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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 556821 January 2022 17:10:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray System Declared Inoperable

The Licensee provided the following information via fax: During performance of a surveillance of the High Pressure Core Spray (HPCS) service water system on January 1, 2022, the HPCS system was declared inoperable for performance of the surveillance. During the surveillance, pump discharge pressure and flow were above the action range curve specified in the surveillance. For the given flow rate, pump discharge pressure was too high. This condition prevents declaring the HPCS service water system and HPCS system operable. The HPCS service water and HPCS systems remain inoperable. The station entered Technical Specification (TS) 3.7.2.A and TS 3.5.1.B at 0910 (PST) on January 1, 2022. In accordance with TS 3.5.1.B, the Reactor Core Isolation Cooling (RCIC) system was verified to be operable. TS 3.5.1 Action B provides a 14-day completion time to restore HPCS to an operable status. All other Emergency Core Cooling systems (ECCS) are operable. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function credited for mitigating the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). The HPCS system is a single train system at Columbia. The NRC resident has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee is investigating the cause of the high pump discharge pressure and verifying instrumentation accuracy.

  • * * RETRACTION ON 1/6/22 AT 1715 EST FROM CHASE WILLIAMS TO TOM KENDZIA * * *

This Notification is to retract EN 55682, Unplanned High Pressure Core Spray (HPCS) Inoperability. On 1/1/2022 at (1735 EST), Columbia Generating Station notified the NRC under 10 CPR 50.72(b)(3)(v)(D) of the inoperability of a single train of safety system (HPCS) for performance of the surveillance. During the surveillance pump discharge pressure and flow were above the action range curve specified in the surveillance. Engineering performed an analysis of this event and concluded the HPCS was operable during the event and would have performed its required safety function. The results of initial IST testing of HPCS-P-2 via OSP-SW/IST-Q703 on 01/01/22 resulted in measured parameters falling outside of the acceptable range specified for this pump. Systematic error was suspected as the cause of the failure and the test was reperformed following taking actions to eliminate the suspected systematic errors. The second performance of the test on 01/01/22 resulted in acceptable pump performance. Evidence exists that the initial performance of the test failed due to imprecise averaging techniques due to difficulties in averaging continuously changing values on the test instrument. The second performance of OSP-SW/IST-Q703 should be considered a successful test and the test of record as the systematic error was eliminated and measured parameters are considered valid. The NRC Resident Inspector has been notified. The HOO notified R4DO (Rolando-Otero).

Service water
Reactor Core Isolation Cooling
High Pressure Core Spray
Emergency Core Cooling System
ENS 5538529 July 2021 23:51:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Inoperable Secondary ContainmentAt 0922 PDT, on 07/28/21, the reactor building roof hatch was opened to support maintenance activities on the roof. Secondary containment differential pressure lowered and was recovered by the operating crew. Secondary containment differential pressure was maintained negative during the transient and was verified to have met technical specification requirements the whole time, however it was not identified at the time that the secondary containment was inoperable due to the roof hatch exceeding the allowable containment breech size and as such a TS 3.6.4.1.A entry was warranted. This report is being made pursuant to 10 CFR 50.72(a)(1)(ii) when it was identified that the secondary containment was inoperable while the roof hatch was open and a report should have been made under 10 CFR 50.72(b)(3)(v)(C) and (D) for loss of safety function. There were no radiological releases, system actuations, or isolations associated with this event. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 5429225 September 2019 06:38:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentLoss of High Pressure Core Spray SystemAt 2338 PDT on September 24, 2019, the High Pressure Core Spray (HPCS) system was declared inoperable due to a leak on DSA-PCV-2C (2 inch Diesel Starting Air Pressure Control Valve). With one of two air headers isolated and being drained for maintenance, this leak caused the remaining starting air header for HPCS-GEN-DG3 (HPCS Diesel Generator) to lower to less than the operability limit. Upon declaring the HPCS system inoperable, TS 3.5.1 Action B was entered. In accordance with Action B, the Reactor Core Isolation Cooling (RCIC) system was verified to be operable. Action B provides a 14 day completion time to restore HPCS to an operable status. All other Emergency Core Cooling Systems (ECCS) were operable during this event. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function credited for mitigating the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). The HPCS system is a single train system at Columbia. The leak was isolated and starting air header pressure restored to the HPCS diesel generator at 0104 PDT on September 25, 2019, and all associated Technical Specifications were exited. The NRC Resident Inspector was notified.Reactor Core Isolation Cooling
High Pressure Core Spray
Emergency Core Cooling System
ENS 529993 October 2017 15:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Inoperable Due to Unexpected Isolation of Exhaust ValveOn October 3, 2017, at 0800 PDT, Reactor Building (Secondary Containment) pressure momentarily rose above the Technical Specification (TS) limit. Secondary Containment was declared inoperable and TS Action Statement 3.6.4.1.A was entered. The pressure rise was due to unexpected isolation of an exhaust valve in the Reactor Building ventilation system during electrical switchgear inspections. The cause of the closure is still under investigation. The Control Room operators reopened the Reactor Building exhaust valve and pressure returned to within limits automatically. Secondary Containment was declared operable at 0802 PDT and TS Action Statement 3.6.4.1.A was exited. This condition is being reported under 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D) for an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material and accident mitigation. The NRC Resident Inspector has been notified.Secondary containment
Reactor Building Ventilation
05000397/LER-2017-007
ENS 5296612 September 2017 19:28:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Pressure Momentarily Above Technical Specification LimitOn September 12, 2017, at 1228 PDT, Reactor Building (Secondary Containment) pressure momentarily rose above the Technical Specification (TS) limit. Secondary Containment was declared inoperable and TS Action Statement 3.6.4.1.A was entered. The pressure rise was due to unexpected isolation of the supply and exhaust valves in the Reactor Building ventilation system due to an electrical transient on the power panel feeding the valve operators' solenoid pilot valves during maintenance. The cause of the electrical transient is under investigation. The Reactor Building differential pressure controller restored the building pressure to within limits. The Control Room operators reopened the Reactor Building ventilation supply and exhaust valves. Secondary Containment was declared operable at 1228 PDT and TS Action Statement 3.6.4.1.A was exited. This condition is being reported under 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D) for an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material and accident mitigation. The licensee notified the NRC Resident Inspector.Secondary containment
Reactor Building Ventilation
05000397/LER-2017-005
ENS 5284811 July 2017 14:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentFlow Indicating Switch for High Pressure Core Spray Unreliable Indication

