ML20197H468

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Insp Rept 50-219/86-06 on 860303-0413.Violations Noted: Failure to Maintain Procedure Per NUREG-0612 Re Movement of Heavy Loads & to Follow Design Review Process Procedures. Annual Emergency Drill Deemed Acceptable
ML20197H468
Person / Time
Site: Oyster Creek
Issue date: 05/08/1986
From: Blough A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20197H402 List:
References
REF-GTECI-A-36, REF-GTECI-SF, RTR-NUREG-0612, RTR-NUREG-612, TASK-A-36, TASK-OR 50-219-86-06, 50-219-86-6, IEB-80-16, IEC-79-12, IEC-80-10, IES-79-12, NUDOCS 8605190174
Download: ML20197H468 (26)


See also: IR 05000219/1986006

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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No.

50-219/86-06

Docket No.

50-219

License No.

OPR-16

Priority

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Category

C

Licensee:

GPU Nuclear Corporation

100 Interpace Parkway

Parsippany, New Jersey

Facility Name: Oyster Creek Nuclear Generating Station

Inspection At: Forked River and Parsippany, New Jersey

Inspection Conducted: March 3 - April 13, 1986

Participating Inspectors:

W. H. Battman, Senicr Resident Inspector

J. F. Wectselberger, Resident Inspector

W. H. Baurack, Project Engineer

Approved by:

l>J O m A 4

rNrt

A. R. Blough, Chief

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Da'te

Reactor Projects Section in

Inspection Summary:

Routine inspections were conducted by the t-esident inspectors and a Region

based inspector (373 hours0.00432 days <br />0.104 hours <br />6.167328e-4 weeks <br />1.419265e-4 months <br />) of activities 1.1 progress including plant opera-

tions, physical security, radiation control, housekeeping, fire protection,

emergency preparedness, and outage preparations. The inspectors also reviewed

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licensee action on previous inspection findt'.igs, made routine tours of the

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facility, participated as observers in the annual emergency drill, observed

licensee action during an Unusual Event declared as the result of a bomb

threat, and reviewed the most recent licensee QA environmental qualification

audit.

In addition, the inspectors visited the GPUN corporate offices and met

with various members of Tech Functions management and also reviewed four

modification packages scheduled to be implem:nted during the 11R outage.

The

inspectors also attended several briefings i.cluding the QA Annual Assessment,

inservice inspection plans for the 11R outag.., PSMS computer system, and the

Maintenance, Construction, and Facilities' Werk Management System.

8605190174 860512

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Results:

Two violations were identified. One involved failure of Plant Engir.eering (PE)

to maintain the station procedure governing their conduct as described in para-

graph 1, as well as failure of PE to properly prioritize and address a licensee

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self-identified concern regarding failure to address NOREG 0612, movement of

heavy loads, at the Intake Structure as described in paragraph 2; and the other

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involved failure of Tech Functions to follow procedures governing the design

review process as discussed in Paragraph 9.

Plant response to the bomb threat was comprehensive. The annual emergency

drill was termed acceptable.

Plant operations were interrupted twice -- once

due to an unexpected reactor trip and once due to an unplanned shutdown to

replace reactor low water level scram sensors.

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At the end of the report period, the plant was shutdown and the 11R outage had

Commenced.

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Details

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1.

Licensee Action on Previous Inspection Findings

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(Open) Inspector Follow Item (219/84-06-02): Closecut Documentation for

Plant Material (PM) Department Plant Engineering Work Requests (PEWR)

Not Always Available

During NRC Region I Inspection 84-06 it was noted that closeout documen-

tation of PM PEWRs was only occasionally available, there was a lack of

status of PEWRs, and a lack of understanding of the priorities for open

requests. These factors were discussed with plant management who indi-

cated that the matter would be reviewed and appropriate action taken.

During this inspection those actions taken by the licensee to resolve

this item were reviewed.

The PM Department, by memorandum dated January 9,1985, notified Plant

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Engineering (PE) of open PM PEWRs. Also, all outstanding PEWRs were

reviewed and those considered no longer applicable were cancelled.

The

PM Department has setup a program establishing a central departmental

contact for liaison between PE and PM.

All PEWRs are to be handled and tracked by this contact. PM, by memo-

randum dated June 19, 1985, also requested from PE all acknowledgements

of acceptance of PEWRs, all completed PEWRs, and any correspondence with

regard to PM PEWRs.

Based on these actions the licensee's Licensing

Action Item written to resolve this matter was closed.

To verify the effectiveness of the licensee's actions, the PM PEWR log was

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reviewed by the inspect 6r.

This log indicated 30 no longer applicable

open PEWRs had been cancelled, 19 PEWRs have been closed, and 115 remain

open. Of the open PEWRs, 36 were written in 1983, 32 in 1984, 43 in 1985,

and 3 in 1986. Some open items indicated acknowledgements from PE,

however, many are logged with no acknowledgements indicated.

The inspector selected 22 of the items identified in the log as still

open for follow-up in the PE files.

Five of the items were found to have

been closed in PE files. Two of these five had documentation indicating

PM had been informed of the closeout.

Four of the items were closed by

PE-by Technical Functions Work Requests, the status of these items was

not tracked by PE, and PM was not notified of this'closecut.

The status

of these items was not tracked by PE.

Eleven were indicated as open in

PE files.

Information relative to two items was not readily available

and no follow up of these was conducted.

Due to the fact.that some

errors still appear to exist in the PM documentation relative to PEWRs,

this item 84-06-02 remains open.

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Because of the discrepancies noted between PM and PE files, particularly

after an effort had been made to improve tracking of PM PEWRs as a result

of NRC Inspection 84-06, the inspector reviewed Station Procedure Number

125, Conduct of Plant Engineering , as it related to tracking of engineer-

ing tasks. This procedure was written to delineate the functions, respon-

sibilities, authorities, and organizational interfaces of the PE organi-

zation. A review of this procedure indicated the procedure had become

outdated in a number of areas. These areas include:

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Organization: the procedure describes an organization different than

the organization that currently exists.

