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05000482/FIN-2018010-042018Q3Wolf CreekFailure to Identify 125 VDC Equalizing Voltage Exceeded Design RequirementsThe team identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to verify or check the adequacy of design calculation NK-E-001, 125 Volt Direct-Current (VDC) Class 1E Battery System Sizing, Voltage Drop and Short Circuit Studies, Revision 4. The licensee failed to recognize that the actual 125 VDC Class 1E bus voltages had exceeded the maximum design limit voltages for downstream equipment identified in the calculation, and they had not placed any limits on voltages which could exceed the design limit of 140 VDC on the Class 1E System components.
05000482/FIN-2018010-032018Q3Wolf CreekFailure to Correct Reoccurring Problems with Time Critical/Sensitive Action ActivitiesThe team identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the licensees failure to correct reoccurring problems with completing Time Critical/Time Sensitive Action issues.
05000482/FIN-2018010-022018Q3Wolf CreekFailure to Establish an Adequate Procedure for Operator Time Critical Actions ValidationThe team identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to have an adequate Procedure. Procedure AI 21-016, Operator Time Critical Actions Validation, Revision 14, Attachment B Time Sensitive Action List, does not have unique identifiers for cross referencing the records to the procedure.
05000482/FIN-2018010-012018Q3Wolf CreekFailure to Follow ProceduresThe team identified two examples of a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to follow procedures.
05000530/FIN-2018003-012018Q3Palo VerdeFailure to Maintain Command and Control During a Feedwater Control Valve MalfunctionWhile reviewing the licensee response to a Unit 3 feedwater pump trip, reactor cutback, reactor trip, and main steam isolation system actuation on June 27, 2018, the inspectors identified that the licensee did not meet the command and control standards outlined in station Procedure 40DP-9OP02 Conduct of Operations, Revision 72. Specifically, senior reactor operators in the control room did not effectively coordinate manual main feedwater output adjustments in the control room or operator actions in the field in response to an apparent valve failure with the activities of non-licensed operators locally evaluating the equipment condition in the field. These uncoordinated actions resulted in a significant plant transient
05000482/FIN-2018010-052018Q3Wolf CreekLicensee-Identified ViolationThis violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, Measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected.Contrary to the above, prior to 2015, the licensee failed to promptly identify and correct a repetitive deficiency or non-conformance. Specifically, the licensee had identified a leaking flange on the residual heat removal heat exchanger since 1997. Prior to 1997 a different data base had been used to record boric acid leakage, and the data was not available during the inspection.Over the years since plant startup, the licensee had been diligent in completing boric acid evaluations on the leaking residual heat removal heat exchanger flange, indicating minimal wastage of the flange closure studs and nuts that had been subjected to boric acid. Corrective actions included cleaning up the boric acid leakage, and checking or re-torqueing the closure nuts. These measures did not correct the problem of the leaking heat exchanger flange. In 2015 the licensee completed an in-depth engineering evaluation of the leaking flange, including discussions with the heat exchanger manufacturer. New corrective measures included changing the torque values on the closure studs and nuts. The licensee is still evaluating the results of the corrective actions taken to preclude further leakage.
05000498/FIN-2018002-012018Q2South TexasLicensee-Identified ViolationThis violation of very low safety significance was identified by the licensee, has been entered into the licensees corrective action program and is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy. Violation: Technical Specification 6.8.1.a requires that, Written procedures shall be established, implemented, and maintained covering the activities referenced below: The applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Section 9.a, Procedures for Performing Maintenance, states, in part, that Maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. The licensee established Procedure COM-0001, Conduct of Maintenance, to guide maintenance craft on what to do if a condition or issue arises during a maintenance activity. Specifically, Section 1.4 Supervisor Responsibilities, states, in part, that, If we cannot find the problem with the component or piece of equipment, the issue must be raised to the Division Manager/General Supervisor BEFORE we close the work control document AND return the equipment to operations. Contrary to the above, on March 10, 2017, Unit 1 E1B undervoltage relay was found outside the technical specification acceptance criteria, and was retested until the relay it was back in tolerance and placed back into service (declared operable) instead of raising the issue up to the division manager for further evaluation. The issue was discussed with the electrical maintenance supervisor and the findings were documented in Condition Report 17-12616. The relay was declared operable and placed back into service. Subsequently, after review of the condition report, approximately 99 hours after the relay was declared inoperable, the relay was replaced, and the system declared operable. Significance/Severity Level: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the undervoltage relay was outside its tolerance and placed back into service without correcting the cause of being outside its tolerance. The inspectors assessed the significance of the finding using Exhibit 2, Mitigating Systems Screening Questions, of Inspection Manual Chapter 0609, Appendix A, Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, and determined this finding is not a deficiency affecting the design or qualification of a mitigating structure, system, and component that maintained its operability or functionality; the finding does not represent a loss of system and/or function; the finding does not represent an actual loss of function of at least a single train for greater than its Technical Specification-allowed outage time; and the finding does not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green). Corrective Action Reference: Condition Report 17-12616
05000482/FIN-2018002-032018Q2Wolf CreekFailure to Adequately Implement Instrumentation and Controls Surveillance ProceduresA self-revealed Green NCV of 10 CFR Part 50, Criterion V, Instructions, Procedures, and Drawings, was identified when the licensee failed to adequately implement surveillance procedures that affected safety-related equipment and plant stability. Specifically, the licensee failed to adequately implement testing and calibration procedures for pressurizer level instrumentation. This resulted in two letdown isolation signals, securing of pressurizer heaters, and a pressurizer level transient on March 29, 2018.
05000482/FIN-2018002-022018Q2Wolf CreekFailure to Maintain Adequate Pressurization of the Control Room EnvelopeA self-revealed Green NCV of 10 CFR Part 50, Criterion III, Design Control, was identified when the licensee failed to adequately recognize that the cable spreading room floor was a control building ventilation isolation boundary. Specifically, the licensee cut openings in the floor/ceiling between the 2,032 foot and 2,016 foot elevations of the control building and the impact on the control room envelopes ability to pressurize was not recognized. This was a primary contributor to the train B control room emergency ventilation system being unable to maintain the appropriate pressure in the control room envelope.
05000482/FIN-2018002-012018Q2Wolf CreekAnnouncement of an NRC Inspectors Presence by Station PersonnelThe inspectors identified a Severity Level IV non-cited violation (NCV) of 10 CFR 50.70(b)(4), Inspections, associated with the licensees failure to ensure the arrival and presence of NRC Inspectors, who had been properly authorized facility access as described in 10 CFR 50.70(b)(3), were not announced or otherwise communicated by its employees or contractors to other persons at the facility without a specific request by the NRC inspector. Specifically, a contract radiation protection technician entered the spent fuel pool building where the resident inspector was present and observing core offload activities, and the technician informed members of a work crew of the whereabouts of an NRC radiation protection inspection team without being requested to do so; this impacts the NRCs ability to regulate and perform unannounced inspections.
05000445/FIN-2018001-052018Q1Comanche PeakFailure to Correct a Significant Condition Adverse to QualityThe inspectors identified a Green,non-cited violation of 10CFR 50, Appendix B, Criterion XVI, Corrective Action, associated with the licensees failure to take corrective action for the identified cause of a significant condition adverse to quality. Specifically, a feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The licensee determined that the cause was an inadequate procedure for performing maintenance on the feedwater bypass control valves, but failed to correct the inadequate procedure after identifying it as the cause of a control valve failure and a turbine trip. This finding was entered into the licensees corrective action program as Condition Report CR-2018-000959.
05000445/FIN-2018001-042018Q1Comanche PeakInadequate Maintenance Procedure for Feedwater ValvesThe inspectors reviewed a self-revealed Green,non-cited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to prescribe adequate procedures for performing maintenance on the feedwater bypass control valves. Specifically, the licensees procedure failed to specify the correct torque on the handwheel screw locknut, resulting in a loose locknut which led to a control valve failure and a turbine trip. This finding was entered into the licensees corrective action program as Condition Report CR-2017-009139.
05000445/FIN-2018001-032018Q1Comanche PeakFailure to Provide an Adequate ProcedureThe inspectors identified a Green,non-cited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to provide procedures appropriate to the circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C Equipment, did not contain adequate instructions for wiring current to pressure (I/P) converters for safety related components which resulted in the steam generator atmospheric relief valve I/P converters being placed in a seismically unqualified configuration. This finding was entered into the licensees corrective action program as Condition Report CR-2017-011922.