This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function. On July 11th, 2017, it was discovered that the flow indicating switch for the high pressure core spray (HPCS) minimum flow valve was providing unreliable indication. There was no flow through the line at the time the condition was discovered. This switch provides the flow signal to the HPCS minimum flow valve logic. The switch was declared inoperable and the required actions of Technical Specification 3.3.5.1 were entered. This condition could have prevented the HPCS system, a single train safety system, from performing its specified safety function. Troubleshooting is underway to determine the cause of and correct the condition. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM DAN SHARPE TO KARL DIEDERICH AT 1710 EDT ON 9/20/17 * * *

The condition reported in Event notification #52848 pursuant to 10 CFR 50.72(b)(3)(v)(D) has been evaluated, and determined not to have met the threshold for classification as an Event or Condition the Could Have Prevented Fulfillment of a Safety Function. Engineering analysis has concluded that the affected switch was capable of performing its required support function to provide the flow signal to the HPCS minimum flow valve logic. Thus, the HPCS system remained capable of performing its specific function for the identified condition. The NRC Resident Inspector has been notified. Notified R4DO (G. Miller).

High Pressure Core Spray
ENS 5283027 June 2017 00:56:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Declared InoperableOn June 26, 2017 at 1756 PDT, Reactor Building (Secondary Containment) pressure rose above the Technical Specification (TS) requirement multiple times from 1756 to 1800. Secondary Containment was declared inoperable and entry into Technical Specification Action Statement 3.6.4.1.A was made. There was a significant change in average wind speed and barometric pressure occurring at that time. At 1800 PDT, Secondary Containment pressure was restored to within limits and TS 3.6.4.1.A was exited. Environmental conditions have stabilized. The Reactor Building Differential Pressure controllers are working as designed. This condition is being reported under 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D) for an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material and accident mitigation. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 5251026 January 2017 02:36:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray System Diesel Room Fan Motor FailureOn January 25, 2017, at 1836 PST, smoke was detected in the High Pressure Core Spray System (HPCS) diesel room with no indication of a fire. Investigation found the motor starter coil for DMA-FN-32 (Diesel Mixed Air Fan 32), HPCS diesel generator room normal cooling fan, failed. This fan is required for operability of the switchgear that powers the HPCS pump. The HPCS pump is currently inoperable due to maintenance being performed on other support systems. This condition is being reported under 10 CFR 50.72(b)(3)(v)(D) for an event or condition that could have prevented fulfillment of a safety function needed to mitigate the consequences of an accident. The licensee has notified the NRC Resident Inspector.High Pressure Core Spray05000397/LER-2017-001
ENS 5244319 December 2016 07:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Unisolable Leak on High Pressure Core Spray

On December 18, 2016 at 2320 (PST), a leak was discovered on the High Pressure Core Spray (HPCS) system minimum flow line. The leak is located at a bolted flange downstream of the manual isolation valve HPCS-V-53. The location of the leak is not isolable from the suppression pool. This provides a direct path from inside the Primary Containment to the Reactor Building. High Pressure Core Spray system is a single train Emergency Core Cooling System (ECCS) system, therefore inoperability is reportable per 10 CFR 50.72(b)(3)(v)(D). Based on the location of the leak, Primary Containment integrity is compromised. Primary Containment was declared inoperable and is reportable per 10 CFR 50.72(b)(3)(ii)(A). The cause of the leak is under investigation. Actions are underway to cool down and enter MODE 4. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM MATT HUMMER TO HOWIE CROUCH AT 2245 EDT ON 5/24/17 * * *

Engineering evaluations indicate that there was neither a High Pressure Core Spray (HPCS) system inoperability nor a condition that resulted in a significantly degraded principal safety barrier (Primary Containment). Therefore, this event does not meet the reporting criteria in 10 CFR 50.72(b)(3)(v)(D) and 10 CFR 50.72(b)(3)(ii)(A), and Event Notification# 52443 is being retracted. Bases for the retraction are: (1) Extent or accumulation of water flooding the HPCS room would not have prevented the system from fulfilling any of its designated safety functions, if the system had received a starting signal due to an emergency; and (2) the consequences of the HPCS Minimum Flow Line leak into the Reactor Building were within the dose limits and did not have a significant effect on Primary Containment integrity; therefore, the Primary Containment was degraded but operable. The licensee has notified the NRC Resident Inspector. Notified R4DO (Groom).

Primary containment
High Pressure Core Spray
Emergency Core Cooling System
05000397/LER-2016-005
ENS 5238220 November 2016 22:02:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Differential Pressure Less than Technical Specification RequirementOn November 20, 2016 at 1402 PST, Reactor Building Exhaust Air Fan 1B, REA-FN-1B, failed to start in manual which caused the Technical Specification (TS) for secondary containment pressure boundary to not be met. The duration of the time that the secondary containment TS was not met was approximately less than one minute. REA-FN-1B was being started in manual during a shift of Reactor Building Ventilation to support a post-maintenance support task on REA-FN-1B. Secondary containment differential pressure was restored within the TS requirement of greater than or equal to 0.25 inch of vacuum water gauge by restarting Reactor Building HVAC Train A. The cause of REA-FN-1B failing to start is currently under investigation. This condition is being reported under 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D) for an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material and accident mitigation. The licensee has notified the NRC Resident Inspector.Secondary containment
HVAC
Reactor Building Ventilation
05000397/LER-2016-003
ENS 5152610 November 2015 04:40:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Building Vacuum Less than Technical Specifications RequirementAt 2040 PST on 11/9/2015, Reactor Building (Secondary Containment) pressure increased to above the Technical Specification Surveillance requirement of 0.25 inches vacuum water gauge for approximately seven minutes. Operators took action to manually start Standby Gas Treatment System to restore Reactor Building pressure. This event is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. The cause of the event is under investigation. There were no radiological releases associated with the event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector.Secondary containment
Standby Gas Treatment System
05000397/LER-2015-007
ENS 5122814 July 2015 06:39:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Pressure Increase Above Technical Specification Limit