Consequently, the proce-

durally described responsibilities are for position titles which do

not exist. How these responsibilities are performed within the

existing organization is not clear.

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Performance of engineering tasks: the current method of initial

review of work requests and the issuance of Plant Engineering Task

Assignments (PETA) differs from that described in the procedure.

Copies of PETAs are not always forwarded to the requestor as required.

Also, close-out of PETAs is not always as procedurally required in

that Form 125-2 is not generally completed in closing-out PETAs.

This form requires a close-out response be provided to the originator.

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Records maintenance differs from that described in the procedure.

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The prioritization of PETAs differs substantially from that described

in the procedure. The PE procedure identifies only two priority

classifications. The actual prioritization is done basically in ac-

cordance with a Technical Functions Division procedure which results

in numerous priorities. PM personnel were unaware of the meaning of

the priority numbers assigned to their items.

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The PEWR form being used differs slightly from that attached to the

procedure.

In addition, there are no instructions in the procedure

detailing how this form is to be used, particularly,'the acknowledge-

ment section.

The above are examples of the more significant deficiencies noted in the

Conduct of Plant Engineering Procedure. These and other procedural

problems were discussed in detail with the PE-and PM Directors. The in-

spector noted the failure to maintain the Conduct of Plant Engineering

Procedure current was considered to be a violation (219/86-06-01). The

PE Director indicated a forthcoming reorganization and the change-over to

a new computerized Action Item Tracking System were th> reason the pen-

cedure was allowed to become outdated.

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It should be noted only the portions of the Conduct of Plant Engineering

Procedure dealing with performance of engineering tasks were reviewed.

Other portions of th'e procedure may also be outdated.

(Closed) Inspector Follow Item (219/84-06-0E): Licensee to revise diesel

generator procedure to include certain checks.

The licensee has revised Station Procedure 636.4.003, Diesel Generator

Load Test, to include verification of filter oil level, verification of

DG battery strip heater energization, and acceptable level for DG fuel

oil day tank.

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(Closed) Inspector Follow Item (219/84-06-03): Plant Materiel mechanical

section to provide equipment failure review to the Vice president and

Director.

The Plant Materiel mechanical section has established a Plant Materiel

Mechanical Equipment Trending Program.

Part of this program is to

provide a quarterly report to the Deputy Director.

In addition, a year

end summary is also provided the Deputy Director. The year end summary

summarizes trends, failures, corrective, and preventive maintenance

performed by system and by individual components. The report also

describes problems and experiences and proposes corrective actions.

(Closed) Inspector Follow Item (219/83-25-01): Licensee audit finding

identified inconsistencies in radiation protection procedures.

A subsequent Quality Assurance Audit S-0C-84-17 performed by the licensee

from October 22, 1984 to January 2, 1985 of radiological controls deter-

mined, based upon a review of the 900 series procedures, all previous

discrepancies have been corrected.

In addition, a major rewrite of the

radiation controls procedures was conducted in 1985. During this rewrite

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many outdated procedures were deleted.

. Closed) Unresolved Item (219/83-24-02): Inaccurate response to IE

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Bulletin 80-16.

Inspection 83-24 identified the installation in the plant-of certain trans-

mitters which the licensees response to IE Bulletin 80-16 indicated were

not used at Oyster Creek. The licensee committed to certain corrective

actions. These included (1) a review of the respense to IE Bulletin 80-16

and the submittal of corrections to the Bulletin response dated July 24,

1980. This was accomplished by licensee letter Fiedler to Murley, dated

November 9, 1982; (2) an audit of IE Bulletins and GE Service Information

Letters (SILs) to assure licensee actions and statements reflect the con-

ditions at the plant.

Licensee Action Item files 83023.02 and 80062.3

contain memoranda which show that these audits have been performed; and

(3) a system will be developed to inform all potential users of the impact

of IE BC.letins and GE SILS to avoid further use of defective components.

The licensee has in place Corporate Procedure 1000-ADM-1216.03, Regulatory

Correspondence Control, which defines and establishes the GPUN system for

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the management of incoming and outgoing regulatory correspondence and the

assignment of tasks associated with that correspondence.

[ Closed) Unresolved Item (219/80-25-03): Review drain time difference of

scram discharge volume (SDV) following two successive scrams.

During Inspection.80-25 a significant difference was noted in the time

for the SDV to drain following an automatic scram and a manual scram (161

sec. vs. 84 sec.).

During the last outage, major modifications were made

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to the SDV system. The existing SDV which had experienced the drain time

difference has been removed and replaced with two separate SDVs. During

startup testing following the modification, SDV drain times were recorded

and no abnormal drain times were noted.

(Closed) Unresolved Item (219/80-09-01): This item deals with the sealing

of electrical connections to limitorque valve operators within the

drywell.

During NRC Region I Inspection 80-09, several concerns were noted. One

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concern dealt with a flexible electrical conduit pulled from its packing

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gland on the solenoid actuator for reactor water sample isolation valve

V-24-29, and the other with the sealing of motor operated valve operator

cable where it exits rigid conduit.

Quality Control Inspection Report 11085 verified that the flexible

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electrical conduit associated with V-24-29 had been repaired. Also, the

licensee performed an evaluation of motor operated valves which might

experience infiltration of steam under accident conditions through cable

exiting rigid conduit. Two valves were identified V-14-36 and 37 for

which sealing at the conduit leading to the valve was recommended.

These

conduits were sealed per Job Order 0450V.

(Closed) Licensee Identified Items (219/81-LO-3E, 81-LO-4E, 81-LO-5E,

81-LO-6E, and 81-LO-7E).

These items deal with Nonroutine Environmental Operating Reports which

were submitted by the licensee. The first four deal with less than the

required number of dilution pumps operating and the last deals with

exceeding the allowable temperature difference between circulating water

intake and discharge due to grass clogging of the intakes.

