ML20223A277
| ML20223A277 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 08/10/2020 |
| From: | Stewart Bailey NRC/RGN-II/DRP/RPB4 |
| To: | Maza K Duke Energy Progress |
| References | |
| IR 2020002 | |
| Download: ML20223A277 (20) | |
See also: IR 05000400/2020002
Text
August 10, 2020
Ms. Kim Maza
Site Vice President
Shearon Harris Nuclear Power Plant
5413 Shearon Harris Road
Mail Code HNP01
New Hill, NC 27562-9300
SUBJECT:
SHEARON HARRIS NUCLEAR POWER PLANT - INTEGRATED INSPECTION
REPORT 05000400/2020002
Dear Ms. Maza:
On June 30, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
Shearon Harris Nuclear Power Plant. On July 29, 2020, the NRC inspectors discussed the
results of this inspection with you and other members of your staff. The results of this
inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding
involved a violation of NRC requirements. We are treating this violation as a non-cited violation
(NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or the significance or severity of the violation documented in this
inspection report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional
Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at
Shearon Harris Nuclear Power Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC
Resident Inspector at Shearon Harris Nuclear Power Plant.
K. Maza
2
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public
Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Stewart N. Bailey, Chief
Reactor Projects Branch 4
Division of Reactor Projects
Docket No. 05000400
License No. NPF-63
Enclosure:
cc w/ encl: Distribution via LISTSERV
ML________________
OFFICE
RII: DRP
RII: DRP
RII:DRP
RII:DRP
RII: DRP
NAME
JZeiler
APatz
ARosebrook
DJackson
SBailey
DATE
8/7/2020
8/7/2020
8/6/2020
8/6/2020
8/10/2020
Enclosure
U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Number:
05000400
License Number:
Report Number:
Enterprise Identifier: I-2020-002-0065
Licensee:
Duke Energy Progress, LLC
Facility:
Shearon Harris Nuclear Power Plant
Location:
New Hill, NC 27562
Inspection Dates:
April 01, 2020 to June 30, 2020
Inspectors:
J. Zeiler, Senior Resident Inspector
A. Patz, Resident Inspector
S. Sanchez, Senior Emergency Preparedness Inspector
J. Walker, Emergency Response Inspector
Approved By:
Stewart N. Bailey, Chief
Reactor Projects Branch 4
Division of Reactor Projects
2
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting an integrated inspection at Shearon Harris Nuclear Power Plant, in
accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs
program for overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Inoperability of 'B' Train ESCW Chiller Due to Trip on High Compressor Oil Temperature
Results in Condition Prohibited by Technical Specifications
Cornerstone
Significance
Cross-Cutting
Aspect
Report
Section
Mitigating
Systems
Green
Open/Closed
[P.2] -
Evaluation
A self-revealed Green non-cited violation (NCV) of Technical Specification (TS) 3.7.13,
Essential Services Chilled Water System, was identified as a result of the B train ESCW
system being inoperable for a period greater than 78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br /> between July 13 through
July 16, 2019, after the B ESCW chiller tripped on high compressor oil temperature due to
low compressor oil level, low refrigerant level, and excessive service water side biofouling in
the chiller condenser heat exchanger.