Reactor Building (Secondary Containment) pressure increased to above the Technical Specification Surveillance requirement of 0.25 inches vacuum water gauge for approximately 2 minutes during a planned surveillance test due to a subsequent failure of REA-FN-1A (Exhaust Fan) to manually start during restoration from the surveillance test. This event is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. Prior to taking test data the surveillance test directs declaring Secondary Containment inoperable in anticipation of potentially exceeding 0.25 inches vacuum water gauge reactor building pressure during the conduct of the surveillance. Consequently Technical Specification LCO 3.6.4.1.A was entered with a 4 hour completion time to restore Secondary Containment to an operable state. Upon failure of REA-FN-1A to start immediate actions were taken to close reactor building ventilation dampers and secure ROA-FN-1A (Supply Fan). Following closure of ventilation dampers and stopping ROA-FN-1A reactor building pressure was quickly restored to less than 0.25 inches vacuum water gauge with Standby Gas Treatment that was already in operation as part of the surveillance test. There were no radiological releases associated with the event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector. Maximum Secondary Containment pressure noted was 0.1 inches positive water gage.

  • * * RETRACTION AT 1351 EDT ON 8/25/2015 FROM MATT HUMMER TO MARK ABRAMOVITZ * * *

Subsequent to the initial report, Columbia has since determined that per NUREG-1022 3.2.7 the event was not reportable as Secondary Containment was 'declared inoperable as a part of a planned evolution ... in accordance with an approved procedure and (Columbia's) TS (Technical Specifications).' No condition has been discovered that would have resulted in the system being declared inoperable prior to the surveillance. Therefore, this event is not considered to be a condition that could have prevented fulfillment of a safety function or a condition prohibited by TS and is not reportable to the NRC as a Licensee Event Report (LEA) per 10 CFR 50.73. The NRC Senior Resident Inspector will be notified. Notified the R4DO (Campbell).

Secondary containment
Reactor Building Ventilation
ENS 4983417 February 2014 08:44:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Secondary Containment Differential PressureReactor Building (Secondary Containment) pressure rose above the Technical Specification Surveillance requirement of 0.25 inches vacuum water gauge multiple times from 0044 (PST) to 0305 (PST) on 2/17/14. The alarm was received in the control room at 0305 (PST). This is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. Reactor Building pressure has been restored to normal (greater than 0.25 inches of vacuum water gauge), returning Secondary Containment to operable status. Highest actual value indicated was +0.21 inches pressure water gauge. The cause of the event is under investigation. There were no radiological releases associated with the event. The NRC Resident Inspector has been notified.Secondary containment
ENS 4972915 January 2014 17:07:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Secondary Containment Differential PressureReactor Building (Secondary Containment) pressure increased to above the Technical Specification Surveillance requirement of 0.25 inches vacuum water gauge briefly (5 minutes or less). This is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. Reactor Building pressure has been restored to normal (greater than 0.25 inches vacuum water gauge), returning Secondary Containment to operable status. Highest actual value was 0.21 inches vacuum water gauge. There were no radiological releases associated with the event. The differential pressure change is believed to have been caused by a momentary shift in Heating and Ventilation Systems dampers. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 4970910 January 2014 01:43:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Secondary Containment Differential PressureReactor Building (Secondary Containment) pressure increased to above the Technical Specification Surveillance requirement of 0.25 inches vacuum water gauge briefly (two minutes or less) on two occasions. This is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. Reactor Building pressure has been restored to normal (greater than 0.25 inches vacuum water gauge) returning Secondary Containment to operable status. The cause of the event is under investigation. There were no radiological releases associated with the event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector.Secondary containment
ENS 4963125 November 2013 23:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentBreach Sizes Exceeded for Control Room Envelope

On December 13, 2013 it was determined that a reportable condition has existed at Columbia Generating Station since 1500 hours (PST) on November 25, 2013. At 1500 hours on November 25, 2013, the Control Room Envelope (CRE) was declared inoperable based on the inability to ensure that the Control Room Emergency Filtration (CREF) System would be able to maintain a positive differential pressure with all areas surrounding the CRE boundary. Columbia does not have the installed instrumentation to directly monitor the differential pressure between the Main Control Room (MCR) and certain areas adjacent to the MCR. The pressure in the adjacent areas is controlled by placing conservative limits on allowed breach size for these adjacent areas. On November 25, 2013, it was identified that the combined breach size associated with several doors in these adjacent spaces resulted in exceeding the allowed limit. Based on exceeding the allowed breach size limit to the adjacent areas, the Control Room Envelope was declared inoperable, and Technical Specification Action Statement 3.7.3.B.1 was entered. An additional breach was discovered on 12/05/13 from a hole in ductwork passing through the cable spreading room, which is one of the adjacent areas to the CRE boundary, and that condition was added to the existing action statement 3.7.3.B.1. These are conditions that could have prevented fulfillment of a safety function of structures that are needed to mitigate the consequences of an accident and are reportable under 10 CFR 50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM BRIAN HEAVILIN TO VINCE KLCO ON 1/21/2014 AT 1720 EST* * *

In the case of this event, the Control Room Envelope (CRE) was declared inoperable and Technical Specification Action Statement 3.7.3.B.1 was entered conservatively based upon limited knowledge at the time of discovery. There is no installed differential pressure indication between the CRE and this area adjacent to the Main Control Room (MCR), therefore conservatively this adjacent area is included in the CRE, and leakage is administratively controlled. The leakage between the MCR and the adjacent area included in the CRE exceeded this administrative limit. Testing performed on November 20, 2013, prior to the December 13, 2013 reported events, as well as testing after the event, January 10, 2014, has demonstrated that the leakage identified does not prevent the Control Room Envelope (CRE) from establishing and maintaining the required differential pressure to ensure fulfillment of its required safety function for Control Room Habitability. The ability of the Control Room Emergency Filtration (CREF) system to perform its function of pressurizing and maintaining the Main Control Room positively pressurized with respect to its surroundings was not lost due to the leaking doors and duct specified in the event. Performance of the surveillance without these breaches sealed validated this conclusion. The event described above should not have been reported, as the Control Room Envelope was always operable and capable of fulfilling its safety function with the existing breaches and did not constitute a reportable event as conditions that could have prevented fulfillment of a safety function of structures that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector. Notified the R4DO (Spitzberg).

