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{{#Wiki_filter:U.S.NUCLEAR REGULATORY Co>'ISSION NRC FgRM 195 I2 76I V IJRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL DOC T NUM R FILE NUMBER INCIDENT REPORT TO: Mr..J.'.Keppler'ROIVI: Indiana&Michigan Power Company Bridgman, Michigan'R.Wi Jurgensen DATE OF DOCUMENT 4/19/77 DATE RECEIVED 4 22/77 LETTER 0 OR I G IN AL JiikcoP Y DESCRIPTION QNOTORIZED StGNC LASS IF I E D PROP INPUT FORM ENCLOSURE NUMBER OF COPIES RECEIVED gC C Ltr, trans the followingPLANT NAME: Cook Unit No.1'e.O WOT.RZ@OVH (1-P)Licensee Event Report (RO 50-315/77-17) on 4/3/77 concerning the 50 foot wind direction recorder being discovered inoperable
{{#Wiki_filter:U.S. NUCLEAR REGULATORY Co> 'ISSION DOC  T NUM  R NRC FgRM 195 I2 76I V                                                                                         FILE NUMBER IJRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL                                 INCIDENT REPORT TO:                                                 ROIVI:                                    DATE OF DOCUMENT Indiana    & Michigan Power    Company            4/19/77 Mr..J.'.         Keppler'                     Bridgman, Michigan' R. Wi Jurgensen DATE RECEIVED 4 22/77 LETTER                   QNOTORIZED          PROP                    INPUT FORM          NUMBER OF COPIES RECEIVED 0 OR I G IN AL         StGNC LASS IF I E D JiikcoP Y                                                                                      gC     C DESCRIPTION                                                        ENCLOSURE Ltr, trans       the following                              Licensee Event Report (RO 50-315/77-17) on 4/3/77 concerning the 50 foot wind direction recorder being discovered inoperable ~ ~
~~(1-P)RJL ACKNOWLEDGED NOTE: IF PERSONNEL EKPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS BRANCH CHIEF: W 3 CYS FOR ACTION LIC ASSTo W CYS ACRS g CYS 1 FOR ACTION/INFORMATION
                                  'e.O WOT. RZ@OVH (1-P)        (1-P)
~REG FILE NRC PDR I6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS INTERNAL D IST Rl BUTION LPDR: TIC: N EXTERNAL DISTRIBUTION CONTROL NUMBER g7((ggooy~O't NRC FORM 195 I2-76)!6~gtfWP fhft l''g g I~m p4>(~.Q lil!DIAIVA 8 MIClllGAlII POL t/EB COIWPANY DONALD C.COOK NUCLEAR PLANT P.O.Box 468, Bridgman, Michigan 49106 April 19, 1977/pp ll g~M~Cay+~~~'7'1 Ugl~.'gm,t 84~@Operating License DPR-58 Docket No.50-315 t'ir.J.G.Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road 59 Glen Ellyn, IL 60137
PLANT NAME:
Cook    Unit      No. 1 RJL                               ACKNOWLEDGED NOTE:                       IF PERSONNEL EKPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION BRANCH CHIEF:
W 3 CYS FOR ACTION LIC ASSTo W       CYS ACRS         g CYS 1 INTERNAL D IST Rl BUTION
      ~
REG FILE NRC PDR I6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J         COLLINS EXTERNAL DISTRIBUTION                                      CONTROL NUMBER LPDR:
TIC:
N g7((ggooy         ~O   't NRC FORM 195 I2-76)
                                                                                                                  !     6~ gtfWP fhft


==Dear ter.Keppler:==
l''g I ~ m g
Pursuant to the requirements o;Appendix A Technical Specifications and the United States Nuclear Regulatory Comission Regulatory Guide'.16, Revision 4, Section 2.b, the following report is submitted:
 
