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 Start dateReport dateSiteReporting criterionSystemEvent description
ENS 5728221 August 2024 16:00:00Millstone10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containmentThe following information was provided by the licensee via fax and phone: At 1200 EDT on 8/21/2024, with Millstone unit 3 in mode 1 at 100 percent power, it was discovered that the secondary containment boundary was inoperable while maintenance activities on the system were in progress. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C) and (D). There is no impact on the health and safety of the public and plant personnel. The NRC Resident Inspector has been notified. Unit 3 continues to operate in mode 1 at 100 percent power with actions in progress to restore the system to operable within the technical specification allowed outage time. There has been no impact to unit 2, which remains at 100 percent power. The state of Connecticut and local towns were notified.
ENS 5713016 May 2024 12:40:00Perry10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary containment
Reactor Water Cleanup
The following information was provided by the licensee via email: On May 16, 2024 at 0840 EDT, operations declared the reactor water cleanup (RWCU) leak detection instruments related to the high differential flow signal inoperable. Technical specification (TS) 3.3.6.1, primary containment and drywell isolation instrumentation, conditions `A and `B were entered as one required channel of instrumentation was inoperable, and an automatic function with isolation capability was not maintained. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). All other RWCU primary containment isolation instrumentation functions remained operable. At 1210 EDT, the affected leak detection instruments were declared operable, and the TS limiting condition for operation 3.3.6.1 was declared met. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 571159 May 2024 12:00:00Beaver Valley10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
The following information was provided by the licensee via phone and email: At 0800 EDT on May 9, 2024, it was identified during leak rate testing that through-wall flaws existed on reactor plant river water piping inside the containment building. This determination resulted in a containment bypass condition such that a gaseous release could have occurred at a location not analyzed for a release in the loss of coolant accident dose consequence analysis. This condition is not bounded by existing design and licensing documents. Evaluation of the condition of the piping is ongoing to support repair prior to startup. With the plant currently in cold shutdown, the containment, as specified in Technical Specification 3.6.1, is not required to be operable. There was no impact on the health and safety of the public or plant personnel. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A), 10 CFR 50.72(b)(3)(ii)(B), and 10 CFR 50.72(b)(3)(v)(C). The NRC Resident Inspector has been notified.
ENS 5698019 February 2024 15:45:00Peach Bottom10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
Reactor Building Ventilation
Standby Gas Treatment System

The following information was provided by the licensee via email: At 1045 EST, on 2/19/2024, during a maintenance activity, a loss of all reactor building ventilation occurred on Unit 2. With no flow past the ventilation radiation monitors, the radiation monitors were inoperable to support their ability to perform primary and secondary containment isolation functions or start the standby gas treatment system. Reactor building ventilation was restored within 15 minutes. Due to this inoperability, the radiation monitor system was in a condition that could have prevented fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector will be notified.

  • * * RETRACTION ON 3/15/24 AT 1315 EDT FROM BILL LINNELL TO ADAM KOZIOL * * *

Upon further investigation, it was verified that the reactor building and the refueling floor radiation monitors are not needed to control the release of radiation for events described in chapter 14 of the updated Final Safety Analysis Report. For the analyzed loss of coolant accident (LOCA), the primary and secondary signals for this purpose were available and unaffected by this event. The radiation monitors provide a tertiary redundant method that is not credited within the station analysis. For all other analyzed accidents, the signal provided by the radiation monitors is not needed, as the secondary containment isolation function and start of the standby gas treatment system are not credited. Additionally, the fuel handling accident was not credible during the time of the event because no activities were in progress on the refueling floor. Therefore, the threshold for reporting the issue as an event or condition that could have prevented the fulfillment of a safety function was not met. The NRC Resident Inspector has been notified. Notified R1DO (Jackson)

ENS 569155 January 2024 15:40:00Davis Besse10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Shield Building

The following information was provided by the licensee via phone and email: At approximately 1111 EST on 01/05/2024, a mechanical penetration room door was discovered unlatched. Based on security badge history, the door was last opened at 1040 EST. The unlatched door resulted in both trains of the station emergency ventilation system being inoperable due to being unable to maintain the shield building negative pressure area. With both trains simultaneously inoperable, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). The door was closed and verified latched upon discovery to restore the systems to an operable status. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 1/17/24 AT 1400 EST FROM CHRIS HOTZ TO ADAM KOZIOL * * *

The station emergency ventilation system (EVS) was tested with the mechanical penetration room door unlatched. The test results showed that the station EVS attained the required negative pressure in the shield building within the time required by the Technical Specifications. Therefore, the station EVS remained operable with the door unlatched, and this issue did not prevent the system from fulfilling its safety function to control the release of radioactive material and mitigate the consequences of an accident. The NRC Resident Inspector has been notified. Notified R3DO (Orlikowski)

ENS 5681122 October 2023 16:49:00Cooper10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containment
Reactor Building Ventilation
The following information was provided by the licensee via fax and phone: On October 22, 2023, at 1149 CDT, with the reactor at 100 percent core thermal power and steady state conditions, the Cooper Nuclear Station secondary containment differential pressure exceeded the Technical Specification (TS) Surveillance Requirement (SR) 3.6.4.1.1 limit of -0.25 inches water gauge. The condition existed for approximately 80 seconds until the reactor building ventilation system responded to restore differential pressure to normal. Investigations identified a hinged duct access hatch found open. The hatch was closed and latched, and ventilation system parameters were returned to normal. There were no radiological releases associated with this event. Declaring secondary containment inoperable as a result of not meeting TS SR 3.6.4.1.1 is reportable under 10 CFR 50.72(b)(3)(v)(C) and (D) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material and mitigate the consequences of an accident. The NRC Senior Resident Inspector has been informed. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: At the time the licensee notified the NRC Headquarters Operations Officer, the cause of the hinged access duct being open had not been determined. This event has been added to the licensee's corrective action program.
ENS 5652016 May 2023 16:27:00Wolf Creek10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material

The following information was provided by the licensee via phone and email: At 1127 CDT on 5/16/2023, during the reperformance of test procedure 'STS PE-006, Charcoal Adsorber In-Place Leak Test' due to a failure from the previous day, both trains of emergency exhaust were rendered inoperable due to incorrect performance of the procedure. Performers incorrectly de-energized the humidity control heating coil for the unit not under test, rendering it inoperable. This issue was identified and rectified at 1138 CDT on 5/16/2023, exiting the LCO (limiting condition of operation) for both trains inoperable at that time. There was no impact to the health and safety of the public.