Control Room Envelope
ENS 4942510 October 2013 15:09:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentLow Pressure Core Spray Declared Inoperable

At 0809 PDT on 10/10/2013, after starting Standby Service Water (SW) pumps, Columbia Generating Station (Columbia) received a flow low alarm for the Low Pressure Containment Spray (LPCS) pump motor cooling water. The flow indicator SW-FIS-19 was reported too low to support pump function. The LPCS system was declared inoperable, and the appropriate Technical Specification action statement was entered. The cause of the low flow alarm has not been determined. This event is reportable under criterion 10 CFR 50.72(b)(3)(v)(D) 'Any Event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (D) Mitigate the consequences of an accident.' Columbia is continuing to troubleshoot and repair as appropriate to restore the SW flow to the LPCS pump. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 10/11/13 AT 1653 EDT FROM MATT HUMMER TO DONG PARK * * *

Subsequent to receipt of the low flow alarm, flushing of the flow indicating switch sensing lines was conducted. It has been determined that the instrument sensing lines are partially blocked providing a flow indication that is slow to respond to actual flow conditions. The flow is currently reading normally. The LPCS pump was declared operable on 10/10/13 at 1447 PDT. The initial notification incorrectly stated 'Low Pressure Containment Spray (LPCS)', the correct description is 'Low Pressure Core Spray (LPCS)'. The licensee has notified the NRC Resident Inspector. Notified R4DO (Hay).

  • * * RETRACTION FROM DAVID HOLICK TO JOHN SHOEMAKER AT 2030 EDT ON 10/18/13 * * *

Subsequent evaluation of this event found there was no actual low flow condition to the LPCS bearing cooler. A flow scan on the SW outlet line from the LPCS pump bearing cooler was conducted on 10/12/13 which confirmed the actual flow conditions were reading normally. The problem resides in the installed flow indication switch. Since there was no actual low flow condition to the LPCS bearing cooler, the LPCS pump could perform its safety function to mitigate an accident. Therefore, this event notification is being retracted. Notified R4DO (Azua). The licensee has notified the NRC Resident Inspector.

Service water
Core Spray
Containment Spray
ENS 4930726 August 2013 01:18:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Secondary Containment Differential PressureReactor Building (Secondary Containment) pressure increased to above the Technical Specification Surveillance requirement of 0,25 inches vacuum water gauge. This event is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. The Reactor Building differential pressure controller was placed in manual operation and Secondary Containment pressure was restored to normal (greater than 0.25 inches vacuum water gauge) returning Secondary Containment to operable status. Secondary Containment pressure was outside the allowable Technical Specification requirement for 4 minutes. There were no radiological releases associated with the event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector.Secondary containment
ENS 4915228 June 2013 00:58:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray and Division 3 Diesel Generator Inoperable for 20 MinutesAt 1758 (PDT) on June 27, 2013, an alarm signaling heating, ventilation and air conditioning (HVAC) trouble in the Division 3 diesel and high pressure core spray (HPCS) room was received in the main control room. Follow-up investigation determined that the switch for the normal room supply fan (DMA-FN-32) was off. It is believed that the switch may have been inadvertently mispositioned during ongoing work in the vicinity. A worker was moving a vacuum nearby and stopped when he heard the local alarm. Columbia Generating Station is performing further investigation to determine if there are other possibilities for DMA-FN-32 control switch being mispositioned. The fan was returned to service at 1819 (PDT). An Operation's supervisor was present when returning the switch to ON and verified the switch operated as expected. Loss of DMA-FN-32 results in both the HPCS diesel (DG-3) and the HPCS system being inoperable due to inadequate cooling of those systems. Offsite power for Division 3 was verified to be operable while DG-3 was inoperable. The loss of the HPCS system results in the loss of safety function for a single train system and thus is reportable under the 10 CFR 50.72 sections noted above. Appropriate Technical Specification actions were entered and exited for DG-3 and HPCS inoperability times. There was no radiological release associated with this event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector.HVAC
High Pressure Core Spray
05000397/LER-2013-006
ENS 4884222 March 2013 05:40:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Momentary Inner and Outer Reactor Building Access Doors Open Simultaneously

During performance of surveillance OSP-CONT-M102, secondary containment had been declared inoperable and Technical Specification 3.6.4.1.A had been entered. Operations personnel performing the surveillance were holding the inner door open and testing the outer door interlock. When the individual presented his badge to the badge reader and attempted to open the outer door, the door opened. Per the surveillance contingency actions, the individual immediately shut the door. Momentarily, both the inner and outer reactor building access doors were open. The surveillance was completed with no further issues. Technical Specification 3.6.4.1.A was exited and secondary containment was declared operable. There were no radiological releases associated with this event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM DIEGO SUAREZ TO DONALD NORWOOD AT 17:55 EDT ON 3/25/2013 * * *

The licensee is retracting this event based on the following: During subsequent evaluation for reportability, guidance in NUREG-1022 was reviewed. NUREG-1022 provides that removal of a system or part of a system from service as part of a planned evolution for maintenance or surveillance testing when done in accordance with an approved procedure and the plant's TS (unless a condition is discovered that could have prevented the system from performing its function) is generally not reportable. In the case of this event, the secondary containment system was removed from service as part of a planned surveillance test. TS Action 3.6.4.1.A was entered as directed by the governing surveillance procedure in anticipation of the airlock interlock testing which, by the very nature of the test, could result in both doors in a given airlock being open simultaneously.

