Information Notice 2018-03, Operating Experience Regarding Failure to Meet Technical Specifications Requirements for Changing Plant Conditions: Difference between revisions
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| issue date = 02/26/2018 | | issue date = 02/26/2018 | ||
| title = Operating Experience Regarding Failure to Meet Technical Specifications Requirements for Changing Plant Conditions | | title = Operating Experience Regarding Failure to Meet Technical Specifications Requirements for Changing Plant Conditions | ||
| author name = | | author name = Mcginty T, Miller C | ||
| author affiliation = NRC/NRO/DCIP, NRC/NRR/DIRS | | author affiliation = NRC/NRO/DCIP, NRC/NRR/DIRS | ||
| addressee name = | | addressee name = | ||
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| page count = 5 | | page count = 5 | ||
}} | }} | ||
{{#Wiki_filter: | {{#Wiki_filter:UNITED STATES | ||
NUCLEAR REGULATORY COMMISSION | |||
OFFICE OF NUCLEAR REACTOR REGULATION | |||
OFFICE OF NEW REACTORS | |||
WASHINGTON, DC 20555-0001 February 26, 2018 NRC INFORMATION NOTICE 2018-03: OPERATING EXPERIENCE REGARDING | |||
FAILURE TO MEET TECHNICAL | |||
SPECIFICATIONS REQUIREMENTS FOR | |||
CHANGING PLANT CONDITIONS | |||
==ADDRESSEES== | ==ADDRESSEES== | ||
All holders of an operating license or construction permit for a nuclear power reactor under Title 10 of the Code of Federal Regulations (10 CFR) Part 50, | All holders of an operating license or construction permit for a nuclear power reactor under | ||
Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of | |||
Production and Utilization Facilities, except those that have permanently ceased operations | |||
and have certified that fuel has been permanently removed from the reactor vessel. | |||
All holders of an operating license for a nonpower reactor (research reactor, test reactor, or | |||
critical assembly) under 10 CFR Part 50, except those that have permanently ceased | |||
operations. | |||
All holders of and applicants for a combined license under 10 CFR Part 52, Licenses, Certifications, and Approvals for Nuclear Power Plants. | |||
==PURPOSE== | ==PURPOSE== | ||
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform addressees of several recent events in which operators failed to ensure that the requirements of the plant technical specifications (TS) were met as the plant conditions | The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform | ||
addressees of several recent events in which operators failed to ensure that the requirements of | |||
the plant technical specifications (TS) were met as the plant conditions changed. The NRC | |||
expects recipients to review the information for applicability to their facilities and to consider | |||
actions, as appropriate, to avoid similar problems. However, suggestions contained in this IN | |||
are not NRC requirements; therefore, no specific action or written response is required. | |||
==DESCRIPTION OF CIRCUMSTANCES== | ==DESCRIPTION OF CIRCUMSTANCES== | ||
Watts Bar Nuclear Plant, Unit 1 On October 22, 2015, the operating crew at the Watts Bar Nuclear Plant, Unit 1 (Watts Bar) | |||
determined that both source range (SR) level trip channels (N-31 and N-32) were in the bypass position with the reactor at 27-percent rated thermal power (RTP). The SR level trip switches were left in bypass, outside of their required configuration, thereby removing a trip function required by the TS during rod | ===Watts Bar Nuclear Plant, Unit 1=== | ||
On October 22, 2015, the operating crew at the Watts Bar Nuclear Plant, Unit 1 (Watts Bar) | |||
determined that both source range (SR) level trip channels (N-31 and N-32) were in the bypass | |||
position with the reactor at 27-percent rated thermal power (RTP). The SR level trip switches | |||
were left in bypass, outside of their required configuration, thereby removing a trip function | |||
required by the TS during rod withdrawal. An incident prompt investigation led by Tennessee | |||
Valley Authority (the licensee) determined that the SR trip functions were inoperable from the | |||
time the reactor trip breakers (RTBs) were closed in Mode 3 on October 19, 2015, until reactor | |||
power exceeded the P-6 permissive interlock (1.66 x 10-4 percent RTP) on October 21, 2015. | |||