Additional Tracking Items
Type
Issue Number
Title
Report
Section
Status
LER
05000400/2019-
002-00
'B' Train Chiller for the Essential Services
Chilled Water System Tripped on High
Compressor Oil Temperature
Closed
3
PLANT STATUS
Unit 1 operated at or near rated thermal power (RTP) until June 5, 2020, when a planned
downpower to 30 percent RTP was initiated to repair a condenser tube leak. On June 9, 2020,
following condenser tube repairs, the licensee initiated power escalation and returned the unit to
near RTP on June 10, 2020. Unit 1 remained there for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President
of the United States on the public health risks of the coronavirus (COVID-19), resident
inspectors were directed to begin telework and to remotely access licensee information using
available technology. During this time the resident inspectors performed periodic site visits each
week and during that time conducted plant status activities as described in IMC 2515, Appendix
D; observed risk significant activities; and completed on site portions of IPs. In addition, resident
and regional baseline inspections were evaluated to determine if all or portion of the objectives
and requirements stated in the IP could be performed remotely. If the inspections could be
performed remotely, they were conducted per the applicable IP. In some cases, portions of an
IP were completed remotely and on site. The inspections documented below met the objectives
and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
(1)
The inspectors evaluated readiness for seasonal extreme weather conditions prior to
the onset of seasonal hot temperatures on May 22, 2020
Impending Severe Weather Sample (IP Section 03.02) (2 Samples)
(1)
The inspectors evaluated the adequacy of the overall preparations to protect risk-
significant systems from impending severe weather for a tornado watch and severe
thunderstorm warning on April 13, 2020
(2)
The inspectors evaluated the adequacy of the overall preparations to protect risk-
significant systems from impending severe weather for Tropical Storm Bertha and an
associated tornado warning on May 27, 2020
4
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1)
'A' containment spray (CS) system with 'B' CS system out of service for scheduled
motor lubrication preventive maintenance on May 7, 2020
(2)
'B' centrifugal and charging injection pump (CSIP) while 'A' CSIP was unavailable for
preventive maintenance on May 19, 2020
(3)
'A' essential services chilled water (ESCW) system while 'B' ESCW system was
unavailable for corrective maintenance on May 26, 2020
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
(1)
The inspectors evaluated system configurations during a complete walkdown of the
main steam relief system on June 15, 2020.
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a
walkdown and performing a review to verify program compliance, equipment functionality,
material condition, and operational readiness of the following fire areas:
(1)
Reactor auxiliary building (RAB) 305' elevation termination cabinet room and rod
control cabinet room (fire zones 12-A-6-RT1 and 12-A-6-RCC1) on April 23, 2020
(2)
RAB 305' and 324' elevation heating, ventilating, and air conditioning areas (fire
zones 12-A-6-CHF1&2 and 12-A-7-HV) on May 4, 2020
(3)
RAB 261' elevation steam tunnel area (fire zone 1-A-46-ST) on May 14, 2020
(4)
Fuel handling building 261' elevation emergency ventilation exhaust equipment rooms
(fire zones 5-F-3-CHFA, 5-F-3-CHFB, 5-F-3-CHF-BAL, 5-F-3-DMNZ1, and 5-F-3-
DMNZ2) on May 20, 2020
(5)
'B' emergency diesel generator (EDG) room and support equipment areas (fire zones
1-D-1-DGB-RM, 1-D-3-DGB-ES, 1-D-DTB, 1-D-1-DGB-ASU, 1-D-1-DGB-ER, and 1-
D-2-DGB-HVD) on June 3, 2020
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
(1)
The inspectors evaluated the onsite fire brigade training and performance during an
announced fire drill on June 19, 2020. The fire drill scenario involved a service air
dryer heater electrical fire on the turbine building 261' elevation.