  • * * RETRACTION ON 6/5/2023 AT 1132 EDT FROM JASON KNUST TO HOWIE CROUCH * * *

The initial failure of the STS PE-006 test was caused by a malfunction of the test equipment which initially injected excessive amounts of tracer gas and caused saturation of the charcoal. Using test equipment sourced from Callaway, and following guidance from the vendor, STS PE-006 test was successfully passed on 5/17/2023. No maintenance or intrusive testing was performed on the unit between initial test failure and satisfactory completion of the test. Because this train of emergency exhaust was not actually inoperable at the time the second train was rendered inoperable due to incorrect procedure performance, there was no loss of safety function. Therefore, this event notification is being retracted. The licensee has notified the NRC Resident Inspector. Notified R4DO (Gepford).

ENS 5618527 October 2022 17:28:00Grand Gulf10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentThe following information was provided by the licensee via email: At 1228 CDT on October 27, 2022, Grand Gulf Nuclear Station (GGNS) was in Mode 1 at 88 percent power when a failure of a draw down surveillance resulted in the loss of secondary containment. During the performance of the surveillance GGNS was unable to maintain secondary containment pressure, as required by Technical Specification Surveillance Requirement 3.6.4.1.4, greater than or equal to 0.266 inches of water vacuum for 1 hour at a flow rate of less than or equal to 4000 cfm. The test was secured. Secondary containment was declared inoperable and Technical Specification 3.6.4.1 A.1 was entered at 1228 CDT. Secondary containment was restored to operable status at 1240 CDT by restoring the configuration to a previously known operable condition. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function. The NRC Resident Inspector was notified.
ENS 5617120 October 2022 09:27:00Grand Gulf10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentThe following information was provided by the licensee via email: At 0427 CDT on October 20, 2022, Grand Gulf Nuclear Station (GGNS) was in Mode 1 at 100 percent power when a failure of a draw down surveillance resulted in the loss of secondary containment. During the performance of the surveillance GGNS was unable to maintain secondary containment pressure, as required by Technical Specification Surveillance Requirement 3.6.4.1.4, greater than or equal to 0.266 inches of water vacuum for 1 hour at a flow rate of less than or equal to 4000cfm. The test was secured. Secondary containment was declared inoperable and Technical Specification 3.6.4.1 A.1 was entered at 0427 CDT. Secondary containment was restored to operable status at 0520 CDT by restoring the configuration to a previously known operable condition. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function. The NRC Resident Inspector was notified.
ENS 5616818 October 2022 19:40:00Browns Ferry10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Standby Liquid ControlThe following information was provided by the licensee via email: On 10/18/2022 at 1440 CDT, Browns Ferry Unit 3 declared both trains of standby liquid control (SLC) inoperable due to acceptance criteria failure of 3-SI-3.1.7.6, 'Standby Liquid Control System ATWS Equivalency Calculation for Newly Established Pump Flow Rate.' The purpose of this surveillance is to ensure the anticipated transient without scram (ATWS) calculation criteria is met after each pump flow test. Chemistry performed the surveillance following pump flow testing and the requirement for equivalency calculation failed low with a result of less than 1.0. CR 1810303 documents this condition in the corrective action program. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(A), 10 CFR 50.72(b)(3)(v)(C), and 10 CFR 50.72(b)(3)(v)(D). This condition is also reportable as a 60-day written report in accordance with 10 CFR 50.73(a)(2)(v)(A),10 CFR 50.73(a)(2)(v)(C), and 10 CFR 50.73(a)(2)(v)(D). The NRC Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officer's report guidance: The plant entered an 8 hour limiting condition for operation based on the above. The condition was resolved at 2053 CDT when the system was restored to normal operation.
ENS 559764 July 2022 06:30:00Quad Cities10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containment
Standby Gas Treatment System
The following information was received from the licensee via email: At 0130 CDT on July 4 2022, it was discovered both trains of Standby Gas Treatment System were simultaneously inoperable due to failure to reach required flow rates. Both trains were capable of starting but failed to reach the required flow of 4000 SCFM. Secondary Containment differential pressure was not able to be maintained at greater than or equal to 0.25 inches of vacuum water gauge, causing Secondary Containment to also be inoperable. Due to this inoperability, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5590723 May 2022 09:55:00Cooper10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containmentThe following information was provided by the licensee via email: On May 23, 2022, at 0455 CST, Cooper Nuclear Station experienced a spike in Secondary Containment differential pressure which exceeded the Technical Specifications Surveillance Requirements 3.6.4.1.1 limit of -0.25 inches of water gauge. Secondary Containment differential pressure restored to Technical Specification limits within two minutes and further investigation is ongoing. This unplanned Secondary Containment inoperability constitutes a condition reportable under 10CFR50.72(b)(3)(v)(C) and (D). The NRC Senior Resident Inspector has been informed.
ENS 5552214 October 2021 17:20:00Fermi10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialPrimary containment

At 1320 EDT, during a Traversing In-Core Probe (TIP) run for a scheduled Local Power Range Monitors (LPRM) calibration, it was reported to the Main Control Room that TIP A would not fully retract to the In-Shield position. With TIP A unable to fully retract to the In-Shield position the TIP A Ball Valve was declared Inoperable due to not being able to close and meet its safety function in that configuration. Furthermore the TIP A Shear Valve was previously declared Inoperable due to the Firing Fuses being removed. With the two valves Inoperable the penetration could not be isolated and Primary Containment boundary isolation could not be established. TIP A was subsequently manually hand cranked and placed back into its In-Shield position at 1333 EDT restoring TIP A Ball Valve Operable. This report is being made pursuant to 10CFR50.72(b)(3)(v)(C) based on control the release of radioactive material. The Senior NRC Resident Inspector has been notified.

  • * * RETRACTION ON NOVEMBER 24, 2021 AT 1232 EST FROM LEVI SMITH TO BRIAN P. SMITH * * *

The purpose of this notification is to retract a previous report made on October 14, 2021 (EN 55522). At 1320 EDT on October 14, 2021 while performing Traversing In-Core Probe (TIP) Machine Gain Adjustment in support of Local Power Range Monitor (LPRM) calibration, an unplanned inoperability of the TIP 'A' Primary Containment Isolation Valve (PCIV) was reported pursuant to 10CFR50.72(b)(3)(v)(C) by EN 55522. On October 14, it was reported to the Main Control Room that TIP 'A' would not fully retract to the In-Shield position. With TIP 'A' unable to fully retract to the In-Shield position, the TIP 'A' Ball Valve PCIV was declared Inoperable due to not being able to close and meet its safety function in that configuration. The TIP 'A' Shear Valve PCIV was previously declared inoperable due to firing fuses being removed. Further investigation determined that a "FAULT: MOVEMENT LIMITED" error was received. This TIP error condition did not present a primary containment isolation issue in the event of a primary containment isolation signal. The Automatic TIP Control Unit (ATCU) is designed to command the TIP drive mechanism to continuously retract a TIP probe to the in-shield position in the event of a containment isolation signal with this condition. In the event of a containment isolation signal, the TIP machine would withdraw the TIP detector back to the in-shield position and the TIP A ball valve PCIV would have closed to perform its safety function. Therefore, the inoperability of TIP 'A' ball valve reported under criterion 10CFR50.72(b)(3)(v)(C) was not met, and EN 55522 is hereby retracted. The NRC Resident Inspector has been notified. Notified R3DO (Peterson)

ENS 5542120 August 2021 13:05:00Sequoyah10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containment
Auxiliary Building Gas Treatment System

At 0905 EDT, it was discovered both trains of Auxiliary Building Gas Treatment System (ABGTS) were simultaneously INOPERABLE due to the auxiliary building secondary containment enclosure (ABSCE) being inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. ABSCE and ABGTS were returned to operable.