ML17303A791 TS 3.3.1, Reactor Trip System Instrumentation, requires these SR trip functions to be operable | |||
with the RTBs closed in Modes 5, 4, 3, and 2 until reactor power exceeds the P-6 (the SR block | |||
permissive) interlock. On October 21, 2015, at 0346 Eastern Daylight Time, the plant entered | |||
Mode 2 with both SR level trip channels inoperable. This was a mode change violation in | |||
accordance with limiting condition for operation (LCO) 3.0.4. Under these conditions, TS 3.3.1, Required Actions 4.1, 1.1 and J.1, required that the operators take immediate actions to | |||
suspend operations involving positive reactivity additions and open the RTBs. Two lit | |||
annunciators on the main control board indicated the bypass condition, but the operators did not | |||
take immediate action to open the RTB because they did not notice that the SR level trip | |||
channels were bypassed. In addition, operators failed to note the lit annunciators during shift | |||
turnovers and board walkdowns from October 19 through October 22, 2015, and during | |||
completion of the mode change checklist board walkdown on October 20, 2015, to transition | |||
from Mode 3 to Mode 2. By the time the operators recognized the improper configuration, reactor power was above the P-6 permissive interlock, and the SR trip functions were no longer | |||
a TS requirement. | |||
The licensee identified that the operators failed to identify a bypassed safety function during | |||
reactor testing and start-up due to inadequate tracking and validation of essential information. | |||
Inadequate operating procedures used to control SR level trip switches prior to core reload were | |||
identified as a contributing cause that led to this event. Specifically, on October 7, 2015, before | |||
core reload, the SR level trips had been placed in bypass, in accordance with the licensees | |||
procedure for power escalation testing to avoid spurious trips and alarms during the core reload | |||
process. On October 9, 2015, core reload was completed, at which point the switches should | |||
have been returned to the normal position. However, a revision to the procedure for power | |||
escalation testing back in July 2013 had inadvertently omitted the step to return the switches to | |||
normal. This issue was entered into the licensees corrective action program. | |||
Further details appear in Watts Bar Licensee Event Report 05000390/2015-006-00, dated | |||
December 21, 2015, and in NRC Integrated Inspection Report 05000390, 05000391/2015004, dated February 12, 2016. These documents are available on the NRCs public Web site under | |||
Agencywide Documents Access and Management System (ADAMS) Accession | |||
Nos. ML15355A525 and ML16043A214, respectively. | |||
Davis-Besse Nuclear Power Station, Unit 1 On May 10, 2016, at approximately 0528 hours, the Davis-Besse Nuclear Power Station | |||
(Davis-Besse) was at approximately 53 percent power and was increasing power following a | |||
refueling outage. During a walkdown of control room indications, a Davis-Besse senior | |||
manager determined that all four anticipatory reactor trip system (ARTS) instrumentation | |||
channels were in bypass. The ARTS initiates a reactor trip following a turbine trip or loss of | |||
both main feed pumps in order to reduce the magnitude of pressure and temperature transients | |||
on the reactor coolant system and lower the probability of a pressurizer pilot-operated relief | |||
valve actuation during these events. | |||
The turbine trip function trips the reactor when the main turbine is lost at high power levels in | |||
anticipation of the associated loss of heat sink. TS 3.3.16, Anticipatory Reactor Trip System | |||
Instrumentation, requires the ARTS turbine trip function to be in normal when the plant is | |||
operating above 45 percent power. As with the Watts Bar event discussed above, the ARTS | |||
channels had been placed in bypass to support work during a refueling outage; however, the | |||
procedure did not address the need to restore the system to a normal state upon completion of | |||
the work. FirstEnergy Nuclear Operating Company (the licensee) investigated this event and determined | |||
that multiple operators were aware that the ARTS was in bypass. Other operators were aware | |||
that the annunciator alarm for the ARTS in bypass was lit and that it remained lit after the main | |||
