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| | number = ML12054A081 | | | number = ML12054A081 |
| | issue date = 09/16/2011 | | | issue date = 09/16/2011 |
| | title = North Anna Earthquake AIT Brief | | | title = Earthquake AIT Brief |
| | author name = Leeds E J | | | author name = Leeds E J |
| | author affiliation = NRC/NRR | | | author affiliation = NRC/NRR |
Revision as of 12:32, 12 April 2019
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MONTHYEARML24215A2652024-08-28028 August 2024 Record of Decision ML22263A2902022-05-0101 May 2022 Alert and Notification System Evaluation Report ANS Evaluation - Redacted Pages 66-130 ML22034A3952022-02-16016 February 2022 Enclosure 3 - IP 96001 CY2021 - IR 8 Baseline Inspection Completion ML22034A3972022-02-16016 February 2022 Enclosure 2 - IP 92707 CY2021 - IR 8 Baseline Inspection Completion ML22034A3992022-02-16016 February 2022 Enclosure 1 - IP 71130.03 Cy 2021 - IR 8 Baseline Inspection Completion ML21239A0682021-09-0202 September 2021 August 27, 2021, Summary: Discussion Between NRC and Dominion Regarding the NAPS Subsequent License Renewal - an Inconsistency in Documentation Regarding RCP Code Case N-481 (EPID No. L-2020-SLR-0000) - List of Attendee ML21221A0322021-08-27027 August 2021 Meeting Summary Regarding Discussion of Dominion'S Response to Select Staff Requests for Additional Information on Subsequent License Renewal Application ML21221A1412021-08-10010 August 2021 Meeting Summary: Discussion of Dominion'S Response to Select Staff Requests for Additional Information on Subsequent License Renewal Application (EPID No. L-2020-SLR-0000) - Attendees ML20246G7002020-08-24024 August 2020 Enclosure 3: North Anna Power Station Subsequent License Renewal Application (CD-ROM Titled: Naps_Slra) ML19011A1712019-01-0404 January 2019 Enclosures 1 to 3 - EAL Scheme Revisions Enclosure Summary, Discussion of Change and Mps EAL Scheme Revisions-Supporting Documents ML15253A4052016-03-11011 March 2016 Enclosure 1 Seven Screening Criteria ML15324A3022015-11-19019 November 2015 Implementation of TB 15-1 R1 and Unlikely Loss of Both RWSTs at NAPS ML15231A3642015-05-27027 May 2015 FOIA/PA-2014-0204 - Resp 1 - Final, Group a ML15065A2382015-02-0606 February 2015 Acord Certificate of Liability Insurance ML13329A5462013-11-27027 November 2013 Restart Action Plan (Public) ML13302B8912013-10-0202 October 2013 Listing of North Anna, Units 1 and 2 TS Basis Changes ML13318A1062013-03-11011 March 2013 Flooding Hazard Re-Evaluation Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.1: Flooding ML13318A1072013-03-11011 March 2013 Near-Term Task Force 2.1: Flooding Hazard Re-Evaluation Initial Assessment of Flooding Hazard Re-Evaluation Results and Interim Actions Plan ML12131A5042012-05-0909 May 2012 Sign in Sheets for the North Anna Annual Assessment Public Meeting ML12056A0522012-03-12012 March 2012 Enclosure 6 - List of Power Reactor Licensees and Holders of Construction Permits in Active or Deferred Status ML11292A1902012-01-18018 January 2012 Supporting Document and Examples for Information Notice Sblc and RWST Issues ML11305A0392011-11-0101 November 2011 Restart Public Meeting, Feedback Form ML12054A0812011-09-16016 September 2011 Earthquake AIT Brief ML1030502072010-07-16016 July 2010 Initial Exam 2010-301 Final Simulator Scenarios ML1019303122010-06-0909 June 2010 Onsite Ground/Surface Water Monitoring Questionnaire for North Anna ML1012600352010-05-0303 May 2010 Public Mtg. Attendees ML0909209562009-03-31031 March 2009 Closed Generic Communication TACs (PA No. 101122CA/B) Summary Report (as of 03/31/2009) ML0732400242007-10-25025 October 2007 Examples of Max Thermal Power License Conditions ML0730400302007-10-0101 October 2007 Sign-In Roster for Public Meeting with Dominion Nuclear ML0711600032007-04-24024 April 2007 Annual Assessment Meeting Cy 2006, List of Attendees ML0634705992006-12-14014 December 2006 Plant Service List ML0513005392005-05-0505 May 2005 Attachment 1, Response to Requests for Additional Information on Nuclear Facility Quality Assurance Program Description ML0513005442005-05-0505 May 2005 Attachment 2, Response to Requests for Additional Information Re Proposed Technical Specifications Changes Associated with Nuclear Facility Quality Assurance Program Description ML0513005562005-05-0505 May 2005 Enclosure 4, Response to Requests for Additional Information Marked Up Discussion of Changes ML0513005592005-05-0505 