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
5
(1)
RAB 305' and 324' elevations on May 27, 2020
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)
(1 Sample)
(1)
The inspectors observed and evaluated licensed operator performance in the control
room during a downpower and return to full power for repairs to condenser tubes in
the west condenser water box during June 5-10, 2020.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
(1)
The inspectors observed and evaluated a simulator scenario for operator training
involving a loss of 'A' emergency AC safety bus followed by a loss of all AC power on
May 7, 2020.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
The inspectors evaluated the effectiveness of maintenance to ensure the following
structures, systems, and components (SSCs) remain capable of performing their intended
function:
(1)
'B' EDG lube oil keep warm pump failure to start due to breaker motor starter
contactor coil failure on December 3, 2019
(2)
'B' ESCW chiller tripped on compressor low oil pressure due to compressor oil filter
piping leak on January 18, 2020
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the
following planned and emergent work activities to ensure configuration changes and
appropriate work controls were addressed:
(1)
Elevated (Green) risk during planned unavailability of the 'A' EDG due to emergent
repair of a fuel oil supply header line leak on April 24, 2020
(2)
Elevated (Green) risk during planned unavailability of the 'A' ESCW and 'A' CSIP
systems on May 19, 2020
(3)
Elevated (Green) risk during unplanned unavailability of the 'B' ESCW system due to
emergent failure of the chiller hot gas bypass valve actuator on May 26-28, 2020
(4)
Elevated (Green) risk during scheduled unit downpower to 30 percent power to repair
condenser tube leakage between June 5-9, 2020
(5)
Elevated (Green) risk during unplanned unavailability of Delta T/Tavg Loop T-0412
due to emergent failure of a reactor protection system circuitry card on
June 17-18, 2020
6
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the
following operability determinations and functionality assessments:
(1)
'A' EDG right bank fuel supply header line leak (NCR 02324923) on April 13, 2020
(2)
'A' boric acid transfer pump differential pressure trending up for unknown reason
(NCR 02325201) on April 15, 2020
(3)
'B' EDG jacket water heater failure to de-energize at designated setpoint
(NCR 02328399) on May 4, 2020
(4)
'A' electrical penetration area cooling fan AH-24X failed to remain running following
repeated starts due to failed breaker auxiliary contacts (NCR 02332720) on
May 30, 2020
(5)
'C' component cooling water (CCW) pump outboard seal has 50 drops per minute
leakage (NCR 02334636) on June 11, 2020
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)
(1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
(1)
Permanent modification engineering changes (ECs) 0000416868 and 0000417450,
'B' and 'A' ESCW chiller hot gas bypass valve and pre-rotation vane setpoint
changes, implemented on April 28 and May 20, 2020
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance test activities to verify system
operability and functionality:
(1)
Work Order (WO) 20354041 post-maintenance test instructions following 'B' CS pump
motor bearing oil replacement on May 7, 2020
(2)
Operations Surveillance Test (OST)-1104, Containment Isolation Valve Inservice
Inspection Valve Test Quarterly Interval Modes 1-6, following scheduled air filter
regulator replacements for main steam isolation bypass valves 1MS-81, 1MS-83, and
1MS-85 on May 14, 2020
(3)
OST-1007, Chemical and Volume Control System/Safety Injection System
Operability, Train A, Quarterly Interval, Modes 1-4, following scheduled maintenance
on safety injection minimum flow valves on May 19, 2020
(4)
Post-modification testing via Operations Periodic Test (OPT)-1512, Essential Chilled
Water Turbopak Units Quarterly Inspection/Checks Modes 1-6, following
implementation of EC 0000416868 on 'A' ESCW chiller on May 20, 2020
(5)
OPT-1512, following repair of 'B' ESCW chiller due to emergent failure of the hot gas
bypass valve actuator on May 28, 2020
7
(6)
Maintenance Surveillance Test (MST)-I0140, Delta T/Tavg Loop (T-0412) Operational
Test, following emergent replacement of failed circuitry card on June 18, 2020
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01) (2 Samples)
(1)
OPT-1529, Alternate Seal Injection Pump Operability Test Quarterly Intervals
Modes 1-3, on April 29, 2020
(2)
OST-1122, Train A 6.9 kV Emergency Bus Undervoltage Trip Actuating Device
Operational Test and Contact Check, Modes 1-6, on June 24, 2020
Inservice Testing (IP Section 03.01) (1 Sample)
(1)
OST-1215, Emergency Service Water System Operability Train B Quarterly Interval
Modes 1 2 3 4 5 6 Defueled, on June 5, 2020
FLEX Testing (IP Section 03.02) (1 Sample)
(1)
WOs 20367683, 20307610, and 20290674, perform six-year inspection and testing of
FLEX auxiliary feedwater and reactor coolant system pumps, on June 2-3, 2020
71114.02 - Alert and Notification System Testing
Inspection Review (IP Section 02.01-02.04) (1 Sample)
(1)
The inspectors evaluated the maintenance and testing of the alert and notification
system during the week of April 20, 2020.
71114.03 - Emergency Response Organization Staffing and Augmentation System
Inspection Review (IP Section 02.01-02.02)
The inspectors evaluated the readiness of the Emergency Response Organization (ERO)
during the week of April 20, 2020. However, the inspectors were unable to complete this
inspection procedure (IP) in its entirety. The aspect that remains to be inspected is the
verification of a sample of key ERO personnels training qualifications and response times
from home to the site.