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By Amendment No. 66 to the Oyster Creek Operating Licensee issued on

May 24, 1983 the non-radiological water quality-related requirements were

deleted from the Environmental Technical Specifications. ' Consequently,

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this type of event is no longer required to be reported to the NRC.

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As a followup to these reports, the inspector verified that certain

improvements have been made to the dilution pumps. These improvements

include changes to the pump seal water and lubricating oil cooling water,

upgrading of piping to more corrosive-resistant material, extensive pump

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maintenance, and the stocking of spare parts. Additional modifications

to improve dilution pump performance are planned for the 1986 refueling

outage. Also, limits associated with the main condenser _ circulating

water system and the thermal dilution pumps are contained in Station

Procedure 323, Main Condenser Circulating Water System, and Procedure

324, Thermal Dilution Pumps, respectively.

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(Closed) IE Circular No. 80-10 (219/80-CI-10): Failure to maintain

environmental qualification of equipment.

This Circular described several instances in which environmental

qualification of equipment was not maintained due to the use of the wrong

class of equipment during maintenance.

The Circular recommended licensees

review maintenance procedures and administrative policies to ensure: (1)

adequate administrative controls exist to ensure that equipment which is

environmentally qualified is identified prior to maintenance; (2) mainte--

nance procedures provide necessary instructions and precautions to ensure

that the environmental qualification of equipment is not degraded when

maintenance is completed; and (3) maintenance personnel are adequately

trained on environmental qualification requirements and the potential for

equipment degradation from improper maintenance.

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The licensee has in effect Station Procedure No. 105.3, Maintenance of

Oyster Creek Environmental Oualified (EQ) equipment.

This procedure has

been prepared to provide administrative control and practices related to

all maintenance performed on EQ equipment and to assure that procurement

of replacement components is in accordance with EQ requirements. The

procedure specifies training of maintenance planning personnel on

requirements to maintain EQ and incorporates appropriate requirements in

tasks on EQ equipment. Also, the procedure requires that maintenance

personnel be trained on requirements to maintain EQ.

The inspector

verified planners received the required training on September 18, 1985,

and the maintenance personnel on September 9, 1985.

2.

Control of Movement of Heavy Loads at the Intake Structure

A review of outstanding Plant Engineering Work Requests (PEWRs) disclosed

a situation wherein a safety concern was identified and submitted to

Plant Engineering (PE) for action that PE had failed to address.

In

particular, a PEWR initiated by Plant Materiel dated 8/19/85 explained

that heavy loads were being moved at the Intake Structure using a mobile

crane in the vicinity of safe' shutdown equipment (four Emergency Service

Water. pumps) without procedural controls.

The PEWR requested that the

movement of heavy loads at the Intake be analyzed to ensure NUREG-0612

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(Control of Heavy Loads) guidelines are met. The NRC inspector determined

that the licensee's response to the NUREG-0612 guidelines for the Intake

stated that since the gantry crane at the Intake had been removed from

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service the Intake was excluded from NUREG-0612 applicability. The

responte also said, "If at some time in the future this crane is placed

back into service, an evaluation will be performed to ensure that

NUREG-0612 criteria are satisfied." The response did not recognize nor

address the use of a mobile crane to move heavy loads at the Intake. The

Plant Materiel group-who identified the issue exhibited a good awareness

of regulatory commitments and onsite conditions.

PE received this PEWR on 8/20/85, assigned it PE Task #512200850635, and

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gave it a priority 2 rating. Paragraph 6.4 of Station Procedure 125,

Conduct of Plant Engineering, Rev. 2, discusses management of PE tasks

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and requires, in part, that tasks which, left undone, would cause a NRC

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commitment deadline to be missed, should be given priority 1 rating.

Although procedure 125 does not explain the significance of a priority 1

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rating, it is implied that priority 1 demands immediate attention. The

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anticipated completion date for this task was listed as 1/1/99, which by

PE definition meant it was unscheduled. The failure of PE to assign the

appropriate priority rating to this PEWR resulted in a nuclear safety

issue not being promptly addressed. This is a violation.

(219/86-06-02)

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Subsequent to identification of this matter by the NRC inspector, the

licensee committed to cease movements of heavy loads at the Intake until

the appropriate evaluations and training are completed.

3.

Surveillance Testing

In Inspection Report 86-04, a summary of events relating to the erratic

performance of Static-0-Ring (SOR) differential pressure sensors was -

presented. During this report period, the erratic. performance continued

and a licensee decision was made to shutdown the plant and replace.the

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reactor low level scram sensors with a slightly different model tisat had

been performing satisfactorily as the reactor low low level sensors. ' SOR

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model number 103 AS-8212-NX-JJTTX6 was replaced with SOR model number 103

AS-BB212-NX-JJTTX6 and some minor modifications were made to the sensor's

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inlet piping. The sensor replacement and piping changes were classified

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as a modification and received a safety evaluation.

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. eekly surveillance of the new sensors was implemented following plant

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startup. Problems with setpoint drift of these sensors was also exper-

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tenced and one. sensor was undergoing daily surveillance the week prior to

plant shutdown for the 11R outage. Neither the licensee nor SOR have.an

explanation for the setpoint drift. At one point it was suspected a

valving sequence to verify reactor vessel communication (referred to as

" bang test") was the cause. However, subsequent evidence has eliminated.

this possibility. The licensee's present plans are to replace the low

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level scram sensors with an analog type-system during the 11R outage and

to delay replacement of other plant sensors that were scheduled to be

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replaced with SOR units.

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other site locations including the site boundary with negative results.

Operations corrected the problem by reestablishing a negative

differential pressure in the turbine building.

During routine surveillance by radcon of trash in dumpsters outside the

RCA, a slightly contaminated piece of an old LPRM box was identified. A

spot the size of a silver dollar was found to read 200 cpm above background.

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The LPRM box was being cut up for disposal and the radiologically clean

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pieces were disposed of as clean trash.

