ML20235T850

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Insp Rept 50-354/87-17 on 870714-0817.Violation Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Maint Activities,Operational Safety Verification,Surveillance Testing,Esf Sys Walkdown & Instrument Calibr Data Cards
ML20235T850
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 10/01/1987
From: Swetland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20235T827 List:
References
50-354-87-17, NUDOCS 8710130249
Download: ML20235T850 (14)


See also: IR 05000354/1987017

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S.' NUCLEAR REGULATORY COMMISSION

REGION I.

050354-870605

050354-870608

Report No.

50-354/87-17

_050354-870611'

050354-870624

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Docket

=50-354

050354-870626

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050354-870629

License

NPF-57

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Licensee:

Public Service Electric and Gas Company

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Facility:

Hope Creek Generating Station

Conducted:

July 14, 1987 - August 17, 1987-

Inspectors:

R. W. Borchardt, Senior. Resident Inspector

D. K. Allsopp, Resident Inspector

R. J. Summers, Project Engineer

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R. R. Brady, k ctor

gineer

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Approved:

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P. Swetland, Chief, Projects Section 2B

Oate

Inspection Summary:

Inspection on July 14, 1987 - August' 17,'1987 (Inspection Report Number

50-354/87-17)

Areas Inspected: Routine onsite resident inspection of theLfo110 wing

areas:

followup on outstanding inspection items, operational ~ safety

verification, surveillance testing,' maintenance activities, engineered

safety feature system walkdown, residual heat removal pressure transmitter-

operability, instrument calibration data cards,' review of non-essential

diesel. generator trips, and licensee event report followup.

This-

inspection involved 189 hours0.00219 days <br />0.0525 hours <br />3.125e-4 weeks <br />7.19145e-5 months <br /> by the inspectors.

Results: One apparent violation of Technical Specifications was identified

concerning the control of plant equipment (paragraph 7)

.Although-this viola-

tion was licensee identified, its similarity to a violation cited in NRC

Inspection Report 50-354/86-48 and to other recent plant equipment control

problems is of concern to the NRC. An enforcement conference will be scheduled

regarding these problems.

Paragraph 8 of this report details the NRC's understanding of the licensee's

corrective action commitments in response to incorrect instrument calibration

data cards.

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8710130249'871005

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PDR

ADOCK 05000354

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DETAILS

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1.

Persons Contacted

Within this report period, interviews and discussions were conducted

with Mr. S. LaBruna and members of the licensee management and staff'

and various contractor personnel as necessary to support inspection

activity.

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2.

Followup on Outstanding Inspection Items

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a.

(Closed) Inspector Follow Item (87-05-01); Mislabeled in-line smoke

detectors in the control room emergency filtration (CREF) system.

While inspecting the "A" CREF train, the inspector identified

incorrect labeling on two in-line smoke detectors (XSH 9588A2, XSH

9588A1). The licensee also determined that the smoke detector

electrical output cables were incorrectly wired and labeled such

that the Al detector lit the A2 annunciator and vice versa.

Since

these are redundant indicators in the same duct, there were minimal

consequences from this wiring problem.

The licensee implemented

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design change DCR 4-HM-0116 to correct the smoke detector and output

cable labeling, and to swap electrical leads at control panel 10C413.

The licensee. conducted a functional retest on the in-line fire

detection system following the design change completion, to insure

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correct alarm point response.

The inspector verified the correct

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labeling on the smoke detectors and output cables in panel 10C413,

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This item is closed.

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b.

(Closed) Unresolved Item (87-16-02); Instrument root valve for

RHR pressure transmitter isolated.

This item has been upgraded to a

violation and is discussed in paragraph 7 of this report.

This item

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is closed.

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(Closed) Unresolved Item (87-14-03); Backflow of drains into the

scram discharge volume (SDV).

The inspector held discussions with

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the system engineer, reviewed the control rod drive hydraulic system-

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isometric drawings, and reviewed the liquid radioactive waste (LRW)

piping and instrument diagram.

The SDV vent and drain valves both

drain to the LRW tank which is vented to preclude an internal

pressure increase. The LRW tank is located a minimum of 38 feet

below the vent and drain taps off the SDV.

The-inspector concluded

there was no feasible scenario in which the LRW tank could backflow

and fill the scram discharge volume. This item is closed.