The necessary documentation used by the inspectors to verify this information is considered
personally identifiable information, which the inspectors chose not to handle while
performing this inspection remotely. The remainder of this IP will be completed at a later
date.
71114.04 - Emergency Action Level and Emergency Plan Changes
Inspection Review (IP Section 02.01-02.03) (1 Sample)
(1)
The inspectors evaluated submitted Emergency Action Level, Emergency Plan, and
8
Emergency Plan Implementing Procedure changes during the week of
April 20, 2020. This evaluation does not constitute NRC approval.
71114.05 - Maintenance of Emergency Preparedness
Inspection Review (IP Section 02.01 - 02.11)
The inspectors evaluated the maintenance of the emergency preparedness program during
the week of April 20, 2020. However, the inspectors were unable to complete this
inspection procedure in its entirety. The aspects that remain to be inspected are the
verification of radiation monitors used in the EALs to ensure proper scale readout of the
instrumentation, emergency response facilitys readiness, including field monitoring team
vehicles and go-kits used for emergencies. The remainder of this IP will be completed at a
later date.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
EP01: Drill/Exercise Performance (IP Section 02.12) (1 Sample)
(1)
April 1, 2019, through December 31, 2019
EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)
(1)
April 1, 2019, through December 31, 2019
EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)
(1)
April 1, 2019, through December 31, 2019
MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)
(1)
Unit 1 (April 1, 2019 - March 31, 2020)
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)
(1)
Unit 1 (April 1, 2019 - March 31, 2020)
BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)
(1)
Unit 1 (April 1, 2019 - March 31, 2020)
71152 - Problem Identification and Resolution
Semiannual Trend Review (IP Section 02.02) (1 Sample)
(1)
The inspectors reviewed the licensees corrective action program for potential
adverse trends that might be indicative of a more significant safety issue.
9
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program
related to the following issues:
(1)
Review of multiple failures of contactors and auxiliary contacts in safety-related and
nonsafety-related 480 volt motor control center electrical breakers (NCRs 02305600,
02318759, 02325498, and 02332720)
71153 - Followup of Events and Notices of Enforcement Discretion
Event Report (IP Section 03.02) (1 Sample)
The inspectors evaluated the following licensee event reports (LERs):
(1)
LER 05000400/2019-002-00, 'B' Train Chiller for the Essential Services Chilled Water
System Tripped on High Compressor Oil Temperature (ADAMS Accession
No. ML19259A072). The inspection conclusions associated with this LER are
documented in this report under Inspection Results Section 71153.
INSPECTION RESULTS
Observation: Semi-Annual Trend Review
The inspectors reviewed issues entered into the licensees corrective action program and
associated equipment performance databases to identify trends that could indicate the
existence of a more significant safety issue. The inspectors focused their review on repetitive
equipment issues, but also considered the results of inspector daily condition report
screenings, licensee trending efforts, and licensee human performance results. The review
nominally considered the 6-month period of January 2020 through July 2020, although some
examples may have extended beyond those dates when the scope of the trend warranted.
The inspectors compared their results with the licensees analysis of trends. Additionally, the
inspectors reviewed the adequacy of corrective actions associated with a sample of the
issues identified in the licensees trend reports. The inspectors also reviewed corrective
action documents that were processed by the licensee to identify potential adverse trends in
the condition of structures, systems and/or components as evidenced by acceptance of long-
standing, non-conforming or degraded conditions.