Radcon management discussed the

inadequate survey with the technician-involved and counseled the individual

as to the importance of a thorough survey.

The licensee discussed their man rem exposure goals for 1986 with the NRC

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inspectors. The estimates include outage related exposure. The man rem

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estimate for 1986 without decon of the recirc piping is approximately

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1700. The licensee plans, however, to decon the recirc piping thereby

r2ducing the estimate to 1000. A goal of 800 has been set.

It is note-

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worthy that the chemical decon of the recirc piping will reduce personnel

exposure by approximately 40 man rem per week.

The investment by the

licensee to reduce personnel exposure is noteworthy.

6.

Operational Safety Verification

6.1 Control Room Safety Verification

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Routinely throughout the inspection period, the inspector indepen-

dently verified plant parameters and engineered safeguard equipment

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availability. The following items were observed:

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Proper Control Room manning and access control;

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Adherence to approved procedures for ongoing activities;

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Proper safety systems and emergency power sources valve and

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breaker alignment; and

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Shift turnover.

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6.2 Review of Logs and Operating Records

The inspector reviewed, on a sampling basis, the following logs and

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instructions for the period March 3 to April 13, 1986:

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Control Room and Group Shift Supervisor's Logs;

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Control Room and Shif t Supervisor's Turnover Check Lists;

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Reactor and Turbine Building Tour Sheets;

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The inspectors considered the licensee's efforts to address the problem

of setpoint drift of the reactor low level scram sensors to be sound in

engineering judgement and conservative regarding safe plant operation.

4.

Review of QA Audit of Environmental Qualification

The licensee's QA group performed an audit of the environmental qualifi-

cation of electrical equipment at Oyster Creek.

The audit number was

0-0C-85-08 and was performed November 11-26, 1985. Because of concerns

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raised during discussions with QA management regarding changes to the

audit after initial issue, the inspectors decided to review the audit to

ensure the changes made did not impact the audit findings. A comparison

of the initial issue of the audit with the final issue indicated that two

subjective statements had been deleted but that the audit recommendations

were unchanged. The NRC inspector did not feel the deletion of the GPUN

QA auditor's opinions from the audit detracted from the effectiveness of

tne audit, especially in light of the fact that the audit's final con-

clusicns remained unchanged.

The NRC inspector did, however, request that

he be informed when Tech Function's Engineering Assurance responds to the

audit recommendations. The inspector will review the responses during a

subsequent inspection.

(219/86-06-03)

5.

Radiation Protection

During entry to and exit from the RCA, the inspectors verified that

proper warning signs were posted, personnel entering were wearing proper

dosimetry, personnel and materials leaving were properly monitored for

radioactive contamination, and monitoring instruments were functional and

in calibration.

Posted extended Radiation Work Permits (RWPs) and survey

status boards were reviewed to verify that they were current and accurate.

The inspector observed activities in the RCA'to verify that personnel

complied with the requirements of applicable RWPs and that workers were

aware of the radiological conditions in the area.

As a result of the reactor trip on March 6, 1986, 8 people working in the

turbine building became slightly contaminated with short-lived radio-

isotopes (cesium 138 and rubidium 88). The turbine building became

slightly airborne when sealing steam was lost to the turbine gland seals.

The contamination was not an unexpected event. The maximum level.was 1500

cpm on a worker's hard hat.

Radcon response to the contamination problem

was prompt and thorough.

On March 21, 1986 water vapor was observed escaping from around the roof

plugs on the turbine building heater bay roof.

Because the heater bay

contained airborne contamination from valve and equipment leakage, radcon

was promptly notified whereupon they sampled the space above the heater

bay roof.

Results of one sample indicated a minor unmonitored release .

was in progress.

Immediate action was taken by Operations to correct the

problem. Additional samples were taken above the heater bay roof and at

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Equipment Control Logs;

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Standing Orders; and

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Operational Memos and Directives.

The logs and instructions were reviewed to:

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Obtain information on plant problems and operations;

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Detect changes and trends in performance;

Detect possible conflicts with Technical Specifications or

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regulatory requirements;

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Assess the effectiveness of the communications provided by the

logs and instructions; and

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Determine that the reporting requirements of Technical

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Specifications were met.

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The reviews indicated the logs and operating records were generally

comple'.e. No inspector concerns were identified.

6.3 Review of Key Events

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Reactor Scram

On March 6, 1986 the facility experienced a reactor trip due to

a spurious turbine stop valve closure signal that occurred during

routine turbine stop valve surveillance testing. Approximately

one minute after the trip, the MSIVs isolated due to reactor

pressure decreasing to less than 850 psig with the Mode switch

still in RUN. At nearly the same time, the Reactor Water Clean-

up (RWCU) System isolated.

Electromatic relief valves were

manually actuated to control pressure until reactor water level

was brought back into the indicating range at which time the

isolation condensers were used to control pressure. Several

minor airborne contamination problems resulted in the turbine

building and minor flooding occurred in the steam jet air ejector

room due to an already leaking gland seal exhauster condenser.

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The exact cause of the scram was subsequently determined to be

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a malfunctioning of the position switch on the No. I turbine

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stop valve (TSV). ~Specifically, the contacts on the open posi-

tion switch were not making continuously.

Similar-switches on

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the other TSVs were checked and verified to be functional. The

No. 1 TSV position switch was replaced.

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The plant equipment response was as expected with the only

significant exception that a RWCU system containment isolation

valve, V-16-14, failed to cpen during one of several cycles.

Follow-up testing of V-16-14 to identify the problem did not

indicate a cause. The NRC inspector further pursued this

matter subsequent to plant restart and was informed by PE that

it has been known for some time that the valve motor is

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slightiy undersized for the valve opening operation.

(Note:

The valve closing function is safety-related, but opening is

not.) Previous problems with operability of this valve resulted

in making a Limitorque gearing change in an attempt to correct

the problem. The licensee has stated the problem with V-16-14

will be corrected prior to restart from the 11R outage.