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3.

Operational Safety Verification

3.1 Inspection Activities

On a daily basis throughout the report period, inspections were

conducted to verify that the facility was operated safely and in

conformance with regulatory requirements.

The licensee's

management control system was evaluated by direct observation of

activities, tours of the facility, interviews and discussions

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with licensee personnel, independent verification of safety

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system status and limiting conditions for operation, and review

of facility records.

The licensee's adherence to the radiological

protection and security programs was also verified on a periodic

basis.

These inspection activities were conducted in accordance with~

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NRC inspection procedures 71707, 71709, and 71881 and included

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weekend and backshift inspections conducted on July 16 (0:30-6:00

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a.m.), July 19(4:30-10:30 p.m.), and August 16 (10:00-1:30 p.m.)

3.2 Inspection Findings and Significant Plant Events

The unit entered this report period at maximum allowable power as

limited by the transmission network stability curves generated after

the damage of the Keeney 500 KV transmission lines.

The unit

continued to operate at full power throughout this report period

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except for short power reductions for testing and as discussed below.

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On July 14, 1987, the plant. experienced a high pressure coolant

injection (HPCI) automatic start in response to an erroneous

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reactor vessel low leesl signal.

The HPCI system was secured

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prior to water injection into the reactor vessel. The low

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vessel level signal was generated from a minor pressure spike in

a level transmitter common reference leg while valving in a fuel

zone level transmitter. The fuel zone level transmitter and

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a wide range reactor vessel level transmitter which share a common

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instrument line were isolated to prevent spurious ESF actuations

while drawing a post accident sample for training. The sample is.

drawn from the same common instrument line used by the level trans-

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mitters.

The wide range transmitter provides an input into the HPCI

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automatic start logic.

During the restoration of the fuel zone

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transmitter, a pressure spike was transmitted to the wide range

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level instrument creating the spurious HPCI actuation,

The root cause of this occurrence was determined

to be related to the high sensitivity of the Rosemount 1153 level

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transmitters.

The level transmitters have a very short response time

and are therefore overly sensitive to minor pressure perturbations in

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the reference leg caused by isolation valve manipulations.

Short

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term corrective actions consisted of reemphasizing to instrument and

calibration technicians the need to valve in level transmitters in a

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slow and deliberate manner.

Longer term corrective actions consist

of implementing a previously identified design change to replace the

electronics module on this and all Rosemount 1153 level transmitters

when environmental qualification of the redesigned module is

complete.

This design change is scheduled for implementation during.

the first refueling outage.

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At 9:10 a.m. on July 30, 1987, the reactor automatically scrammed due

to a reactor vessel low water level condition.

The HPCI and Reactor

Core Isolation Cooling (RCIC) systems automatically initiated and

injected water into the vessel until secured by the operators.

The

plant responded as designed and vessel water level was quickly

restored to normal.

The low water leve1 condition was caused by a

temporary loss of power to the feedwater control logic normally

energized by miscellaneous instrumentation power supply IBD483.

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loss of power occurred when an equipment operator made an error while

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switching power supplies to inverter 180483.

The power supplies were

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being switched to allow performance of preventative maintenance on

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the inverter. While attempting to transfer the inverter power supply

from an alternate to normal source, the transfer switch was

momentarily placed in an incorrect position which caused the main

fuse on the inverter section to blow, deenergizing the feedwater

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level control (FWLC) system and other loads normally supplied by

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IBD483. The loss of power to the FWLC system caused reactor vessel

water level to decrease until the low water level scram setpoint was

reached. The unit remained in hot standby until the restart was

authorized following the identification of the root cause of the

event.

The reactor was made critical at 9:36 p.m. on July 31.

Hope

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Creek was synchronized with the grid at 4:45 a.m. on August 1 and

reached full power at 6:05 p.m. the same day.

On July 30, 1987, the "E" Filtration Recirculation Ventilation

System (FRVS) fan automatically started for no apparent reason.

The "E" FRVS fan was quickly secured and returned to its normal

line-up. There are six FRVS units, five of which are normally

running, with the remaining unit in standby.

The standby unit

automatically starts on either an accident actuation signal or low

flow in one of the other units. The licensee determined the cause of

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the FRVS fan start signal was due to dirty contacts on the low flow

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switches for the "A" FRVS fan.