As a result of the semi-annual trend review, the inspectors noted a continued negative trend
in equipment performance challenges associated with the ESCW system; specifically, with
the B train ESCW chiller. Performance problems and issues with the ESCW chillers were
previously documented in NRC Inspection Report 05000400/2019004, dated
February 20, 2020. Continued equipment performance issues during the latest semi-annual
trend review period with the B ESCW chiller were documented in the following
licensee NCRs:
NCR 02311457, B ESCW chiller tripped on compressor low oil pressure due to oil
leak from compressor oil filter assembly pipe nipple through-wall crack on
January 18, 2020
10
NCR 02331982, B ESCW chiller declared TS inoperable due to high compressor
motor winding temperature and inability to control chill water outlet temperature within
the required temperature setpoint on May 26, 2020
The licensee acknowledged the existence of continued equipment reliability issues with the
ESCW system. As a result of the January 18, 2020, B ESCW chiller failure, B train ESCW
exceeded its 10 CFR 50.65 (Maintenance Rule) reliability performance monitoring criteria
goal of less than four functional failures in a rolling 36-month monitoring period. In response
to exceeding this performance monitoring criteria, the B train ESCW was placed in
Maintenance Rule (a)(1) monitoring condition, requiring the licensee to evaluate the system
performance issues in detail and develop an action plan with corresponding improvement
goals to address the unacceptable equipment performance. The inspectors reviewed the
licensees (a)(1) evaluation results documented in NCR 02311457 and determined that it met
the requirements of 10 CFR 50.65. On April 28, 2020, the licensee completed implementation
of a major (a)(1) corrective action item designed to improve reliability of the B ESCW
chiller. This improvement initiative involved implementation of a modification to mitigate the
likelihood of the chiller operating in surge/stall conditions when normally operating in a lightly
loaded condition by adjusting the chiller hot gas bypass valve and pre-rotation vane setting to
place greater load on the chiller during normal operation. The inspectors noted, however, that
a subsequent B ESCW chiller problem occurred on May 26, 2020, following the
implementation of this reliability improvement item, indicating continued licensee attention
was needed to address the adverse equipment performance problems with the ESCW
system.
Inoperability of 'B' Train ESCW Chiller Due to Trip on High Compressor Oil Temperature
Results in Condition Prohibited by Technical Specifications
Cornerstone
Significance
Cross-Cutting
Aspect
Report
Section
Mitigating
Systems
Green
Open/Closed
[P.2] -
Evaluation
A self-revealed Green non-cited violation (NCV) of Technical Specification (TS) 3.7.13,
Essential Services Chilled Water System, was identified as a result of the B train ESCW
system being inoperable for a period greater than 78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br /> between July 13 through
July 16, 2019, after the B ESCW chiller tripped on high compressor oil temperature due to
low compressor oil level, low refrigerant level, and excessive service water side biofouling in
the chiller condenser heat exchanger.
Description: On July 14, 2019, at 9:48 p.m., the B ESCW chiller tripped on high compressor
oil temperature after being started 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> earlier and operating for the entire time in a
surge condition. Chiller surge occurs when the refrigerant reverses flow and moves
backwards from the condenser through the compressor and back into the evaporator creating
increased chiller vibrations and compressor bearing loads resulting in higher oil
temperatures. The chiller was declared TS inoperable at the time of the trip and the action
statement for TS Limiting Condition for Operation (LCO) 3.7.13 was entered requiring the B
ESCW chiller to be restored to operability within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in Mode 3 (hot standby) with
the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Mode 5 (cold shutdown) within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Chiller
troubleshooting and investigation identified both slightly low compressor oil levels and
refrigerant levels, as well as excessive condenser tube biofouling on the service water side of
the condenser heat exchanger. It was determined that as a result of the condenser biofouling,
11
the reduction in heat transfer between the refrigerant and service water along with slightly
reduced oil and refrigerant volumes likely increased the pressures in the compressors oil
sump disrupting the proper operation of the refrigerant oil reclaim system causing the high oil
temperature trip setpoint to be reached. Following the addition of a small amount of
compressor oil and refrigerant, the B ESCW system was tested and declared operable on
July 16, 2019, at 10:14 p.m.; however, during the operability testing, the chiller continued to
exhibit some surging, although to a lesser extent than prior to the addition of compressor oil
and refrigerant. Subsequently, on July 17, 2019, the chiller was removed from service to
mechanically clean the chiller condenser heat exchanger tubes, at which time, significant
biofouling was confirmed.