feed pump trip input for the ARTS was taken from bypass to normal during the startup. All of | |||
the operators involved assumed that the startup procedure would direct the system to be placed | |||
in normal. In fact, the applicable procedures required an operator to verify that the system was | |||
returned to normal before the reactor reaches 40 percent power. However, the operator on shift | |||
at that time misinterpreted the requirement as not applicable because the reactor had not yet | |||
reached 40 percent power. | |||
The licensee determined that the operators failed to work together effectively as a team to | |||
ensure that the ARTS was operable before the plant entered the mode of applicability during | |||
startup. The system was placed in normal upon discovery at 53 percent power to restore | |||
operability. This issue was entered into the licensees corrective action program. | |||
Further details on this event appear in Davis-Besse Licensee Event | |||
Report 05000346/2016-005-00, dated July 11, 2016 (ADAMS Accession No. ML16194A343), | |||
and in NRC Integrated Inspection Report 05000346/2016003, dated November 4, 2016 (ADAMS Accession No. ML16309A098). | and in NRC Integrated Inspection Report 05000346/2016003, dated November 4, 2016 (ADAMS Accession No. ML16309A098). | ||
Grand Gulf Nuclear Station, Unit 1 On September 8, 2016, Entergy Operations, Inc. (the licensee), manually shut down the Grand Gulf Nuclear Station (Grand Gulf, Unit 1) reactor to replace pump A of the residual heat removal (RHR) system after a failed TS | ===Grand Gulf Nuclear Station, Unit 1=== | ||
and in NRC Special Inspection Report 05000416/2016008, dated October 27, 2017 (ADAMS Accession No. ML17303B200). | On September 8, 2016, Entergy Operations, Inc. (the licensee), manually shut down the Grand | ||
Gulf Nuclear Station (Grand Gulf, Unit 1) reactor to replace pump A of the residual heat removal | |||
(RHR) system after a failed TS surveillance. Grand Gulf TS 3.4.10, Residual Heat Removal | |||
(RHR) Shutdown Cooling SystemCold Shutdown, requires two trains of RHR to be operable | |||
when the reactor is shut down. With the A train of the RHR system inoperable for the pump | |||
replacement, the TS requires verification that an alternate method of decay heat removal is | |||
available. This action must be completed within 1 hour of one RHR pump being taken out of | |||
service and once every 24 hours thereafter while the plant is in Mode 4. To meet this | |||
requirement, the licensee placed the alternate decay heat removal (ADHR) system in standby | |||
after the plant reached Mode 4 on September 9, 2016, and verified its availability daily until the | |||
A train of the RHR system was restored to operability on September 23, 2016. | |||
Following replacement of the A RHR system pump and while attempting to place the ADHR | |||
system in operation, licensee personnel identified that the ADHR system had not actually been | |||
available as an alternate method of decay heat removal. Since August 10, 2016, the ADHR | |||
heat exchanger tube-side cooling water system had been clearance tagged as closed to support | |||
cleaning of the heat exchanger tubes. The licensees daily verification of the availability of the | |||
ADHR system in accordance with the TS action statement had been administrative in nature. | |||
The licensee did not require a physical walkdown of the ADHR system to verify its availability. | |||
In addition, although the operators verified that no clearance tagouts were impacting the ADHR | |||
system, they failed to consider that a clearance tagout on the plant service water system could | |||
also affect the availability of the ADHR system. The licensee determined that when the work | |||
requiring the tagout had been completed on August 10, 2016, the work complete box had | |||
never been checked; therefore, the tags were left hanging. The licensees procedure for placing | |||
the ADHR system in standby did not specify that the plant service water isolation valves for the | |||
ADHR heat exchanger needed to be open. This issue was entered into the licensees corrective | |||
action program. Additional information appears in the Grand Gulf Licensee Event Report | |||
05000416/2016-008-01, dated August 16, 2017 (ADAMS Accession No. ML17228A233), | |||