RO 50-315/77-17.
p4>(~. Q lil!DIAIVA8 MIClllGAlIIPOL t/EB COIWPANY                    /pp DONALD C. COOK NUCLEAR PLANT P.O. Box 468, Bridgman, Michigan 49106    ll g~M~
Sincerely,<R.M.Jurgensen Plant Hanager/bab cc: R.S.Hunter J.E.Dolan G.E.Lien R.Ki 1 burn R.J.Vollen BPI R.C.Callen HPSC K.R.Baker RO: III P.H.Steketee, Esq.-R.llalsh, Esq.G.Charnoff, Esq.G.Olson J.th.Hennigan PNSRC R.S.Keith Dir., IE (30 copies)Dir., HIPC (3 copies)
Cay+~~    ~ '
I~4 i~$)ll~
April 19,      1977 7 '1 t'ir. J.G. Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region      III                                              'gm,t 84~@
Form No.4494 P CONTROL BLOCK: y LICENSEE EVENT REPORT~L'PLEASE PRINT ALL REQUIMD siJFDTINAYlDII]
59Ugl~
UCENSEE NAME~o r II I D C C I 0 7 09 14 15 EVENT TYPE UCENSE NUMOEA 0-0 0 0 0 0 0 0 4 1 1 1 1 LOL3..l 30.31'32 25 26 CATFGOAY TYPE SOURCE AEPOAT REPORT OOCKET NUMOEA EVENT OATE'EPOhT OATE~>oowr~L L 0 5 0-0 3 I 5 0 4 0 7 0 57 58 5S 60 61 68 69 74 75 80 EVENT DESCRIPTION QOQ'HHILE IN t<ODE 1 s AT 98/o POHERs THE 50 FOOT I'JIND DIRECTION RECORDER HAS DISCOVERED 00 7 8 9 Jog TECHNICAL SPECIFICATION; 3.3.3.4 ON 4/4/77.80 RO-50-315 77-17 7 8 9 Q~g 7 8 9 80[pro I INOPERABLE ON 4/3/77.THE PROBLEM I!AS IDENTIFIED AS A BROKEN RECORDER DRIVE CA~0 7 09 80 I A NEI'I DRIVE CABLE I'IAS INSTALLED AND THE SYSTEII DECLARED OPERABLE IN COMPLIANCE NEITH 7 8 9 SYSTEM CAUSE CODE COOE COMPONENT CODE PRME COHIPONENT SUPPLIEA COMPONEPIT MAMUFACTUAEA L X 9 9 9 48 CD I~Jog LPERSONNEL PERFORMING RECORDER MAINTENANCE HERE INSTRUCTED TO ADD THE RECORDER DRIVE 7 0 9~go UNITS TO THEIR ROUTINE INSPECTIOINS.
799 Roosevelt Road                                                .
VIOLATCN[oo~]L!IEI 5 I 7 8 S 10 11 12 17'3 44 47 CAUSF.DESCRIPTION 0 8 CAUSE OF THE EVENT HAS THE BROKEN DRIVE CABLE HHICH FAILED DUR NG NORMAL OPERATION~80 80 OTHER STA'TUS tiA AMOUNT OF ACTIVITY NA 7 8 9 LOSS OR DAMAGE TO FACILITY TYPE OESCAIPTION C1Ds Z NA 7 89 10 PUBLICITY NA 7 89 ADDITIONAL FACTORS Q~g NA 7 09~s NA 7 89-,,.TERRY BEILHAN 7 89 FACILITY STATUS 55 POWER~OS 0 7 8 9 10 12 13 FOAM OF ACTIVITY CO!)TENT 7 8 9'10'11 PERSONNEL EXPOSURES 7 8 9 11.12 13 PERSONNEL IN JURIES 7 89 1'I 1 2 OFFSITE CONSEQUENCES t115I NA METHOD OF OISCOVEAY 45 DISCOVERY OESCA!PTION LOCATION OF RELEASE{616 465-5901(368) 00 80 00 00 80 80 00 00 80 GPO SOT 66'g  
Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315
'I r, 1}}
 
==Dear ter. Keppler:==
 
Pursuant to the requirements o; Appendix A Technical Specifications and the United States Nuclear Regulatory Comission Regulatory Guide'. 16, Revision 4, Section 2.b, the following report is submitted:
RO 50-315/77-17.
Sincerely,
< R.M. Jurgensen Plant Hanager
  /bab cc:     R.S. Hunter J.E. Dolan G.E. Lien R. Ki 1 burn R.J. Vollen BPI R.C. Callen HPSC K.R. Baker RO:   III P.H. Steketee, Esq.
        -R. llalsh, Esq.
G. Charnoff, Esq.
G. Olson J.th. Hennigan PNSRC R.S. Keith Dir., IE (30 copies)
Dir.,   HIPC (3   copies)
 