The event described above should not have been reported in consideration of the guidance provided in NUREG-1022 and did not constitute a reportable event as a condition that could have prevented the fulfillment of a safety function under 10CFR50.72(b)(3)(v). The licensee will notify the NRC Resident Inspector. Notified R4DO (Pick).

Secondary containment
ENS 486567 January 2013 22:27:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Momentarily InoperableTechnical Specification 3.6.4.1 (Secondary Containment) requires that the secondary containment be operable. Surveillance requirement 3.6.4.1.3 requires verifying each secondary containment access inner door or each secondary containment access outer door in each access opening is closed. Maintenance personnel were moving scaffolding through Reactor Building outer security door (R-304) when an equipment operator opened inner door (R-305) to exit the Reactor Building. This resulted in both the Reactor Building inner and outer access doors being simultaneously open for a short duration. Normally, the doors are interlocked in which the inner door would not be able to be opened prior to the outer security door being closed. The equipment operator immediately closed the door and notified the Main Control Room. The outer security door (R-304) has been key-locked closed, until corrective actions can be determined. Columbia Generating Station is investigating why the interlock feature failed. There were no radiological releases associated with this event. No safety system actuations or isolations occurred. The licensee has notified the NRC Resident Inspector. Note: See similar event reported by licensee on 12/30/12, EN #48639, involving containment door interlock failure on doors R-204 and R-205.Secondary containment05000397/LER-2013-001
ENS 4863930 December 2012 13:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Momentarily InoperableTechnical Specification 3.6.4.1 (Secondary Containment) requires that the secondary containment be operable. Surveillance requirement 3.6.4.1.3 requires verifying each secondary containment access inner door or each secondary containment access outer door in each access opening is closed. During a fire tour, a security officer proceeded through Reactor Building outer security door (R-204) and opened the inner door (R-205) prior to the outer security door completely closing. This resulted in both the Reactor Building inner and outer access doors being simultaneously open for a short duration. Normally, the doors are interlocked in which the inner door would not be able to be opened prior to the outer security door being closed. The security officer immediately notified the Main Control Room and operations personnel verified both doors were locked and closed. The outer security door (R205) has been key-locked closed until corrective actions are determined. Columbia Generating Station is investigating why the interlock feature failed. There were no radiological releases associated with the event. No safety system actuations or isolations occurred. The Licensee has notified the NRC Resident Inspector.Secondary containment05000397/LER-2013-001
ENS 4813124 July 2012 18:22:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Secondary Containment Differential Pressure Due to the Trip of Secondary Containment Supply and Exhaust FansReactor Building (Secondary Containment) Supply Fan 1B (ROA-FN-1B) and Reactor Building Exhaust Fan 1B (REA-FN-1B) inadvertently tripped. Secondary containment pressure exceeded atmospheric pressure which does not meet the surveillance requirement to have secondary containment vacuum greater than or equal to 0.25 inches of water vacuum. This event is reportable as an event that could have prevented fulfillment of a safety function needed to control the release of radiation and mitigate the consequences of an accident. Alternate supply and exhaust fans were manually started within 4 minutes and Secondary Containment pressure was restored to normal (greater than 0.25 inches water vacuum) within 5 minutes, returning Secondary Containment to operable status. Event investigation is on-going to determine exact cause of the fans tripping; however, electrical maintenance activities were in progress at the time. There were no radiological releases associated with the event. No safety system actuations or isolations occurred. The licensee notified the NRC Resident Inspector.Secondary containment05000397/LER-2012-003
ENS 4751610 December 2011 12:56:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Inoperable Due to Icing of Reactor Building Intake FiltersSecondary containment pressure exceeded atmospheric pressure which does not meet the surveillance requirement to have secondary containment vacuum greater than or equal to 0.25 inches of water vacuum. Secondary containment was declared inoperable and the Limiting Condition for Operation (LCO) Action Statement was entered. Manual control of the reactor building pressure control system was taken. Vacuum was less than 0.25 inches of water for approximately 1 minute. Secondary containment is (now) operable. There were no actual radiological releases associated with the event. Actual secondary containment integrity was not challenged. The secondary containment pressure excursion was a result of icing of the reactor building intake filters which caused the automatic reactor building pressure control system to function improperly. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 4660420 December 2010 12:38:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentFuse Failure Causes Low Pressure Core Spray to Be InoperableOn December 20, 2010, the low pressure core spray (LPCS) system was declared inoperable due to loss of power to the LPCS minimum flow valve. The minimum flow valve supports operability by providing a flow path to prevent pump damage during situations where the LPCS pump has been started in response to a transient, but reactor vessel pressure is not low enough to allow LPCS injection. The power loss was caused by the clearing of all 3 line power fuses for the motor starter for the minimum flow valve. An apparent cause evaluation concluded that the most likely cause of the fuses clearing was a random fuse failure of one of the fuses at less than design amperage attributable to a defect in the fuse solder joint. The Technical Specification (TS) Required Action for LCO 3.5.1 Condition A, one low pressure ECCS injection/spray subsystems inoperable, was complied with by restoring the LPCS system to operable within the allowed completion time. The safety functions for LPCS are to provide inventory makeup and spray cooling during large breaks in the reactor coolant system that uncover the core. All remaining ECCS subsystems were operable and at no time did this event result in the loss of a safety function. The low pressure injection function was not challenged due to all three loops of the Residual Heat Removal (RHR) system Low Pressure Coolant Injection (LPCI) mode being operable while the core spray function was satisfied by the operable High Pressure Core Spray (HPCS) system. This event is being reported under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident tor a single train system. Historically, LPCS inoperabilities at Columbia (including initial review of this event) were not considered to be a single train system for reportability purposes. The basis for the historical consideration was assessment of LPCS inoperabilities consistent with the plant safety analysis and the associated system and safety function groupings which do not single out LPCS as a single train system. There are two pertinent groupings in the safety analyses which are aligned with the credited safety functions of LPCS. The two groupings are the low pressure injection system function (combined with LPCI), and a core spray system function (combined with HPCS). Industry precedent has been consistent with the historical position. However, recent NRC interpretations have considered safety function at the lowest system level which result in LPCS being considered as a single train performing a safety function in scope of the reportability rules in 10 CFR 50.72 and 50.73. A Licensee Event Report will be submitted for this event. As a result of the recent interpretation with regard to LPCS, a review of prior LPCS inoperabilities within the past three years is being performed to determine if the reporting criteria were met during prior events. If necessary, additional 10 CFR 50.72 and 10 CPR 50.73 notifications/reports will be made on prior LPCS inoperabilities . The licensee will notify the NRC Resident Inspector.Reactor Coolant System
High Pressure Core Spray
Core Spray
Residual Heat Removal
Low Pressure Coolant Injection
05000397/LER-2010-002
ENS 458167 April 2010 00:47:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentInitiation of Technical Specification Required Shutdown Due to Control Room Emergency Filtration System Being Declared Inoperable