and in NRC Special Inspection Report 05000416/2016008, dated October 27, 2017 (ADAMS | |||
Accession No. ML17303B200). | |||
==DISCUSSION== | ==DISCUSSION== | ||
As specified in 10 CFR 50.36, | As specified in 10 CFR 50.36, Technical specifications, plant TS are derived from the analysis | ||
and evaluation included in the plant safety analysis report and constitute a part of the license | |||
authorizing operation of each reactor plant. Each LCO in the TS lists the mode(s) of | |||
applicability for that condition and the actions to be taken if the conditions are not met. In each | |||
event summarized above, the licensees took systems out of service for activities while the | |||
plants were in a mode that did not require the systems. In doing so, the licensees failed to | |||
ensure that the systems were restored to operable when required by TS LCOs. | |||
Multiple administrative practices, including maintenance tracking systems, operating | |||
procedures, operational checklists, and operator walkdowns, aid operators in maintaining an | |||
understanding of the configuration of plant systems to ensure TS operability before entering a | |||
mode of applicability that requires a system. In each case discussed in this IN, these practices | |||
failed to accomplish their intended function when procedures were incomplete or misunderstood | |||
and when plant personnel failed to effectively and aggressively communicate concerns about | |||
unexpected tags, alarms, or indications. Industry operating experience has shown that best | |||
practices, such as noting conditional LCOs when taking equipment out of service that is | |||
required in another mode, caution-tagging equipment in an abnormal alignment, and issuing | |||
return-to-service checklists to ensure that systems are returned to their expected condition | |||
when work is complete, provide additional barriers to configuration control issues and | |||
noncompliance with TS operability requirements. When followed appropriately, these practices | |||
may significantly reduce the potential for TS violations. | |||
==CONTACT== | ==CONTACT== | ||
This IN requires no specific action or written | This IN requires no specific action or written response. Please direct any questions about this | ||
matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor | |||
Regulation (NRR) project manager. | |||
/RA/ (Paul G. Krohn for) /RA/ | |||
Timothy J. McGinty, Director Christopher G. Miller, Director | |||
Division of Construction Inspection Division of Inspection and Regional Support | |||
and Operational Programs Office of Nuclear Reactor Regulation | |||
===Office of New Reactors=== | |||
Technical Contacts: Rebecca Sigmon, NRR Margaret Chernoff, NRR | |||
301-415-0895 301-415-2240 | |||
Rebecca.Sigmon@nrc.gov Margaret.Chernoff@nrc.gov | |||
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under NRC Library. | |||
ML17303A791 *via email | |||
OFFICE TECH EDITOR* NRR/DIRS/IOEB* NRR/DSS/SSTB* NRR/DSS/SSTB/BC* NRR/IOEB/DIRS/BC* | |||
NAME JDougherty RSigmon MChernoff VCusumano RElliott | |||
DATE 11/22/17 12/21/17 12/22/17 1/12/18 12/22/17 OFFICE NRR/DIRS/IRGB/PM NRR/DIRS/IRGB/LA NRR/DIRS/IRGB/BC NRO/DCIP/D NRR/DIRS/D | |||
NAME TMensah* ELee HChernoff TMcGinty (PKroh for) CMiller | |||
DATE 1/12/18 1/29/18 2/6/18 2/20/18 2/26/18}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} |
Latest revision as of 11:02, 29 October 2019
ML17303A791 | |
Person / Time | |
---|---|
Issue date: | 02/26/2018 |
From: | Mcginty T, Chris Miller Division of Construction Inspection and Operational Programs, Division of Inspection and Regional Support |
To: | |
Tanya Mensah | |
References | |
IN-18-003 | |
Download: ML17303A791 (5) | |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
OFFICE OF NEW REACTORS
WASHINGTON, DC 20555-0001 February 26, 2018 NRC INFORMATION NOTICE 2018-03: OPERATING EXPERIENCE REGARDING
FAILURE TO MEET TECHNICAL
SPECIFICATIONS REQUIREMENTS FOR
CHANGING PLANT CONDITIONS
ADDRESSEES
All holders of an operating license or construction permit for a nuclear power reactor under
Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of
Production and Utilization Facilities, except those that have permanently ceased operations
and have certified that fuel has been permanently removed from the reactor vessel.
