ML20235G254

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Insp Rept 50-344/87-18 on 870412-0523.Major Areas Inspected: Operational Safety Verification,Maint Surveillance, Refueling Activities & Followup on Previous Items
ML20235G254
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 06/23/1987
From: Rebecca Barr, Mendonca M, Suh G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20235G225 List:
References
50-344-87-18, NUDOCS 8707140178
Download: ML20235G254 (13)


See also: IR 05000344/1987018

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U.S. NUCLEAR REGULATORY COMMISSION

REGION Y

Report No. 50-344/87-18

Docket No. 50-344-

License No. NPF-1

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Licensee: .

Portland _ General Electric Company

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121.S. W. Salmon Street

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Portland, Oregon 97204

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Facility Name: Trojan

Inspection at:

Rainier, Oregon

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Inspection conducted: April 12 - May 23, 1987

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Inspectors:

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R. C. Barr

Date Signed

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Senior Resident Inspector

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G. Y. Suh

Date Signed

Resident Inspector

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Approved.By:

M. M. Mendonca, Chief

Date Signed

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Reactor Projects Section 1

Summary:

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Inspection on April 12 - May 23, 1987 (Report 50-344/87-18)

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Areas Inspected: Routine inspection of operational safety verification,

maintenance, surveillance, refueling activities, and follow-up on previously

identified items.

Inspection procedures 30703, 60710, 61726, 62703, 71707,

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71710, 90712, 92700, 92701 and 93702 were used as guidance during the conduct

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of the inspection.

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Results:

Of the areas inspected, apparent violations involving failure to obtain a

deviation from Trojan operating procedures, Technical Specification 6.8.1,

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. and failure to establish adequate controls using QC hold tags or danger and

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caution tags were identified.

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870714017G B70623

PDR

ADOCK 05000344

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PDR

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DETAILS

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1.

Persons Contacted

  • C. A. Olmstead, Plant General Manager

R. C. Jarman, Manager, Nuclear Quality Assurance Department

R. P. Schmitt, Manager, Operations and Maintenance

D. R. Keuter, Manager, Technical Services

J. K..Aldersebaes,' Manager, Plant Modifications

J. D. Reid, Manager, Plant Services

R. E. Susee Operations Supervisor

R. L. Russell, Assistant Operations Supervisor

D. W. Swan, Maintenance Supervisor

R. A. Reinart, Instrument and Control Supervisor

T. O. Meek, Radiation Protection Supervisor

R. W.-Ritschard, Security Supervisor

R. E. Fowler Manager, Mechanical Engineering

C. M.- Dieterle, Supervising Engineer, Nuclear Plant Engineering

G. A. Zimmerman, Manager, Nuclear Regulation

  • D. K. Nordstrom, Engineer, Nuclear Regulation

The inspectors also interviewed and talked with other licensee employees

during the course of the inspection. These included shift supervisors,

reactor and auxiliary operators, maintenance personnel, plant technicians

and engineers, and quality assurance personnel.

  • Denotes those-attending the exit interview.

2.

Operational Safety Verification

During this inspection period, the inspectors observed and examined

activities to verify the operational safety of the licensee's facility.

The observations and examinations of those activities were conducted on a

daily, weekly, or biweekly basis.

On a daily basis, the inspectors observed control room activities to

verify the licensee's adherence to limiting conditions for operation as

prescribed in the facility Technical Specifications. Logs,

instrumentation, recorder traces, and other operational records were

examined to obtain information on plant conditions, trends, and

compliance with regulations. On occasions when a shift turnover was in.

progress, the turnover of information on plant status was observed to

determine that all pertinent information was relayed to the oncoming

shift personnel.

During each week, the inspectors toured the accessible areas of the

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facility to observe the following items:

a.

General plant and equipment conditions,

b.

Maintenance requests and repairs.

c.

Fire hazards and fire fighting equipment.

d.

Ignition sources and flammable material control.

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e.

Conduct of activities in accordance with the licensee's

administrative controls and approved procedures,

f.

Interiors of electrical and control panels.

g.

Implementation of the licensee's physical security plan.

h.

Radiation protection controls.

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Plant housekeeping and cleanliness.

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Radioactive waste systems.

