ML061160469: Difference between revisions
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{{#Wiki_filter:viIauz1-11 -I.- ru2 flAJII I'1I MI vpudIu ivl | {{#Wiki_filter:viIauz1-11 -I.- ru2 flAJII I'1I MI vpudIu ivl WauI~ rayq Lfla ,IjuicuitrvisaII ~ uaLPP 100OU~r roqu II From: Brian McDermott To: Adam Stiebeling; Alela Salame-Alfie; Barbara Youngberg; C.J. Miller; Daniel Greeley; dleach@3ntergy.com; Dominick Greene; Geri Shapiro; Jack Spath; James Baranski; Paul Eddy; Peter Feroe; Robert Bondi; Steve Gross; Tony Sutton Date: Wed, Nov 30, 2005 11:46 AM | ||
==Subject:== | ==Subject:== | ||
FYI: Forthcoming Update to NRC Web Page on Indian Point Spent Fuel Pool Issues Attached for your information is a status update on the Indian Point 2 Spent Fuel Pool investigation that will be posted to the NRC's Web Page in the next day or so. | FYI: Forthcoming Update to NRC Web Page on Indian Point Spent Fuel Pool Issues Attached for your information is a status update on the Indian Point 2 Spent Fuel Pool investigation that will be posted to the NRC's Web Page in the next day or so. Ifyou have any questions, please feel free to give me a call or raise your questions during our next conference call - tomorrow, Thursday 1211 at 3:30 p.m. | ||
-Region I 475 Allendale Road King of Prussia, PA | The existing NRC Web Page on the Indian Point 2 Spent Fuel Pool and tritium contamination can be found at: | ||
http://wwN.nrc.pov/reactors/Plant-soecific-itemslindian-ooint-issues.html Regards, Brian Brian J. McDermott, Chief, Projects Branch 2 U.S. Nuclear Regulatory Commission - Region I 475 Allendale Road King of Prussia, PA 19406 ork: 610-337-5233 Cell _: | |||
.vte3IIlJU.2VV j~sjuuv i a uvar raye Mail Envelope Properties (438DD75F.20F: | &M* | ||
12: 55450)Subjecit: | ax: E 0-337-5349 bjm nrc.gov CC: John Boska; John White; Raeann Shane Information inthis record was deleted inaccordance withthe Freedom of lnmnation Act exemptons _ | ||
FYI: Forthcoming Update to NRC Web Page on Indian Point Spent Fuel Pool Issues Creation Date: Wed, Nov 30,2005 11:46 AM From: Brian McDermott Created By: BJM@nrc.gov Recipients Action Date & Time aol.com Transferred 11/30 11:46 AM GeriShapiro (Geri Shapiro)bestweb.net Transferred 11/30 11:47 AM Abs]?cbes (Adam Stiebeling) co.orange.ny.us Transferred 11/30 11:47 AM dgreene (Dominick Greene)SGross (Steve Gross)co.rockland.ny.us Transferred 11/30 11:47 AM greeleyd (Daniel Greeley)mill -rc (C.J. Miller)dps.stal:e.ny.us Transferred 11/30 11:47AM pde (Paul Eddy)entergy.com Transferred 11/30 11:47 AM dleach (dleach@entergy.com) gw.dec.state.ny.us Transferred 11/30 11:47AM bayoungb (Barbara Youngberg) health. ;tate.ny.us Transferred 11/30 11:47 AM asa0l. (Alela Salame-Alfie) mail.house.gov Transferred 11/30 11:47 AM Petcr.Feroe (Peter Feroe)nrc.gov TWGWPO02.HQGWDO01 Delivered 11/30 11:46 AM RMS2 CC (Raeann Shane) Opened 11/30 11:59 AM nrc. | FDIA. =L-M | ||
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Priority: Reply Requested: | .vte3IIlJU.2VV j~sjuuv i a uvar raye Mail Envelope Properties (438DD75F.20F: 12: 55450) | ||
Return Notification: | Subjecit: FYI: Forthcoming Update to NRC Web Page on Indian Point Spent Fuel Pool Issues Creation Date: Wed, Nov 30,2005 11:46 AM From: Brian McDermott Created By: BJM@nrc.gov Recipients Action Date & Time aol.com Transferred 11/30 11:46 AM GeriShapiro (Geri Shapiro) bestweb.net Transferred 11/30 11:47 AM Abs]?cbes (Adam Stiebeling) co.orange.ny.us Transferred 11/30 11:47 AM dgreene (Dominick Greene) | ||