All holders of an operating license for a nonpower reactor (research reactor, test reactor, or
critical assembly) under 10 CFR Part 50, except those that have permanently ceased
operations.
All holders of and applicants for a combined license under 10 CFR Part 52, Licenses, Certifications, and Approvals for Nuclear Power Plants.
PURPOSE
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform
addressees of several recent events in which operators failed to ensure that the requirements of
the plant technical specifications (TS) were met as the plant conditions changed. The NRC
expects recipients to review the information for applicability to their facilities and to consider
actions, as appropriate, to avoid similar problems. However, suggestions contained in this IN
are not NRC requirements; therefore, no specific action or written response is required.
DESCRIPTION OF CIRCUMSTANCES
Watts Bar Nuclear Plant, Unit 1
On October 22, 2015, the operating crew at the Watts Bar Nuclear Plant, Unit 1 (Watts Bar)
determined that both source range (SR) level trip channels (N-31 and N-32) were in the bypass
position with the reactor at 27-percent rated thermal power (RTP). The SR level trip switches
were left in bypass, outside of their required configuration, thereby removing a trip function
required by the TS during rod withdrawal. An incident prompt investigation led by Tennessee
Valley Authority (the licensee) determined that the SR trip functions were inoperable from the
time the reactor trip breakers (RTBs) were closed in Mode 3 on October 19, 2015, until reactor
power exceeded the P-6 permissive interlock (1.66 x 10-4 percent RTP) on October 21, 2015.
ML17303A791 TS 3.3.1, Reactor Trip System Instrumentation, requires these SR trip functions to be operable
with the RTBs closed in Modes 5, 4, 3, and 2 until reactor power exceeds the P-6 (the SR block
permissive) interlock. On October 21, 2015, at 0346 Eastern Daylight Time, the plant entered
Mode 2 with both SR level trip channels inoperable. This was a mode change violation in
accordance with limiting condition for operation (LCO) 3.0.4. Under these conditions, TS 3.3.1, Required Actions 4.1, 1.1 and J.1, required that the operators take immediate actions to
suspend operations involving positive reactivity additions and open the RTBs. Two lit
annunciators on the main control board indicated the bypass condition, but the operators did not
take immediate action to open the RTB because they did not notice that the SR level trip
channels were bypassed. In addition, operators failed to note the lit annunciators during shift
turnovers and board walkdowns from October 19 through October 22, 2015, and during
completion of the mode change checklist board walkdown on October 20, 2015, to transition
from Mode 3 to Mode 2. By the time the operators recognized the improper configuration, reactor power was above the P-6 permissive interlock, and the SR trip functions were no longer
a TS requirement.
The licensee identified that the operators failed to identify a bypassed safety function during
reactor testing and start-up due to inadequate tracking and validation of essential information.
Inadequate operating procedures used to control SR level trip switches prior to core reload were
identified as a contributing cause that led to this event. Specifically, on October 7, 2015, before
core reload, the SR level trips had been placed in bypass, in accordance with the licensees
procedure for power escalation testing to avoid spurious trips and alarms during the core reload
process. On October 9, 2015, core reload was completed, at which point the switches should
have been returned to the normal position. However, a revision to the procedure for power
escalation testing back in July 2013 had inadvertently omitted the step to return the switches to
normal. This issue was entered into the licensees corrective action program.