  • * * RETRACTION ON 10/14/2021 AT 0756 EDT FROM TRACY SUDOKO TO THOMAS HERRITY * * *

This is a retraction of the 8-hour Immediate notification (EN55421) made to the NRC by Sequoyah Nuclear Plant on August 20, 2021. Sequoyah is retracting this event notification based on the following: Regulatory Guidance in NUREG-1022, Revision 3, 'Event Reporting Guidelines 10 CFR 50.72 and 50.73', Sections 2.8 'Retraction and Cancellation of Event Reporting', and 4.2.3 'ENS Notification Retraction'. On August 20, 2021 personnel found door A-118 open. This door is part of the ABSCE. During the initial investigation, it was found that other personnel had the door open using Precaution A of 0-TI-SXX-000-016.0 which allows material access through ABSCE doors if the door is closed within three minutes. It was found that A-118 door had been open for greater than three minutes. With this door open the ABSCE was beyond its capability for ABGTS fan to maintain the required pressure during an Aux. Building Isolation. Thus, the site declared the ABSCE and both Trains of ABGTS inoperable per LCO 3.7.12 Conditions A, B and E. With the ABSCE being a single train system, this caused a condition that "could have prevented the fulfillment of the safety function" which requires an Immediate Notification to the NRC within eight hours under 10 CFR 50.72 (b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D). This Immediate Notification was reported on August 20, 2021 at 1600 EDT. It was later determined that at 'Time of Discovery', although Door A-118 was open, it was not obstructed, the door was open by normal means, was capable of being closed and was now attended. The time requirement per 0-TI-SXX-000-016.0 for closure of an open ABSCE door is within three minutes of notification. Although the individual found holding the door was unaware of the requirement of 0-TI-SXX-000-016.0 to close the door, communications were established and the Main Control Room (MCR), upon discovery of the 'Open Door', could have directed closure starting at the Time of Discovery if required. Since the MCR was aware the door was open, had communications established with personnel at the door, the door was capable of closure and not restricted, the three minute closure requirement of 0-TI-SXX-000-016.0 was met. Subsequently, the door was closed within approximately two minutes of notification to close. The closure of the door with these procedural measures met confirmed the integrity of the ABSCE and therefore Operability of ABGTS. Based on the above critical thinking, entry into LCO 3.7.12 Condition A, B, and E was retracted on August 22, 2021 at 2044 EDT. With the LCO conditions retracted and the above determination that at the Time of Discovery safety function was maintained, the Immediate Notification per 10 CFR 50.72 (b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D) was not required. The issue of Past Operability remains for instances in time that the door did not have appropriate compensatory measures in place. Any further notification required for this event will be submitted as a Licensee Event Report. Notified R2DO (Miller)

