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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20216C057 + (ML20216C057)
- ML20216C063 + (ML20216C063)
- ML20216C065 + (ML20216C065)
- ML20216C067 + (ML20216C067)
- ML20216C069 + (ML20216C069)
- ML20216C073 + (ML20216C073)
- ML20216C074 + (ML20216C074)
- B17102, Proposed Tech Specs Changing TSs 3.4.4, RCS - Pressurizer, 3.6.1.5, Containment Sys - Air Temp & 3.7.1.5, Plant Sys - Msli Valves + (ML20216C076)
- ML20216C077 + (ML20216C077)
- ML20216C078 + (ML20216C078)
- PNO-II-98-013, on 980308,util Declared NOUE Due to High River Level & Subsequent Flooding.Licensee Established Constant Communications W/Early,Ga & Houston County,Al.Resident Inspectors Are Monitoring Licensee Activities + (ML20216C079)
- 05000245/LER-1997-032, Forwards LER 97-032-00 Which Documents an Event That Occurred at Mnps,Unit 1 on 970731,per 10CFR50.73(a)(2)(i). Commitments Made within Ltr,Listed + (ML20216C080)
- ML20216C081 + (ML20216C081)
- 05000412/LER-1997-004-01, :on 970911,discovered That Four Containment Isolation Valves Were Not Tested IAW Ts.Caused by Inadequate Mgt Change.Will Revise Licensing Requirements Manual Table 5.1-1 & UFSAR Table 6.2-60 + (ML20216C082)
- L-98-054, Provides Notification of Changes or Errors in LOCA Evaluation Models Reportable Annually,Per 10CFR50.46. Licensee Plans to Complete Both Large Break LOCA & Small Break LOCA Reanalyses by June 1999 + (ML20216C086)
- ML20216C087 + (ML20216C087)
- PNO-II-98-014, on 980309,licensee Reported Theft of Troxler Moisture Density Gauge.Stolen Gauge Contains 8 Mci Cs-137 & 40 Mci Am-241/Beryllium.Notified Local Law Enforcement Officials & Intitiated Investigation + (ML20216C088)
- ML20216C091 + (ML20216C091)
- NRC-98-0053, 1997 Annual Financial Rept for Detroit Edison Company + (ML20216C092)
- ML20216C094 + (ML20216C094)
- ML20216C096 + (ML20216C096)
- 05000245/LER-1997-032-01, :on 970731,SW Effluent Monitoring Composite Sampling Was Performed IAW Radiological Effluent Monitoring. Caused by Inadequate Procedure Guidance.Revised Sampling Procedure + (ML20216C098)
- ML20216C100 + (ML20216C100)
- ML20216C101 + (ML20216C101)
- ML20216C102 + (ML20216C102)
- ML20216C104 + (ML20216C104)
- ML20216C105 + (ML20216C105)
- 0CAN068706, 1986 Annual Environ Radiological Monitoring Rept for Arkansas Nuclear One Units 1 & 2 + (ML20216C106)
- ML20216C107 + (ML20216C107)
- ML20216C108 + (ML20216C108)
- ML20216C109 + (ML20216C109)
- IA-98-062, Forwards NRC Year 2000 Status Rept as of 971115.Following Completion of Assessment Phase of Year 2000 Program,Nrc Taken Steps to Accelerate Efforts to Renovate Year 2000 Noncompliant mission-critical Systems + (ML20216C110)
- ML20216C110 + (ML20216C110)
- ML20216C111 + (ML20216C111)
- ML20216C112 + (ML20216C112)
- ML20216C115 + (ML20216C115)
- ML20216C116 + (ML20216C116)
- PNO-IV-98-011, on 980310,licensee RSO Reported Leaking Sealed Source Received at Halliburton Energy Services in Duncan,Ok.Leak Test Detected 0.14 Microcuries of Removable Contamination.Will Place Source in Storage + (ML20216C118)
- ML20216C120 + (ML20216C120)
- ML20216C121 + (ML20216C121)
- B16641, Application for Amend to License DPR-65,reducing Max Allowed Value for Containment Pressure Specified in TS 3.6.1.4 + (ML20216C124)
- ML20216C125 + (ML20216C125)
- ML20216C126 + (ML20216C126)
- ML20216C131 + (ML20216C131)
- 05000245/LER-1997-033-01, :on 970801,unmonitored Airborne Radioactivity Release Paths Were Discovered.Caused by Lack of Adequate Monitoring Program.Placed Low Vol Air Samplers at Areas in Question + (ML20216C132)
- ML20216C133 + (ML20216C133)
- ML20216C134 + (ML20216C134)
- ML20216C137 + (ML20216C137)
- ML20216C138 + (ML20216C138)
- ML20216C139 + (ML20216C139)
- ML20216C140 + (ML20216C140)