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Proper storage of compressed gas bottles.

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The licensee's equipment clearance control was examined weekly by the

inspectors to determine that the licensee complied with technical

specification limiting conditions for operation with respect to removal

of equipment from service. Active clearances were spot-checked to ensure

that issuance was consistent with plant status and maintenance

evolutions.

During each week, the inspectors conversed with operators.in the control

room, and with other plant personnel. The discussions centered on

pertinent topics relating to general plant conditions, procedures,

security, training, and other topics aligned with the work activities

involved.

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The inspectors examined the licensee's nonconformance reports (NCR) to

confirm that deficiencies were identified and tracked by the system.

Identified t.anconformances were being tracked and followed to the

completion of corrective action.

Logs of jumpers, bypasses, caution, and test tags were examined by the

inspectors.

Implementation of radiation protection controls was verified

by observing portions. of area surveys being performed, when possible, and

by examining radiation work permits currently in effect to see that

prescribed clothing and instrumentation were available and used.

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Radiation protection instruments were also examined to verify operability

and calibration ste.tus.

The inspectors verified the operability of selected engineered safety

features. This was done by direct visual verification of the correct

position of valves, availability of power, cooling water supply, system

integrity and general condition of equipment, as applicable.

ESF systems

verified operable during this inspection period included the "A" train of

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the Emergency Power Generation System.

No violations or deviations were identified.

3.

Maintenance

Motor Operated Yalve (M0V) Maintenance

The inspector observed selected portions of the licensee's preventive

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maintenance efforts on MOVs. The licensee initiated this program on

approximately 122 out of 138 Environmentally Qualified MOVs for the

current refueling outage.

In this program the licensee found several

MOVs with frayed electrical lead wires. The licensee initiated

corrective maintenance activities of repotting and resleeving the M0V

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lead wire. The inspector observed this work which was conducted in

accordance with Field Change Notices #5 for RDC 86-033 DCP2. The

involved engineers and maintenance personnel seemed knowledgeable and

qualified for the maintenance activity.

Other discrepancies obrerved by the licensee included one brake

application problem, one loose stake in a stem nut, and discolored or

separated grease. The c:tuse of the brake application problem has not

been identified, but the brake has been replaced. The loose stem nut has

been attributed to inadequate stake installation. The discolored or

separated grease was determined to be an aging effect, and analysis of

the grease found it would still maintain its lubricating qualities.

The

inspector observed the discolored grease and reviewed licensee analyses

based on similar findings at the LaSalle plant in 1985.

Additionally, the licensee removed a large number of terminal blocks from

MOV motors as unnecessary and connected lead wires directly to motor

studs. The licensee also replaced a small number of cracked limit and

torque switches.

Finally, the licensee found a number of wire nuts and

taped connections for the valves and replaced these connections. The

inspector observed selected portions of the corrective maintenance

activities on these topics.

Problems observed at another plant were also discussed with the licensee.

Specifically, M0V over thrust conditions and valve internal damage, and

undersized power cables on MOV operators and pickup / dropout voltage

problems. The licensee's recent M0 VATS testing identified some minor

problems in valve thrust conditions in relation to possible motor

overcurrent conditions which have been corrected, but no indication of

valve internal damage has been found. Also, the licensee has measured

and is measuring motor voltage conditions and found no problem in

relation to cable size or voltage condition.

The licensee is currently evaluating the significance of these findings,

but preliminarily has determined that the findings did not impact valve

operability (0 pen item 87-18-01).

Auxiliary Feedwater Pump Diesel Engine

The inspectors observed maintenance work being performed on the diesel

engine of the diesel-driven auxiliary feedwater pump. The work was

controlled by Maintenance Request (MR) 87-1485 which was prepared in

response to Event Report 86-124. ER 86-124 reported the failure of

gasketed compression-type fittings in the copper lubricant lines during

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routine testing of the diesel engine. MR 87-1485 provided for the

replacement of all lube oil fittings and copper lines with compression

type fittings and stainless steel lines. The inspectors verified that

required administrative approvals and tagouts were in place, that the

work instructions were adequate to control the activity, and that quality

control hold points were being observed. The work was being performed

with continuous quality control coverage during disassembly and

reassembly of the diesel engine,

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4.