ENS 5538529 July 2021 23:51:00Columbia10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containmentAt 0922 PDT, on 07/28/21, the reactor building roof hatch was opened to support maintenance activities on the roof. Secondary containment differential pressure lowered and was recovered by the operating crew. Secondary containment differential pressure was maintained negative during the transient and was verified to have met technical specification requirements the whole time, however it was not identified at the time that the secondary containment was inoperable due to the roof hatch exceeding the allowable containment breech size and as such a TS 3.6.4.1.A entry was warranted. This report is being made pursuant to 10 CFR 50.72(a)(1)(ii) when it was identified that the secondary containment was inoperable while the roof hatch was open and a report should have been made under 10 CFR 50.72(b)(3)(v)(C) and (D) for loss of safety function. There were no radiological releases, system actuations, or isolations associated with this event. The licensee has notified the NRC Resident Inspector.
ENS 5537925 July 2021 16:38:00Sequoyah10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialAt 1238 EDT on July 25, 2021, the Unit 2 Ice Bed became INOPERABLE due to SR (Surveillance Requirement) 3.6.12.1 exceeding its surveillance interval. LCO (Limiting Condition for Operation) 3.6.12 was declared not met as required by SR 3.0.1. SR 3.6.12.1 to verify maximum ice bed temperature is less than or equal to 27 degrees F could not be completed due to a failed temperature recorder. The results of the backup method of temperature verification were verified satisfactory at 1258 EDT and the LCO condition was then exited. The ice bed is a single train system which functions to control radiation release and mitigate the consequences of an accident by scrubbing radioactive iodine and providing a heat sink to limit containment pressure within design limits, therefore the requirements of 10 CFR 50.72 (b) (3) (v) (C) and (D) were met. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 550989 February 2021 07:53:00Cooper10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentOn February 9, 2021, at 0153 CST, Cooper Nuclear Station experienced a spike in Secondary Containment differential pressure which exceeded the Technical Specifications Surveillance Requirements 3.6.4.1.1 limit of -0.25 inches of water gauge. Secondary Containment differential pressure oscillated coincident with barometric pressure oscillations. Three additional spikes occurred which exceed the Technical Specification limit. The duration of each spike was less than one minute. The last spike occurred at 0232 CST. Secondary Containment differential pressure has restored to Technical Specification limits and further investigation is ongoing. This unplanned Secondary Containment inoperability constitutes a condition reportable under 10CFR50.72(b)(3)(v)(C) and (D), "An event or condition that at the time of discovery could have prevented the fulfillment of the safety function of (Structures, Systems, and Components) SSCs that are needed to control the release of radioactive material and mitigate the consequences of an accident. The NRC Senior Resident Inspector has been informed.
ENS 549272 October 2020 13:45:00Millstone10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentAt 0945 hours (EDT) on 10/02/2020, with Millstone Unit 3 in Mode 4, Operations discovered a door in the Secondary Containment boundary blocked open. Investigation determined the door was blocked open at 1842 (EDT) on 10/01/2020, rendering Secondary Containment inoperable. The door was closed at 1002 ((EDT) on 10/02/2020), restoring Secondary Containment to operable status. Since Secondary Containment was rendered inoperable, Dominion Energy is reporting this as a condition that could have prevented the fulfillment of the safety function to control the release of radioactive material and mitigate the consequences of an accident. This condition is being reported as an eight hour report pursuant to 10 CFR 50.72 (b)(3)(v)(C) and (D). There was no release of radioactivity to the public. The NRC Senior Resident Inspector has been notified. With the door blocked open, the plant was in a 24-hour shutdown action statement. The state of Connecticut and local towns were notified.
ENS 5480024 July 2020 05:05:00Sequoyah10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialAt 0105 (EDT) on 7/24/20 it was discovered Unit 2 Ice Bed was INOPERABLE. Therefore, since this is a single train system the requirements of 50.72 (b)(3)(v)(C) and (D) have been met. This condition is being reported as an 8-hour non-emergency NRC Notification. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. This condition put the unit in a 48-hour LCO. The old chillers were put into service to bring the temperature of the ICE bed down. At 0833 EDT, the technical specification limit was no longer exceeded and the unit exited the LCO.
ENS 546901 May 2020 13:31:00Cooper10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentAt 0831 CDT, the Main Control Room received a 'Reactor Building 903 ft. Access Both Doors Open' alarm. Investigation found the interlock between the inner and outer doors did not prevent the opening of both doors while personnel were accessing the Reactor Building. The doors were immediately closed. Based on alarm times, both doors were open for less than one second. With both doors open, SR 3.6.4.1.3 was not met and Secondary Containment was declared inoperable. This unplanned Secondary Containment inoperability constitutes a condition reportable under 10 CFR 50.72(b)(3)(v)(c) and (d), 'An event or condition that at the time of discovery could have prevented the fulfillment of the safety function of SSCs that are needed to control the release of radioactive material and mitigate the consequences of an accident.' Secondary Containment was declared operable at 0836 CDT after independently verifying at least one Secondary Containment access door was closed. The NRC Senior Resident Inspector has been informed.
ENS 545675 March 2020 17:35:00Fermi10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentOn March 05, 2020, at 1235 EST, with the reactor at 100 percent core thermal power and steady state conditions, plant personnel notified the main control room that both doors in the secondary containment airlock on the reactor building fifth floor were opened simultaneously for a period of approximately three seconds (i.e., from 12:35:00 to 12:35:03 EST). The failure of this interlock, which is intended to prevent both doors from being opened simultaneously, resulted in the Technical Specification (TS) Surveillance Requirement (SR) 3 .6.4.1.3 not being met. The maximum secondary containment pressure observed during that time remained within TS limits. There were no radiological releases associated with this event. Declaring secondary containment inoperable as a result of not meeting TS SR 3.6.4.1.3 is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The licensee has notified the NRC Resident Inspector.
ENS 5445218 December 2019 14:08:00Fermi10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
HVAC
Standby Gas Treatment System
On December 18, 2019, at 0908 EST, with the East and Center Reactor Building HVAC (RBHVAC) trains in service, secondary containment pressure degraded to the point where the Technical Specification (TS) requirement for secondary containment pressure was not met and secondary containment was declared inoperable. Secondary containment pressure did not meet the TS required limit for approximately four minutes. The maximum secondary containment pressure observed during that time was approximately 0.064 inches of vacuum water gauge. Secondary containment pressure was returned to within the TS operability limit of greater than or equal to 0.125 inches of vacuum water gauge (TS SR 3.6.4.1.1) by starting Division 1 of the Standby Gas Treatment System (SGTS). Secondary containment was declared Operable at 0912 EST. A modulating damper associated with the Center train of RBHVAC was identified as not properly controlling; an investigation is in progress. RBHVAC was manually secured to support problem identification and resolution. Secondary containment pressure is currently stable with Division 1 SGTS in service. There were no radiological releases associated with this event. Declaring secondary containment inoperable is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector has been notified.
ENS 5429930 September 2019 02:28:00Fermi10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
HVAC
On September 29, 2019 at 2228 EDT, during a planned swap of Reactor Building HVAC trains, the exhaust fan discharge damper for the train being removed from service failed to close when the train was shutdown, which resulted in the Technical Specification (TS) for secondary containment pressure not being met for approximately 2 minutes and 15 seconds. The maximum secondary containment pressure observed during that time was approximately 0.1 inches of water gauge (positive). Secondary containment pressure was returned to within the TS operability limit of greater than or equal to 0.125 inches of vacuum water gauge (TS SR 3.6.4.1.1) by restarting the train of RBHVAC. Secondary containment pressure is currently stable. Secondary containment was declared Operable at 2235 EDT. There were no radiological releases associated with this event. Declaring secondary containment inoperable is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The Licensee has notified the NRC Resident Inspector.
ENS 5427111 September 2019 22:19:00Grand Gulf10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialPrimary containmentOn September 11, 2019 at 1719 CDT, plant personnel identified a condition in which the 208 foot elevation inner primary containment airlock door was not in its fully seated and latched position while the 208 foot elevation outer primary containment airlock door was opened. The 208 foot elevation outer containment airlock door was subsequently closed by the individual exiting the area. The time that both 208 foot elevation containment airlock doors were not in their fully seated and latched positions was less than 1 minute. Following this occurrence, maintenance personnel inspected the 208 foot elevation inner containment airlock door and re-positioned this door to its fully seated and latched position. There was no radioactive release as a result of this event. This condition requires an 8-hour non-emergency notification in accordance with 10CFR50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector has been notified.
ENS 542576 September 2019 02:15:00South Texas10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Coolant System

EN Revision Text: CONTAINMENT PENETRATION DISCOVERED NOT ISOLATED At 2115 CDT on 9/5/2019, an inside containment test connection and inoperable outside containment isolation valve were discovered to be open for a containment air sample penetration. This resulted in the containment penetration not being isolated. The inside containment test connection was closed at 2322 CDT on 9/5/2019.

This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and (D) and 10 CFR 50.72(b)(3)(ii)(B).

There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM PAUL BURTON TO HOWIE CROUCH AT 1342 EST ON 11/7/19 * * *

This event was originally reported on September 6, 2019 under 10 CFR 50.72(b)(3)(v)(C) and (D) and 10 CFR 50.72(b)(3)(ii)(B). Upon completion of the investigation of the event, it was determined that the event had insignificant safety consequences because the containment breach was disconnected from the Reactor Coolant System by a series of closed valves for the duration of the event. Additionally, the lines to the inside containment connection and the outside inoperable containment isolation valve that was found to be open as well as the main line connecting and passing through the penetration were one-inch diameter lines. Analysis determined that containment breaches that are less than a three-inch diameter do not lead to a large radiation release. The event did not place the plant in an unanalyzed condition that significantly degrades plant safety. Therefore, 10 CFR 50.72(b)(3)(ii)(B) did not apply to this event and this notification is to retract reporting under that criterion. The licensee notified the NRC Resident Inspector. Notified R4DO (Drake).