Concealed | SGross (Steve Gross) co.rockland.ny.us Transferred 11/30 11:47 AM greeleyd (Daniel Greeley) mill -rc (C.J. Miller) dps.stal:e.ny.us Transferred 11/30 11:47AM pde (Paul Eddy) entergy.com Transferred 11/30 11:47 AM dleach (dleach@entergy.com) gw.dec.state.ny.us Transferred 11/30 11:47AM bayoungb (Barbara Youngberg) health. ;tate.ny.us Transferred 11/30 11:47 AM asa0l. (Alela Salame-Alfie) mail.house.gov Transferred 11/30 11:47 AM Petcr.Feroe (Peter Feroe) nrc.gov TWGWPO02.HQGWDO01 Delivered 11/30 11:46 AM RMS2 CC (Raeann Shane) Opened 11/30 11:59 AM nrc.gov kplpo.KPDO Delivered 11/30 11:46 AM | ||
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- --- ---- U raye e-JRi'l1 CC (John White) Opened 11/30 12:47 PM nrc.gov owf4_.po.OWFN_DO Delivered 11/30 11:46 AM JPB1 CC (John Boska) Opened 12/06 7:19 AM nyserda.org Transferred 11/30 11:47 AM jps (Jack Spath) | |||
PutnamrCountyNY.com Transferred 11/30 11:47 AM Robrt.Bondi (Robert Bondi) semo.sltate.ny.us Transferred 11/30 11:47 AM james.baranski (James Baranski) westchestergov .com Transferred 11/30 11:47 AM aws I (Tony Sutton) | |||
Post Office Delivered Route aol.com bestweb.net co.orange.ny.us co.rockland.ny.us dps.state.ny.us entergy.com gw.dec.state.ny.u; health.state.ny.us mail.house.gov TWGWPO02.HQGWDO01 11/30 11:46 AM nrc.gov kpl.pD.KPLDO 11/30 11:46 AM nrc.gov owf4,_po.OWFN_DO 11/30 11:46 AM. nrc.gov nyserda.org PutnamCountyNY.com semo.state.ny.us westchestergov.com Files SiU 5e Date & Time MESSAGE 20A Wednesday, November 30, 2005 11:46 AM NRC VebPageUpdatel 1-30-05.pdf 15798 Wednesday, Noverr.ber 30, 2005 11:44 AM Options Auto ]Delete: No | |||
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Expiration Date: None Notify Recipients: No Priority: High Reply Requested: No Return Notification: None Concealed | |||
==Subject:== | ==Subject:== | ||
Security: | No Security: Standard To Be Delivered: Immediate Status Tracking: All Information | ||
Status Tracking: | |||
Stored spent fuel in portions of the pool prevent full examination with currently available video equipment. | On-going Activities; 11/29/2005 Unit 2 spent Fuel Pool: Entergy has completed visual examination and video taping of about 50% of the spent fuel pool liner surface in an effort to identify locations of potential leakage. | ||
Accordingly, Entergy has informed the NRC that it is investigating the use of other video equipment to affect more complete examination of the pool liner. Divers physically examined three locations of interest with a vacuum box to determine if leakage wEas present., however, in each case, leakage was not positively detected. | This represents all the surfaces that can be accessed with the currently available video camera equipment. Stored spent fuel in portions of the pool prevent full examination with currently available video equipment. Accordingly, Entergy has informed the NRC that it is investigating the use of other video equipment to affect more complete examination of the pool liner. Divers physically examined three locations of interest with a vacuum box to determine if leakage wEas present., however, in each case, leakage was not positively detected. Notwithstanding, Entergy is examining methods to apply an underwater coating to these locations to assure these areas of interest remain leak-tight. | ||
Notwithstanding, Entergy is examining methods to apply an underwater coating to these locations to assure these areas of interest remain leak-tight. | The leak rate from the previously identified cracks in the spent fuel pool concrete wall is current y about 10 to 25 milliliters per day. Previously, leakage was measured to be about 1)300 to 150C milliliters per day. Entergy is investigating the cause of the decreased leak rate. | ||