05000445/FIN-2018001-022018Q1Comanche PeakFailure to Incorporate Design Information Into System Test ProceduresThe inspectors identified a Green,non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the licensees failure to ensure that station test procedures incorporated all requirements contained in applicable design documents. Specifically, the stations test procedures for the component cooling water system failed to test the safeguards loops supply and return train isolation valves for leakage. Excess leakage from these valves could prevent the performance of a safety function. This finding was entered into the licensees corrective action program as Condition Report CR-2017-012024.
05000445/FIN-2018001-012018Q1Comanche PeakFailure to Follow Commercial Grade Dedication ProcessThe inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to accomplish activities affecting quality in accordance with documented procedures. Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms to safety related without following the requirements of station procedure ECE-6.02-03, Critical Characteristics Development. The licensee entered this issue into the corrective action program as Condition Reports CR-CR-2016-009733 and CR-2017-007811.
05000275/FIN-2017002-022017Q2Diablo CanyonFailure to Conduct Required Biennial Medical Examinations Within Two YearsSL -IV. The inspectors identified a Severity Level IV, non -cited violation of 10 CFR 55.21, Medical Examination, for the licensees failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1) requirements was conducted every 2 years for two licensed senior operators. Specifically, one licensed senior operator exceeded the two- year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017. A second licensed senior operator exceeded the 2 -year medical examination requirement by 4 months between November 19, 2016, and April 6, 2017. As a corrective action, the licensee has conducted the required medical examination for one senior operator and initiated a license termination request for the other senior operator. This issue was entered into the licensees corrective action program as Notification 50912407. The failure of the facility licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two operators compromised the facility licensees ability to assure conformance to medical standards, detect non -conforming medical conditions, and report non-conformances to the NRC. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators. This section states, Severity Level IV violations involve, for example ... (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Condit ions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition. No cross -cutting aspect was assigned because the violation was processed using traditional enforcement.
05000275/FIN-2017002-032017Q2Diablo CanyonFailure to Report a Permanent Medical Condition Within 30 DaysSL -IV. The inspectors identified a Severity Level IV, non -cited violation of 10 CFR 55.25, Incapacitation Because of Disability or Illness, for the licensees failure to notify the NRC within 30 days of a change to one licensed senior operators medical condition. Specifically, the licensed senior operator developed a permanent medical condition which caused him to permanently leave the site on December 1, 2014, and transition into a long- term disability program on April 23, 2015. The licensee did not notify the NRC of this change in medical condition. As a corrective action, the licensee initiated a license termination request for the affected operator, effective April 6, 2017. This issue was entered into the licensees corrective action program as Notification 50912407. The failure of the facility licensee to notify the NRC within 30 days of a change in a licensed senior operators medical condition was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to report 4 changes in a licensed senior operators medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators. This section states, Severity Level IV violations involve, for example (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition. No cross -cutting aspect was assigned because the violation was processed using traditional enforcement
05000445/FIN-2017002-012017Q2Comanche PeakFailure to Control Transient Combustible Material in Accordance with a Fire Protection ProcedureGreen. The inspectors identified a non- cited violation of Operating Licenses NPF -87 and NP F-89, License Condition 2.G, Fire Protection Program, for the failure to control transient combustibles in accordance with the station s fire protection report. Specifically, Fire Protection Report, Revision 29, Section 5.3.8, Fire Area EO Control Room, includes Deviation 3c -1, Control Room Missile Door, which requires, in part, that since the control room missile door in the west wall is not a 3 -hour rated fire door, the area of the turbine deck within 100 feet of the door is to be void of combustibles. Contrary to this, the licensee allowed storage of combustible materials in this area without required compensatory measures. This issue does not represent an immediate safety concern because the licensee removed the combustible materials upon identification. The licensee entered this issue into corrective action program as Condition Report CR -2017 -5564. The failure to control transient combustible material in accordance with the approved fire protection report is a performance deficiency. The performance deficiency was more than minor and therefore a finding because it was associated with the protection against external factors attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the introduction of transient combustible materials decreased the external event mitigation for fire prevention. Using NRC Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, June 19, 2012, the inspectors determined that the finding pertained to a failure to adequately implement fire prevention and administrative controls for transient combustible materials. As a result, the inspectors were directed to Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process, September 20, 2013. The inspectors evaluated the finding through Appendix F, Attachment 1, Fir e Protection Significance Determination Process Worksheet, September 20, 2013, and determined that the finding was of very low safety consequence (Green) because the Fire Prevention and Administrative Controls finding would not prevent the reactor from re aching and maintaining a safe shutdown condition. The finding has a problem identification and resolution cross -cutting aspect associated with resolution, in that, the licensee failed to take effective corrective actions to address issues in a timely manner. 3 Specifically, the licensee had previously identified this issue in Condition Report CR- 2014010224 but had failed to take corrective actions to address it (P.3)
05000445/FIN-2017002-032017Q2Comanche PeakRelays not Environmentally QualifiedGreen. The inspectors identified a non- cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, associated with the licensees failure to assure that design changes were subject to design control measures commensurate with those applied to the original design. Specifically, the licensee changed internal components for safety -related, steam generator atmospheric relief valve booster relays but failed to verify that these new components could withstand the environment created during a high energy line break. This issue does not represent an immediate safety concern because the licensee performed an operability determination which established a reasonable expectation for operability, and implemented corrective actions to replace the relays with qualified relays. The licensee 4 entered this issue into the corrective action program for resolution as Condition Report CR- 2017- 006236. The failure to ensure that changes to the facility were subject to design control measures commensurate with those applied to the original design was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At -Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because the finding: (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality, (2) did not represent a loss of system and/or function, (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out -of-service for longer than their technical specification allowed outage time, and (4) does not represent an actual loss of function of one or more non- technical specification trains of equipment designated as high safety -significant for greater than 24 hours in accordance with the licensees maintenance rule program. The inspectors did not assign a cross -cutting aspect because the performance deficiency was not reflective of present performance
05000445/FIN-2017002-042017Q2Comanche PeakFailure to Adequately Assess Risk and Implement Risk Management Actions for Proposed MaintenaneGreen. The inspectors identified a non- cited violation of 10 CFR 50.65(a)(4), Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees failure to adequately assess risk and implement required risk management actions for a planned maintenance activity. Specifically, the licensee failed to evaluate the risk and implement required risk management actions associated with disabling a hazard barrier and breeching the control room envelope when blocking open door E -40A. This issue did not represent an immediate safety concern because, at the time of identification, the licensee stopped the activity and secured the door. The licensee entered this issue into the corrective action program for resolution as Condition Report CR- 2017- 006019. The failure to adequately assess the risk and implement required risk management actions for proposed maintenance activities was a performance deficiency. This performance deficiency was more than minor, and therefore a finding, because it was associated with the configuration control attribute o f the Barrier Integrity Cornerstone and affected the associated objective to ensure physical design barriers protect the public from radionuclide releases caused by accidents or events. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, dated May 19, 2005, Flowchart 2, Assessment of Risk Management Actions, the inspectors determined the need to calculate the risk deficit to determine the significance of this issue. A senior reactor analyst determined the finding to have very low safety significance (Green) based on combining the effects of the degradation of the radiological barrier and tornado missile barrier functions. The analyst performed a qualitative review of the screening criteria in Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At -Power, for the degradation of the radiological barrier function for the control room and considered the short exposure time (2.9E -5 years) and the Comanche Peak specific high winds frequency (3.0E -4/year) for the tornado missile barrier function of the control room to determine that the incremental core damage probability deficit and the incremental large early release probability deficit were less than 1E -6 and 1E -7, respectively. The finding has a human performance cross -cutting aspect associated with procedure adherence, in that operations personnel failed to follow procedures when allowing door E -40A to be opened