ENS 542015 August 2019 14:36:00Grand Gulf10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentOn August 5, 2019, at 0936 CDT, Grand Gulf entered Technical Specification (TS) 3.6.4.1 due to a Secondary Containment personnel door, 1A401B, not being able to meet its design function. Door 1A401B was unable to be closed and latched. This condition is being reported as a loss of safety function. The station also entered 05-S-01-EP-4, Auxiliary Building Control (Secondary Containment) to address Auxiliary Building differential pressure due to the opened Secondary Containment penetration. Actions were taken to close and latch Door 1A401B. Secondary Containment has been declared operable. TS 3.6.4.1 and 05-S-01-EP-4 were exited. The NRC Resident Inspector was notified of the condition.
ENS 5412720 June 2019 17:40:00Watts Bar10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialShield BuildingAt 1340 EDT on June 20, 2019, a breach in excess of allowable margin in the Unit 2 Shield Building annulus was identified. T.S. LCO 3.6.15, Condition A was entered. The breach is expected to be repaired within the 24 hours allowed LCO time. No other equipment issues were identified. The Shield Building ensures that the release of radioactive material from the containment atmosphere is restricted to those leakage paths and associated leakage rates assumed in the accident analysis during a Loss of Coolant Accident (LOCA). This event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(C). NRC Resident Inspector has been notified. The breach consists of a tear in a flexible boot seal for a penetration associated with the suction path for gas treatment fans. There is no release of radioactive material associated with this event.
ENS 5411111 June 2019 16:32:00Monticello10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary containmentAt 1132 CDT on 6/11/2019, both manual primary containment isolation valves in a one-inch service air line were found open. This resulted in an open primary containment penetration. Both valves are required to be closed for Primary Containment Isolation Valve Operability. Both valves were closed and independently verified closed at 1149 CDT on 6/11/2019. This is being reported under 10 CFR 50.72(b)(3)(v)(C) and (D), and 10 CFR 50.72(b)(3)(ii)(B). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee also notified the State of Minnesota State Duty Officer.
ENS 5409430 May 2019 02:10:00Fermi10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentOn May 29, 2019, at 2210 EDT, plant personnel notified the Main Control Room that both doors in the Secondary Containment Airlock on the Reactor Building First Floor were opened simultaneously for a period of approximately two seconds. This resulted in Technical Specification (TS) Surveillance Requirement (SR) 3.6.4.1.3 not being met. Secondary Containment pressure observed during that time remained unchanged and within TS limits. There were no radiological releases associated with this event. Declaring Secondary Containment inoperable as a result of not meeting TS SR 3.6.4.1.3 is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The licensee has notified the NRC Resident Inspector.
ENS 5407822 May 2019 06:56:00Susquehanna10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
HVAC

On 5/22/2019, the 'A' Control Structure Chiller (Div I) tripped due to a loss of (motor control center) MCC 0B136. The 'B' Control Structure Chiller was already inoperable due to Div II (Emergency Service Water) ESW being out of service for planned maintenance. With the loss of Control Structure HVAC System the ability to maintain temperatures in various spaces including relay rooms, Control Room Floor Cooling and Emergency Switchgear rooms was lost. The 'B' Control Structure Chiller was restarted at 0251 EDT and cooling was reestablished to the required areas, however the 'B' chiller is not considered operable at this time. Units 1 and 2 entered (Technical Specification) TS 3.0.3 at 0256 EDT and a controlled shutdown of both units commenced, Unit 2 at 0340 EDT and Unit 1 0350 EDT. This constitutes a TS required shutdown and requires a 4 hour (Emergency Notification System) ENS notification in accordance with 10 CFR 50.72(b)(2)(i). The failure also requires an 8 hour ENS notification in accordance with 10 CFR 50.72(b)(3)(v) due to the loss of a safety function. The licensee needs to restore the 'B' loop of ESW to exit the Limiting Condition of Operation (LCO). The licensee is currently performing a flow surveillance, once complete and assuming the data is acceptable, the licensee will be able to exit the LCO. The units are in a normal electrical lineup. The licensee will be notifying the state of Pennsylvania FEMA Operations Center. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 05/22/2019 AT 1302 FROM SCOTT MYRTHEL TO THOMAS KENDZIA * * *

On 5/22/2019 at 0601 EDT Susquehanna Steam Electric Station reported a shutdown had been commenced at 0340 EDT for Unit 2 and 0350 EDT for Unit 1 due to inoperability of both control structure chillers. Power has been restored to MCC 0B136, and at 0901 EDT the 'A' control structure chiller was declared operable and LCO 3.0.3 was exited. Power reduction for both units was halted at 0901 EDT and preparations for power restoration initiated. As of 1255 EDT on 5/22/2019, Unit 1 power is 94% and Unit 2 power is 92%. Notified the R1DO (Arner).

ENS 5406212 May 2019 15:39:00Grand Gulf10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Feedwater
Service water
Reactor Protection System

At 1039 CDT the reactor was manually (scrammed) due to a partial loss of plant service water. The loss of plant service water was caused by a loss of (balance of plant) BOP transformer 23. Reactor power was reduced in an attempt to restore pressure to plant service water. Reactor level is being maintained with condensate and feedwater. Reactor pressure is being maintained with bypass control valves. Standby Service Water A and B were manually initiated to supply cooling to Control Room A/C and (Engineered Safety Feature) ESF switchgear room coolers. The cause is under investigation. The NRC Resident Inspector has been notified. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical and also reported under 10 CFR 50.72(b)(3)(iv)(A), as any event or condition that results in actuation of RPS and Standby Service Water. The plant is currently in a normal electrical lineup.

  • * * UPDATE ON 5/12/19 AT 1846 EDT FROM GERRY ELLIS TO JEFFREY WHITED * * *

This is an update to the original notification. The Drywell and Containment exceeded the technical specification (TS) temperature limits of 135 degrees F (TS Limiting Condition of Operation (LCO) 3.6.5.5) and 95 degrees F (TS LCO 3.6.1.5), respectively. An 8-hour notification is being added for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material per 10 CFR 50.72(b)(3)(v)(C). Notified R4DO (Alexander).