The inspectors noted that evidence of unexpected biofouling in other plant heat exchangers
cooled by normal and emergency service water systems was identified as far back as April
2019; however, actions to address potential adverse impact from biofouling in the ESCW
system had not been adequately considered up until the time of the B ESCW chiller trip. In
addition, other weaknesses in licensee chiller heat exchanger performance monitoring were
identified. Specifically, condenser and evaporator approach temperatures, which provide
early indication of degrading heat transfer in the chiller, were not being monitored or trended,
even though the raw data was being collected during routine chiller testing. The inspectors
also noted that unexpected chiller surging was identified during B chiller operations dating
back to May 27, 2019, and continued to get longer in duration leading up to the chiller
trip. These surging conditions were indicative of degrading heat transfer due to increasing
chiller condenser fouling and the naturally occurring increase in service water temperature
that occurs during the summer period.
Due to the extent of the B chiller degradation, the licensee determined that most likely, it was
unable to perform its safety function prior to the actual time of the trip on July 14,
2019. Based on the last time the chiller was operated successfully, the time of initial
inoperability was moved to July 13, at 3:50 p.m. This resulted in the B ESCW chiller being
inoperable for over 78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br /> (i.e., from July 13, at 3:50 p.m. through July 16, at 10:14
p.m.). Consequently, TS LCO 3.7.13, which requires an inoperable ESCW chiller be restored
within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, was not met. On September 16, 2019, an
LER was submitted to the NRC under 10 CFR 50.73(a)(2)(i)(B), for an operation or condition
which was prohibited by the plants Technical Specifications.
Corrective Actions: The licensee completed cleaning of both the A and B ESCW
condenser heat exchangers to remove biofouling buildup. A service water margin recovery
program initiative was implemented to evaluate the conditions causing the unexpected
service water biofouling conditions in order to address long-term corrective actions. ESCW
chiller operational test procedures were revised to include condenser and evaporator
monitoring of approach temperatures to provide an early indication of degrading heat transfer
conditions.
Corrective Action References: NCRs 02278242, 02281819, and 02286887
Performance Assessment:
Performance Deficiency: The licensee failed to adequately monitor and identify degrading B
ESCW chiller operational performance issues resulting from excessive biofouling in the
ESCW chiller condenser heat exchanger.
12
Screening: The inspectors determined the performance deficiency was more than minor
because it was associated with the Equipment Performance attribute of the Mitigating
Systems cornerstone and adversely affected the cornerstone objective to ensure the
availability, reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences. Specifically, the finding resulted in the B ESCW chiller tripping
on high compressor oil temperature, rendering the chiller inoperable and causing a condition
prohibited by TS.
Significance: The inspectors assessed the significance of the finding using Appendix A, The
Significance Determination Process (SDP) for Findings At-Power. The finding was screened
by Exhibit 2, Mitigating Systems Screening Questions, under Section A, Mitigating SSCs
and PRA Functionality, and it was determined the performance deficiency required a detailed
risk evaluation because the degraded condition represented a loss of probabilistic risk
analysis (PRA) function of one train of a multi-train TS system for greater than its TS allowed
outage time. A detailed risk evaluation of the performance deficiency was performed by a
Region II Senior Reactor Analyst (SRA) in accordance with NRC IMC 0609, Appendix A. The
SRA conservatively assumed the B ESCW chiller would fail to run for its mission time over a
50-day exposure period and chiller supported equipment would also fail in order to bound this
condition. Using SAPHIRE 8 Version 8.1.8 and Harris SPAR Model Version 8.54, dated
February 26, 2017, the SRA set CHW-CHL-FR-1B (B ESCW chiller fails to run) to True. The
dominant accident sequence was a Small Break Loss of Coolant Accident with a failure of
High Pressure Safety Injection Pumps and Failure of Secondary Side Reactor Coolant
System Cooldown. Change in plant risk for this conservative bounding analysis was less
than 2.0 E-7 per year, corresponding to a finding of very low safety significance (Green).