I
  ~ 4 i~$)ll~
 
P Form No. 4494 CONTROL BLOCK:
y     LICENSEE EVENT REPORT
                                                                                                                      ~
L'PLEASE PRINT ALL REQUIMD siJFDTINAYlDII]
UCENSEE                                                                                                               EVENT NAME                                           UCENSE NUMOEA                                                          TYPE
  ~o   r         II I     D     C       C   I           0   0       0   0   0   0     0       0   0       4   1   1     1   1       LOL3..l
                    ~
7      09                                    14      15                                                25      26                  30 . 31   '32 CATFGOAY AEPOAT TYPE REPORT SOURCE               OOCKET NUMOEA 0
EVENT OATE           'EPOhT           OATE
  ~>oowr                                   L           L       0   5   0             3     I   5       0   4   0 7       0           57       58           5S         60     61                                   68     69                       74     75                       80 EVENT DESCRIPTION
                'HHILE IN         t<ODE 1       s   AT 98/o POHERs         THE 50 FOOT I'JIND DIRECTION RECORDER HAS DISCOVERED QOQ 7 8 9                                                                                                                                                               80
[pro     I INOPERABLE             ON   4/3/77.         THE PROBLEM I!AS           IDENTIFIED       AS A BROKEN RECORDER DRIVE                   CA~0 7     09                                                                                                                                                           80 A NEI'I DRIVE CABLE I'IAS INSTALLED AND THE SYSTEII DECLARED OPERABLE IN COMPLIANCE NEITH I
7    8 9                                                                                                                                                          00 Jog          TECHNICAL SPECIFICATION;                            3.3.3.4    ON    4/4/77.
7     8 9                                                                                                                                                         80 Q~g                                                                                                                                  RO-50-315 77- 17 7      8 9                                                                        PRME                                                                            80 SYSTEM       CAUSE                                               COHIPONENT            COMPONEPIT CODE         COOE                   COMPONENT CODE               SUPPLIEA             MAMUFACTUAEA           VIOLATCN
                                                                                '3
 
[oo~]
7 8 S L!IEI10 5
11           12 I
17 L
44 X  9  9    9 47         48 CAUSF. DESCRIPTION 0 8 CD        I~  CAUSE OF THE EVENT HAS THE BROKEN DRIVE CABLE HHICH FAILED DUR NG NORMAL OPERATION                                                               ~
Jog LPERSONNEL                      PERFORMING RECORDER MAINTENANCE HERE INSTRUCTED TO ADD THE RECORDER DRIVE 7     0 9                                                                                                                                                         80
~go          UNITS TO THEIR ROUTINE INSPECTIOINS.
7     89       FACILITY                                                                 METHOD OF STATUS               55 POWER                   OTHER STA'TUS          OISCOVEAY                      DISCOVERY OESCA!PTION
                                  ~OS             0             tiA 7     8         9               10                 12   13                                                                                                       00 FOAM OF ACTIVITY         CO!)TENT AMOUNT OF ACTIVITY                                              LOCATION OF RELEASE NA 7     8         9                 '10       '11                                               45                                                                80 PERSONNEL EXPOSURES 7     8 9                 11     .12       13                                                                                                                   00 PERSONNEL INJURIES 7     89                 1'I   12                                                                                                                                00 OFFSITE CONSEQUENCES t115I         NA 7 8 9                                                                                                                                                              80 LOSS OR DAMAGE TO FACILITY TYPE        OESCAIPTION C1Ds      Z                  NA 7      89            10                                                                                                                                            80 PUBLICITY NA 7      89                                                                                                                                                          00 ADDITIONAL FACTORS Q~g          NA 7      09                                                                                                                                                          00
~s            NA 7      89                                                                                                                                                          80
                          -,,. TERRY            BEILHAN                                                                { 616 465-5901(368)
GPO SOT   66'g
 
'I r,
1}}

Revision as of 18:52, 20 October 2019

LER-1977-017-00 for Donald C. Cook, Unit 1 - Discovery of Inoperability of 50 Foot Wind Direction Recorder
ML18219C250
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 04/19/1977
From: Jurgensen R
American Electric Power Service Corp, Indiana Michigan Power Co, (Formerly Indiana & Michigan Power Co)
To: James Keppler
NRC/IE, NRC/RGN-III
References
LER-1977-017-00
Download: ML18219C250 (6)


Text

U.S. NUCLEAR REGULATORY Co> 'ISSION DOC T NUM R NRC FgRM 195 I2 76I V FILE NUMBER IJRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL INCIDENT REPORT TO: ROIVI: DATE OF DOCUMENT Indiana & Michigan Power Company 4/19/77 Mr..J.'. Keppler' Bridgman, Michigan' R. Wi Jurgensen DATE RECEIVED 4 22/77 LETTER QNOTORIZED PROP INPUT FORM NUMBER OF COPIES RECEIVED 0 OR I G IN AL StGNC LASS IF I E D JiikcoP Y gC C DESCRIPTION ENCLOSURE Ltr, trans the following Licensee Event Report (RO 50-315/77-17) on 4/3/77 concerning the 50 foot wind direction recorder being discovered inoperable ~ ~

'e.O WOT. RZ@OVH (1-P) (1-P)

PLANT NAME:

Cook Unit No. 1 RJL ACKNOWLEDGED NOTE: IF PERSONNEL EKPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION BRANCH CHIEF:

W 3 CYS FOR ACTION LIC ASSTo W CYS ACRS g CYS 1 INTERNAL D IST Rl BUTION

~

REG FILE NRC PDR I6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS EXTERNAL DISTRIBUTION CONTROL NUMBER LPDR:

TIC:

N g7((ggooy ~O 't NRC FORM 195 I2-76)

! 6~ gtfWP fhft

lg I ~ m g

p4>(~. Q lil!DIAIVA8 MIClllGAlIIPOL t/EB COIWPANY /pp DONALD C. COOK NUCLEAR PLANT P.O. Box 468, Bridgman, Michigan 49106 ll g~M~

Cay+~~ ~ '

April 19, 1977 7 '1 t'ir. J.G. Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 'gm,t 84~@

59Ugl~

799 Roosevelt Road .

Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315

Dear ter. Keppler:

Pursuant to the requirements o; Appendix A Technical Specifications and the United States Nuclear Regulatory Comission Regulatory Guide'. 16, Revision 4, Section 2.b, the following report is submitted:

RO 50-315/77-17.

Sincerely,

< R.M. Jurgensen Plant Hanager

/bab cc: R.S. Hunter J.E. Dolan G.E. Lien R. Ki 1 burn R.J. Vollen BPI R.C. Callen HPSC K.R. Baker RO: III P.H. Steketee, Esq.

-R. llalsh, Esq.

G. Charnoff, Esq.

G. Olson J.th. Hennigan PNSRC R.S. Keith Dir., IE (30 copies)

Dir., HIPC (3 copies)

I

~ 4 i~$)ll~

P Form No. 4494 CONTROL BLOCK:

y LICENSEE EVENT REPORT

~

L'PLEASE PRINT ALL REQUIMD siJFDTINAYlDII]

UCENSEE EVENT NAME UCENSE NUMOEA TYPE

~o r II I D C C I 0 0 0 0 0 0 0 0 0 4 1 1 1 1 LOL3..l

~

7 09 14 15 25 26 30 . 31 '32 CATFGOAY AEPOAT TYPE REPORT SOURCE OOCKET NUMOEA 0

EVENT OATE 'EPOhT OATE

~>oowr L L 0 5 0 3 I 5 0 4 0 7 0 57 58 5S 60 61 68 69 74 75 80 EVENT DESCRIPTION

'HHILE IN t<ODE 1 s AT 98/o POHERs THE 50 FOOT I'JIND DIRECTION RECORDER HAS DISCOVERED QOQ 7 8 9 80

[pro I INOPERABLE ON 4/3/77. THE PROBLEM I!AS IDENTIFIED AS A BROKEN RECORDER DRIVE CA~0 7 09 80 A NEI'I DRIVE CABLE I'IAS INSTALLED AND THE SYSTEII DECLARED OPERABLE IN COMPLIANCE NEITH I

7 8 9 00 Jog TECHNICAL SPECIFICATION; 3.3.3.4 ON 4/4/77.

7 8 9 80 Q~g RO-50-315 77- 17 7 8 9 PRME 80 SYSTEM CAUSE COHIPONENT COMPONEPIT CODE COOE COMPONENT CODE SUPPLIEA MAMUFACTUAEA VIOLATCN

'3

[oo~]

7 8 S L!IEI10 5

11 12 I

17 L

44 X 9 9 9 47 48 CAUSF. DESCRIPTION 0 8 CD I~ CAUSE OF THE EVENT HAS THE BROKEN DRIVE CABLE HHICH FAILED DUR NG NORMAL OPERATION ~

Jog LPERSONNEL PERFORMING RECORDER MAINTENANCE HERE INSTRUCTED TO ADD THE RECORDER DRIVE 7 0 9 80

~go UNITS TO THEIR ROUTINE INSPECTIOINS.

7 89 FACILITY METHOD OF STATUS 55 POWER OTHER STA'TUS OISCOVEAY DISCOVERY OESCA!PTION

~OS 0 tiA 7 8 9 10 12 13 00 FOAM OF ACTIVITY CO!)TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE NA 7 8 9 '10 '11 45 80 PERSONNEL EXPOSURES 7 8 9 11 .12 13 00 PERSONNEL INJURIES 7 89 1'I 12 00 OFFSITE CONSEQUENCES t115I NA 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE OESCAIPTION C1Ds Z NA 7 89 10 80 PUBLICITY NA 7 89 00 ADDITIONAL FACTORS Q~g NA 7 09 00

~s NA 7 89 80

-,,. TERRY BEILHAN { 616 465-5901(368)

GPO SOT 66'g

'I r,

1