ENS 5406112 May 2019 04:05:00Callaway10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
On 5/11/19, Callaway Energy Center entered Mode 4 at 1217 (CDT). At 2305, the door from the Auxiliary Building to the RAM Storage building was found blocked open. This door is an Auxiliary Building pressure boundary for the Emergency Exhaust system. The Emergency Exhaust system is required in Modes 1,2,3,4, and during movement of irradiated fuel assemblies in the Fuel Building. The door was being blocked open with a large ramp. This rendered the Emergency Exhaust system not capable of performing its design safety function. LCO (Limiting Conditions for Operation) 3.7.13.B was entered, and preparations to move the ramp commenced. LCO 3.7.13.B is for two Emergency Exhaust trains being inoperable due to an inoperable auxiliary building boundary. The allowed outage time is 24 hrs. to restore the boundary to Operable. The door was closed and LCO 3.7.13.B was exited at 0111 on 5/12/19. This event is reportable per 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (C) control the release of radioactive material, or (D) mitigate the consequences of an accident. The NRC Senior Resident has been notified.
ENS 540495 May 2019 19:05:00Cooper10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment

EN Revision Text: SECONDARY CONTAINMENT DECLARED INOPERABLE DUE TO POTENTIAL EQUIPMENT FAILURE At 1405 CDT, Secondary Containment differential pressure exceeded the Technical Specification limit due to a potential equipment failure. This required entry into (Limiting Condition of Operation) LCO 3.6.4.1 Condition A for Secondary Containment inoperability. An event or condition that could have prevented the fulfillment of a safety function requires an 8 hour report per 10 CFR 50.72(b)(3)(v)(C) for Control of Rad Release. Secondary Containment differential pressure was restored to greater than or equal to 0.25 inches vacuum, water gauge in accordance with plant procedures. Secondary Containment was declared operable at 1600 CDT. The issue has been entered in the Corrective Action Program and investigation of the cause is in progress. The NRC Senior Resident Inspector has been informed of this condition.

  • * * RETRACTION AT 1759 EDT ON 5/30/2019 FROM ROY GILES TO JEFF HERRERA * * *

CNS (Cooper Nuclear Station) is retracting the 8-hour notification made for event 54049 which occurred on May 5, 2019 at 1405 CDT. Subsequent evaluation determined that no equipment failure occurred. In addition, there were no procedure inadequacies or human performance issues identified. The indications observed were expected and part of a pre-planned evolution which included entry into a planned LCO for the Secondary Containment. The NRC Resident Inspector has been notified. Notified the R4DO (Kozal).

ENS 539681 April 2019 03:06:00Palo Verde10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Emergency Core Cooling System

At 2006 (MST), on 3/31/2019, the Palo Verde Nuclear Generating Station Unit 1 Shift Manager was informed that leakage was measured from the Train A Emergency Core Cooling System (ECCS) piping at approximately 100 ml/minute through a High Pressure Safety Injection (HPSI) A drain valve. This value exceeds the assumed 3000 ml/hour ECCS leakage for a large break loss of coolant accident analysis. At 0230 (MST) on April 1, 2019, the valve was flushed and the leakage reduced to 10 ml/minute (600 ml/hour) and was no longer above the limit of the safety analysis. This condition is being reported as an unanalyzed condition per 10 CFR 50.72(b)3)(ii)(B) and a condition that could have prevented the fulfillment of a safety function to the control the release of radioactive material per 10 CFR 50.72(b)(3)(v)(C). This event did not result in an abnormal release of radioactive material. Notification received by Caty Nolan and emailed to HOO.HOC@NRC.GOV The NRC asked a followup question: Why was the criterion for Control of Radioactive Material selected? per the PVNGS Unit 1 Shift Manager, this criterion was selected due to the potential of exceeding offsite dose projections, post recirculation, following a Design Basis Accident. The resident inspector has been notified.

  • * * UPDATE ON 05/15/19 AT 1417 EDT FROM SEAN DORNSEIF TO BETHANY CECERE * * *

An engineering evaluation concluded that the as-found ECCS leakage would not have degraded the performance of the Pump Room Exhaust Air Cleanup system; therefore, it remained operable. The evaluation also concluded that the as-found leakage was within the analysis margins for HPSI pump hydraulic performance and containment flood level following a Large Break Loss of Coolant Accident; therefore, the ECCS also remained operable. Based on the above information, the condition identified on March 31, 2019, was an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B), but did not prevent the fulfillment of the safety function of the structures or systems that are needed to control the release of radioactive material per 10 CFR 50.72(b)(3)(v)(C). The NRC resident inspectors have been informed. Notified R4DO (Proulx).

ENS 5388319 February 2019 17:53:00Fermi10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentOn February 19, 2019, at 1307 EST, with the reactor at 100 percent Core Thermal Power and steady state conditions, plant personnel notified the Main Control Room that both doors in the Secondary Containment Airlock on the Reactor Building Fifth Floor were opened simultaneously for a period of approximately five minutes (i.e., from 1253 to 1258 EST). The failure of this interlock, which is intended to prevent both doors from being opened simultaneously, resulted in the Technical Specification (TS) Surveillance Requirement (SR) 3.6.4.1.3 not being met. The maximum Secondary Containment pressure observed during that time remained within TS limits. There were no radiological releases associated with this event. Declaring Secondary Containment inoperable as a result of not meeting TS SR 3.6.4.1.3 is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The licensee has notified the NRC Resident Inspector. The repair to the failed interlock is in progress. As a compensatory measure signs are posted on the doors to notify personnel to not access the Reactor Building via those doors.
ENS 5385130 January 2019 15:10:00Dresden10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
Standby Gas Treatment System
At 0910 (CST) on January 30, 2019, the Dresden Station Heater Boiler 'B' tripped while placing the station Heater Boiler 'A' in service. With colder temperatures, the density of the supply air increased and contributed to a greater quantity of air entering the Reactor Building than what was previously being supplied with heating steam in service. The Reactor Building differential pressure (DP) degraded and dropped below 0.25 inches water column vacuum. This condition represents a failure to meet Technical Specification (TS) Surveillance Requirement 3.6.4.1.1. Entry into TS 3.6.4.1 Condition A was made due to Secondary Containment becoming inoperable. Standby Gas Treatment System was initiated to assist with Reactor Building DP control. Reactor Building DP was restored to greater than 0.25 inches water column vacuum. TS 3.6.4.1 Condition A was exited. This event is being reported under 10 CFR 50.72(b)(3)(v)(C), 'Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to ... control the release of radioactive material.' The NRC Resident Inspector has been notified.
ENS 5382816 January 2019 05:00:00FitzPatrick10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
Reactor Building Ventilation
Standby Gas Treatment System
On January 16, 2019, with James A. Fitzpatrick Nuclear Power Plant operating at 100 percent power, the Emergency and Plant Information Computer (EPIC) indicated that Secondary Containment differential pressure exceeded the Technical Specification Surveillance Requirement of greater than or equal to 0.25 inches of vacuum water gauge while isolating Reactor Building Ventilation. The Secondary Containment differential pressure was less than 0.25 inches of vacuum water gauge for approximately ten (10) seconds, and then immediately returned to greater than or equal to 0.25 inches of vacuum water gauge. This condition did not impact the leak tightness of Secondary Containment or the ability of the Standby Gas Treatment system to establish and maintain the required differential pressure. When Secondary Containment did not meet the Technical Specification Surveillance Requirement 3.6.4.1.1 for differential pressure, the Limiting Condition of Operation (LCO) was not met. Therefore, Secondary Containment was inoperable. This event is being reported under 10 CFR 50.72(b)(3)(v)(C). The licensee has notified the NRC Resident Inspector.
ENS 538111 January 2019 05:00:00Fermi10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Feedwater
Control Rod
On January 1, 2019 at approximately 0454 EST, while performing planned maintenance activities on the Feedwater Distributed Control System (FW DCS), it was discovered that the automatic trip instrumentation of the Gland Seal Exhauster (GSE) was inoperable. The automatic GSE trip is assumed in the safety analysis for the Control Rod Drop Accident (CRDA) and is required when Thermal Power is less than or equal to 10%. The automatic trip function of the GSE was inoperable for 1 minute, 19 seconds. No Control Rod movement occurred while the automatic trip of the GSE was inoperable. There was no adverse impact to public health and safety or to plant employees and there was no radiological release. This report is being made pursuant to 10CFR50.72(b)(3)(v)(C) and 10CFR50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified.
ENS 537785 December 2018 05:00:00FitzPatrick10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
Reactor Building Ventilation
Standby Gas Treatment System
At 1010 (EST) on December 5, 2018, Secondary Containment differential pressure exceeded the Technical Specification Surveillance Requirement of greater than or equal to 0.25 inches of vacuum water gauge. This condition existed for approximately 3 minutes before the differential pressure was restored to normal when the Standby Gas Treatment system was manually initiated. This event was caused by a trip of the service air compressor 39AC-2A. The loss of instrument air pressure caused Reactor Building ventilation to isolate and raise Secondary Containment differential pressure. The instrument air pressure was restored when 39AC-2A was isolated and the two backup air compressors started. This condition did not impact the leak tightness of Secondary Containment or the ability of the Standby Gas Treatment system to establish and maintain the required differential pressure. When Secondary Containment did not meet the Technical Specification Surveillance Requirement 3.6.4.1.1 for differential pressure, the Limiting Condition of Operation (LCO) was not met. Therefore, Secondary Containment was inoperable. This event is being reported under 10 CFR 50.72(b)(3)(v)(C). The licensee notified the NRC Resident Inspector.
ENS 5375627 November 2018 06:00:00River Bend10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialMain Steam Isolation Valve
Safety Relief Valve
Main Steam