05000445/FIN-2017002-052017Q2Comanche PeakFailure to Translate Design Requirements Into the As Built FacilityGreen. The inspectors identified a non- cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, associated with the licensees failure to assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structure, systems and components to which this appendix applies, were correctly translated into specifications, drawings, procedures, and instructions. Specifically, from initial construction through March 2017, the licensee failed to fully incorporate applicable moderate energy line break design requirements for fire protection piping located in the vicinity of the station service water pumps, the latter which are needed to ensure the capability to shut down the reactor and maintain it in a safe shutdown condition following a moderate energy line break. This issue does not represent an immediate safety concern because when the lines were identified the licensee took prompt action to isolate and depressurize them, and the licensee has implemented plant modifications. The licensee entered this issue into the corrective action program as Condition Report CR -2016- 008147. The failure to incorporate applicable design requirements into specifications for moderate energy line break protection was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, from initial construction through March 2017, the licensee failed to fully incorporate applicable design requirements for components needed to ensure the capability to shut down the reactor and maintain it in a safe shutdown condition following a moderate energy line break. Using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated July 1, 2012, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At -Power , Exhibit 2, Mitigating Systems Screening Questions, dated 5 October 7, 2016, the inspectors determined the finding required a detailed risk evaluation because the finding involved a deficiency affecting the design and qualification of a mitigating structure, system, or component, and resulted in a loss of operability, and represented an actual loss of function of at least a single train for longer than its allowed outage time. A senior reactor analysts from Region IV performed a detailed risk evaluation and determined that the bounding increase in core damage frequency for this issue was 5.1E -8/year for Unit 1 and 2.9E -10/year for Unit 2, and was therefore of very low safety significance (Green ). The inspectors did not assign a cross -cutting aspect because the performance deficiency was not reflective of present performance
05000445/FIN-2017002-062017Q2Comanche PeakUnanalyzed Condition Involving Potential Moderate Energy Line BreakInspection Scope On September 13, 2016, based on initial observations by NRC inspectors, the licensee determined that pressurized fire protection piping in the service water intake structure was not properly shielded for moderate energy line break protection of service water components which resulted in inoperability of one train of service water for both Unit 1 and Unit 2. During extent of condition walk downs conducted on October 6, 2016, October 10, 2016, November 17, 2016, December 5, 2016, and December 22, 2016, additional piping in the Unit 1 and Unit 2 safeguards and auxiliary buildings was found to not be shielded correctly as well, resulting in inoperability of one train of various safety related equipment for both units. The licensee determined the most likely cause of this event was that the methodology used to conduct the initial moderate energy line break walk downs was flawed and allowed some threats to be missed. The licensees corrective actions include shielding the affected piping, performing a 100 percent walk down of rooms containing moderate energy line break piping identified for shielding, and revising the systems interaction program maintenance procedure. These activities constituted completion of one event follow -up sample, as defined in Inspection Procedure 71153. b. Findings Introduction. The inspectors identified a non- cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, associated with the licensees failure to assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structure, systems and components to which this appendix applies, were correctly translated into specifications, drawings, procedures, and instructions. Specifically, from initial construction through March 2017, the licensee failed to fully incorporate applicable design requirements for components needed to ensure the capability to shut down the reactor and maintain it in a safe shutdown condition following a moderate energy line break. Description. On September 13, 2016, inspectors performed walkdowns in the service water intake structure and identified a vertical run of unshielded, pressurized fire protection piping that appeared to pose a moderate energy line break threat to the service water pumps. Inspectors determined that in the event of a moderate energy line break crack along any portion of the unshielded piping, the resultant spray had the potential to impact the function of any one of the four service water pumps. However, only one train would have been affected during the event due to the physical configuration/separation relative to the source line and target pumps and/or associated motor control centers that support pump operation. Inspectors informed the licensee of their concern. Engineering personnel performed a subsequent walkdown of the intake structure and determined that the identified piping was not correctly shielded and operability of the service water pumps was in question. The licensee took immediate action to isolate and depressurize the fire protection line in question which addressed the operability concern. The licensee entered this issue into the station corrective action program as Condition Report CR -2016 -008147 for resolution. Part of the licensees actions was to perform extent of condition walkdowns for unshielded moderate energy piping in the safeguards building for Unit 1 and 2. During the extent of condition walk downs conducted on October 6, 2016, October 10, 2016, November 17, 2016, December 5, 2016, and December 22, 2016, additional piping in the Unit 1 and Unit 2 safeguards and auxiliary buildings was found to not be appropriately shielded against a moderate energy line break, resulting in the inoperability of various safety related equipment for both units. Unit 2 Train B 480 VAC motor control center 2EB2- 1 (Unit 2 Train B emergency core cooling, battery charger, containment spray, and containment isolation valve equipment) Unit 1 Train B 480V MCC 1EB4- 2, and Unit 1 Train B Distribution Panel 1ED2- 2 (Unit 1 Train B safety -related pumps, panels, sequencer, and transformers) Unit 1 Train B 480V MCC 1 EB4- 1 (Unit 1 Train B safety -related pumps, valves, fans, battery chargers, and transformers) Unit 2 Train B 480V MCC 2E134- 1 (Unit 2 Train B safety -related pumps, valves, fans, battery chargers, and transformer) Unit 1, Train B 480V MCC 1E84- 1 (Unit 1 Train B safety -related pumps, valves, fans, battery chargers, and transformers) In each of these instances the licensee took prompt action to isolate and depressurize the identified moderate energy piping pending modification. The licensee subsequently determined that the most probable cause of the issue was the use of a flawed methodology during the initial moderate energy piping walkdowns conducted in 1989. The licensee reported this issue to NRC in Event Report 52239, and Licensee Event Report 16 -002- 00. Analyses. The failure to incorporate applicable design requirements into specifications for moderate energy line break protection was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, from initial construction through March 2017, the licensee failed to fully incorporate applicable design requirements for components needed to ensure the capability to shut down the reactor and maintain it in a safe shutdown condition following a moderate energy line break. Using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated July 1, 2012, and Inspection Manual Chapter 0609, Appendix A , Significance Determination Process for Findings At -Power , Exhibit 2, Mitigating Systems Screening Questions, dated October 7, 2016, the inspectors determined the finding required a detailed risk evaluation because the finding involved a deficiency affecting the design and qualification of a mitigating structure, system, or component, and resulted in a loss of operability, and represented an actual loss of function of at least a single train for longer than its allowed out age time. A senior reactor analysts from Region IV performed a detailed risk evaluation and determined that the bounding increase in core damage frequency for this issue was 5.1E -8/year for Unit 1 and 2.9E -10/year for Unit 2 , and was therefore of very low safety significance (Green). Additional information is included in the detailed risk evaluation in Attachment 3 of this report. The inspectors did not assign a cross -cutting aspect because the performance deficiency was not reflective of present performance. Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part, that, measures shall be established to assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies, are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, measures established by the licensee did not assure that applicable regulatory requirements and the design bases, as defined in 10 CFR 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies, were correctly translated into specifications, drawings, procedures, and instructions. Specifically, from initial construction through March 2017, the licensee failed to fully incorporate applicable design requirements for components needed to ensure the capability to shut down the reactor and maintain it in a safe shutdown condition following a moderate energy line break. This issue does not represent an immediate safety concern because when the lines were identified the licensee took prompt action to isolate and depressurize them, and the licensee has implemented plant modifications. Since this violation was of very low safety significance (Green) and has been entered into the corrective action program as Condition Report CR- 2016- 008147, this violation is being treated as a non -cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000445/2017002 -05; 05000446/2017002- 05, Failure to Translate Design Requirements Into the As Built Facility)
05000446/FIN-2017002-022017Q2Comanche PeakInadequate Operability Evaluation for Safety - related Pipe SupportsGreen . The inspector s identified a non- cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, that occurred when the licensee failed on two occasions to perform an adequate operability determination associated with multiple safety -related pipe supports. Specifically, the operability determination of multiple carbon steel pipe support clamps exposed to boric acid and a bent sway strut pipe restraint lacked the engineering rigor necessary to provide a high degree of confidence to support the operability of the components. Subsequently, the inspector s concluded that the licensee established reasonable expectation for operability once engineering provided the control room with further analysis on the degraded conditions, and the new information was reviewed and accepted. This issue was entered into the licensees corrective action program as Condition Report CR -2017- 05418. The licensee's failure to perform adequate operability determinations per plant procedures was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating System cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee: (1) failed to perform the required corrosion evaluation for a comparison of material wastage against design dimensions of the pipe support clamps; (2) failed to perform a visual inspection of the material condition of the pipe support clamps as required by the work order; ( 3) used non- seismic design tolerances for the qualification of a seismically qualified strut in the immediate operability determination; and (4) failed to consider that the bent condition of the strut occurred after the previously accepted visual examinations on the same pipe support. All these issues could have resulted in safety -related components failing to perform their specified safety function during accident conditions. Using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At -Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because the finding: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; (4) and did not result in the loss of a high safety - significant non- technical specification train. This finding had a cross -cutting aspect in the area of problem identification and resolution associated with resolution because the licensee failed to adequately assess the degraded condition of the pipe supports in a complete and accurate manner to support a reasonable expectation of operability (P.1).