Operator response to the trip indicated that past problems with

reactor water level control during trips has become a major

operator concern. As a result, during this trip recovery, the

control room operator gave his primary attention to control of

water level and neglected to place the Mode Selector switch to

SHUTDOWN. Within one minute of the trip, plant pressure had

decreased to less than 850 psig and, with the Mode switch still

in RUN; a MSIV closure occurred. The closure of the MSIVs

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added additional complications to the scram recovery in that

the EMRVs and the Isolation Condenser system had to be used for

heat sink purposes. A review of Station Procedure

2000-ABN-3200.01, Rev. O, Reactor Scram, indicated the first

two steps an operator should perform after an automatic trip

are to depress both manual scram pushbuttons and place the Mode

switch to SHUTDOWN. However, this procedure is prefaced by the

statement, "If while executing this procedure, any entry

condition for any Emergency Operating Procedure (EOP) occurs,

Then immediately exit this procedure and enter the appropriate

E0P."

One of the peculiarities of Oyster Creek is that a low

level scram signal is received each time a scram occurs. This

is a genuine signal and demands immediate entry into the level

control E0P. This E0P does not address the initial steps

required by the reactor scram procedure.

During past trips

operators have properly positioned the Mode Selector switch but

this time it was overlooked due to concerns for water level

control. The inspector reviewed the licensee's Post Trip

Review of this event and noted that the failure of the operator

to reposition the Mode Selector switch was a major concern.

The licensee committed in their Post Trip Review to evaluate

operator priorities following reactor trips and to make any

necessary procedural changes. The inspectors will follow up

licensee actions in a subsequent inspection.

(219/86-06-04)

B.

Some problems occurred during the subsequent restart from the

3/6/86 reactor trip.

Instrumentation associated with th

'C'

EMRV indicated seat leakage. The licensee operated the

.lve

several times in an attempt to reseat it.

The attempts were

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not successful and the plant continued to operate until

shutdown for the 11R outage with minor seat leakage past the 'C'

EMRV.

Instrumentation associated with the 'D'

and 'E'

EMRV in-

dicated they were also experiencing minor seat leakage through-

out the remainder of the operating cycle.

The EMRVs are

scheduled for overhaul during the outage.

During one of the attempts to reseat the

'C' EMRV, the plant

nearly experienced a reactor low level scram.

Prior to lifting

an EMRV the reactor water level control system is placed in

manual to preclude the system response that would occur if

control was in automatic.

If left in automatic the swell

caused by lifting the EMRV would signal the control system to

throttle down feedwater flow. This action, combined with a

greater feed flow / steam flow mismatch, would result in a rapid

decrease in reactor water level. What apparently occurred

during this attempt was a malfunction of the level control

switch such that, although the switch was in the manual

position, the contacts remained in automatic. The result was a

rapid decrease in reactor water level and a half scram signal

caused by low reactor water level. This switch problem and

other problems with the Mode Selector and IRM Range switches

caused the inspector to express a concern regarding operator

confidence in operation of these switches.

Plant management

plans are to replace the Water Level Control switch and modify

the IRM Range switch prior to restart from the 11R outage.

Actions are also underway to purchase a new Mode switch,

although it is uncertain whether it will be installed prior

to restart.

C.

Throughout the latter portion of the operating cycle, leakage

of condensate from the gland seal exhauster condenser caused

problems.

Each time plant load was reduced, condensate header

pressure increased making the leakage worse, thereby, causing

erratic operation of the gland seal exhaust fans.

Plans are to

repair the condenser during the outage.

D.

During performance of augmented surveillance of the reactor low

level sensors, an ECCS initiation occurred. The initiation

signal was generated when one of the sensors was being valved

back into service following surveillance. The licensee deter-

mined that a slight flow surge and pressure drop in the variable

leg occurred when a test gauge, used to confirm sensor communi-

cation with the reactor vessel, was valved in. This variable

leg also serves the reactor low low water level sensors. The

filling of the empty tubing between the isolation valve and the

gauge caused the transient. This transient was sensed by the

reactor low low level sensor which in turn initiated the ECCS

signal. Two Core Spray main and booster pumps started, both

emergency diesel generators started, and one half an ATWS trip

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signal occurred. All systems responded normally and the oper-

ators recovered from the event without incident.

No actual

ECCS injection to the vessel occurred. The surveillance proce-

dure was subsequently modified to require filling the tubing

between the isolation valve and the gauge prior to opening the

isolation valve.

F.

As mentioned in paragraph 5 above, an unmonitored release of

radioactivity occurred from the turbine building heater bay

roo f.

This rerulted because of gradual degradation of turbine

building exhaust fan 1-7 and subsequent positive pressurization

of the turbine building. Operator response to correct the

problem was prompt. However, follow-up as to why the gradual

change in turbine building to atmosphere differential pressure

(d/p) from nep tive to positive was not detected, disclosed

that the control room instrumentation for this d/p was out of

service and the local instrumentation in the turbine building

was not logged and reviewed. The inspector suggested to the

licensee that when control room instrumentation is taken out of

service that compensatory action be taken to log and review

3

readings from local instrumentation. The licensee agreed.

7.

Scram Reduction Task Force

Based, in part, on the above average number'of plant scrams in 1985, the

licensee formed a scram reduction task force to investigate causes of

trips and make recommendations for reducing plant trips.

The task force

issued a document entitled "0yster Creek Scram Experience" (TDR 724).

The

inspectors reviewed this document to ensure the conclusions reached en-

ccmpassed their concern for balance of p' ant impact on the primary side.

The document analyzed all plant trips from January 1976 to December 1985.