EN Revision Text: INOPERABILITY OF EQUIPMENT FOR CONTROL OF RADIOLOGICAL RELEASE At 2130 CST on 11/27/2018, Division 1 Main Steam Positive Leakage Control System (MS-PLCS) was declared inoperable because of a leaking check valve that caused excessive cycling of the associated air compressor. Division 2 MS-PLCS had been declared inoperable on 11/27/2018 at 1400 CST when a pressure control valve in the system exceeded the maximum allowable stroke time. Because MS-PLCS supplements the isolation function of the main steam isolation valves (MSIVs) by processing fission products that could leak through the closed MSIVs, both divisions of MS-PLCS inoperable at the same time represents a condition that could prevent the fulfillment of a safety function of an SSC (Structures, Systems and Components) that is needed to control the release of radioactive material. The station diesel air compressor is available to supply backup air to the safety relief valves as required by the Technical Requirements Manual." (This is associated with operability of the safety relief valves, due to the inoperable MS-PLCS air compressor.) The unit is in a 7 day shutdown Limiting Condition for Operation (LCO), 1-TS1-18-Div 1 & 2 MSPLCS-685, for the two divisions of MS-PLCS being inoperable. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 12/03/18 AT 1551 EST FROM TIM GATES TO BETHANY CECERE * * *

This event was initially reported under 10 CFR 50.72(b)(3)(v)(C) as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function to control the release of radioactive material. Division I was declared inoperable due to a failed component. Division II was declared inoperable due to a pressure control valve in the system exceeding the maximum allowable time to close by 0.50 seconds. An engineering evaluation has since been performed and concluded that the 2 second maximum allowable time to close was based on the pressure control valve being classified as a rapid closure valve and was established from the original baseline data of 0.50 seconds. This baseline data is an administrative target value per the In-Service Testing Program. There are no technical specification requirements associated with the 2 second closure time. The engineering evaluation also determined that the volume of air supplied through the pressure control valve during the extra 0.50 seconds of valve closure would have an inconsequential effect on the pressure within the volume of leakage barrier between the Main Steam Isolation Valves associated with the MS-PLCS pressure control valve or have any effect on containment over-pressurization. Based on the information provided by the engineering evaluation, the Division II MS-PLCS has been declared operable-degraded non-conforming since time of initial discovery. Consequently, this event is not reportable as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function. The (NRC) Resident Inspector has been notified via e-mail. Notified the R4DO (Gaddy).