05000275/FIN-2017002-012017Q2Diablo CanyonInadequate Expansion Scope of Risk - Informed WeldsGreen . The inspectors identified a non -cited violation of the licensees risk -informed inservice inspection program (which is their alternative to portions of the ASME Code, Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z)) for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer spray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded the inspection scope by four additional welds, but failed to select those assigned with the same degradation. For immediate corrective actions, the licensee identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk -informed inservice inspection program. This issue was entered into the licensees corrective action program as Notification 50920222. The licensees failure to properly expand the weld examination scope as required by the risk -informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB -378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP ) for Findings At-Power, dated June 19, 2012, the inspector s determined the finding screened as having very low significance (Green) because: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and (4) did not result in the loss of a high safety -significant non -technical specification train. This finding had a cross -cutting aspect in the area of human performance associated with 3 change management because leaders failed to use a systematic process for evaluating and implementing the change to a risk -informed inservice inspection program. The implementing procedure failed to include the reference to degradation mechanism allowing for a misinterpretation of weld expansion requirements once a flaw was identified in a weld WIB -378 (H.3).
05000275/FIN-2017002-042017Q2Diablo CanyonFailure to Follow Procedures Results in Partial Loss of Cooling Flow to Shutdown CoolingGreen . The inspectors reviewed a self -revealing, non- cited violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, because PG&E personnel failed to follow the requirements of AD7.ID14, Assessment of Integrated Risk, Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in- service shutdown cooling residual heat removal heat exchangers and subsequent perturbation in reactor coolant system temperature during refueling outage 1R20. The inspectors determined that PG&E s failure to follow AD7.ID14, Assessment of Integrated Risk, Section 5.14 Performing Work on Posted Protected Equipment, was a performance deficiency within PG&Es ability to foresee and correct. This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately 8 degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, and determined to be of very low safety significance (Green) since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross- cutting aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision- making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close component cooling water cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling (H.14 ).
05000298/FIN-2017001-012017Q1CooperFailure to Maintain Alternate Shutdown Emergency ProcedureThe inspectors identified a non-cited violation of Technical Specification 5.4.1.a for the licensees failure to maintain Emergency Procedure 5.1ASD, Alternate Shutdown, Revision 17, for establishing reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit. Specifically, the licensee failed to maintain Emergency Procedure 5.1ASD with adequate instructions to place the reactor equipment cooling system north or south critical loop in service and verify reactor equipment system flow to the high pressure cooling injection system fan coil unit during some control room evacuation scenarios. The immediate corrective actions were to assess operability of the high pressure coolant injection system during control room evacuations that are not related to fire scenarios, and to revise Emergency Procedure 5.1ASD with instructions to open the criticalloop supply valves (REC-MOV-711 or REC-MOV-714) in the control room or locally, and verify reactor equipment system flow to the high pressure coolant injection fan coil unit. The licensee entered this deficiency into the corrective action program as Condition ReportCR-CNS-2017-01403. The licensees failure to maintain Emergency Procedure 5.1ASD to establish reactor equipment cooling system flow to the high pressure coolant injection fan coil unit during some control room evacuation scenarios, in violation of Technical Specification 5.4.1.a, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the procedural quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, the licensee did not provide instructions to establish reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit, which would have complicated operator response during a control room evacuation. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant nontechnical specification train. The finding had a cross-cutting aspect in the area of problem identification and resolution associated with identification. Specifically, the licensee failed to implement a corrective action program with a low threshold for identifying issues during the required annual review of emergency procedures (P.1).
05000298/FIN-2017001-022017Q1CooperFailure to Identify a Condition Adverse to Quality Associated with the 250 Vdc Electrical SystemThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to identify a condition adverse to quality associated with Station Procedure 2.2.24.1, 250 Vdc Electrical System (Div 1), Revision 14, in accordance with Station Procedure 0-CNS-LI-102, Corrective Action Process, Revision 6. Specifically, the licensee failed to identify that Station Procedure 2.2.24.1 contained inadequate instructions to ensure the oncoming charger 1C output voltage was matched with the bus 1A voltage when transferring bus 1A from charger 1A to charger 1C, so that technical specification bus voltage requirements would remain met. This resulted in an unexpected and initially unrecognized decline in voltage on the bus to below the required minimum of 260.4 Vdc. This condition required the licensee to declare the Division 1 250 Vdc electrical system and Division 1 residual heat removal low pressure coolant injection system inoperable. The immediate corrective action was to adjust the charger 1C float voltage greater than 260.4 Vdc to restore operability of the Division 1 250 Vdc electrical and residual heat removal low pressure coolant injection systems. The licensee entered this deficiency into the corrective action program as Condition Reports CR-CNS-2016-08658 and CR-CNS-2017-00750. The licensees failure to identify a condition adverse to quality associated with Station Procedure 2.2.24.1, to ensure technical specification bus voltage requirements were met, in violation of Station Procedure 0-CNS-LI-102, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the procedural quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, charger 1C, when in service, did not maintain battery 1A terminal voltage within the requirements of Surveillance Requirement 3.8.4.1, which required the licensee to declare the Division 1 250 Vdc electrical system and the Division 1 residual heat removal low pressure coolant injection system inoperable. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant, nontechnical specification train. The finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate the charger 1C float voltage issue to ensure that the resolution addressed the cause and extent of condition commensurate with the safety significance (P.2).
05000298/FIN-2017001-032017Q1CooperFailure to Identify a Condition Adverse to QualityThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to identify a condition adverse to quality for Division 1 residual heat removal service water booster pump A, in accordance with Station Procedure 0-CNS-LI-102, Corrective Action Process, Revision 6. Specifically, on January 5, 2017, the inspectors identified an oil level lower than normally expected, oil on the pump skid, and an oil droplet formed on the Division 1 residual heat removal service water booster pump A inboard bearing sight glass. The inspectors informed the control room of this condition, and the licensee determined the oil leakage from the pumps sight glass would have prevented the pump from operating for the required 30 days during a design basis accident. The immediate corrective action was to repair the Division 1 residual heat removal service water booster pump A inboard bearing sight glass, restoring operability of the pump. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2017-00054. The licensees failure to identify a condition adverse to quality for Division 1 residual heat removal service water booster pump A, in violation of Station Procedure 0-CNS-LI-102, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, the oil leakage from the service water booster pump A inboard bearing sight glass would have prevented the pump from operating for its required 30-day mission time during a design basis accident and resulted in the pump being declared inoperable. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety significant nontechnical specification train. The finding had a cross-cutting aspect in the area of human performance associated with challenge the unknown because the licensee failed to stop when faced with uncertain conditions and failed to ensure that risks are evaluated and managed before proceeding. Specifically, the licensee did not maintain a questioning attitude during job-site reviews to identify and resolve unexpected conditions, including lower than the expected oil level in the service water booster pump A inboard bearing sight glass, oil on the pump skid, and an oil droplet formed on the bottom of the sight glass (H.11).
05000298/FIN-2017001-042017Q1CooperFailure to Address Nonconforming Pipe Thinning in Accordance with the ASME CodeThe inspectors identified a non-cited violation of 10 CFR 50.55a(g)(4) for the licensees failure to use an approved method to disposition an American Society of Mechanical Engineers Code nonconforming condition in the residual heat removal service water system. Specifically, the licensee identified multiple locations with localized pipe thinning below the American Society of Mechanical Engineers Code B31.1 design minimum pipe-wall thickness during an ultrasonic examination but failed to use an approved method to calculate a new acceptable pipe-wall thickness. As a corrective action to restore compliance, the licensee replaced this section of piping on November 1, 2016, during Refueling Outage 29. The licensee entered this issue into the corrective action program as Condition Reports CR-CNS-2016-05558 and CR-CNS-2016-05963. The licensees failure to use an approved method to calculate a new minimum allowable pipe-wall thickness, in violation of 10 CFR 50.55a(g)(4), was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, calculating an allowable minimum pipe-wall thickness value that is below the American Society of Mechanical Engineers code design minimum value reduces the pipings structural integrity, potentially leading to the failure of the piping. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings AtPower, dated June 19, 2012, inspectors determined the finding screened as having very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant nontechnical specification train. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the licensee failed to operate and maintain the residual heat removal service water system within the American Society of Mechanical Engineers code minimum pipe-wall thickness. Specifically, having identified that the affected pipe location was below the allowable pipe-wall thickness, the licensee opted to calculate and accept a new minimum pipe-wall thickness value that was not consistent with code requirements instead of repairing the affected piping at the time of discovery (H.6).