There were a total of 35 scrams during this period. The 6 trips experi-

enced in 1985 were only exceeded by the 7 trips in 1979. Of the 6 trips

in 1985, 4 were attributed to equipment failure and 2 were considered

human related. This is in contrast to 1979 when only one was considered

equipment failure and 6. human related. An analysis of all 35 trips indi-

cated 40% of all scrams were due to human related causes while starting up

or shutting down. Twenty-six percent were due-to human related causes

while performing testing or maintenance activities, and the remaining 34%

were due to equipment failure, mostly in balance of plant systems. The

nuclear industry has set a goal of no more than 3 unplanned trips per

i

plant year for plants with greater than 3 years operating experience. The

1

average for BWRs in 1984 was 3.6.

Oyster Creek was shutdown for all but 2

months of 1984 and experienced 2 trips during the 2 months of operation.

The report was generally well done. Recommendationsweremadethatcould

help in reducing the number of reactor trips. The statement was made

that it was too early to determine if a trend existed regarding balance

of plant equipment failures. Only one scram occurred during the first 3

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months of 1986 and it resulted from a balance of plant equipment failure.

The inspectors had anticipated the report would have recommended more

intensive investigation of the potential impact of balance of plant

components on plant operation.

For example, there was no recommendation

to investigate periodic replacement of equipment that interfaces with the

reactor protection system. This was discussed with plant management who

stated that, even though this was not a specific recommendation of the

i

report, it was being reviewed by Plant Materiel as a separate job action.

The inspectors will follow up the review by Plant Materiel in a subsequent

4

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inspection.

8.

Review of Periodic and Special Reports

,

Upon receipt, periodic and special reports submitted by the licensee pur-

suant to Technical Specification requirements were reviewed by the inspec-

tors. This review included the following considerations: the report in-

cludes the information required to be reported to the NRC;

planned

corrective actions are adequate for resolution of identified problems;

and the reported information is valid.

'

The following reports were reviewed:

i

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Monthly Operating Reports for January and February 1986

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Annual Exposure Data Report for 1985

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Second 1985 Semi-Annual Effluent Release Report.

The effluent release report stated there were no releases of radioactive

liquids during the period.

No concerns were identified.

I

9.

Technical Function Division Inspection

The inspectors made two separate visits to the GPUN Corporate Engineering

t

offices in Parsippany, N.J.-during this report period. The first visit

involved meetings with various Tech Functions department managers to gain

,

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an understanding of the organization.

The managers were all very helpful

1

and appeared to have a comprehensive understanding of their department and

~

interfaces with other departments. The spirit of cooperation experienced

during this visit contributed to helping the inspectors gain a rudimentary

4

understanding of the Tech Functions organization.

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The second visit involved a review of the following four modification

packages scheduled for work during the 11R outage:

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.BA 328145 Reactor Head Flange Thermocouples

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BA 402207 Recirculation Valve Interlock

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BA 402775 Diesel Generator Lubrication System

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BA 402786 460V USS 1A2, 182 Transformer Cooling Fans

l

The following Tech Functions procedures were referred to during the

package reviews:

'

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EMP-002, Mini-Mods, Rev. 0-00

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EMP-014, Project Reviews, Rev. 1-01

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EP-008, Control, Evaluation and Resolution of Review Comments

on Technical Documents, Rev. 1-00

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EP-009, Design Verification, Rev. 1-00

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EP-016, Nuclear Safety / Environmental Impact Evaluation, Rev.

I

1-00

--

LP-009, Independent Safety Reviews, Rev. 1-00

The review of the modification packages included the aspects of environ-

mental qualification and fire hazards analysis considerations, proper

design review implementation, proper safety reviews, specification

completeness, establishment of functional criteria, quality assurance

considerations, and adherence to governing procedures. A summary of the

review follows:

9.A The 460V 1A2 and 182 Transformer Cooling Fans (BA 402786) modifica-

tion was initiated as a result of an electrical load study performed

at Oyster Creek. The study determined that the 460 volt 1A2 and 182

4

buses may be overloaded during a loss of coolant accident with off-

site power available and a loss of either IA2 or 182. A licensee

evaluation determined that the transformers' capacity could be in-

creased by adding cooling fans.

This was reported by LER 85-009.

The following documents were reviewed:

--

Procurement Specification SP-1302-11-21R1

--

Purchase Order (Reg. 5350-85-0158-001; P.O. No. PP-027569)

Statement of Justification

--

--

System Design Description I (0C-732A Rev. 0)

(includes 50DII requirements)

--

GPU drawings

Nuclear Safety / Environmental Impact Evaluation (SE 4027862001)

--

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Preliminary Engineering Design Review (PEDR) comments

'

Installation Specification (OCIS 402786-001)

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Fire Hazards Analysis

The following concerns were identified as a result of the review:

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A Memorandum of Concurrence was not submitted by the plant

operations representative to communicate the plant's concurrence

as required by Procedure EMP-014, Project Reviews.

If receipt

of the concurrence memo does not occur within four weeks from

the completion of the PEDR, the project engineer is required to

notify in writing the Plant Vice President and Vice President

Technical Functions that further progress on the specific modi-

fication is terminated pending receipt of plant concurrence.

This was not accomplished.

--

The PEDR chairman for the modification was the Electrical Power

Manager, the responsible manager for this particular modifica-

'

tion. Procedure EMP-014, Project Reviews, requires that the

formal members of the PEDR board, as defined in EMP-14, not be

involved in the engineering or managing the engineering of the

design package being reviewed.

The PEDR was conducted by mail

as allowed by EMP-14, but no distinction is made regarding the

PEDR chairman eligibility if the review is conducted by mail.

EMP-14 was not adhered to regarding the PEDR chairman

eligibility.

--

The Operability / Maintainability /Constructability Review (OMCR)

was conducted on 1/15/86 in accordance with EMP-14.

EMP-14

requires mandatory participation by Plant Operations, Plant

'

Maintenance / Material, Maintenance and Construction (M&C),

Startup and Test, Radiological Engineering, GPUNC Quality

Assurance (QA), and the project and design engineers.

In

'

addition to the project and design engineers the following

organizations were represented: Maintenance and Construction

(contract employee), Startup and Test, and Plant Engineering.