Surveillance

The surveillance testing of safety-related systems was witnessed by the

inspectors. Observations by the inspectors ir.cludea . verification that

proper procedures were used, test instrumentation was calibrated and that

the system or component being tested was properly removed from service if

required by the test procedure.

Following completion of the surveillance

tests, the inspectors verified that the test results met the appropriate

acceptance criteria. Any necessary corrective maintenance was completed

during the conduct of the tests in accordance with approved maintenance

request (s). Surveillance tests witnessed during this period included:

P0T-10-2 DA, " Fire Protection System, Motor Driven Fire Pump Performance."

No violations or deviations were identified.

5.

Refueling Activities

During the current refueling outage, the inspectors conducted an

inspection of activities to determine whether pre-refueling activities

specified in the Technical Specifications have been completed and whether

refueling activities are being controlled and conducted as required by

Technical Specifications and approved procedures. The licensee primarily

uses two procedures to control the conduct of refueling operations and

for establishing and maintaining control of plant conditions.

Fuel

Handling Procedure (FHP) 5-2, titled " Refueling Procedure," serves as the

controlling document governing the refueling operation.

FHP 5-2 includes

checkoff lists for the performance of surveillance testing required to be

performed as prerequisites for refueling, for checkout of tools and

equipment for proper functioning, and for control of the actual fuel

handling operations. General Operating Instruction (G0I) 11, titled

" Plant Operation for Refueling," is used to establish compliance with

surveillance testing requirements prior to the start of and during

performance of core alterations. G01-11 uses a checkoff list which is

maintained by the control room operator with completed copies of the

checkoff list to be kept with the Fuel Handling Senior Reactor Operator's

record copy of FHP 5-2.

The inspectors performed various walkdown inspections of the refueling

cavity, fuel transfer canal, and spent fuel pool areas during the

performance of equipment checkout and of fuel handling operations. The

inspectors verified that the refueling crew in containment and at the

spent fuel pool had copies of the current revision of FHP 5-2, that

direct communication was being maintained between the control room and

the refueling crew, that an engineering advisor was present in the

control room during the performance of fuel handling operations, and that

tool and item accountability was being maintained by a quality control

representative who maintained a tool accountability log.

The record copy of FHP 5-2 kept by the Fuel Handling Senior Reactor

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Operator (SRO) was reviewed. The inspectors verified that quality

assurance and quality control hold points were being observed and signed

off and that completed copies of the G01-11 checkoff list were being kept

in the Fuel Handling SR0's Fuel Handling Procedure binder. The

inspectors reviewed a sampling of applicable surveillance t! sting data

sheets and the control room log to confirm that technical s) edification

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surveillance tests were performed in a timely manner.

In particular, it

was verified that containment integrity was established within 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />

prior to the start of core alterations and that channel functional

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testing of the source range neutron flux monitors was performed within 8

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hours prior to the start of core alterations. The inspectors also

reviewed the " Refueling Periodic Surveillance Checkoff List" of G01-11 to

confirm that required surveillance tests were being performed during Mode

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6 and during core alterations.

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The inspector confirmed that the licensee had conducted a 10 CFR 50.59

safety evaluation of the reload core which was documented in License

Change Request 87-10. The safety evaluation discussed changes to the

licensee's facility as described in the updated FSAR which included

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reevaluation of the rod ejection accident for beginning of cycle

conditions and revised margins and limits for the shutdown margin

analysis. The licensee's evaluation concluded that these changes did not

involve unreviewed safety questions.

No violations or deviations were identified.

6.

Followup on Open Items

Followup Item 86-31-01(Closed): Based on review of a similar occurrence

at another plant, the inspectors had identified to the licensee an

apparent discrepancy in the valve stroke time for the pressuri7er power

operated relief valves (PORVs) used in the overpressure mitigt. tion

system. The licensee's Technical Specifications and inservice test

procedures did not specify acceptance criteria for PORV strohe times.

The safety evaluation for the technical specification ammendnent that

deals with the overpressure mitigation system assumed a PORV opening time

of 0.6 seconds. A review of recent PORV inservice tests showed opening

times which ranged from 2.8 to 9.2 seconds.