At 1650 PDT Columbia Generating Station entered LCO 3.0.3 as required by LCO 3.7.3 for both divisions of Control Room Emergency Filtration (CREF) (being) inoperable. Entry into LCO 3.0.3 was required by Condition E of LCO 3.7.3, 'Two CREF subsystems inoperable in MODE 1, 2, or 3 for reasons other than Condition B' and has a Required Action to enter LCO 3.0.3 with an immediate Completion Time. Columbia commenced a plant shutdown at 1747 as required by LCO 3.0.3. (Columbia Generating Station) entered into Condition E of LCO 3.7.3 when it was determined that Radwaste Building Outside Air Smoke Detectors WOA-SMD-1A and WOA-SMD-1B did not meet seismic qualifications. Actuation of these smoke detectors would cause Radwaste Building Mixed Air Fire Dampers WMA-FD-1 and WMA-FD-2 to close. These fire dampers shutting would cause all CREF airflow to cease, preventing the control room from achieving a positive pressure. Both divisions of CREF (being) inoperable is an unanalyzed condition requiring immediate entry into LCO 3.0.3. This event is reportable under 50.72(b)(2)(i) due to the initiation of a plant shutdown as required by Columbia's Technical Specifications. This event is also reportable under 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. WMA-FD-1 and WMA-FD-2 have been deactivated in the open position for the smoke actuation function. (Columbia Generating Station) entered RFOLCS (Requirements for Operability of Licensee Controlled Specifications) 1.10.6 for these fire dampers (being) nonfunctional. (Columbia Generating Station) completed the required actions of LCS 1.10.6. The CREF system remains inoperable pending completion of a TMR (Temporary Modification Request). The licensee notified the NRC Resident Inspector.

* * * UPDATE FROM QUOC VO TO CHARLES TEAL ON 4/7/10 AT 1957 * * * 

Question posed by NRC at time of initial report: Have these smoke detectors been installed since startup? Response: These smoke detectors have been installed since initial plant startup. A temporary modification request was installed to de-energize the non-seismic detector logic that causes automatic fire damper actuation for the two dampers identified above. The alarm function of the smoke detectors remains active with this temporary modification. Entry into this condition was made when it was determined that the smoke detectors were not seismically qualified and there is a possible failure mode that during an earthquake the detectors would actuate the electro-thermal link and cause the associated fire damper (WOA-FD-1 or WOA-FD-2) to close, hence impacting control room emergency filtration function. With implementation of the temporary modification at 2218 PDT on 4/6/10, the CREF system is now considered to be in an 'operable but non-conforming' status. As such, LCOs 3.7.3 and 3.0.3 were exited at 2218 PDT on 4/6/10. This event was initially reported pursuant to paragraph 50.72(b)(2)(i) as an initiation of a plant shutdown required by Columbia's Technical Specifications. Reporting pursuant to paragraph 50.72(b)(2)(i) is being retracted because negative reactivity was not inserted into the reactor prior to exiting the LCOs described above. Reporting pursuant to paragraph 50.72(b)(2)(i) would not be consistent with the guidance provided in NUREG-1022 in that no negative reactivity was inserted and the condition was corrected before exceeding the required action times. The licensee notified the NRC Resident Inspector.

* * * RETRACTION FROM KYLE CHRISTIANSON TO PETE SNYDER AT 1550 EDT ON 4/29/2010 * * *

Subsequent to the April 7, 2010, event report (EN #45816), an Energy Northwest engineering evaluation concluded that the identified smoke detectors would not inadvertently actuate during a design basis safe shutdown earthquake (SSE). This conclusion is based on a seismic response spectrum test report for the smoke detectors. Therefore, since the safety function of the CREF system needed to mitigate the consequences of an accident would not be affected by an SSE, the event notification made pursuant to 10 CFR 50.72 (b)(3)(iv)(D) is hereby retracted. The NRC Senior Resident Inspector (Cohen) has been notified. Notified R4DO (Clark).

Control Room Emergency Filtration System
ENS 4149916 March 2005 17:43:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray System Inoperable Due to Degraded Pump Motor Air DeflectorThe following information was provided by the licensee via facsimile (licensee text in quotes): At 0943 with Columbia Generating Station operating at 100% power the High Pressure Core Spray (HPCS) system was taken out of service for maintenance. During the maintenance activity, severe cracking and degradation was discovered on the upper air deflector of the HPCS pump motor. This component functions to direct air into the motor housing to provide cooling while the system is operating. A preliminary evaluation determined this represents a condition that at the time of discovery could have prevented fulfillment of the safety function of the HPCS system to mitigate the consequence of an accident and is reportable pursuant to 10 CFR 50.72(b)(3)(v)(D). Upon discovery of this condition plant operators fulfilled the action required by Technical Specifications LCO 3.5.1 condition B to verify by administrative means that the Reactor Core Isolation Cooling (RCIC) system is operable and took action to restore the HPCS system to operable status within 14 days. No other systems were required to function in response to this event. The licensee notified the NRC Resident Inspector.Reactor Core Isolation Cooling
High Pressure Core Spray
05000397/LER-2005-002
ENS 4144225 February 2005 02:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentPotential Breach of Secondary Containment During Seismic Event.