When low flow was spuriously sensed

at the "A" FRVS fan, the "E" FRVS fan received an automatic start

signal.

The licensee has cleaned the low flow switch contacts on

both the "A" and "B" FRVS fans and has received no additional spurious

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FRVS actuations.

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On August 6, 1987, the licensee identified a potential environmental

qualification problem on flow switches in the FRVS (Dwyer EP

Switches, Model No. 1950-00-2B)' system. The flow' switches.in

question, will auto start the "E"

and "F" FRVS fans upon low flow in

either the "A", "B", "C" or "D"

trains.

Upon identifying the

potential problem, the licensee replaced the affected switches with

qualified equipment (Dwyer EP Switch, Model No. 1950-00-2F) taken

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from another system at the plant that did not need to meet the " harsh"

environmental qualification requirement.

Following the replacement,

on August 7, the inspector met with the licensee to deterraine the

cause of this problem.

The preliminary investigation indicates that

the vendor (Dwyer) substituted a different flow switch. - for a licensee

replacement parts order, resulting in the licensee receiving equipment

for which they had no record of environmental qualification. The

vendor was contacted and assured the licensee that the flow switches

were, in fact, environmentally qualified and'provided a copy of the-

environmental qualification (EQ) test data to the licensee.

Subsequently, the inspector determined that this same EQ test data

was, in fact, onsite during this occurrence, but had not been

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identified by licensee engineers.

On August 7, 1987, the licensee found an emergency diesel generator

(EDG) room recirculation fan control switch in the "off" position.

The licensee performed a walkdown of all control switches in the four

diesel generator rooms to verify that all other controls were

properly positioned. The affected EDG and one other were test

started satisfactorily. This is similar to a previous event in which

manual control switches for certain EDG support equipment were found

mispositioned. The EDG would have started and operated properly even

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with the recirculation fan off.

The licensee increased the security

patrols in the area and plans to add a checklist of switch positions

to the equipment operator daily log.

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On August 16, 1987, the licensee declared,and termina'ted an unusual

event for a reactor scram with HPCI injection which occurred at 2:07

a.m. the same day.

The plant was operating at 85's power prior to the

scram. All systems functioned as designed.

The reactor scram

occurred while operators were attempting to return the'"C" reactor

feedpump turbine (RFPT) to service after corrective maintenance and

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inadvertently blew a RFPT rupture disc.

This rupture disc protects

the RFPT exhaust piping and the main condenser from overpressure

conditions. After the disc blew out, condenser vacuum quickly

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dropped and tripped the two operating RFPTs.

Reactor' vessel level

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decreased until the scram occurred at level 3.

The licensee con-

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cluded that the most probable cause for the blown rupture disc was

due to steam leak-by past the RFPT steam isolation. valve. The

licensee has implemented an on-the-spot change to the RFPT startup

procedure to modify the valve sequence to minimize leakage past the

RFPT steam isolation valve. The licensee's declaration of the

unusual event was made approximately four hours after the reactor-

scram occurred. The licensee's failure to initially identify the

ECCS actuation with discharge to the vessel as an unusual event was

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due to poor indexing in the event classification guide (ECG). The

licensee has conducted operator training on the ECG as an interim

action, and will upgrade the ECG index as long term corrective action.

The licensee made the reactor critical at 3:10 p.m. on August 17.

and synchronized with the grid at 7:30 p.m. the same day.

No further inadequacies were identified.

4.

Surveillance Testing

4.1 Inspection Activity

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During this inspection period the inspector performed detailed

technical procedure reviews, witnessed in progress surveillance

testing, and reviewed completed surveillance packages.

The

inspector verified that the surveillance tests were performed in

accordance with Technical Specifications, licensee approved

procedures, and NRC regulations.

These insnection activities

were conducted in accordance with NRC ins;+ction procedure

61726.

The following surveillance tests were reviewed, with portions

witnessed by the inspector:

- IC-FT.SE-020

Functional Test of "B" Rod Block Monitor

- IC- FT . S E-006

Functional Test of Intermediate Range

Monitor (IRM) "B"

IC-FT.SE-011

Functional Test of IRM "G"

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- IC-SC.BJ-010

High Pressure Coolant In.jection (HPCI)

Suppression Pool' Level sensor calibration

OP-IS.BJ-001

HPCI Inservice Test

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No violations were identified.