In response to this apparent discrepancy, the licensee prepared

Nonconformance Report 86-215 which declared the overpressure mitigation

system to be inoperable and initiated corrective action and an evaluation

of contributing causes as documented in Event Report 86-119. The cause

of this event was determined to be lack of documentation and cognizance

of the opening time requirements for the PORVs. A reanalysis was

performed on the impact of the longer PORY opening times on the ability

of the overpressure mitigation system to perform its design function.

The overpressure mitigation system provides protection against pressure

transients during cold shutdown, heat up, and cooldown operations in

order to minimize the potential for impairing reactor vessel integrity

when operating at or near the vessel ductility limits (as specified in 10 CFR Part 50 Appendir G).

The inspector reviewed Event Report 86-119 and the reanalysis of the

overpressure mitigation system with the longer PORV opening times. The

reanalysis supported the conclusion that overpressure mitigation system

met technical specification operability requirements with a PORV opening

time of 10 seconds. The reanalysis demonstrated that either one of the

two PORVs had adequate relieving capability to protect the reactor

coolant system from overpressurization when the transient is limited to

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either the start of an idle reactor coolant pump with the secondary water

temperature of the steam generator 50 degrees Fahrenheit above the

. reactor coolant system cold leg temperature or the mass addition from

sircultaneous operation of one safety injection pump, two centrifugal

charging pumps, and one positive displacement pump injecting into a water

solid system.

Based on the results of this reanalysis, the overpressure

mitigation system'was declared to be operable. The licensee's other

corrective actions included plans to prepare a Design Basis Document for

the overpressure mitigation system per Commitment Tracking List item

20115 and the addition of PORV stroke time requirements in the Inservice

Testing Program. The ins

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Periodic Operating Test (pectors verified that the current revision of

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POT) 1-5, which provides instructions for

full-stroke inservice exercising of the pressurizer PORVs, block valves,

and reactor vessel head vent valves, specifies PORV stroke times

consistent with the assumptions made in the reanalysis. This item is

considered to be closed.

LER 87-06 (0 pen): The licensee reported in Revision 0 of LER 87-06 that

flood relief louvers in the west wall of the turbine building were

inadequately designed to prevent flooding of safety-related equipment

located on the 45 foot level of the turbine building. The safety-related

equipment include the emergency diesel generators, auxiliary feedwater

puns, and the remote shutdown panel. The turbine building internal

flooding design bases as stated in the updated FSAR assumes a maximum

flood rate of 500,000 gpm from a failure in the circulating water system

piping. Safety-related equipment are located in rooms protected against

flooding up to elevation 47 feet by flood dikes. At the time of

discovery, the flood relief louvers and a large portion of the turbine

building wert wall had been removed in preparation for condenser tube

changeout performcd during the current refueling outage. This would have

provided an adequate flood relief capacity in the event of a failure in

the circulating water system piping.

The inspec', ors held discussions with licensee representatives and

reviewed tne licensee's documentation, including Nonconforming Activity

Report (NLAR) P87-011M, Event Report 87-018, and Temporary Modification

(TM)87-045.

The determination that the flood relief louvers were

inadequately designed resulted from the evaluation of NCAR P87-001M,

which reported that the flood relief louvers had been temporarily

replaced by plywood and sheet metal in the process of removing a portion

of the turbine building west wall for condenser tube changeout work. The

evaluation concluded that the plywood and sheet metal arrangement

provided flood relief capacity equivalent to the louvers, but also

identified design errors in the original plant design of the flood relief

louvers. The licensee's corrective actions include the following. The

flood relief louvers will be redesigned to provide less flow resistance

with the area occupied by the louvers to remain open in the interim.

Safety related equipment located on 45 foot elevation of the turbine

buildir g will be protected to elevation 48 feet by raising the flood

dikes per TM 87-045. The flood dike extensions are currently being

installed. The licensee's calculations indicate that the turbine

building would be able to withstand a 500,000 gpm flood rate and prevent

flooding of safety-related equipment with flood dikes raised to 48 feet

and redesigned flood louvers. The licensee will also submit revised

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turbine building internal flooding design bases to the NRC. Based on

discussions with the NRR project manager, t.he inspectors understand that

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NRR plans to review the licensee's revised design bases and applicable

revisions to the updated FSAR. This item will remain open pending

completion of licensee corrective actions.

