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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20138G532 + (ML20138G532)
- ML20138G533 + (ML20138G533)
- ST-HL-AE-1440, Forwards Responses to Draft SER Open Items 14.2-1,14.2-5, 14.2-6,14.2-7,14.2-9,14.2-12 & 14.2-15.Changes to FSAR Section 14.2 Also Encl + (ML20138G534)
- ML20138G537 + (ML20138G537)
- ML20138G538 + (ML20138G538)
- ML20138G541 + (ML20138G541)
- ML20138G542 + (ML20138G542)
- ML20138G543 + (ML20138G543)
- ML20138G546 + (ML20138G546)
- ML20138G548 + (ML20138G548)
- ML20138G551 + (ML20138G551)
- ML20138G553 + (ML20138G553)
- PNO-III-96-077, on 961224 & 1229,3 Curie Am-241 Source & 2 Curie Cs-137 Source Became Snagged in an Oil & Gas Well. Efforts to Retrieve Sources Have Been Unsuccessful.Licensee Will Submit Specific Abandonment Procedures in Few Days + (ML20138G555)
- ML20138G556 + (ML20138G556)
- ML20138G557 + (ML20138G557)
- PNO-IV-96-072A, on 961230,licensee Nuclear Gauge Containing 100 Mci of Cs-137 Was Reported Missing 961223 Still Unaccounted For.Improved Weather Conditions Expected Will Aid in Recovery of Source + (ML20138G558)
- ML20138G561 + (ML20138G561)
- PNO-IV-96-073, on 961231,steam Leak Was Identified in Basement of Turbine Bldg.Leak Was Caused by Failed Gasket. Repairs Are Expected to Take Approximately 2 Hours W/Power Escalation Planned + (ML20138G566)
- ML20138G570 + (ML20138G570)
- ML20138G572 + (ML20138G572)
- PNO-II-96-086, on 961231,moisture/density Gauge Containing Sealed Source w/10 Mci of Cs-137 & Sealed Source w/50 Mci of Am-241 Was Reported Stolen.Local Law Enforcement Authorities & Radio & Television Stations Were Informed + (ML20138G573)
- ML20138G575 + (ML20138G575)
- ML20138G578 + (ML20138G578)
- ML20138G579 + (ML20138G579)
- CY-97-046, Forwards Proposed Rev 1 to Cyap QA Program for Haddam Neck Plant + (ML20138G581)
- ML20138G583 + (ML20138G583)
- ML20138G584 + (ML20138G584)
- ML20138G587 + (ML20138G587)
- ML20138G590 + (ML20138G590)
- ML20138G592 + (ML20138G592)
- ML20138G593 + (ML20138G593)
- ML20138G597 + (ML20138G597)
- 05000498/LER-1996-004, :on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures + (ML20138G600)
- 05000366/LER-1985-021, :on 850707,reactor Water Cleanup Pump Inboard & Outboard Suction Isolation Valves Isolated on High Sys Differential Flow.Caused by Incompletely Closed Valves Due to Misaligned Indicators.Valves Closed + (ML20138G601)
- ML20138G602 + (ML20138G602)
- ML20138G603 + (ML20138G603)
- ML20138G606 + (ML20138G606)
- 2CAN129608, Monthly Operating Rept for Nov 1996 for Arkansas Nuclear One-Unit 2 + (ML20138G608)
- ML20138G609 + (ML20138G609)
- 1CAN129603, Monthly Operating Rept for Nov 1996 for Arkansas Nuclear One-Unit 1 + (ML20138G610)
- ML20138G611 + (ML20138G611)
- ML20138G616 + (ML20138G616)
- ML20138G617 + (ML20138G617)
- ML20138G620 + (ML20138G620)
- 05000362/LER-1985-025-01, :on 850916,containment Purge Isolation Sys a Spuriously Actuated by Signal from Containment Area Radiation Monitor.Cause Not Determined.Completion of Ground Sys Study Scheduled for 851101 + (ML20138G621)
- ML20138G623 + (ML20138G623)
- ML20138G627 + (ML20138G627)
- ML20138G628 + (ML20138G628)
- ML20138G631 + (ML20138G631)
- ML20138G632 + (ML20138G632)
- ML20138G638 + (ML20138G638)