5.

Maintenance Activities

5.1

Inspection Activity

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During this inspection period the inspector observed selected

maintenance activities on safety related equipment to ascertain

that these activities were conducted in accordance with approved

procedures, Technical Specifications, and appropriate industrial

codes and standards.

These inspections were conducted-in accordance

with NRC inspection procedure 62703.

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5.2. Inspection Findings

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Portions of the following activities were observed by the

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inspector:

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Work Order

Procedure

Description

87-07-017-039-4

CH-DC.ZZ-002

Troubleshoot,

rework, and

calibrate the

"B"

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hydrogen oxygen.

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analyzer

870810050

DCP 4-HM-0156

Standby liquid

control system

relay replacement

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870805082

MD AP.ZZ-15(Q)

Standby liquid

CJP-H-87-043

control system

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squib valve

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replacement and

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hydrostatic test.

Additional details on the standby liquid control system maintenance

can be found in paragraph 6 of this report.

No violations were identified.

6.

Engineered Safety Feature (ESF) System Walkdown

6.1 Inspection Activity

The inspectors independently verified the operability of . selected ESF

systems by performing a walkdow1 of accessible portions of the system

to confirm that system lineup procedures match plant drawings and the

as-built configuration.

This ESF system walkdown was also conducted

to identify equipment conditions that might degrade performance, to

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determine that instrumentation is calibrated and functioning, and to

verify that valves are properly positioned and locked as appropriate.

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This inspection was conducted in accordance with NRC inspection

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procedure 71710.

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6.2 Inspection Findings

The standby liquid control (SLC) system was inspected and in plant

conditions were found to be acceptable. _The inspector verified that

certain technical specification surveillance test requirements are

satisfied through a review of the following procedures

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OP-ST.BH-001

SLC Valve Operability Test - Monthly

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OP-ST.BH-002

SLC Flow Test - 18 Month

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OP-ST.BH-003

SLC System Tank Flow Test - 18 Month

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OP-ST.BH-004

SLC Storage Tank Operability Test - 18 Month

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OP-IS.BH-001

Standby Liquid Control Pump Inservice _ Test

Although a number of minor material deficiencies such as valve

packing leaks were noticed by the inspector, the licensee had

previously identified these items and had scheduled repairs.

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The NRC staff has expressed concern that the current Hope Creek

technical specification requires a SLC pump minimum flow of 41.2 gpm

(82.4 gpm total) as compared to the 10 CFR 50.62(c)(4) minimum flow

rate of 86 gpm at a 13.0 weight percent (w/o) sodium pentaborate

solution.

The SLC pumps currently produce a total flow of 89.9 gpm.

The licensee has responded to NRC's concern by submitting a license

change request dated July 14, 1987 to increase the minimum required

sodium pentaborate solution concentration to 14.0 w/o, thereby

ensuring that a sufficient amount of sodium pentaborate will enter

the reactor vessel when required, even with reduced SLC pump flow.

This amendment request is currently under review by NRC:NRR.

At 9:44 p.m. on August 4, 1987, the plant experienced an automatic

initiation of the "B" SLC pump and firing of the associated squib

valve.

The control room operator secured the pump 12 seconds after

it started since it was obvious from control room indications that

there was no valid reason for the auto start. At 10:10 p.m., the "B"

SLC pump automatically started again and was secured by the operator

after a 7 second run.

In order to prevent further automatic starts,

the electrical power supply breaker for the pump was opened and the

SLC system was declared inoperable.

The licensee conducted an

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investigation into the cause of these automatic starts and found that

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the redundant reactivity control system (RRCS) self test circuit

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pulses were causing a fluttering movement of the Struthers-Dunn

isolation relays located between RRCS and the Bailey 862 logic

cards. Although not proven conclusively, the l',ensee believes that

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under the right circumstances, the relay fluttering could momentarily

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pass an initiation signal from RRCS to the Bailey logic which has a

" seal in" feature.

Troubleshooting efforts did not identify any

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problems with the RRCS or the specific Bailey 862 logic cards.

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SLC system is the only Hope Creek system which utilizes isolation

relays to isolate the Bailey 862 logic cards from a self test circuit

pulse.