05000298/FIN-2017001-052017Q1CooperLoss of Shutdown Cooling due to Relay MaintenanceThe inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to implement Maintenance Procedure 7.3.16, Low Voltage Relay Removal and Installation, Revision 22, for relay replacement work. Specifically, on October 28, 2016, the licensee failed to evaluate the potential impact of primary containment isolation system relay PCIS-REL-K27 work on shutdown cooling relay PCIS-REL-K30, which was mounted next to K27 and shared a common mounting rail. As a result, the licensee did not identify the potential of losing residual heat removal shutdown cooling, and while installing the K27 relay and snapping it into the mounting rail, workers caused a momentary actuation of relay K30 and a loss of residual heat removal shutdown cooling. Corrective actions to restore compliance included restoration of shutdown cooling, completion of the K27 relay maintenance with shutdown cooling out of service, and an outage risk management procedure change that prohibited work on or near shutdown cooling relays while the system was required to be in service. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2016-07645. The licensees failure to implement Maintenance Procedure 7.3.16, in violation of Technical Specification 5.4.1.a, was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Initiating Events Cornerstone and affected the associated cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown operations. Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance Process Phase 1 Initial Screening and Characterization of Findings, dated May 9, 2014, the inspectors determined that the finding did not require a quantitative assessment because the event occurred when the refuel canal/cavity was flooded. Therefore, the finding screened as very low safety significance (Green). The finding had a cross-cutting aspect in the area of human performance associated with work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the need for coordination with different work groups or job activities. Specifically, the licensee failed to control, execute, and coordinate safety-related primary containment isolation system relay work activities to ensure residual heat removal shutdown cooling was not adversely impacted (H.5).
05000298/FIN-2017001-062017Q1CooperFailure to Install Correct Mechanical Stop and Verify Proper OperationThe inspectors reviewed a self-revealed, non-cited violation of Technical Specification 3.0.4 for the licensees failure to install the correct reactor core isolation cooling pressure control valve, RCIC-AOV-PCV23, mechanical stop and verify proper operation of the system prior to entering a mode of applicability for Technical Specification 3.5.3. This condition resulted in RCIC-AOV-PCV23 going fully open during surveillance testing following Refueling Outage 29, causing a pressure transient. This transient caused a failure of the reactor core isolation cooling turbine lube oil cooler gasket, lifting of a pressure relief valve, and a water leak. The licensee immediately shut down the reactor core isolation cooling system and declared it inoperable. The immediate corrective actions were to restore RCIC-AOV-PCV23 from the closed mechanical stop to the required open mechanical stop and to replace the turbine lube oil cooler gasket to restore operability of the system. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2016-08122 and initiated a root cause evaluation to investigate this condition. The licensees failure to install the correct reactor core isolation cooling pressure control valve, RCIC-AOV-PCV23, mechanical stop and verify proper operation of the system prior to entering a mode of applicability for Technical Specification 3.5.3, in violation of Technical Specification 3.0.4, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, the licensee installed RCIC-AOV-PCV23 with the incorrect mechanical stop, and proper valve operation was not verified after installation during Refueling Outage 29, which caused the reactor core isolation cooling system to lose function during surveillance testing. This transient caused a failure of the reactor core isolation cooling turbine lube oil cooler gasket and an associated water leak. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding required a detailed risk evaluation because it represented a loss of system and/or function. In the detailed risk evaluation, the analyst assumed the reactor core isolation cooling system was unavailable for 50 hours. The analyst used the Test/Limited Use Version COOPER-DEESE-HCI03 of the Cooper SPAR model run on SAPHIRE, Version 8.1.5. The analyst updated the initiating event frequencies for transients, losses of condenser heat sink, losses of main feed water, grid related losses of offsite power, and switchyard centered losses of offsite power to the more recent values from the 2014 update to the industry data found in INL/EXT-14-31428, Initiating Event Rates at U.S. Nuclear Power Plants, 1998-2013, Revision 1. From this, the finding was determined to have an increase in core damage frequency of 8.4E-8/year and to be of very low safety significance (Green). Transients, losses of condenser heat sink, and losses of main feed water were the dominant core damage sequences. The automatic depressurization system and the reactor protection system remained to mitigate these sequences. The finding had a cross-cutting aspect in the area of human performance associated with documentation because the licensee failed to create and maintain complete, accurate, and up-to-date documentation associated with RCIC-AOV-PCV23 design drawings and the maintenance procedure for setting and testing the mechanical stop (H.7).
05000313/FIN-2016008-022016Q4Arkansas NuclearFailure to Incorporate NRC Safety Guide 9 Criteria into Surveillance ProceduresGreen. The team identified Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, which states, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Additionally, Test results shall be documented and evaluated to assure that test requirements have been satisfied. Specifically, as of December 2, 2016, Units 1 and 2 emergency diesel generator surveillance procedures failed to incorporate the applicable voltage and frequency limits of NRC Safety Guide 9, and did not consistently document or evaluate results to assure test requirements have been satisfied. In response to this issue, the licensee provided the team test results which demonstrated that an immediate safety concern was not present. This finding was entered into the licensees corrective action program as Condition Reports CR-ANO-1-2016-4785 and CR-ANO-2-2016-4257. The team determined that the failure to incorporate the acceptance limits of NRC Safety Guide 9 into surveillance test procedures for emergency diesel generators and assure that test requirements have been satisfied in accordance with 10 CFR Part 50, Appendix B, Criterion XI, Test Control, was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to respond to initiating events to prevent undesirable consequences, and would have the potential to lead to a more significant safety concern. Specifically, the failure to incorporate appropriate acceptance criteria in test procedures and assure that the criteria have been satisfied had the potential to lead to a worse condition, if left uncorrected. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding did not have a cross-cutting aspect because the performance deficiency did not reflect current licensee performance.
05000313/FIN-2016008-032016Q4Arkansas NuclearFailure to Monitor Startup Transformers 1, 2, and 3 Voltage Regulator/Tap Changer FunctionGreen. The team identified a Green finding for the failure to meet the surveillance standards of IEEE 308-1971, Criteria for Class 1E Electric Systems for Nuclear Power Generating Stations, Section 5.2.3, Preferred Power Supply. Specifically, from 2001 to December 2, 2016, the licensee failed to monitor the operation of the voltage regulator/load tap changer functions on startup transformers 1, 2, and 3. In response to this issue, the licensee provided reasonable assurance that the voltage regulator/load tap changer was operating properly based on review of plant computer voltage plot data following an Arkansas Nuclear One, Unit 1 trip that occurred on December 14, 2015. This finding was entered into the licensees corrective action program as Condition Reports CR-ANO-C-2016-4777, CR-ANO-C-2016-4879, and CR-ANO-C-2016-5015. The team determined that the failure to monitor startup transformers 1, 2, and 3 voltage regulator/load tap changers to the extent that they are shown to be ready to perform their intended function, in accordance with IEEE Standard 308-1971, was a performance deficiency. The finding was determined to be more than minor because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to respond to initiating events to prevent undesirable consequences. Specifically, the failure to monitor the adequacy of the voltage supplied from startup transformers 1, 2, and 3 voltage regulator/load tap changer did not ensure that offsite power would be available to perform its necessary functions to provide power to the safety-related mitigation equipment. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding did not have a cross-cutting aspect because the performance deficiency did not reflect current licensee performance.