Cross-Cutting Aspect: P.2 - Evaluation: The organization thoroughly evaluates issues to
ensure that resolutions address causes and extent of conditions commensurate with their
safety significance. Specifically, the license failed to thoroughly evaluate unexpected service
water biofouling in the B ESCW chiller condenser as evidenced by increased surging
conditions during chiller operation resulting in the chiller tripping on high compressor oil
temperature.
Enforcement:
Violation: Shearon Harris TS 3.7.13, Essential Services Chilled Water System, requires two
ESCW systems to be operable in Modes 1 through 4, and if one ESCW system is inoperable,
it shall be returned to an operable condition within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the unit shall be shut down and
be in Mode 3 (hot standby) within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Mode 5 (cold shutdown) within the
following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Contrary to the above, from July 13, 2019, to July 16, 2019, while operating in Mode 1, the
licensee failed to follow the action requirements of TS 3.7.13, in that, following 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> of
inoperability associated with the B ESCW system, the licensee failed to be in hot standby
within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> or restore the B ESCW to an operable condition.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
The disposition of this violation closes LER 05000400/2019-002-00, 'B' Train Chiller for the
Essential Services Chilled Water System Tripped on High Compressor Oil Temperature.
13
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On July 29, 2020, the inspectors presented the integrated inspection results to Kim
Maza and other members of the licensee staff.
On May 20, 2020, the inspectors presented the Emergency Preparedness Program
inspection results to Kim Maza and other members of the licensee staff.
14
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
Resulting from
Inspection
Procedure
Revision Request
(PRR) 02332256
Change AP-301 Attachment 5 Hot Weather Monitoring of
Critical Plant Equipment
05/27/2020
Procedures
AP-300
Severe Weather Response
Rev. 34
AP-301
Seasonal Weather Preparations and Monitoring
Rev. 86
Corrective Action
Documents
Resulting from
Inspection
Nuclear Condition
Report (NCR)
02335261
Reactor auxiliary building steam tunnel roof leak
6/16/2020
Procedures
Chemical and Volume Control System
Rev. 117
Containment Spray System
Rev. 46
Main Steam, Extraction Steam, and Steam Dump Systems
Rev. 41
Essential Services Chilled Water System
Rev. 80
Fire Plans
CSD-HNP-PFP-
DGB
Diesel Generator Building Pre-Fire Plan
Rev. 1
CSD-HNP-PFP-
FHB
Fuel Handling Building Pre-Fire Plan
Rev. 1
CSD-HNP-PFP-
RAB-261
Reactor Auxiliary Building Elevation 261 Pre-Fire Plan
Rev. 1
CSD-HNP-PFP-
Turbine Building Pre-Fire Plan
Rev. 3
Procedures
AD-EG-ALL-1520
Transient Combustible Control
Rev. 13
AD-EG-ALL-1522
Duties of a Compensatory Fire Watch
Rev. 11
AD-OP-ALL-0207
Fire Brigade Administrative Controls
Rev. 3
CSD-HNP-PFP-
RAB-305-324
Reactor Auxiliary Building Elevations 305 and 324 Pre-Fire
Plan
Rev. 4
Fire Protection Program Manual
Rev. 44
Fire Emergency
Rev. 45
Corrective Action
Documents
Resulting from
Pipe Break Exemptions for Rod Control Cabinet and
Termination Cabinet Rooms (RAB 305) Not Documented
05/27/2020
15
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Inspection
Engineering
Evaluations
PRA-F-E-0008
Reactor Auxiliary Building Unit 1 El. 305' Internal Flooding