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As corrective action for this event, the licensee performed a design

change (DCR 4-HM-0156) to replace the Struthers-Dunn isolation relays

with Agastat relays in the circuitry for both SLC pumps. Testing and

post installation experience has shown that the Agastat relays are

not subject to the same fluttering movement because they have a

substantially larger. relay coil.

The design change package including

retest, safety evaluation, infield work, and system restoration was

observed by the inspector and found to be acceptable.

The licensee

intends to instrument the SLC circuitry so that should another

spurious initiation occur more troubleshooting data would be

available.

Based upon reactor vessel water samples and calculations considering

pump flow rate and run times it does not appear that any sodium

pentaborate entered the reactor vessel.

The SLC system piping was

drained and flushed to the maximum extent possible during power

operations and will be completely flushed during the upcoming fall

outage.

No violations were identified.

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7.

Control of Plant Equipment

During the previous inspection period, the licensee discovered that the

instrument root valve, P-BC-9993, for the

"C" RHR pump pressure

transmitters (PT-N055H and PT-N056D) was out of position (closed), thereby

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disabling an input to the automatic depressurization system (ADS)

permissive logic.

Each train of the ADS logic is set up such that the

ADS relief valves will not open unless either 1) both pumps in the

associated core spray loop are running or 2) one of the two RHR pumps

(Low Pressure Coolant Injection Mode) are running.

Having BC-9993 closed

prevented the possibility of actuating ADS using the "C" RHR pump.

This

condition requires entry into technical specification action statement 3.3.3

which declares the "C" RHR pump inoperable and allows continued operation

in this mode for 30 days. Once the licensee became aware of the mispositioned

valve it was immediately opened, returning the pressure transmitters to

service and fully restoring the ADS logic.

The licensee has been unable

to determine why, and for how long this instrument root valve (IRV) was

closed. The IRV was last known to be open during a routine surveillance

test on April' 10, 1987. At the time this event was identified, the pressure

transmitters for the other RHR pumps as well as the core spray pumps were

inservice, and would have resulted in normal actuation of the ADS logic.

However, since the licensee was unaware of the mispositioned root valve

other redundant components may have been voluntarily removed from service,

relying on the operability of the

"C" RHR pump and technical specification 3.3.3 action statement was exceeded because the IRV could have been isolated

longer than the 30 day allowed by the technical specification.

Licensee

corrective action included identifying each ADS IRV and affixing operator

aide tags to each, specifying the correct position and actions to be taken

when the IRVs are manipulated.

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During dayshift on July 25, 1987, the control switches for both of the

High Pressure Coolant Injection (HPCI) room coolers were placed in the

stop. position to prevent fan operation while maintenance personnel were

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welding in the HPCI room. While both HPCI room cooler . switches are in

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"off", the HPCI turbine is considered inoperable.

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Specification 3.5.1 action statement for an inoperable HPCI pump requires

the pump to be returned to service within 14 days or shutdown the plant.

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The welding job was postponed, but the room cooler switches were not

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returned to automatic.

The licensee identified the out of service HPCI .

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room coelers and returned them to automatic at 6:00 p.m. on July 28. All

other emergency core cooling systems and the reactor core isolation

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cooling system were operable during this time period.

Since the coolers

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were out of service less than 14 days, the TS limiting condition for

operation had not been exceeded.

Another example of a mispositioned instrument root valve was identified by

the licensee on August 13, 1987.

/tn equipment operator found that

isolation valve P-FD-V9991 to HPCI exhaust pressure transmitter PT-N056E

was shut. Although this transmitter-is not required to be operable by

technical specifications it does provide an input to a HPCI turbine trip.

A contributing factor into this valve being mispositioned was an error in

the licensee's valve lineup database.

The inspector will followup on the

licensee's verification of the valve lineup database as part of the above

violation followup.

The licensee's administrative procedure OP-AP.ZZ-108(Q), Removal and

Return of Equipment to Service, requires that all TS LCO's be reviewed to

determine if entry into an action statement is required prior to placing

equipment out of service. A similar event was identified and cited in

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NRC Inspection Report 50-354/86-48. Although the above events were

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licensee-identified, they are indicative of continued licensee problems

with control of plant equipment despite corrective action implemented for

the previous violation. NRC determined that an-enforcement conference

was necessary to discuss these concerns.