The licensee provided the following information: This event notification is being made to report an event that could have prevented fulfillment of the safety function to mitigate the consequences of an accident IAW 10CFR50.72(b)(3)(v)(D). The potential for creation of an actual hole through Secondary Containment (SC) via the Plant Service Water (TSW) system high point reactor building auto vents (TSW-AV-1A and TSW-AV-1 B) exists if a seismic event occurs and the Seismic Category 2 TSW loop-seal piping outside of Secondary Containment is breached (e.g., because of a pipe break) and has drained. Neither of the above conditions presently exists. However, a Secondary Containment breach could occur as a result of a single passive failure (i.e., pipe break in the TSW loop-seal piping described above). TSW-AV-1A and TSW-AV-1B are designed to open automatically when neither TSW system pump is operating to break the vacuum condition that would otherwise exist in the piping. When TSW-AV-1A and TSW-AV-1B are open in vacuum breaker mode, the resultant hole size into the TSW system piping would exceed the allowable Secondary Containment cumulative hole size ( of 32 square inches total), if the loop seal were also breached as described above. Due to this condition Secondary Containment was declared INOPERABLE at 1800 PST 2/24/05. As a compensatory measure to prevent exceeding the allowable Secondary Containment cumulative hole size, one of the two TSW reactor building auto vents (TSW-AV-1B) was isolated by closure of a manual valve (TSW-V-55B). This action was completed at 1828 PST 2/24/05 and the Secondary Containment was declared OPERABLE. One TSW auto vent is sufficient to perform the vacuum breaker function. This condition was found by the licensee's System Engineer. The extent of condition and long term corrective action is under review by licensee. Licensee will inform the NRC Resident Inspector.

  • * * RETRACTION FROM FRED SCHILL TO HOWIE CROUCH @ 1535 EDT ON 04/05/05 * * *

The following information was obtained from the licensee via facsimile (licensee text in quotes): On 2/25/05, Columbia Generating Station reported (ref: EN 41442) a condition that was discovered while reviewing service water (TSW) system design documents. During the review, it was determined that Seismic Category II TSW piping in the turbine (TG) and radwaste (RW) buildings could rupture and drain during a seismic event. This event would result in an inoperable secondary containment (SC) because TSW system high point vent valves located within the SC would automatically open when the piping drained after rupturing. Such an event would allow direct communication between the SC atmosphere and the TG/RW atmospheres and exceed the leakage rate assumed in Columbia's accident analysis. There are two principal accidents in Columbia's safety analysis for which SC is credited as a mitigating system. These are the Loss Of Coolant Accident (LOCA) and the Fuel Handling Accident (FHA). The SC performs no active function in response to either of these limiting events, however, its leak tightness is required to ensure that the release of radioactive materials from the primary containment is restricted to those leakage paths and associated leakage rates assumed in the accident analysis, and that fission products entrapped within the SC structure will be treated prior to discharge to the environment. Assuming a seismic event of the magnitude (0.25g) of the Safe Shutdown Earthquake (SSE) occurred and ruptured the TSW piping causing SC to become inoperable, it is beyond Columbia's safety analysis to postulate a release of radioactive material beyond Part 100 limits for that event. This is because analysis shows that the SSE will not in itself cause a LOCA or an FHA and Columbia's design and licensing bases do not assume a LOCA or FHA coincident with a seismic event. In the event that the SSE made SC inoperable, the Technical Specifications (LCO 3.6.4.1.B) require that the plant be in mode 3 in 12 hours and in mode 4 in 36 hours. Since this is achievable, it is reasonable to conclude that, in the event previously reported, plant shutdown can be accomplished without radiological release and within the completion time of the action required by the Technical Specifications. The discussion in the guidance document (NUREG 1022) for reporting under Part 50.72(b)(3)(v) states the level of judgment for reporting under these criteria is a reasonable expectation of preventing fulfillment of a safety function. It also states that the intent of the criteria is to capture those events where there would have been a failure of a safety system to properly complete a safety function regardless of whether there was an actual demand. This discussion however, as the Part 50.72(b)(3)(v) and Part 50.73(a)(2)(v) criteria state, apply to safety functions of systems or structures that are needed to control the release of radioactive material, because safe shutdown of the plant without radiological release is assured post SSE (sans SC), as described in Columbia's design and licensing bases, SC would not be needed to control the release of radioactive material and therefore the reporting criteria is not met. The licensee will be voluntarily submitting a Licensee Event Report as a method of information sharing with the rest of the industry. The licensee has notified the NRC Resident Inspector. Headquarters Operations Officer notified R4DO (Howell).

Secondary containment
Service water
Primary containment
ENS 4121623 November 2004 01:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentInadvertent Isolation of the Reactor Core Isolation Cooling SystemThis ENS notification is made to report that on November 22, 2004 at 17:30 PST the Reactor Core Isolation Cooling (RCIC) system was rendered inoperable when its inboard steam supply containment isolation valve inadvertently closed during the performance of a routine surveillance procedure. The surveillance procedure was stopped and plant operators entered the appropriate Technical Specification Action Statements. The RCIC system was restored to its normal standby lineup and declared operable two hours and three minutes after the isolation. NRC guidance in NUREG 1022 (Rev. 2), 'Event Reporting Guidelines,' and NRC Regulatory Issue Summary (RIS) 2001-14, 'Position on Reportability Requirements for Reactor Core Isolation Cooling System Failure,' indicates that RCIC failures are not reportable unless the RCIC system is specifically credited in the plant's Final Safety Analysis Report for mitigating the consequences of a Control Rod Drop Accident (CRDA). Columbia Generating Station has determined that the current licensing basis and docketed correspondence is not clear regarding RCIC credit for CRDA mitigation. Proposed FSAR changes were recently submitted by Energy Northwest to the NRC that would clarify that RCIC is not credited for CRDA mitigation. However, the NRC staff has not yet approved these proposed changes. Therefore, Columbia Generating Station has decided to conservatively report this event under 10 CFR 50.72(b)(3)(v)(D). A follow-up LER will be issued under 10 CFR 50.73(a)(2)(v)(D). The licensed has notified the NRC Resident Inspector.Reactor Core Isolation Cooling
Control Rod
ENS 4078530 May 2004 18:37:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray System Inoperable