Analysis
Rev. 3
Miscellaneous
Design Basis
Document (DBD)-
323
High Energy and Moderate Energy Line Breaks
Rev. 1
71111.11Q Corrective Action
Documents
AOP-012 Entry for Partial Loss of Condenser Vacuum
06/06/2020
Miscellaneous
Reactivity Manipulation Plan (H1C23 Condenser Tube
Leakage Repair)
Rev. 0
Procedures
AD-EP-ALL-0111
Control Room Activation of the ERO
Rev. 1
AD-OP-ALL-1000
Conduct of Operations
Rev. 17
AD-OP-ALL-1001
Conduct of Abnormal Operations
Rev. 3
Loss of One Emergency AC Bus (6.9KV) or One Emergency
DC Bus (125V)
Rev. 45
Loss of All AC Power
Rev. 10
GP-005
Power Operation (Mode 2 to Mode 1)
Rev. 107
GP-006
Normal Plant Shutdown from Power Operation to Hot Standby
(Mode 1 to Mode 3)
Rev. 92
Corrective Action
Documents
Replace blown control power fuse in 'B' EDG lube oil keep
warm pump breaker
12/03/2019
1CY014 fitting oil leak caused WC-2B chiller trip
01/18/2020
Procedures
AD-EG-ALL-1210
Rev. 2
Work Orders
WOs 20378550
and 20383218
Repair of WC-2B chiller following 1CY-14 fitting oil leak
caused chiller trip
01/18/ 2020
Calculations
HNP-F/PSA-0011
Rev. 15
HNP-F/PSA-0119
Online Phoenix PRA Model
Rev. 1
Corrective Action
Documents
Resulting from
Inspection
Heater Drain Pump 1A-NNS Discharge to 4-1A-NNS Conduit
Knocked Loose by Vibration
06/10/2020
Procedures
AD-NF-ALL-0501
Electronic Risk Assessment Tool (ERAT)
Rev. 5
AD-WC-ALL-0200 On-Line Work Management
Rev. 17
AD-WC-ALL-0240 On-Line Risk Management Process
Rev. 2
16
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
AD-WC-ALL-0410 Work Activity Integrated Risk Management
Rev. 10
CSD-WC-HNP-
0240-00
Rev. 0
Work Orders
'A' EDG emergent repair of fuel oil supply header line leak
04/24/2020
Corrective Action
Documents
'C' CCW pump seal leak
01/03/2015
'C' CCW pump seal leakage degraded
06/15/2020
Miscellaneous
NRC IMC 0326
10/01/2019
Nuclear Energy
Institute (NEI) 18-
03
Rev. 0
Procedures
AD-OP-ALL-0105
Rev. 6
Work Orders
'B' EDG jacket water heater stuck energized
05/04/2020
Engineering
Evaluations
Action Request
(AR) 02319363
10 CFR 50.59 evaluation of EC 0000416868
03/05/2020
Procedures
AD-EG-ALL-1132
Preparation and Control of Design Change Engineering
Changes
Rev. 16
AD-EG-ALL-1133
Preparation and Control of Design Equivalent Change
Engineering Changes
Rev. 12
Procedures
AD-EG-ALL-1155
Post Modification Testing
Rev. 4
MPT-M0084
Motor Lubrication, Westinghouse
Rev. 13
PLP-400
Post Maintenance Testing
Rev. 64
Work Orders
Replace air filter regulators for main steam isolation bypass
valves 1MS-81, 1MS-83, and 1MS-85
05/14/2020
Implement EC 0000416868 on 'A' ESCW
05/20/2020
Implement EC 0000416868 on 'B' ESCW
04/28/2020
Delta T/Tavg Loop (T-0412) Operational Test
6/17-18/2020
Implement EC 0000417450 on 'B' ESCW
04/28/2020
Implement EC 0000417450 on 'A' ESCW
05/19/2020
Repair 'B' ESCW chiller failure to maintain chill water outlet
temperature within setpoint
05/28/2020
WOs 20275346
and 20267416
Limitorque stem lubrication on 'A' CSIP recirculation valves
05/19/2020
71151
Miscellaneous
2019 - 2020
17
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Licensee Event
Reports
2019 - 2020
Operator Log
Entries
Procedures
AD-PI-ALL-0700
Performance Indicators
Rev. 4
OST-1026
Reactor Coolant System Leakage Evaluation, Computer
Calculation Daily Interval, Mode 1-4
Rev. 53
Corrective Action
Documents
AD-PI-ALL-0100
Corrective Action Program
Rev. 23
AD-PI-ALL-0101
Root Cause Evaluation
Rev. 7
AD-PI-ALL-0102
Apparent Cause Evaluation
Rev. 4
AD-PI-ALL-0106
Cause Investigation Checklists
Rev. 4