Further details appear in Watts Bar Licensee Event Report 05000390/2015-006-00, dated
December 21, 2015, and in NRC Integrated Inspection Report 05000390, 05000391/2015004, dated February 12, 2016. These documents are available on the NRCs public Web site under
Agencywide Documents Access and Management System (ADAMS) Accession
Nos. ML15355A525 and ML16043A214, respectively.
Davis-Besse Nuclear Power Station, Unit 1 On May 10, 2016, at approximately 0528 hours0.00611 days <br />0.147 hours <br />8.730159e-4 weeks <br />2.00904e-4 months <br />, the Davis-Besse Nuclear Power Station
(Davis-Besse) was at approximately 53 percent power and was increasing power following a
refueling outage. During a walkdown of control room indications, a Davis-Besse senior
manager determined that all four anticipatory reactor trip system (ARTS) instrumentation
channels were in bypass. The ARTS initiates a reactor trip following a turbine trip or loss of
both main feed pumps in order to reduce the magnitude of pressure and temperature transients
on the reactor coolant system and lower the probability of a pressurizer pilot-operated relief
valve actuation during these events.
The turbine trip function trips the reactor when the main turbine is lost at high power levels in
anticipation of the associated loss of heat sink. TS 3.3.16, Anticipatory Reactor Trip System
Instrumentation, requires the ARTS turbine trip function to be in normal when the plant is
operating above 45 percent power. As with the Watts Bar event discussed above, the ARTS
channels had been placed in bypass to support work during a refueling outage; however, the
procedure did not address the need to restore the system to a normal state upon completion of
the work. FirstEnergy Nuclear Operating Company (the licensee) investigated this event and determined
that multiple operators were aware that the ARTS was in bypass. Other operators were aware
that the annunciator alarm for the ARTS in bypass was lit and that it remained lit after the main
feed pump trip input for the ARTS was taken from bypass to normal during the startup. All of
the operators involved assumed that the startup procedure would direct the system to be placed
in normal. In fact, the applicable procedures required an operator to verify that the system was
returned to normal before the reactor reaches 40 percent power. However, the operator on shift
at that time misinterpreted the requirement as not applicable because the reactor had not yet
reached 40 percent power.
The licensee determined that the operators failed to work together effectively as a team to
ensure that the ARTS was operable before the plant entered the mode of applicability during
startup. The system was placed in normal upon discovery at 53 percent power to restore
operability. This issue was entered into the licensees corrective action program.
Further details on this event appear in Davis-Besse Licensee Event
Report 05000346/2016-005-00, dated July 11, 2016 (ADAMS Accession No. ML16194A343),
and in NRC Integrated Inspection Report 05000346/2016003, dated November 4, 2016 (ADAMS Accession No. ML16309A098).
Grand Gulf Nuclear Station, Unit 1
On September 8, 2016, Entergy Operations, Inc. (the licensee), manually shut down the Grand
Gulf Nuclear Station (Grand Gulf, Unit 1) reactor to replace pump A of the residual heat removal
(RHR) system after a failed TS surveillance. Grand Gulf TS 3.4.10, Residual Heat Removal
(RHR) Shutdown Cooling SystemCold Shutdown, requires two trains of RHR to be operable
when the reactor is shut down. With the A train of the RHR system inoperable for the pump
replacement, the TS requires verification that an alternate method of decay heat removal is
available. This action must be completed within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of one RHR pump being taken out of
service and once every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> thereafter while the plant is in Mode 4. To meet this
requirement, the licensee placed the alternate decay heat removal (ADHR) system in standby
after the plant reached Mode 4 on September 9, 2016, and verified its availability daily until the
A train of the RHR system was restored to operability on September 23, 2016.