QA was not represented, but did provide written comments after

the meeting. Plant Operations was not directly represented,

although Plant Engineering was in attendance. Plant

Maintenance / Material and Radiological Engineering were not

present.

The PEDR meeting was conducted by issuing the preliminary

--

design package for review and comment in accordance with

EMP-14.

The project engineer received comments from the

following organizations: Plant Operations, Plant Engineering,

and Startup and Test. The preliminary design package received

much wider distribution and Startup and Test, QA Engineering,

System Engineering, MC&F, Planning and Scheduling, Engineering

Projects, BWR licensing, M&C Technical Support, M&C Workload

and Control Support, Engineering and Design, Maintenance

Engineering, Operations Engineering, M&C Planning, Mechanical

Systems, and Quality Assurance and Engineering Configuration.

a

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9.8 The drywell thermocouple modification (BA 328145) was initiated to

improve the drywell temperature sensing capabilities in the reactor

head flange area. Previous thermocouples mounted in this area pro-

vided less than optimum indications as a result of their particular

mounting device. This modification is intended to seismically mount

'

two upgraded thermocouples that will provide accurate drywell temper-

ature readings. The modification was conducted in accordance with

the mini-mod procedure EMP-002 as authorized by a letter from the

Director Engineering and Design dated November 25, 1985. Similar

procurement and design documentation was reviewed for this modifica-

tion as was accomplished for BA 402786.

The following concerns were identified as a result of this review:

.

--

An OMCR meeting was conducted on January. 29, 1986 in accordance

with procedure EMP-014. The following organizations were repre-

sented at the meeting: Plant Engineering, Maintenance and Con-

struction, and the project and design engineers. Although not

present at the meeting, Startup and Test did send a "to comments"

memoranda to the project engineer.

EMP-014 requires mandatory

participation by the organizations delineated in EMP-011. Not

all of the required organizations were represented.

--

The drywell thermocouple modification is being conducted as non-

environmentally qualified (EQ).

The licensee considers the

thermocouples associated with the Gemac reactor vessel water

level reference leg as the required instrumentation to measure

j

drywell atmospheric temperature. The water level reference leg

thermocouples' primary purpose is to provide indication of ref-

erence leg flashing and, therefore, an indication of correct

reactor vessel water level readings. The licensee has conducted

some analysis to indicate that these reference leg thermocouples

could provide drywell atmosphere temperature indication.

Regu-

latory Guide 1.97 requires drywell atmosphere -temperature instru-

mentation to be qualified as category 1 under equipment qualifi-

,

'

cation. The licensee document, TDR 528 requires drywell temper-

ature to be qualified to category 1.

The licensee is in the

process of revising their commitment in TOR 528 by developing a

new document that will require drywell atmosphere temperature to

be qualified to category 2.

TDR 528 (June 1984) was written in

response to Generic Letter 82-33. An order confirming this

commitment was issued in June 1984.

TDR 528 indicated that drywell temperature is a direct indication

of approaching design temperature limits which could lead to

violation of the safety function of preserving primary contain-

4

ment integrity. Also, drywell temperature is an entry condition

to the Emergency Operating' procedures and an action level to

initiate containment spray and scram the reactor. The safety

functions are reactor coolant integrity and containment integrity.

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The licensee's revised document states that the reactor water

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level cold reference leg temperatures are indicative of drywell

temperatures. Due to their locations and post accident drywell

conditions, plant analysis indicates that these thermocouples

are representative of drywell temperature. TDR 528 also indi-

cated that drywell temperature was in compliance with EQ require-

ments and that the licensee planned to upgrade the system during

11R.

In addition, the TDR indicated that a system for measuring

i

drywell bulk temperature did not exist. The environmental quali-

fication requirements for drywell atmosphere . temperature elements

will be clarified in further discussions with the licensee.

This

will remain an unresolved item. (219/86-06-05).

9.C The recirculation valve interlock modification (BA 402207) resulted

from corrective action to address a low low low reactor water level

condition that occurred in May 1979. On 5/2/79 an inadvertent

1

reactor high pressure scram occurred during surveillance of the

isolation condenser high pressure initiation switches. The high

1-

pressure signal inadvertently induced during the surveillance also

caused all 5 recirc pumps to trip. Operator action resulted in

isolation of the five recirc loops which broke the continuity

between the core region and annulus region. Because reactor water

level instrumentation sensors connect to the annulus region, there

was no indication of actual water level in the core until the triple

4

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low level alarm occurred.

(Triple low alarm signal is generated

from different instrument lines that sense water ' level in the core

region.) A licensee investigation determined it is necessary to

maintain a minimum of two recirc loops open to preclude this type of

scenario. This was consistent with Tech Spec requirements which

';

also requires a minimum of two loop operation. The decision was

made to install an interlock scheme to prevent isolating more than 3

3

j

loops. Subsequent to the licensee's investigation, the NRC issued

NUREG-0660 and 0626 that also required this type of an interlock to

i

be installed.

Over 6 years later, corrective action will be implemented during the

11R outage when an alarm will be installed to alert the operators

when the fourth recirc loop is isolated. The replacement of an

!.

interlock scheme to prevent less'than 3 loop operation to an alarm

that activates when the fourth loop is . isolated represents a

i

substantial scope change.' The inspector questioned the licensee

!

about the scope change, alarm logic, and the lengthy delay in

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implementation of the corrective action. The licensee referred to

NRC Licensing correspondence that tracked the changes.and delays,

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The following documents, in addition to others, were reviewed:

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Design Criteria 391-80-3 dated 9/12/80

Engineering Evaluation 391-80-1 dated 7/29/80

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Installation Specification 391-80-4 dated 3/20/81

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Modification Proposal 391-80-2 dated 8/18/81

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Installation Specification 391-80-5 dated 12/10/81

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Request for Project Approval dated 2/14/86