The leak rate from the previously identified cracks in the spent fuel pool concrete wall is current y about 10 to 25 milliliters per day. Previously, leakage was measured to be about 1)300 to | Monitoring Wells: Entergy has completed drilling of one of nine wells currently planned in its initial effort to characterize groundwater flow and the on-site tritium contamination. Tritium concentration in this well (MW-30, located in the Unit 2 Fuel Handling Building, in the excavated area adjacent to the Unit 2 Spent Fuel Pool, i.e., within 5 feet of the pool) ranged as high as 6 E-4 uCi/ml. For comparison, the EPA Drinking Water standard for tritium is 20000 pCVL, i.e., 2 E-5 uCi/ml. Drilling activities for the remaining initial wells are in progress. Entergy informed the NRC that additional wells will be constructed, as necessary, to characterize the tritium contamination. | ||
Tritium concentration in this well (MW-30, located in the Unit 2 Fuel Handling Building, in the excavated area adjacent to the Unit 2 Spent Fuel Pool, i.e., within 5 feet of the pool) ranged as high as 6 E-4 uCi/ml. For comparison, the EPA Drinking Water standard for tritium is 20000 pCVL, i.e., 2 E-5 uCi/ml. Drilling activities for the remaining initial wells are in progress. | Unit 1 Spent Fuel Pool Conditions: Entergy is continuing efforts to monitor and investigate the leakage from the Unit 1 Spent Fuel Pool system. Entergy reports that the information gathered to-date from water inventory balance activities and tritium measurements continue to indicate that the Unit I curtain drain and sphere foundation sump systems effectively capture the leakage from the Unit 1 spent fuel pool systems. Currently, Entergy is investigating data that suggests that more tritium activity, than has been attributed to Unit I spent fuel pool system leakage, is being captured within the Unit 1 drain system. Notwithstanding the investigation of the data, all leakage from the Unit I drain system continues to be processed and released as a monitored liquid effluent discharge in accordance with NRC regulatory requirements; and radiological effluent discharges continue to be a faction of NRC regulatory limits.}} | ||
Entergy informed the NRC that additional wells will be constructed, as necessary, to characterize the tritium contamination. | |||
Unit 1 Spent Fuel Pool Conditions: | |||
Entergy is continuing efforts to monitor and investigate the leakage from the Unit 1 Spent Fuel Pool system. Entergy reports that the information gathered to-date from water inventory balance activities and tritium measurements continue to indicate that the Unit I curtain drain and sphere foundation sump systems effectively capture the leakage from the Unit 1 spent fuel pool systems. Currently, Entergy is investigating data that suggests that more tritium activity, than has been attributed to Unit I spent fuel pool system leakage, is being captured within the Unit 1 drain system. Notwithstanding the investigation of the data, all leakage from the Unit I drain system continues to be processed and released as a monitored liquid effluent discharge in accordance with NRC regulatory requirements; and radiological effluent discharges continue to be a faction of NRC regulatory limits.}} |
Latest revision as of 19:26, 23 November 2019
ML061160469 | |