This item remains unresolved

pending the results of that meeting.

(37-17-01)

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Instrument Calibration Data Cards

At 11:00 p.m. on July 29, an unusual event was declared and a plant

shutdown commenced after it was determined that the filtration,

recirculation and ventilation system (FRVS) flow transmitters were

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previously calibrated using incorrect calibration data.

The

incorrect and non-conservative calibrations would have prevented the

FRVS recirculation fans from reaching the design flow rate of 30,000

SCFM per fan.

The actual flow rates would have bean limited to

approximately 23,000 SCFM per fan. The root cause of the miscalibration

was that subsequent to startup testing, a Bechtel gene n ted instrument

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calibration data (ICD) card was inadequately reviewed and substituted for

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correct data determined during the startup test program.

The FRVS

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ventilation fans were similarly_affected although their design flow rate

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is 9000 SCFM/ fan.

By 1:15 a.m. on July 30,. one FRVS vent fan and five

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FRVS recirculation fans were declared operable and the unusual event / plant

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shutdown terminated.

The unit remained in a 7 day LCO until the second

FRVS vent fan was declared operable.

As of 7:00 a.m. on July 30, the unit

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had returned to 100*; power.

The licensee has reviewed all "Q" systems and

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determined the only suspect ICD card calculations involve pitot tubes used

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for flow measurement in heating, ventilation, and air conditioning (HVAC)

systems. As corrective action, the licensee has committed to.

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Conduct a detailed review of all "Q" pitot tube instrument ICD

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card calculations to verify agreement with the test package

review and infield configuration.

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Conduct a detailed review of all "Q" ICD card calculations

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altered subsequent to the startup test program.

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In addition, the remaining 2000 safety related ICD cards will be

verified within the next 4 months (7,000 safety related ICD.

cards have already been verified).

Also as part of this

commitment, for any instrument found to be in excess of 10

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percent of its normal tolerance band, the ICD calibration data

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will be verified correct prior to resetting the instrument.

This issue will be remain unresc'ved pending NRC review of the

significance of reduced FRVS flow rnes and the completion of licensee

corrective action.

(87-17-02)

9.

Bypass of Non-Essential Diesel Generator Trips (Region TI:87-04)

The inspector reviewed the detailed logic for diesel engine trips and the

integrated emergency diesel generator surveillance test, and held

discussions with the system engineer. All non-essential emergency diesel

generator trips are bypassed for a loss of coolant accident (LOCA), loss

of offsite power (LOOP) or both simultaneously. The only automatic diesel

trips active during a LOCA or LOOP signal are:

a switchgear fault, low

lube oil pressure, and engine overspeed.

The switchgear fault trip

includes generator differential current, generator overcurrent, and bus

differential current trips.

The capability to bypass non-essential diesel

trips with a LOCA or LOOP signal present is routirely tested during the 18

month integrated diesel surveillance test (0P-ST.KJ-008).

No violations were identified.

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Review of Licensee Written Reports

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The licensee submitted the following event and routine reports during the

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inspection period.

These_ reports were reviewed for accuracy and timely _

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submission.

The asterisked reports received additional followup by the

inspector for corrective action implementation.

The (#) items iden.tify

reports which involve licensee identified technical specification

violations which are not being cited based upon meeting the criteria of

10 CFR 2 Appendix C.

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Monthly Operating Report for June, 1987

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LER 87-023

Technical Specification Violation'- Emergency Diesel

Generators B and C Starting Air Pressure Low Due to Alarm

Setpoint/ Technical Specification' Inconsistency

LER 87-024

Unanticipated Primary Containment Isolation System (PCIS)

Trip - ESF Actuation

LER 87-025

Non-Conservative Liquid Effluent Sampling Frequency Due to

Inconsistency Between Technical Specification Requirements

and Procedural Requirements

LER 87-026

Technical Specification Violation - MOV Thermal Overloads

Installed Without Bypass Capability Due to Inadequate

Technical Specification and Design Reviews

LER 87-027

Spurious Isolation of High Pressure Coolant Injection

Inboard Steam Isolation Valve Due to Failed Temperature

Module

LER 87-028

Isolations of the RWCU System of High Differential Flow

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Due to Design Deficiencies

LER-023 details the events which resulted in the "B" and "C" emergency

diesel generators (EDG) starting air pressures dropping below the minimum

technical specification (TS) limit.