Information Notice No. 86-53 and LER 87-09 (0 pen):

IE Information Notice No. 86-53, " Improper Installation of Heat Shrinkable Tubing", dated June

26, 1986, alerted licensees to a potentially generic safety problem

involving improper installation of heat shrinkable tubing manufactured by

Raychem over electrical splices and terminations. As discussed in the

information notice, if actual installation configurations do not conform

to the manufacturer's installation instructions, the status of the

equipment qualification of safety-related electrical equipment would be

indeterminate and the licensee would need to take appropriate actions to

establish compliance regarding system operability.

Upon receipt of IN 86-53, the licensee initiated its preparations for inspecting Raychem

splices on environmentally qualified safety-related equipment. The

preparations included compiling a list of all applicable equipment which

were documented as having Raychem heat shrinkable tubing splices,

purchasing Raychem splice material to replace those splices destroyed

during the inspection process and splices determined to need rework as a

result of the inspections, preparing inspection plans and training

licensee personnel on inspection and installation mettods. Review of the

listing of applicable Raychem splices to be inspected showed that most of

the splices were located inside containment. Actual inspection was

initiated during the current refueling outage.

As reported in LER 87-09, the licensee's inspections revealed a number of

Raychem splices, including splices on electrical connections for the

solenoid valves which control the pressurizer power operated relief valve

and splices on containment penetration power and control valves, which

were not installed in accordance with Raychem installation instructions.

Most of the splices had been installed during original plant construction.

Installation defects included excessive bending of the Raychem tubing,

the use of improperly sized tubing, and the lack of adequate insulation

tubing length. The inspectors discussed the inspection program with

licensee representatives, inspected two cases of Raychem splices which

failed the inspection criteria, and reviewed Maintenance Request (MR)

87-1758 which controls the inspection and rework of applicable Raychem

splices. Additional NRC inspection of the licensee's program is further

discussed in Inspection Report 50-344/87-13.

The licensee's corrective actions were to expand the scope of the

inspection program from its initial sampling basis to a complete 100%

inspection of environmentally qualified Raychem splices inside and

outside the containment, to rework all splices which fail to meet the

inspection criteria, and to rework all Raychem splices on containment

penetration cables where a high failure rate on inspection was

experienced. Exceptions were made to the above which included cases

where the applicable splices would be subject to rework in concurrent or

near-term design change packages and cases where recent maintenance work

had been performed with documentation which showed the Raychem

installation instructions had been followed.

The Raychem splice

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inspection and rework program is currently nearing completion. The

inspectors will. complete review of this item upon completion of licensee

corrective actions.

7.

Event Follow-Up

A.

Fill Line Failures of the 'A' Cold Leg Safety Injection Accumulator

On May 12, 1987, while attempting to transfer borated water (sluice)

from the 'A' to 'D' Cold Leg Safety Injection (SI) Accumulator, the

fill line of the 'A' Accumulator failed near the fill line to vessel

nozzle weld. The reactor was in the refueling mode and the

accumulators were not required by technical specification. The

licensee generated a ' ROUTINE' event repcrt and assigned maintenance

as the event evaluator. Additionally, a Nonconformance Report (NCR)

was generated by Quality Assurance and assigned to maintenance for

dispositioning. From May 12, 1987, maintenance reviewed the event

for root cause. On May 21, 1987, maintenance concluded engineering

expertise was needed to determine the root cause of the fill line

failure and transferred responsibility of dispositioning the NCR to

the Nuclear Plant Engineering Department (NPED). Preliminary NPED

determination based on a metallurgical analysis indicated the

failure was caused by low cycle-high load fatigue failure. The

failure was initially believed to be caused by individuals walking

on the fill line. [ Subsequent calculations confirmed that

-individuals walking on the fill line could not have caused the

failure.]