05000313/FIN-2016008-042016Q4Arkansas NuclearFailure to Perform an Adequate Emergency Feedwater Pump Suction Transfer Design Calculation or Testing (EA 2017-017)Green. The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, which states, in part that, design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. Specifically, prior to December 22, 2016, the licensee failed to verify the adequacy of the emergency feedwater suction transfer procedure by determining if the qualified condensate storage tank will be completely empty of water, possibly causing an air ingestion failure of the Unit 1 emergency feedwater pumps, prior to transferring to the credited safety-related alternate suction source. In response to this issue, the licensee resolved the immediate safety concern by revising the emergency feedwater pump operating procedure, removing the steps that were the cause of the concern. This finding was entered into the licensees corrective action program as Condition Reports CR-ANO-1-2016-5166, CR-ANO-1-2016-5725, and CR-ANO-1-2017-0040. The team determined that the failure to verify the adequacy of the design of the Unit 1 emergency feedwater suction from the qualified condensate storage tank to alternate sources of water by performance of design review, by use of calculational methods, or by performance of a suitable testing program in accordance with 10 CFR Part 50, Appendix B, Criterion III, Design Control, was a performance deficiency. This finding was more than minor because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the reliability, availability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee failed to have adequate measures in place to ensure an acceptable design analysis or a suitable test program would verify that the process of transferring emergency feedwater suction from the qualified storage tank to the alternate sources ensures the capability of the Unit 1 emergency feedwater system to perform its safety function. In accordance with Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, dated June 19, 2012, the team determined this finding affected the secondary short term heat removal function of the Mitigating Systems Cornerstone. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the finding represented a loss of the emergency feedwater system and function. Therefore, a detailed risk evaluation was necessary. The senior reactor analyst determined that the change in core damage frequency of this finding was 7 x 10-7 per year, therefore the significance was of very low safety significance (Green). This finding did not have a cross-cutting aspect because the performance deficiency did not reflect current licensee performance.
05000313/FIN-2016008-052016Q4Arkansas NuclearFailure to Ensure Safety Systems Would Survive Sustained Degraded Voltage ConditionsGreen. The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, which states, in part, design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. Specifically, from December 17, 1979, to December 2, 2016, the licensee did not verify that the design of the protective devices for the loads required at the beginning of a loss-of-coolant accident were adequate to prevent tripping these devices under degraded voltage conditions, which would render the affected loads non-functional. In response to this issue, the licensee performed a preliminary analysis to determine that the protective overload devices would not cause safety equipment to fail at degraded voltages allowed by technical specifications. This finding was entered into the licensees corrective action program as Condition Reports CR-ANO-C-2016-5027 and CR-ANO-C-2016-5191. The team determined that the failure to ensure that safety-related electrical components would not fail during the allowable time duration of a degraded voltage condition (in accordance with NRC Multi-Plant Action B-23, Position 1.C) was a performance deficiency. The finding was determined to be more than minor because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to respond to initiating events to prevent undesirable consequences. Specifically, the failure to ensure that the protective devices for the loads required at the beginning of a Loss of Control Accident would not fail under degraded voltage conditions did not ensure that these loads would be available to perform their mitigating functions. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. The team determined that this finding did not have a cross-cutting aspect because the most significant contributor did not reflect current licensee performance.
05000313/FIN-2016008-012016Q4Arkansas NuclearFailure to Verify the Adequacy of Motor Operated Valve Thermal Overload DevicesGreen. The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, which states, in part, design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. Specifically, prior to December 2, 2016, the licensee failed to use appropriate assumptions in thermal overload device calculations and failed to establish a suitable periodic test program for safety-related Unit 1 motor operated valve thermal overload device trip setpoints, as discussed in Regulatory Guide 1.106, Regulatory Position C.2. In response to this issue, the licensee demonstrated reasonable assurance of operability by using the results of the 18-month high pressure injection system valve testing which required multiple stroking of block valves to obtain various flows without tripping the thermal overload devices. This finding was entered into the licensees corrective action program as Condition Reports CR-ANO-C-2016-5017 and CR-ANO-1-2016-5130. The team determined that the failure to meet the intent of Regulatory Guide 1.106, Regulatory Position C.2 was a performance deficiency. The finding was determined to be more than minor because it was associated with the Mitigating Systems Cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to respond to initiating events to prevent undesirable consequences. Specifically, the failure to verify the adequacy of the design and perform suitable testing for thermal overload device setpoint drift did not ensure that the safety-related motor operated valves would be available to throttle the associated system flows during a design basis accident. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluations because the licensee failed to thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the licensee failed to thoroughly evaluate Condition Report CR-ANO-1-2016-0778 which documented NRC inspector concerns associated with design and testing of motor operated valve thermal overload devices (P.2).
05000313/FIN-2016008-062016Q4Arkansas NuclearReadiness to Cope with External FloodingGreen. The team identified three examples of a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which states, in part that, activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances. Specifically, prior to December 2, 2016, Unit 1 Operating Procedure OP 1203.025, Natural Emergencies, Revision 60 and Unit 2 Operating Procedure OP 2203.008 Natural Emergencies, Revision 42 failed to ensure all actions required to establish external flood protection, as specified by flood protection design basis engineering report CALC-ANOC-CS-00003, Revision 00 were implemented. This issue was entered into the licensees corrective action program as Condition Report CR-ANO-2-2016-4265. The licensees failure to prescribe procedures appropriate to the circumstances for combating emergencies or other significant acts of nature such as flooding was a performance deficiency. The performance deficiency was more than minor because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to respond to initiating events to prevent undesirable consequences, and would have the potential to lead to a more significant safety concern. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it does not involve the loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identification and resolution associated with identification because the licensee failed to identify issues, completely, accurately, and in a timely manner in accordance with the corrective action program. Specifically, the licensee failed to identify these deficiencies during a review of these same procedures as part of actions to close significant performance deficiencies as documented in Arkansas Nuclear One Area Action Plan FP-6 (P.1).
05000397/FIN-2016007-012016Q2ColumbiaProgrammatic Concern Pertaining to Columbia Generating Stations ProceduresThe team identified a Green, non-cited violation of Technical Specification 5.4, Procedures, Section 5.4.1, which states, in part, Written procedures shall be established, implemented, and maintained covering the following activities: a. The applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978; Regulatory Guide 1.33, Revision 2, Appendix A, Section 1, Administrative Procedures, Subsection d, specifies Procedure Adherence and Temporary Change Method. This requirement includes plant Procedure SWP-PRO-01, Procedure and Work Instruction Use and Adherence, Revision 27; Procedure SWP-PRO-02, Preparation, Review, Approval and Distribution of Procedures, Revision 42; and Procedure SWP-PRO-03, Writers Manual, Revision 21, which identify the requirements governing procedural requirements utilized at Columbia Generating Station. Specifically, from June 6 through June 23, 2016, multiple examples of procedural compliance were identified with the station procedures. These examples include failure to follow procedures, inadequate procedures, not correctly translating design requirements into procedures, validation of procedures, and the distribution of procedures. In response to this issue, the licensee reviewed each individual concern and confirmed that there were no operability concerns. The licensee has also placed each identified concern into their corrective action program and will address each issue. This finding was entered into the licensees corrective action program as Action Request (AR) 00351364. The team determined that the licensees failure to follow guidance procedures for implementation, adherence, accuracy, verification, and distribution of station procedures, was a performance deficiency. This finding was more than minor because it was associated with the procedures attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failing to have accurate procedures, and to comply with these procedures, was a significant programmatic deficiency that could adversely affect the reliability and capability of systems used to prevent undesirable consequences. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of nontechnical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. The team determined that this finding had a cross-cutting aspect in the area of human performance, resources, where the licensee will ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety. Specifically, the licensee had not ensured that site procedures were adequate to support plant activities (H.1).
05000528/FIN-2016002-012016Q2Palo VerdeLeakage From Reactor Coolant Pump 2B Discharge Pipe Instrument NozzleThe inspectors identified an unresolved item for pressure boundary leakage from reactor coolant pump 2B discharge pipe instrument nozzle. On April 10, 2016, during the Unit 1 Refueling Outage 19, the licensee discovered reactor coolant system pressure boundary leakage at instrument nozzle 1JRCETW0121Y on the 2B reactor coolant pump discharge piping. The leakage was discovered during a planned visual inspection of Unit 1 hot and cold leg nozzles. The leak was not detectable by either the reactor coolant system leak rate procedure or the containment radiation monitor trend reviews while the unit was operating. Additionally, the leak had not been visually detected during the previous refueling outage. The leakage was consistent with a small leak characterized by moderate boric acid accumulation at the leakage site. The licensee determined that the cause of the leakage was primary water stress corrosion cracking of the Alloy 600 instrument nozzle. The licensee corrected the leakage using a mechanical nozzle seal assembly repair method utilizing ASME Code Case N-733, Mitigation of Flaws in NPS 2 (DN 50) and Smaller Nozzles and Nozzle Partial Penetration Welds in Vessels and Piping by Use of a Mechanical Connection Modification, Section XI, Division 1. The evaluation of the 2B cold leg RTD nozzle leakage is being evaluated by the licensee as part of Palo Verde Action Request 15-01640-012. The inspectors reviewed the circumstances surrounding the discovery of the leak and observed portions of the repair activity during the refueling outage. Once the licensee completes their evaluation, the inspectors will review and complete an inspection to determine if a performance deficiency exists as a result of the nozzle failure.