Person / Time | |
---|---|
Site: | Indian Point |
Issue date: | 11/30/2005 |
From: | Brian Mcdermott NRC Region 1 |
To: | Baranski J, Bondi R, Eddy P, Feroe P, Greeley D, Delores Greene, Gross S, Chris Miller, Salame-Alfie A, Shapiro G, Spath J, Stiebeling A, Sutton T, Youngberg B - No Known Affiliation, Entergy Nuclear Operations, Orange County, NY, Putnam County, NY, Rockland County, NY, State of NY, State of NY, Dept of Environmental Conservation, State of NY, Dept of Health, State of NY, Dept of Public Service, Westchester County, NY |
References | |
FOIA/PA-2006-0081 | |
Download: ML061160469 (5) | |
Text
viIauz1-11 -I.- ru2 flAJII I'1I MI vpudIu ivl WauI~ rayq Lfla ,IjuicuitrvisaII ~ uaLPP 100OU~r roqu II From: Brian McDermott To: Adam Stiebeling; Alela Salame-Alfie; Barbara Youngberg; C.J. Miller; Daniel Greeley; dleach@3ntergy.com; Dominick Greene; Geri Shapiro; Jack Spath; James Baranski; Paul Eddy; Peter Feroe; Robert Bondi; Steve Gross; Tony Sutton Date: Wed, Nov 30, 2005 11:46 AM
Subject:
FYI: Forthcoming Update to NRC Web Page on Indian Point Spent Fuel Pool Issues Attached for your information is a status update on the Indian Point 2 Spent Fuel Pool investigation that will be posted to the NRC's Web Page in the next day or so. Ifyou have any questions, please feel free to give me a call or raise your questions during our next conference call - tomorrow, Thursday 1211 at 3:30 p.m.
The existing NRC Web Page on the Indian Point 2 Spent Fuel Pool and tritium contamination can be found at:
http://wwN.nrc.pov/reactors/Plant-soecific-itemslindian-ooint-issues.html Regards, Brian Brian J. McDermott, Chief, Projects Branch 2 U.S. Nuclear Regulatory Commission - Region I 475 Allendale Road King of Prussia, PA 19406 ork: 610-337-5233 Cell _:
&M*
ax: E 0-337-5349 bjm nrc.gov CC: John Boska; John White; Raeann Shane Information inthis record was deleted inaccordance withthe Freedom of lnmnation Act exemptons _
FDIA. =L-M
!2)
.vte3IIlJU.2VV j~sjuuv i a uvar raye Mail Envelope Properties (438DD75F.20F: 12: 55450)
Subjecit: FYI: Forthcoming Update to NRC Web Page on Indian Point Spent Fuel Pool Issues Creation Date: Wed, Nov 30,2005 11:46 AM From: Brian McDermott Created By: BJM@nrc.gov Recipients Action Date & Time aol.com Transferred 11/30 11:46 AM GeriShapiro (Geri Shapiro) bestweb.net Transferred 11/30 11:47 AM Abs]?cbes (Adam Stiebeling) co.orange.ny.us Transferred 11/30 11:47 AM dgreene (Dominick Greene)
SGross (Steve Gross) co.rockland.ny.us Transferred 11/30 11:47 AM greeleyd (Daniel Greeley) mill -rc (C.J. Miller) dps.stal:e.ny.us Transferred 11/30 11:47AM pde (Paul Eddy) entergy.com Transferred 11/30 11:47 AM dleach (dleach@entergy.com) gw.dec.state.ny.us Transferred 11/30 11:47AM bayoungb (Barbara Youngberg) health. ;tate.ny.us Transferred 11/30 11:47 AM asa0l. (Alela Salame-Alfie) mail.house.gov Transferred 11/30 11:47 AM Petcr.Feroe (Peter Feroe) nrc.gov TWGWPO02.HQGWDO01 Delivered 11/30 11:46 AM RMS2 CC (Raeann Shane) Opened 11/30 11:59 AM nrc.gov kplpo.KPDO Delivered 11/30 11:46 AM
.U ItI LOJ\
A. WVtUVv I. I11\\11
- --- ---- U raye e-JRi'l1 CC (John White) Opened 11/30 12:47 PM nrc.gov owf4_.po.OWFN_DO Delivered 11/30 11:46 AM JPB1 CC (John Boska) Opened 12/06 7:19 AM nyserda.org Transferred 11/30 11:47 AM jps (Jack Spath)
PutnamrCountyNY.com Transferred 11/30 11:47 AM Robrt.Bondi (Robert Bondi) semo.sltate.ny.us Transferred 11/30 11:47 AM james.baranski (James Baranski) westchestergov .com Transferred 11/30 11:47 AM aws I (Tony Sutton)