On May 23, 1987, following the weld repair of the fill line and a

hydrostatic test of the weld, the licensee again attempted to

transferboratedwater(sluice)fromthe'A'to'D'SIaccumulators

via the fill lines. On the first attempt to sluice in this manner,

the operator stopped sluicing when a great deal of noise was

observed by personnel inside containment. After discussions with

operators that had previously been involved in such sluicing

operations, it was determined that the noise was normal for sluicing

operations, ar.d the sluicing restarted. Operators stopped sluicing

a second time when plant personnel notified the control room of a

great deal of noise around the accumulator. Again operators stopped

sluicing, but restarted once they convinced themselves that it was

not unusual. This sluicing resulted in failure of the fill line of

the ' A' SI accumulator again with the reactor in the refueling mode.

An ' URGENT' event report was generated, the Performance

Monitoring / Event Analysis Group was immediately activated and the

system was quarantined.

Licensee's procedure 01 5-2 required that

transfer of borated water between SI accumulators be accomplished

using the accumulator sample lines vice the fill lines. A deviation

to the procedure, as required by Plant Procedure A0 4-4, was not

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obtained prior to attempting transfer between the SI accumulators

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using the fill line on May 12 or May 23, 1987. This is an apparent

violation (50-344/87-18-02). Also, the fact that licensee failed

to establish hold tags so that the fill line would not be utilized

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prior to resolution of the problem, is considered an apparent

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violation (50-344/87-18-05). Based on the inspection of these

events, licensee personnel should have known from training and

procedure use that these actions were violations and avoided the

violation.

Further, the fact, that operators ignored several warnings of

unusual noise and the fact that this fill line had previously

failed, is a significant concern.

In a subsequent management

meeting on June 5,1987, the Regional Administrator emphasized that

this fact indicates that operators performance not only was in

violation of procedures but also potentially inconsistent with the

basic fundamental of running a nuclear power plant. Specifically,

even though operators were fully aware of abnormal noise and system

vibration that occurred for each time they sluiced in this manner,

they continued the traasfer to a second failure of the fill line.

The licensee's event analysis is expected to be complete by June 5,

1987. Additionally, the licensee has developed a detailed and

comprehensive plan of action to determine the failure mechanism,

repair the failure and prevent further event recurrence.

B.

'B' Feedwater Line Seismic Restraint Damage

On May 19, 1987, the licensee identified damage to the 'B' feedwater

line seismic restraint EBB-3-1-SR8. The knee brace anchor bolts had

pulled out of their concrete foundation. Since the damage of the

seismic restraint was identified, the licensee had developed an

action plan to determine the root cause, redesign the system

support, evaluate other potential system damage and repair the

support. On a daily basis the licensee is updating Regional

Management of their findings. The licensee has categorized the

understanding, resolution and repair of the feedwater support system

as a ready for startup item.

(0 pen,87-18-03)

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C.

Main Steam Line Wall Thickness

art of their program to identify

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the licensee, as p(wall thinning), discovered the

On May 15, 1987,

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piping that is undergoing erosion

pipe spool piece containing the steam line venturi on the 'B'

steam

line had a wall thickness of .78 inches which is less than the

minimum required thickness of .858.

Subsequent examination of the

A, C and D main steam lines also indicated a wall thickness less

than the minimum required. The licensee has developed an action

plan to determine the cause of the less than minimum wall thickness,

evaluate its impact to continued operation and determine why the

wall thinning was not recognized as a result of previous

measurements. The licensee on a daily basis is updating Regional

Management of their findings. The licensee has categorized the

resolution of this issue as a ready for startup item.

(0 pen,

87-18-04)

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Shutdown Cooling During hid-Loop Operation

On May 1,1987, a Regiorh1 based senior reactor engineer and the resident

, inspector met with the Mcensee to review the April 10, 1987, extended

7lossofResidualHeatRai. oval (RHR)coolingduringmid-loopReactor

Coolant System (RCS) operation that occurred at Diablo Canyon Unit 2.

During the meeting the event root causes, the potential. vulnerability of

the Tro,ian fccility to a like event and design chr.nges that had already

been implemented by the licensee were discussed. The licensee stated

previous difficulties which they had experienced during mid-loop RCS-RHR

operation caused them to change level indication design and operating

procedures. Since changing the level indicating system design, changing

operating procedures and training operators to the challenges of mid-loop

operation no further losses or near miss losses of RHR cooling while in

mid-loop RCS operation have been experienced. Additionally, the licensee

acknowledged the need to be able to rapidly reestablish containment

integrity and be aware of actions required to establish containment

integrity during mid-loop RCS operation. Since the meeting, the licensee-

has operated in mid-loop on RHR cooling with no difficulty. The licensee

has'since also received NRC IN 87-23: Loss of Decay Heat Removal During

Low Reactor Coolant Level Operation and placed it on their commitment

tracking log.