05000528/FIN-2016002-032016Q2Palo VerdeInadequate Engineering and Radiological Controls Resulting in a Unit 1 Containment Building Airborne Radioactivity Event with Unplanned IntakesThe inspectors identified a non-cited violation of 10 CFR 20.1701 due to the licensees failure to implement adequate processes and engineering controls necessary to reduce airborne radioactivity and prevent internal dose to workers in Unit 1. On April 20, 2016, inspectors identified that procedures and instructions for monitoring high efficiency particulate air ventilation filter unit to prevent worker exposures to radiation and airborne radioactivity were being inadequately implemented. On April 21, 2016, the licensees inadequate engineering and radiological controls during a high efficiency particulate air operations caused an airborne radioactivity event in containment, resulting in the evacuation of 41 potentially contaminated workers of whom 8 had measurable intakes of radioactive material. The licensees immediate corrective actions included stopping work in the Unit 1 containment, evacuating workers in containment, assessing workers for external and internal contamination, and investigating the cause and source of the contamination event. This matter was placed in the licensees corrective action program as Condition Reports16-06499 and 16-06578 and the licensee initiated a root cause investigation. The inspectors determined that the failures to implement adequate engineering and radiological controls to reduce airborne radioactivity during a high efficiency particulate air unit operations in accordance with 10 CFR 20.1701 and radiation protection procedures were performance deficiencies. The performance deficiencies were more than minor because they were associated with the Occupational Radiation Safety Cornerstone attribute of program and process (exposure control) and adversely affected the cornerstone objective to ensure the adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. This was evident by the Unit 1 containment airborne radioactivity event on April 21, 2016, that resulted in at least eight workers with unplanned intakes. Using Inspection Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance Determination Process, dated August 19, 2008, the inspectors determined the finding had very low safety significance (Green) because: (1) it was not an as low as is reasonably achievable planning and controls finding, (2) there was no overexposure, (3) there was no substantial potential for an overexposure, and (4) the ability to assess dose was not compromised. The inspectors concluded that the finding has a cross-cutting aspect in the human performance area, associated with the resources component, because the licensee leaders failed to ensure that personnel, equipment, procedures, and other resources were available and adequate to support nuclear safety. Specifically, procedures and radiation exposure permits failed to have adequate instructions for ensuring a high efficiency particulate air filter loading and dose rates were monitored to prevent overloading, and safe handling of loaded a high efficiency particulate air filters (H.1).
05000528/FIN-2016002-022016Q2Palo VerdeFailure to Implement High Radiation Area Controls in an Area with a Dose Rates Greater Than 1 rem per HourThe inspectors reviewed a Green, self-revealing, non-cited violation of Technical Specification 5.7.2, which was caused by the licensees failure to control a high radiation area with radiation levels greater than 1 rem per hour in the Unit 1 containment. A radiation protection technician received an unexpected dose rate alarm while conducting surveys on piping in the 87-foot elevation of the 2B reactor coolant pump bay area near a high efficiency particulate air unit in containment. Licensee personnel corrected the error by guarding the area, posting the area, and changing the pre-filters in the adjacent portable a high efficiency particulate air units to reduce the dose rates. This issue was entered into the licensees corrective action program as Condition Reports 16-06515 and 16-07479. The inspectors determined that the failure to identify a locked high radiation area through timely surveys and adequate a high efficiency particulate air maintenance procedures that could have revealed changing radiological conditions was a performance deficiency. The performance deficiency was more than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of program and process (exposure control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation because licensee personnel did not implement barriers intended to prevent workers from receiving unexpected dose. Using Inspection Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance Determination Process, dated August 19, 2008, the inspectors determined the violation had very low safety significance (Green) because: (1) it was not an as low as is reasonably achievable finding, (2) there was no overexposure, (3) there was no substantial potential for an overexposure, and (4) the ability to assess dose was not compromised. This finding has a cross-cutting aspect in the human performance area, associated with the resources component, because the licensee leaders failed to ensure that personnel, equipment, and procedures were available and adequate to support nuclear safety. Specifically, the licensee failed to ensure that procedures were adequate to ensure radiation levels around portable high efficiency particulate air units were monitored to evaluate changing radiological conditions in a timely manner such that hazards were appropriately controlled (H.1).
05000285/FIN-2016001-012016Q1Fort CalhounImplementing a Procedure Change for Alternative Shutdown Cooling that would have Required NRC ApprovalThe inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests, and Experiments, for the failure to recognize that a change to the facility as described in the Updated Safety Analysis Report would require prior NRC review and approval. Specifically, the 10 CFR 50.59 evaluation revised a site procedure, without NRC approval, to substitute automatic flow control of shutdown cooling flow and temperature with manual control using the low pressure safety injection loop injection valves. The licensees corrective actions included revising the affected procedure to reflect the original automatic flow control. The licensee entered this issue in the corrective action program as Condition Report 2013-15342. The licensees failure to implement the requirements of 10 CFR 50.59 and adequately evaluate changes to determine if prior NRC approval is required was a performance deficiency. Because this violation had the potential to impact the NRCs ability to perform its regulatory function, the inspectors evaluated the violation using traditional enforcement. In accordance with Section 2.1.3.E.6 of the NRC Enforcement Manual, the team evaluated this finding using the significance determination process to assess its significance. The inspectors performed an initial screening of the finding in accordance with NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated July 1, 2012. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was determined to have very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees Maintenance Rule program. Therefore, in accordance with Section 6.1.d.2 of the NRC Enforcement Policy, the inspectors characterized this performance deficiency as a Severity Level IV violation. The inspectors determined that a cross-cutting aspect was not applicable because the issue involving the failure to perform an adequate 10 CFR 50.59 evaluation was strictly associated with a traditional enforcement violation.
05000285/FIN-2016001-022016Q1Fort CalhounLicensee-Identified ViolationTechnical Specification 2.6(1) requires containment integrity to be maintained unless the reactor is in a cold or refueling shutdown condition. If containment integrity is not maintained and the reactor does not meet these cold or refueling shutdown conditions, then containment integrity must be restored within one hour or the reactor is required to be in hot shutdown within the next six hours. From November 22, 2013, through June 27, 2014, a test connection cap was left off of a containment penetration which constituted a loss of containment integrity. Upon discovery of this condition on June 27, 2014, the licensee entered Technical Specification 2.6(1) and Abnormal Operating Procedure 12 for loss of containment integrity. The cap was re-installed and containment integrity was restored within one hour. The violation is more than minor because it is associated with the configuration control attribute of the Barrier Integrity Cornerstone. Failure to install the containment penetration cap following local leak rate testing on November 22, 2013, resulted in a loss of containment integrity until it was discovered missing on June 27, 2014. This adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (i.e., containment) protect the public from radionuclide releases caused by accidents or events. The violation was reviewed by a Senior Reactor Analyst and was determined to be of very low safety significance because the test connection fitting was a 14-inch diameter opening. Inspection Manual Chapter 0609, Significance Determination Process, Appendix H, identifies that small lines (less than 1 to 2 inches in diameter) would not generally contribute to large early release frequency. Therefore, this finding screens to Green. The licensee entered the issue into their corrective action program as Condition Report 2014-07958.
05000382/FIN-2015004-012015Q4WaterfordFailure to Properly Pre-Plan and Perform Maintenance on the Core Element Assembly CalculatorsThe inspectors reviewed a self-revealing, non-cited violation of Technical Specification 6.8.1.a, associated with the licensees failure to properly pre-plan and perform maintenance in accordance with EN-DC-153, Preventative Maintenance Component Classification. The licensee entered this condition into their corrective action program as condition report CR-WF3-2015-06438. The licensee restored compliance by properly classifying the components as High Critical in accordance with EN-DC-153, Revision 2, and by initiating development of appropriate preventative-maintenance for the control element assembly calculators (CEACs). In addition, the licensee initiated work to improve the reliability of the CEACs, including reviewing card refurbishments to ensure circuit card reliability is enhanced. The performance deficiency was more than minor because it is associated with the Equipment Performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, inappropriate preventative maintenance on the circuit cards associated with the CEACs ultimately resulted in a plant trip on October 3, 2015. The inspectors screened the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609, Significance Determination Process. Using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined that the finding was of very low significance (Green) because the finding did not cause a trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Because the performance deficiency occurred in 2008, the inspectors concluded that the finding does not reflect current licensee performance and therefore did not assign a cross-cutting aspect.
