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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- 05000315/LER-1983-069-03, /03L-0:on 830719,during Surveillance Testing on Diesel Generator Load Shedding Relays,Six GE Model NGV-13b Loss of Voltage Relays Exceeded Tech Spec Limit.Caused by Instrument Drift.Relays Readjusted + (ML20076F765)
- BSEP-83-1280, Responds to NRC Re Violations Noted in IE Special Training Assessment Repts 50-324/83-04 & 50-325/83-04. Corrective Actions:Orientation for New Employees Accomplished in Accordance w/TI-301 + (ML20076F766)
- ML20076F769 + (ML20076F769)
- ML20076F776 + (ML20076F776)
- 05000315/LER-1983-070-03, /03L-0:on 830723,during Refueling Operation,Fire Door 373 to Elevation 587 Vestibule Area Would Not Latch Properly.Caused by Barrel Retaining Ring in Contact W/Knob. Ring Adjusted & Set Screw Tightened + (ML20076F778)
- 05000260/LER-1983-043-03, /03L-0:on 830720,during Transient Operation, Following Control Rod Sequence Exchange,R Calculation Less than R Setpoint.Caused by Xenon Transient W/Operation Closer to Thermal Limits.Control Rods Repositioned + (ML20076F782)
- 05000302/LER-1983-029-03, /03L-0:on 830721 & 27,emergency Feedwater Ultrasonic Flow Indicator on Steam Generator B Inoperable. Caused by Electrical Malfunction in Transducers & Improperly Mounting Replacement Transducers,Respectively + (ML20076F784)
- ML20076F786 + (ML20076F786)
- 05000260/LER-1983-044-03, /03L-0:on 830712,during Performance of 4.2.B-26, Level Switches LS-73-56A & B Mfg by Robertshaw Failed to Operate Properly.Caused by Dirt in Mechanical Linkage. Switches Cleaned + (ML20076F787)
- ML20076F794 + (ML20076F794)
- ML20076F799 + (ML20076F799)
- 05000416/LER-1983-100-03, /03L-0:on 830718,during HPCS Monthly Functional Test,Diesel Generator Tripped While Attempting to Parallel Generator W/Bus 17AC.Caused by Operator Error.Engine Restarted + (ML20076F803)
- ML20076F805 + (ML20076F805)
- RA-20-0075, Response to NRC Regulatory Issue Summary 2020-01 Preparation and Scheduling of Operator Licensing Examinations + (ML20076F807)
- ML20076F809 + (ML20076F809)
- ML20076F813 + (ML20076F813)
- ML20076F814 + (ML20076F814)
- ML20076F820 + (ML20076F820)
- ML20076F821 + (ML20076F821)
- 05000302/LER-1983-027-03, /03L-0:on 830718,during Routine Sampling,Rcs Dissolved Oxygen Concentration at Approx 4 Ppm.Caused by Personnel Error.Hydrazine Added to Lower Dissolved Oxygen Concentration.Personnel Reinstructed + (ML20076F825)
- ML20076F826 + (ML20076F826)
- 05000369/LER-1983-058-03, /03L-0:on 830717,channel III Reactor Coolant Loop C Flow Instrumentation Read Low & Declared Inoperable.Caused by Out of Tolerance Westinghouse Veritrak 59DP4E99-7050 Flow Transmitter + (ML20076F827)
- 05000338/LER-1983-051-03, /03L-0:on 830723,post-reactor Shutdown Specific Activity RCS Samples Indicated Dose Equivalent I-131 Level Above Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core.Sampling Frequency Accelerated + (ML20076F829)
- 05000395/LER-1983-084-03, /03L-0:on 830722,licensee Notified NRC Inspector That Surveillance Test Procedure 115.001 Did Not Adequately Address Tech Spec.Caused by Inadequate Procedure.Revised Procedure to Be Issued 830820 + (ML20076F831)
- 05000348/LER-1983-040-03, /03L-0:on 830720,steam Generator 1B Level Transmitter LT-486 Instrumentation Channel Declared Inoperable Due to Loss of Power Supply.Caused by Power Supply Failure on Signal Comparator Card.Card Replaced + (ML20076F833)
- ML20076F834 + (ML20076F834)
- ML20076F835 + (ML20076F835)
- ML20076F839 + (ML20076F839)
- ML20076F840 + (ML20076F840)
- 05000395/LER-1983-085-03, /03L-0:on 830721-24,ambient Temp in Svc Water Pump House Exceeded Tech Spec Limits.Caused by Outside Air Temp Above Average.Mod to Evaluate Need for Installing Cooling Coils Being Processed + (ML20076F844)
- ML20076F845 + (ML20076F845)
- 1CAN088306, Forwards Results of Station Electrical Distribution Voltage Verification Test Completed During Fifth Refueling Outage. Test Met Criteria Outlined in NRC ,Except 30% Loading of 1E Buses Down to 480-volt Level + (ML20076F847)
- ML20076F849 + (ML20076F849)
- ML20076F854 + (ML20076F854)
- ML20076F857 + (ML20076F857)
- ML20076F860 + (ML20076F860)
- ML20076F861 + (ML20076F861)
- ML20076F863 + (ML20076F863)
- ML20076F864 + (ML20076F864)
- ML20076F867 + (ML20076F867)
- 05000316/LER-1983-069-03, /03L-0:on 830718,east Component Cooling Water Pump Discharge Crosstie Valve CMO-412 Would Not Close Completely. Caused by Low Valve Operator Torque Switch Setting. Switch Adjusted + (ML20076F876)
- 3F1094-05, Monthly Operating Rept for Sept 1994 for Crystal River Unit 3 + (ML20076F878)
- ML20076F881 + (ML20076F881)
- ML20076F883 + (ML20076F883)
- 05000316/LER-1983-070-03, /03L-0:on 830726,channel 2 Containment Pressure Indication Failed Low.Caused by Dirty Contacts in Toggle Switch Test Circuit.Toggle Switch Cleaned & Exercised + (ML20076F884)
- ML20076F885 + (ML20076F885)
- 05000373/LER-1983-087-03, /03L-0:on 830718,all Five Turbine Bypass Valves Went Open Due to Work on Electrohydraulic Control Sys & MDRFP Tripped on High Due to Swell.Caused by Loss of -22 Volt Dc Power Supply Due to Personnel Error + (ML20076F888)
- 05000458/LER-1994-026, :on 940915,deficiency in STP 055-0101, Ifts Pre-OP & Weekly Interlock Operability Test, Identified as Part of Ongoing TS Review Project.Caused by Inadequate Oversight of STP Development.Ts Implemented + (ML20076F899)
- ML20076F902 + (ML20076F902)
- ML20076F903 + (ML20076F903)
- ML20076F909 + (ML20076F909)