The "B" and "C" EDG air compressors

had both been turned off by an operator checking compressor oil levels

who subsequently failed to return the compressors to automatic operation.

A contributing cause of this incident was a low air pressure alarm that

is set at a value below the TS limit, and this does not provide warning

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of low system pressure prior to exceeding the TS limit.

Corrective

action included an addition to operator logs to periodically check _the

status of starting air compressor handswitches, changing the method of

checking compressor oil level which precludes switch operation, and a

review to resolve the actual alarm setpoint and TS operability

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requirements. This constitutes a licensee-identified ~TS violation.

(87-17-03)

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LER 87-025 describes a station procedural deficiency in the sampling

frequency requirements for composite-tritium and gross alpha which

resulted in.a violation of TS sampling requirements _ The root cause of

this TS and station procedure inconsistency was an inadequate review'of

final draft TS by the TS coordinator.and responsible chemistry department

reviewers.

Immediate corrective actions included revising the affected-

chemistry department procedure and reviewing all other chemistry

department procedures against TS surveillance requirements.

Long term

corrective actions consist of reviewing current station administrative

programs to e m ure adequate identification of TS changes to affected

departments.

This constitutes a licensee-identified TS violation.

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(87-17-04)

LER 87-026 describes the failure to install required thermal overload

protection bypass circuits on service water intake screen spray wash

isolation valves and the turbine auxiliary cooling to' safety auxiliary

cooling system return isolation valves.

This failure was cited as a

violation and is discussed in detail in paragraph 3.2 of NRC inspection

report 354/87-16.

LER 87-028 describes two reactor water cleanup (RWCU) isolations on

high differential flow due to design deficiencies. The first RWCU

isolation occurred during an attempt to backwash the resin trap.

The

second RWCU isolation occurred due to leak-by through the RWCU precoat

inlet valve.

The RWCU system is susceptible to high differential flow

isolations because the leak detection flow transmitters ar'e only partially

compensated for temperature and density differences. Without this com-

pensati,an, the leak detection logic can sense high system leakage due to

temperature differences at the inlet and outlet of.the system when

a smaller leakage actually exists.

The licensee believes that RWCU

isolations are a result of this lack of temperature / density compensation

coupled with water leak-by between single isolations valves which separate

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the high and low pressure portions of the RWCU system. .The latter

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leakage is normally manifested during resin trap backwashing evolutions.

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As corrective action, the licensee has made procedural and operational

changes to improve the performance of resin trap backwashing. The procedure

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for operation of RWCU has been revised to explicitly define the valving

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sequence to be followed when backwashing an outlet resin trap.

The chemistry

department has instructed their technicians not to backwash the outlet

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resin traps unless the associated filter / demineralized (F/D) is out of

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service and depressurized. As long term corrective action, the licensee

plans to complete installation of the following design changes prior to

the first refueling outage.

A design change to RWCU F/D logic to allow a F/D to be returned to

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service following a RWCU isolation without having'to backwash the F/D

first. This change will permit the F/D to be reset and returned to

service immediately rather than having to be.first backwashed and

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precoated.

This change will reduce the frequency of backwash /precoat

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operations necessary and also reduce'the volume of radwaste

generated.

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A second design change will provide double valve isolation prior

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to pressurizing the F/D. This design change will reduce the

number of isolations caused by seat leakage on the single

isolation valves which form the pressure boundary between the

high and low pressure portions of the RWCU system.

11. NRC Region I Administrator's Visit

William Russell met with licensee management and toured the'PSE&G

Nuclear Training Center on August 3, 1987, and inspected the Hope

Creek Generating Facility the following day.

The inspection included

the control room, reactor building, diesel generators, IE switchgear,

and the remote shutdown panel.

12. Unresolved Items

Unresolved items are matters about which more information is required

in order to determine whether they are acceptable, an item of

noncompliance or a deviation.

Unresolved items disclosed during the

inspection are discussed in paragraph 8.

13.

Exit Interview

The inspectors met with Mr. S. LaBruna and other licensee personnel

periodically and at the end-of the inspection report to summarize the

scope and findings of their inspection activities.

Based on Region I review and discussions with the licensee, it was

determined that this report does not contain information subject to

10 CFR 2 restrictions.

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