plant;

Level of Oversight to be Increased

The Nuclear Regulatory Commission will increase its level of oversight at the Millstone Unit 3

nuclear power plant following the finalization of a white (low to moderate safety significance)

inspection finding for the Waterford, Conn., facility. The finding, which involves a violation of NRC

requirements, is based on the plant owners failure to promptly identify and correct repetitive problems

involving a pump that is part of a reactor safety system.

Specifically, NRC inspectors determined that from May 2013 through February 2014, Millstone

Unit 3s turbine-driven auxiliary feedwater pump was operated improperly due to the installation of an

incorrect bearing. This manifested itself in two cases of oscillations, or unexpected fluctuations, in

reactor coolant flow from the pump and three trips, or shutdowns, of the pump because of

overspeeding.

The auxiliary, or back-up, feedwater system is one of several that can be used to help cool down

the reactor following a shutdown by pumping water into the secondary side of the plants steam

generators. The steam generators are essentially large heat exchangers that convert heat produced by

the reactor into steam, which in turn is used to spin the plants turbine and generate electricity.

Although Dominion Nuclear Connecticut Inc., the plants owner and operator, has taken action to

repair the pump and has completed a root-cause evaluation, the NRC is taking enforcement action

because of the length of time it took for the issue to be addressed.

Our inspectors have carefully documented multiple problems involving this pump that occurred

over the course of many months, Acting NRC Region I Administrator David Lew said. What

concerns the NRC is that despite repeated efforts to repair this important component, the problems

persisted and called into the question the pumps past reliability.

Under the NRCs Reactor Oversight Process, inspection findings are classified by color based on

their safety significance. The colors range from green, for a very low safety issue, to white,

yellow or red, which connotes high safety significance. Because this finding has been finalized as

white, Millstone Unit 3 will move from the Licensee Response Column of the NRCs Action Matrix

to the Regulatory Response Column and be subject to additional inspections by the agency.

The NRC conducted a Special Inspection at Millstone Unit 3 in February and May in response to

the problems involving the auxiliary feedwater pump. Among the areas that were reviewed during the

inspection were Dominions responses to the issues, including the adequacy and completeness of

testing on the pump and a root-cause evaluation of the problems.

On Sept. 15, 2014, the NRC initiated an additional Special Inspection at Millstone Unit 3 in

response to further unrelated problems with the pump. This action occurred after the pump failed

quarterly surveillance tests in July and September. That Special Inspection is still in progress, and the

results will be detailed in an inspection report to be issued within 45 days of its completion.

Page l 2