ENS 5375124 November 2018 05:00:00Sequoyah10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containment
Auxiliary Building Gas Treatment System
Emergency Core Cooling System
At 1420 (EST) on November 24, 2018, operators discovered that a door was blocked open creating a breach of the auxiliary building secondary containment enclosure (ABSCE) boundary that exceeded the allowed ABSCE breach margin (of three minutes). As a result, Unit 1 entered Technical Specification Limiting Condition of Operation (LCO) 3.7.12 Condition B for two trains of Auxiliary Building Gas Treatment System (ABGTS) inoperable due to an inoperable ABSCE boundary in MODE 1, 2, 3, or 4, and both Units entered Condition E for one required ABGTS train inoperable with fuel stored in the spent fuel pool. In MODES 1, 2, 3, and 4, the analysis of the loss of coolant accident (LOCA) assumes that radioactive materials leaked from the Emergency Core Cooling System are filtered and absorbed by the ABGTS. For the fuel handling accident, the analysis assumes that the ABSCE boundary is capable of being established to ensure releases from the auxiliary and containment buildings are consistent with the dose consequence analysis. The event is reportable in accordance with 10 CFR 50.72(b)(3)(v) as an event or condition that could have prevented fulfillment of the safety function of structures or systems that are needed to: (C) control the release of radioactive material and (D) mitigate the consequences of an accident. No actual LOCA or fuel handling accident occurred while both trains of ABGTS were inoperable. The condition had no impact on the health and safety of the public. The NRC Resident Inspector has been notified. This situation occurred because of maintenance activities. A breeching permit had been initiated however, the required personnel to ensure the door could be closed within the required three minutes were not assigned. The door was closed approximately 15 minutes after the situation was noticed.
ENS 5359711 September 2018 05:00:00Monticello10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Core Spray
Emergency Core Cooling System
On 9/10/2018, the 11 Core Spray (CSP) loop was placed in service to support quarterly surveillance testing. With the 11 CSP pump in service it was identified that the check valves isolating the 11 CSP system from the keep fill supply were leaking by. At 1129 CDT on 9/11/2018, it was identified that this leakage may have exceeded the leakage rate assumptions made in the dose analysis calculation for emergency core cooling system (ECCS) leakage outside containment following a loss of coolant accident (LOCA). Therefore, this is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades plant safety and 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. The potential ECCS leak pathway has been isolated. There is no impact to health and safety of the public. The NRC Resident Inspector has been notified.
ENS 534969 July 2018 05:00:00Duane Arnold10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentAt approximately 1334 CDT on 7/9/18, both doors of a Secondary Containment Airlock were reported to be open simultaneously for a period of less than 3 seconds. The brief time that the doors were simultaneously open constituted an inoperable condition of Secondary Containment. Secondary Containment was immediately restored to operable by closing the airlock doors. Subsequently, the airlock interlock was verified to operate correctly. This event is being reported pursuant of 10 CFR 50.72(b)(3)(v)(C). The Senior NRC Resident Inspector has been notified.
ENS 5343531 May 2018 18:20:00Fermi10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary containment
Reactor Water Cleanup
On May 31, 2018 at 1420 EDT, the Reactor Water Cleanup (RWCU) System Isolation Differential Flow - High function was declared inoperable as a result of indicating downscale. This condition would have prevented the primary containment isolation valves for the RWCU system from automatically isolating on a high differential flow condition. At 1519 EDT, RWCU was shutdown and the affected penetration flow paths were isolated in accordance with station procedures per Fermi Technical Specifications. The cause of the event is under investigation. There was no radiological release associated with this event. All other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators throughout the event. However, the condition is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C), and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.
ENS 5342927 May 2018 10:30:00Fermi10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary containment
Reactor Water Cleanup
On May 27, 2018 at 0630 EDT, the Reactor Water Cleanup (RWCU) System Isolation Differential Flow - High function was declared inoperable as a result of indicating downscale. This condition would have prevented the primary containment isolation valves for the RWCU system from automatically isolating on a high differential flow instrumentation signal. At 0753, RWCU was shutdown and the affected penetration flow paths were isolated in accordance with station procedures per Fermi Technical Specifications. The cause of the event is under investigation. There was no radiological release associated with this event. All other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators throughout the event. However, the condition is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.
ENS 5339811 May 2018 14:11:00Watts Bar10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Shield Building
Emergency Gas Treatment System
At 1011 EDT on May 11, 2018, Containment Shield Building Annulus differential pressure exceeded the required limit. The Shield Building was declared inoperable requiring entry into Technical Specification (TS) 3.6.15 Conditions A and B. The event was initiated by failure of the operating annulus vacuum fan. Main Control Room Operators manually started the stand-by annulus vacuum fan to recover pressure. Shield Building Annulus differential pressure was restored to the required value at 1016 EDT and TS 3.6.15 Condition A and B were exited on May 11, 2018 at 1016 EDT. The failure mechanism for the annulus vacuum fan is being investigated. The Containment Shield Building ensures the release of radioactive material from the containment atmosphere is restricted to those leakage paths and associated leakage rates assumed in the accident analysis during a Loss of Coolant Accident (LOCA). The Emergency Gas Treatment System (EGTS) would have automatically started and performed its design function to maintain the Shield Building Annulus differential pressure within required limits. The event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident has been notified.
ENS 533175 April 2018 16:17:00Grand Gulf10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary containmentOn Thursday, April 5, 2018, at approximately 1117 hours Central Daylight Time, Entergy contract personnel opened the personnel hatch allowing access to the roof of the Secondary Containment Building for the purposes of performing an inspection of various items located on the roof. During the time period the individuals were on the roof, the hatch was left open. An individual was adjacent to the door with a radio and had constant communication link with the control room operator. Pursuant 10 CFR 50.72(b)(3)(v)(C), and 10 CFR 50.72(b)(3)(v)(D) this event is being reported as an event or condition that could have prevented the fulfillment of a safety function. Because the site had an individual briefed and at the door in constant communications with the control room to close the hatch if condition required such an action, this event is not viewed as an actual loss of safety function. The NRC Resident Inspector was notified.
ENS 533103 April 2018 04:19:00Susquehanna10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containmentOn April 3, 2018 at 0019 (EDT), the Susquehanna control room received indication that a loss of Secondary Containment Zone 3 differential pressure had occurred. Control room operators noted the loss following completion of surveillance testing. The cause is under investigation. Zone 3 differential pressure was restored to greater than 0.25 inches WC (water column) at 0145 (EDT). Zone 3 differential pressures being less than 0.25 inches WC constitutes a loss of Secondary Containment based on not meeting requirements of SR (Surveillance Requirement) 3.6.4.1.1. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG-1022, Revision 3, Section 3.2.7, as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The NRC Resident Inspector has been notified.
ENS 5330431 March 2018 07:06:00Grand Gulf10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary containment
Standby Gas Treatment System
At 0206 (CDT) on March 31, 2018, with the plant in Mode 1 at 100% rated core thermal power, Grand Gulf Nuclear Station experienced a loss of Secondary Containment. During the performance of a Standby Gas Treatment System (SGTS) drawn down test with Auxiliary Building train bay door (1A319A) as the secondary containment boundary, Grand Gulf was unable to maintain secondary containment pressure, as required by SR (surveillance requirement) 3.6.4.1.4, greater than or equal to 0.266 inches of water vacuum for 1 hour. Following initial vacuum draw down, secondary containment pressure degraded to 0.225 inches of water vacuum with operators in the field reporting air leakage from door 1A319A. The test was secured and Secondary Containment was declared inoperable and Technical Specification 3.6.1.4 A.1 was entered. Following completion of the failed surveillance test, Secondary Containment was returned to an operable status at 0315 hours on March 31, 2018, by returning the system to a previously known operable configuration by closing doors 1A310, 1A312 and 1A319. This is being report under 10 CFR 50.72(b)(3)(v)(C). The licensee has notified the NRC Resident Inspector.
ENS 5330330 March 2018 18:05:00Clinton10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary containmentOn March 30, 2018 at 1305 CDT, with the reactor at 98 percent core thermal power and steady state conditions, plant personnel identified that both doors of the containment personnel airlock were open simultaneously due to failure of the interlock. Personnel were at both the outside and inside doors. Immediate action was taken to close the inner containment personnel airlock door and it was verified closed. Both doors of the containment personnel airlock were open for less than one minute. There was no radioactive release as a result of the event. The cause of the interlock failure is under investigation. This condition requires an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(ii)(A), the condition of the nuclear power plant, including its principal safety barriers (primary containment), being seriously degraded. This condition is also reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector was notified.