05000285/FIN-2015002-062015Q2Fort CalhounFailure to Identify and Correct Loose Incore Instrument Nozzle ConnectionThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure to identify and correct a condition adverse to quality. Specifically, maintenance personnel failed to document a loose connection on incore instrument port 44 in the corrective action program. As a result, the connection was not tightened and boric acid leaked onto the reactor vessel head during operation. This issue was entered into the licensees corrective action program as Condition Report 2015-05864. The failure of maintenance personnel to document a loose connection on incore instrument port 44 in the corrective action program was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the equipment performance attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not result in exceeding the RCS leak rate for a small loss-of-coolant accident, and did not affect other systems used to mitigate a loss-of-coolant accident resulting in a total loss of their function. The inspectors determined that the finding had a field presence cross-cutting aspect in the area of human performance because the licensee did not ensure supervisory and management oversight of work activities, including contractors and supplemental personnel. (H.2)
05000285/FIN-2015002-092015Q2Fort CalhounFailure to Follow Instructions and Procedures Related to Snubber ActivitiesThe inspectors identified a non-cited violation of very low safety significance of 10 CFR Part 50, Appendix B, Criterion V Instructions, Procedures, and Drawings, because activities affecting quality were not accomplished in accordance with instructions and procedures established by the licensee. Specifically, the licensee failed to document a degraded condition associated with a safety related seismic snubber affecting the auxiliary feedwater system, did not notify operations of the degraded condition, and did not assess the risk of the inoperable snubber in accordance with licensee instructions and procedures. The licensee entered this violation into their corrective action program. Immediate actions taken to address this violation included a review of all other snubber inspections that were rejected to ensure that other degraded conditions were reported to the control room, a review of all planned snubber maintenance with respect to online risk, and the issuance of interim guidance to all Shift Managers on the subject of snubber operability and risk. The inspectors determined that the licensees failure to follow instructions and procedures associated with safety related snubbers was a performance deficiency. The finding is more than minor because if left uncorrected, the performance deficiency could have led to a more significant safety concern. Specifically, the failure to follow instructions and procedures associated with safety related snubbers could result in unacceptable risk configurations that are not analyzed under technical specifications and could challenge the reliability of safety related equipment during a seismic event. Using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2 Mitigating System Screening Questions Part B, dated July 1, 2012, the inspectors determined the finding to be of very low safety significance (Green) since the finding did not result in the loss of equipment specifically designed to mitigate a seismic initiating event. The finding has a cross-cutting aspect in the area of Human Performance, the Work Management aspect, since the licensee did not implement a work process that ensured the identification and management of risk commensurate to the work. (H.5)
05000285/FIN-2015002-082015Q2Fort CalhounFailure to Submit Summaries of the Impact of Changes to the Emergency Plan and Implementing ProceduresThe inspector identified a non-cited violation of 10 CFR 50.54(q)(5) for the licensees failure to submit reports of its analysis of the impact of changes to the emergency plan and implementing procedures on the emergency plan. Specifically, the inspector identified three examples between February 21 and June 18, 2015, of the licensee submitting changes to the emergency plan and implementing procedures without the required summaries. The issue was entered into the licensees corrective action program as Condition Report CR 2015-04934. The failure to submit a summary of the analysis of the effect of changes to emergency plan implementing procedures on the site emergency plan is a performance deficiency within the licensees ability to foresee and correct. The issue is more than minor because the licensees failure to submit the required summary affects the NRCs ability to perform its regulatory function, and the licensee has not incorporated this requirement into its program. The inspectors evaluated the issue using Section 6.6.d of the NRC Enforcement Policy, dated July 12, 2011, and determined it to be a Severity Level IV violation because the issue involved the licensees ability to implement a regulatory requirement not related to assessment or notification. Traditional enforcement violations are not assigned a crosscutting aspect.
05000285/FIN-2015002-072015Q2Fort CalhounFailure to Perform Functionality Assessments for the Spent Fuel Pool Cooling SystemThe inspectors identified a finding associated with the failure of operations personnel to follow procedures used to perform functionality assessments. Specifically, operations personnel failed to provide sufficient technical justification for the reasonable assurance of functionality of the spent fuel pool cooling system when boric acid leaks were identified on discharge header vent valve AC-898. Vent valve AC-898 was replaced and the issue was entered into the licensees corrective action program as Condition Report 2015-05856. The failure of operations personnel to follow station procedures to perform functionality assessments was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the design control attribute of the Barrier Integrity Cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not adversely affect decay heat removal capabilities from the spent fuel pool causing the pool temperature to exceed the maximum analyzed temperature limit specified in the site-specific licensing basis, did not result from fuel handling errors, dropped fuel assembly, dropped storage cask, or crane operations over the SFP that caused mechanical damage to fuel clad and a detectible release of radionuclides, did not result in a loss of spent fuel pool water inventory decreasing below the minimum analyzed level limit specified in the site-specific licensing basis, and did not affect the SFP neutron absorber, fuel bundle misplacement or soluble boron concentration. The inspectors determined that the finding had a training cross-cutting aspect in the area of human performance because the licensee did not provide training and ensure knowledge transfer to maintain a knowledgeable, technically competent workforce and instill nuclear safety values. (H.9)
05000285/FIN-2015002-052015Q2Fort CalhounFailure to Promptly Identify and Correct a Condition Adverse to Quality Involving a Spent Fuel Pool Cooling Vent Valve LeakThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions, for the failure to promptly identify and correct a condition adverse to quality. Specifically, the licensee failed to take corrective action to replace spent fuel pool cooling system discharge header vent valve AC-898 after a leak was identified. A work order for the condition was opened in 2009 but was never implemented. Subsequently, a pressure boundary leak was identified in 2013 and misidentified in 2014 but was never addressed. The licensee replaced vent valve AC-898 and repaired the affected weld in April 2015. This issue was entered into the licensees corrective action program as Condition Report 2015-05038. The failure to promptly identify and correct a condition adverse to quality was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the design control attribute of the Barrier Integrity Cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not adversely affect decay heat removal capabilities from the spent fuel pool causing the pool temperature to exceed the maximum analyzed temperature limit specified in the site-specific licensing basis, did not result from fuel handling errors, dropped fuel assembly, dropped storage cask, or crane operations over the SFP that caused mechanical damage to fuel clad and a detectible release of radionuclides, did not result in a loss of spent fuel pool water inventory decreasing below the minimum analyzed level limit specified in the site-specific licensing basis, and did not affect the SFP neutron absorber, fuel bundle misplacement or soluble boron concentration. The inspectors determined that the finding had a basis for decision cross-cutting aspect in the area of human performance because leaders failed to ensure that the bases for operational and organizational decisions were communicated during multiple instances where the leak in valve AC-898 could have been repaired. (H.10)
05000285/FIN-2015002-012015Q2Fort CalhounFailure to Include a Class 1 Component in the Reactor Vessel Pressure Boundary Integrity TestThe inspectors identified a non-cited violation of 10 CFR 50.55a(g)(4), involving the failure to adequately perform periodic reactor coolant system (RCS) integrity inspections as required by ASME Code Section XI. Specifically, Procedure OP-ST-RC-3007, Periodic Reactor Coolant System Integrity Test, required testing of all ASME Class 1 pressure boundary components of the reactor vessel pressure boundary but failed to include reactor vessel head vent line RC-2501R. As a result, the requirements of ASME Code Section XI were not met. This issue was entered into the licensees corrective action program as Condition Report 2015-05858. The inspectors concluded that the failure to include reactor vessel head vent line RC-2501R within the reactor vessel pressure boundary in the periodic RCS integrity inspection was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not result in exceeding the RCS leak rate for a small loss-of-coolant accident, and did not affect other systems used to mitigate a loss-of-coolant accident resulting in a total loss of their function. The inspectors determined that the finding had a conservative bias cross-cutting aspect in the area of human performance because the licensee failed to use decision making-practices that emphasized prudent choices over those that are simply allowable. (H.14