9.

Allegation Follow g

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A11egath Tracking Syntem No. RV-86-A-0097

Characterization

Potentially fraudulent Laterial supplied by Familian Northwest may

have been installed in safety-related o- important to safety

applications.

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Implied Significance to Design, Construction or Operation

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The use of potentially fraudulent material of an indeterminate

quality could result in an unanalyzed safety condition.

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Assessment of Safety Significance

The licensee was reinformed that potentially fraudulent material

could have been installed in plant applications by the Office of

Investigations in November 1986. The licensee initiated an

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investigation of procurement and maintenance records to identify

installed Familian Northwest supplied components. This

investigation identified Familian Northwest supplied products as

follows:

(1) stainless steel piping and flanges for the gaseous

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radwaste system; (2) stainless steel piping and fittings for the

gaseous radwaste return to containment line; (3) stainless steel

piping for containment hydrogen sampling system; (4) wrapped piping

and fittings for the service water strainer to the discharge and

I

isolation structures; and (5) carbon steel flanges used for Reactor

Vessel Level Instrumentation System (RVLIS) support.

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11

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The licensee's Nuclear Plant Engineering Department recently

completed an analysis of the identified Familian Northwest supplied

components (Memorandum ANR-491-87M dated April 27,1987). This

analysis assumed that the components in question failed in all

applications, except for the RVLIS support flanges.

For the

components assumed to fail, the analyses concluded that the

potentially fraudulent material would not have an adverse impact on

FSAR safety analyses or an unreviewed safety question. The

analyses, for the RVLIS support flange, verified by visual

examination and engineering judgement, that the material would not

fail in.its application.

An NRC inspector had independently observed selected portions of the

licensee's investigation of procurement and maintenance records to

identify Familian Northwest supplied components and had observed

samplingofthreeofthecomponents(InspectionReport86-47). The

three samples were taken from components on the gaseous radwaste

system. All samples were analyzed by an independent laboratory for

the NRC and were verified to be the material specified for the

component. During the current outage, the licensee plans to remove

the Familian Northwest supplied stainless steel pipe from the

containment hydrogen supply system. The licensee plans to have the

removed piping material tested, and provide the results to the NRC.

When the questioned components were originally identified, the

Region V management and inspection personnel independently

determined that failure of the components would not increase the

probability of an accident or result in an accident that was more

severe than the FSAR accident analysis. The staff verified that

failure of the Familian Northwest supplied components on the

radwaste system would not result in any gaseous radioactivity

release beyond the limiting analysis in FSAR section 15.7.

The

staff also concluded that failure of the components in the

containment hydrogen sampling system would still allow sampling of

containment hydrogen from the other train and would not effect

containment isolation capability as required by the FSAR for this

system.

For the service water line to the discharge structure, the

(

staff determined that the failure of the Familian Northwest supplied

components would not result in any additional loss of service water

flow beyond that already assumed in the FSAR.

Finally, the staff

concluded that the RVLIS support flanges would not affect FSAR

analyzed accidents in that the RVLIS is an indicating system which

has specified procedural and/or equipment ahernates in case of its

failure.

The inspector reviewed the licensee's engineering evaluation of the

Familian Northwest supplied components. The inspector's review of

the licensee's evaluation concurred in the licensee's conclusion

that there was no safety concern in relation to the Familian

Northwest supplied components. As previously discussed, this

evaluation was verified by the independent staff review which

assumed component failure for the Familian Northwest products.

,

.

.

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12

,

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Staff Position

The staff determined that (1) based on samples taken, the Familian

Northwest supplied materials were probably as specified by design

and (2) that failure of the Familian Northwast supplied components

would not result in an increased probability or more severe

consequences than already analyzed in the FSAR.

Action

None

10. Exit Interview

The inspectors met with the licensee representatives denoted in paragraph

1 on June 4, 1987, and summarized the scope and findings of the

inspection activities.