The High Pressure Core Spray (HPCS) system was declared inoperable due to the pump's failure to meet the flow requirement specified in TS Surveillance Requirement 3.5.1.4. This surveillance is normally performed on a quarterly basis in accordance with the plant's In-service Testing (IST) Program. The flow values measured during the performance of this surveillance were below both the normal and alert ranges. This test had also been run on 5/27/04 with results in the alert range; HPCS system instruments had been vented between the two tests to rule out the possibility that the results were due to measurement errors. Upon declaring the HPCS pump inoperable, TS 3.5.1 Action B was entered. In accordance with Action B, the Reactor Core Isolation Cooling (RCIC) system was verified to be operable. With the RCIC system verified operable, Action B provides a 14-day completion time to restore HPCS to an operable status. All other Emergency Core Cooling Systems (ECCS) were operable during this event. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function credited for mitigating the consequences of an accident. The HPCS system is a single train system at Columbia. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 06/14/04 @1752 BY MIKE BRANDON TO C. GOULD * * * RETRACTION

On May 30, 2004, Energy Northwest provided an 8-hour notification pursuant to 10 CFR50.72(b)(3)(v)(D). This notification reported the apparent failure of the High Pressure Core Spray (HPCS) system's pump to meet the flow requirements of Surveillance Requirement (SR) 3.5.1.4. Upon the apparent failure to satisfy this SR, Energy Northwest entered Action B of Technical Specification (TS) 3.5.1 (14 day completion time) and initiated actions to investigate the cause of this apparent failure. This investigation determined the cause of this apparent failure was due to an anomaly in the processing of the pressure and flow input signals and the instrumentation used for documenting the results of the surveillance. Additional testing using alternative instrumentation determined the HPCS pump was fully capable of providing flow within the existing acceptance criteria of the plant's In-service Testing (IST) Program and thus capable of satisfying the SR. This investigation determined that no actual degradation of the pump existed that would have caused a valid failure of the SR. This was an instrumentation issue only. The HPCS system would have been capable of performing its specified safety function in the as-found condition and was capable of fully satisfying the SR. Therefore, this condition would not have prevented the fulfillment of a safety function and is therefore not reportable under 10CFR50.72. The HPCS system was declared OPERABLE on June 03, 2004 at 22:59 PDT. The NRC Resident Inspector was notified.

Reactor Core Isolation Cooling
High Pressure Core Spray
Emergency Core Cooling System
ENS 4053621 February 2004 16:41:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentRcic System Inoperable Due to Possible Undervoltage Relay FailureThis ENS notification is made to report that on February 21, 2004 at 0841 PST Reactor Core Isolation Cooling was rendered inoperable due to RCIC-V-13 (RPV injection valve) motor operator losing power. Preliminary investigation indicates the undervoltage relay may have failed, resulting in a loss of control power for the valve and loss of valve position indication. The event is considered reportable to the NRC under 10 CFR 50.72(b)(3)(v)(D) based on guidance contained in NUREG 1022, "Event Reporting Guidelines," and NRC Regulatory Issue Summary (RIS) 2001-14, 'Position on Reportability Requirements for Reactor Core Isolation Cooling System Failure.' A follow-up LER will be issued under 10 CFR 50.73(a)(2)(v)(D). This event placed the plant in technical specifications LCO 3.5.3 which has a 14 day duration. The licensee notified the NRC Resident Inspector.Reactor Core Isolation Cooling
ENS 402872 November 2003 01:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accidentan Event That Could Have Prevented Fulfillment of the Safety Function to Mitigate the Consequences of an Accident,
ENS 402297 October 2003 19:31:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray Declared Inoperable (Hpcs)At 1231 hours on October 7, 2003, the High Pressure Core Spray (HPCS) system at Columbia Generating Station was declared inoperable due to a failure to maintain system pressure while the system was being operated with the keep-fill piping isolated for maintenance on the system waterleg pump. This action rendered the HPCS system unable to perform its safety function to mitigate the consequences of an accident. Upon discovery of the inoperable condition, the Reactor Core Isolation Cooling system was verified to be operable and HPCS was restored to operable status at 1538 in accordance with the Required Action of plant Technical Specifications Limiting Condition for Operability 3.5.1, Conditions B.1 and B.2. All other Emergency Core Cooling System (ECCS) were operable during the time the HPCS system was inoperable. This event is being reported pursuant to the guidance for reporting under 50.72(b)(3)(v)(D) contained in NUREG 1022, which states for single train systems that perform a safety function, loss of a single train would prevent the fulfillment of the safety function and therefore is reportable. The NRC Resident Inspector will be notified of this event by the licensee.Reactor Core Isolation Cooling
High Pressure Core Spray
Emergency Core Cooling System
ENS 4009822 August 2003 09:34:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentReactor Core Isolation Cooling System InoperableThis ENS notification is made to report that on August 22, 2003 at 02:34 PDT Reactor Core Isolation Cooling was isolated due to the discovery of a degraded pilot cell in the Division 1 250 VDC battery. Operators isolated the steam inlet valve to the RCIC turbine (RCIC-V-1) because the minimum flow bypass valve, RCIC-V-19, (a primary containment isolation valve) was declared inoperable and isolated to comply with the plant TS. Isolation of RCIC-V-1 effectively removed RCIC from service since it is the containment isolation valve. The event is considered reportable to the NRC under 10 CFR 50.72(b)(3)(v)(D) based on guidance contained in NUREG 1022, "Event Reporting Guidelines," and NRC Regulatory Issue Summary (RIS) 2001-14, "Position on Reportability Requirements for Reactor Core Isolation Cooling System Failure." A follow-up LER will be issued under 10 CFR 50.73(a)(2)(v)(D). The licensee will be notifying the NRC Resident Inspector.Reactor Core Isolation Cooling
Primary containment