May 2005 Enclosure 5, Response to Requests for Additional Information Replacement Discussion of Changes ML0511502442005-02-16016 February 2005 Proposal for Information Collection - North Anna Power Station Submittal for Agency Review and Comments on 316(b) Cooling Water Intake Structures ML0423803102004-08-10010 August 2004 Background on RCP Seal Cooling for North Anna ML0523507332004-08-0606 August 2004 mei-Primary ML0410702362004-04-0606 April 2004 Attachment 1, List of Attendees for North Anna Annual Assessment Meeting of 04/06/04 ML0404104922004-02-20020 February 2004 Order EA-03-009 Service List ML0505404692004-02-10010 February 2004 Dynamic Web Page Printout Dated 02/10/2004, ROP PIM Report - All Sites - Event Dates: 01/01/2003 - 02/10/2004 ML0505404642004-02-0909 February 2004 Dynamic Web Page Printout Dated 02/09/2004 Regarding Applied Violations for Nuclear Power Plants ML0505402642003-10-22022 October 2003 Summary of EB1 Findings (07-09/03) ML0403506912003-08-27027 August 2003 DRS Open Items Status ML0403502122003-08-13013 August 2003 DRS Open Items Status ML0224003322002-08-27027 August 2002 Outline for Phone Calls with Licensees for: Davis-Besse, H.B. Robinson, North Anna Unit 2 and Surry Unit 2 ML0213304862002-04-29029 April 2002 Dominion'S SBO Supplemental Response, Final Draft Dated 04/29/2002 ML0205206932002-03-0404 March 2002 Enclosure to North Anna, Unit 1 ASME ISI Program Relief Request Request NOE-Partial-2 ML0201003882002-01-24024 January 2002 Enclosufigures Depicting the Locations of the Surry and North Anna Power Stations and Their Associated Transmission Lines 2024-08-28
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North Anna Earthquake AIT Brief Eric Leeds, Director, NRR 9116/2011 Purpose of the AIT: To assess the circumstances surrounding the total loss of offsite power and dual unit reactor trip, 2H emergency diesel generator coolant leak and other plant equipment issues following a seismic event on August 23, 2011, at the North Anna Power Station.Observations
- 1) Rx trips -For both Ul and U2, neutron negative rate flux signals resulted in reactor trips.These signals occurred early in the seismic event and prior to LOOP. The licensee continues a root cause investigation.
- 2) Electrical System Performance
-Earthquake ground motion is the probable cause of the Generator Step Up Transformer bushing damage, sudden pressure trips, and Reserve Station Service Transformer sudden pressure trips.3) On-Shift HU Performance -Operators responded to the event in accordance with approved procedures and in a manner that maintained public health and safety.4) Plant parameter review -To this point, no significant damage to SSCs has been identified.
- 5) ISFSI -No significant damage is noted based on walkdowns.
Potential Generic Issues (1) Seismic panel power supply failure and EAL/OD reliance.(2) Seismic monitors are located on the structures and not located on the free surface in the free field; therefore, the recorded ground motion is not a good indicator for determining whether OBE and DBE was exceeded.
No monitors for ISFSI are installed.
URIs (1) 2H EDG JW leak -An incorrectly installed gasket appears to have contributed to the JW leak. Work order documents indicate that the failed gasket was installed on May 25, 2010.(2) 1J EDG Frequency Oscillations -While the EDG performed its function during the event, frequency oscillations potentially exceeding TS limits were observed by operators.
The licensee planned to test the EDG in isochronous mode.(3) Seismic Panel Power -Panel power was lost during the seismic event affecting EAL and Operability calls.(4) Seismic Instrument Implementation
-training, labeling, data collection and orientation issues.(5) 1J and 2J EDG orifice plates -missing JW orifice plates were identified by licensee.Impact of this is still under review.(6) 'A' AFW Terry Turbine LO level switch power -low lube oil alarm came in because switch is powered from non-vital.
Operators did not know why the alarm was in. This may be a knowledge and procedures deficiency for operators or possible design issue that could affect decisions on starting an AFW pump.(7) Safety Related Instrument Qualification
-Anomalies were observed on some safety related equipment instrumentation calling into question instrument qualification (depending on determination of final cause and seismic acceleration experienced.
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