Following replacement of the A RHR system pump and while attempting to place the ADHR
system in operation, licensee personnel identified that the ADHR system had not actually been
available as an alternate method of decay heat removal. Since August 10, 2016, the ADHR
heat exchanger tube-side cooling water system had been clearance tagged as closed to support
cleaning of the heat exchanger tubes. The licensees daily verification of the availability of the
ADHR system in accordance with the TS action statement had been administrative in nature.
The licensee did not require a physical walkdown of the ADHR system to verify its availability.
In addition, although the operators verified that no clearance tagouts were impacting the ADHR
system, they failed to consider that a clearance tagout on the plant service water system could
also affect the availability of the ADHR system. The licensee determined that when the work
requiring the tagout had been completed on August 10, 2016, the work complete box had
never been checked; therefore, the tags were left hanging. The licensees procedure for placing
the ADHR system in standby did not specify that the plant service water isolation valves for the
ADHR heat exchanger needed to be open. This issue was entered into the licensees corrective
action program. Additional information appears in the Grand Gulf Licensee Event Report
05000416/2016-008-01, dated August 16, 2017 (ADAMS Accession No. ML17228A233),
and in NRC Special Inspection Report 05000416/2016008, dated October 27, 2017 (ADAMS
Accession No. ML17303B200).
DISCUSSION
As specified in 10 CFR 50.36, Technical specifications, plant TS are derived from the analysis
and evaluation included in the plant safety analysis report and constitute a part of the license
authorizing operation of each reactor plant. Each LCO in the TS lists the mode(s) of
applicability for that condition and the actions to be taken if the conditions are not met. In each
event summarized above, the licensees took systems out of service for activities while the
plants were in a mode that did not require the systems. In doing so, the licensees failed to
ensure that the systems were restored to operable when required by TS LCOs.
Multiple administrative practices, including maintenance tracking systems, operating
procedures, operational checklists, and operator walkdowns, aid operators in maintaining an
understanding of the configuration of plant systems to ensure TS operability before entering a
mode of applicability that requires a system. In each case discussed in this IN, these practices
failed to accomplish their intended function when procedures were incomplete or misunderstood
and when plant personnel failed to effectively and aggressively communicate concerns about
unexpected tags, alarms, or indications. Industry operating experience has shown that best
practices, such as noting conditional LCOs when taking equipment out of service that is
required in another mode, caution-tagging equipment in an abnormal alignment, and issuing
return-to-service checklists to ensure that systems are returned to their expected condition
when work is complete, provide additional barriers to configuration control issues and
noncompliance with TS operability requirements. When followed appropriately, these practices
may significantly reduce the potential for TS violations.
CONTACT
This IN requires no specific action or written response. Please direct any questions about this
matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
/RA/ (Paul G. Krohn for) /RA/
Timothy J. McGinty, Director Christopher G. Miller, Director
Division of Construction Inspection Division of Inspection and Regional Support
and Operational Programs Office of Nuclear Reactor Regulation
Office of New Reactors
Technical Contacts: Rebecca Sigmon, NRR Margaret Chernoff, NRR
301-415-0895 301-415-2240
Rebecca.Sigmon@nrc.gov Margaret.Chernoff@nrc.gov
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under NRC Library.
ML17303A791 *via email
OFFICE TECH EDITOR* NRR/DIRS/IOEB* NRR/DSS/SSTB* NRR/DSS/SSTB/BC* NRR/IOEB/DIRS/BC*
NAME JDougherty RSigmon MChernoff VCusumano RElliott
DATE 11/22/17 12/21/17 12/22/17 1/12/18 12/22/17 OFFICE NRR/DIRS/IRGB/PM NRR/DIRS/IRGB/LA NRR/DIRS/IRGB/BC NRO/DCIP/D NRR/DIRS/D
NAME TMensah* ELee HChernoff TMcGinty (PKroh for) CMiller
DATE 1/12/18 1/29/18 2/6/18 2/20/18 2/26/18