Post Office Delivered Route aol.com bestweb.net co.orange.ny.us co.rockland.ny.us dps.state.ny.us entergy.com gw.dec.state.ny.u; health.state.ny.us mail.house.gov TWGWPO02.HQGWDO01 11/30 11:46 AM nrc.gov kpl.pD.KPLDO 11/30 11:46 AM nrc.gov owf4,_po.OWFN_DO 11/30 11:46 AM. nrc.gov nyserda.org PutnamCountyNY.com semo.state.ny.us westchestergov.com Files SiU 5e Date & Time MESSAGE 20A Wednesday, November 30, 2005 11:46 AM NRC VebPageUpdatel 1-30-05.pdf 15798 Wednesday, Noverr.ber 30, 2005 11:44 AM Options Auto ]Delete: No
- "*'"*' a- t .......
S*v raycts-!
Expiration Date: None Notify Recipients: No Priority: High Reply Requested: No Return Notification: None Concealed
Subject:
No Security: Standard To Be Delivered: Immediate Status Tracking: All Information
On-going Activities; 11/29/2005 Unit 2 spent Fuel Pool: Entergy has completed visual examination and video taping of about 50% of the spent fuel pool liner surface in an effort to identify locations of potential leakage.
This represents all the surfaces that can be accessed with the currently available video camera equipment. Stored spent fuel in portions of the pool prevent full examination with currently available video equipment. Accordingly, Entergy has informed the NRC that it is investigating the use of other video equipment to affect more complete examination of the pool liner. Divers physically examined three locations of interest with a vacuum box to determine if leakage wEas present., however, in each case, leakage was not positively detected. Notwithstanding, Entergy is examining methods to apply an underwater coating to these locations to assure these areas of interest remain leak-tight.
The leak rate from the previously identified cracks in the spent fuel pool concrete wall is current y about 10 to 25 milliliters per day. Previously, leakage was measured to be about 1)300 to 150C milliliters per day. Entergy is investigating the cause of the decreased leak rate.
Monitoring Wells: Entergy has completed drilling of one of nine wells currently planned in its initial effort to characterize groundwater flow and the on-site tritium contamination. Tritium concentration in this well (MW-30, located in the Unit 2 Fuel Handling Building, in the excavated area adjacent to the Unit 2 Spent Fuel Pool, i.e., within 5 feet of the pool) ranged as high as 6 E-4 uCi/ml. For comparison, the EPA Drinking Water standard for tritium is 20000 pCVL, i.e., 2 E-5 uCi/ml. Drilling activities for the remaining initial wells are in progress. Entergy informed the NRC that additional wells will be constructed, as necessary, to characterize the tritium contamination.
Unit 1 Spent Fuel Pool Conditions: Entergy is continuing efforts to monitor and investigate the leakage from the Unit 1 Spent Fuel Pool system. Entergy reports that the information gathered to-date from water inventory balance activities and tritium measurements continue to indicate that the Unit I curtain drain and sphere foundation sump systems effectively capture the leakage from the Unit 1 spent fuel pool systems. Currently, Entergy is investigating data that suggests that more tritium activity, than has been attributed to Unit I spent fuel pool system leakage, is being captured within the Unit 1 drain system. Notwithstanding the investigation of the data, all leakage from the Unit I drain system continues to be processed and released as a monitored liquid effluent discharge in accordance with NRC regulatory requirements; and radiological effluent discharges continue to be a faction of NRC regulatory limits.