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OMCR Meeting Conference Notes No. 59 dated 10/16/85

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TOR 528, Rev. 1, Oyster Creek Reg Guide 1.97 Implementation

Construction Release Checklist dated 11/4/85

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Installation Specification OCIS-402207-001 dated 11/4/85

--

--

GPUN Drawing E0447, Rev. 2, Elementary Diagram Recirculating

Loop Annunciator Logic

--

Fire Hazards Analysis Input and Status, FPE No. OC-402207-001,

Rev.0, dated 11/5/85

--

Procurement Release Checklists - various

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Purchase Orders - miscellaneous

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Burns and Roe Work Order 3731-46

GPUN Tech Spec for A/E Engineering and Design Services,

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SP-1302-56-082 dated 5/9/85

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System Design Description (SDD) Div. 1 for Recirc Valve

Interlock Modification, SDD OC-6278 dated 8/30/85

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SDD OC-6278, Rev. 2, Div. II dated 9/9/85

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Nuclear Safety / Environmental Impact Evaluation Summary Sheet

for Recirc Valve Interlock Modification, SE No. 402207-001,

dated 9/18/85

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Work Authorization 415A-30207

PEDR Review conducted 8/8/85

--

The documentation file on this modification was quite lengthy based

on the long history. Various correspondence documented licensee

commitments to the NRC to implement an interlock scheme.

It was not

until just before the start of the 11R outage that the licensee

~

received relief from NRC Licensing to change the scope of the

modification. The engineering for the alarm modification was

performed by Burns and Roe.

The following concerns were identified as a result of this review:

The inspector questioned the alarm logic in that it would seem

--

more appropriate to alarm when 3 loops are isolated. This

could prevent isolating a fourth loop.

This would appear to be

more consistent with the requirements in the Tech Specs and the

intent of the original requirement for an interlock that would

prevent isolating a fourth and fifth lonp. The NRC inspector

pursued this concern with NRC Licensing who stated they

reviewed the licensee's logic and found it acceptable.

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Paragraph 6.1 of the System Design Description (SDO) stated a

Class IE surveillance and ISI program for the new relays should

be implemented and should be consistent with the existing pro-

gram for similar Class 1E relays in the Control Room. The in-

spector requested a specific procedure be referenced, if there

is one, or the statement be deleted.

The licensee stated they

interded to delete the-statement.

The inspector requested clarification of a-jumper that appears

--

on drawing E0501 in that it was not clear from either the

drawing or the related documentation whether the jumper was

existing or new. The licensee agreed to state in the SDD that

a jumper must be added as part of the circuit to supply 125VDC

control power to the alarm reflash unit.

--

Similarly, as discussed in paragraphs A and B above, not all

participants required by EMP-014 were in attendance at the

OMCR.

--

Based on certain memos in the file, it became apparent that

Plant Operations was not responsive to the PEDR process in that

they did not attend the PEDR nor did they comment within 4 weeks

as required by EMP-014. The inspectors asked Tech Functions

management if this was a chronic problem and were informed it

had been a problem in the past but had recently improved.

--

The inspectors were concerned about the time delay in

implementing the corrective action to the 5/2/79 event.

--

Other potential concerns were raised during the review and were

satisfactorily addressed by the licensee.

9.0 The Emergency Diesel Generator (EDG) lube oil modification (BA 402775)

resulted from a recommendation by both the NRC in. Circular 79-12 and

the manufacturer, GM-EMD, to accomplish improved lubrication capacity

to the turbo charger and main engine components.

The recommended

modifications are intended to:

--

Eliminate engine bearing potential failure

'

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Reduce maintenance by continual oil replenishment of the oil

cooler and filters to full level regardless of oil temperature

and viscosity

Remove restart restrictions imposed on unit surveillance and.

--

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test schedules

Provide consistent oil circulation through the engine

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crankshaft bearings

Provide consistent circulation through the turbo charger

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bearings

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Vent trapped air which may impede oil flow through the system.

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Oyster Creek is one of the last owners of turbo charged EMD MP45

diesel generators to accomplish this modification. GPUN considers

the modification an improvement and, therefore, not urgent and, there-

fore, the time delay in implementation. The decision to implement

the modification at this time is most likely due to recent problems

experienced with the #10 bearing on the #1 EDG.

The modification

adds an AC and DC lube oil pump, increases some pipe sizes, adds

vents, and adds an improved design lube oil cooler core. The bulk

of the design and installation work has been contracted to Power

Systems with some electrical work contracted to Burns and Roe.

Power

Systems will provide technical direction of installation including

supervision of crafts and labor.

The following documents, in addition to others, were reviewed:

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Tech Functions Work Request (TFWR) A00642 to evaluate and

implement modifications as recommended by GM-EMD

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Croneberger Memo dated 11/19/85, E&D/0C-2426, invoking mini-mod

,

process for this modification

1

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Oyster Creek Installation Specification 402775-001, Rev. 1,

Oyster Creek EDG Lube Oil Modification

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Request for Project Approval

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Engineering Services Project Cost Estimate

Project Scope Checklist

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Short Form Specification, SP 1302-12-217, Rev. 1, Lube Oil

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System Modification Equipment for GM-EMD MP 45 Diesel Generator

Units

PEDR/0MCR scheduling memo date 2/14/86 that scheduled combined

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PEDR/0MCR for 2/21/86

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Memo MC-86-3603 issued 2/24/86 documenting OMCR meeting on

2/21/86

Memo 5511-86-034 issued 3/19/86 documenting PEDR meeting on

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2/21/86

Safety Evaluation No. 402775-001, Rev. 1, dated 1/30/86.

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Subsequently updated on 2/26/86 and 3/17/86.

Power Systems Proposal No. 83751

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Fire Hazards Analysis FPE No. OC-402775-001

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Verification General Checklist V-1302-86-001 signed 2/4/86

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The following concerns were identified as a result of this review:

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The Memo dated 11/19/85 stated that in accordance with paragraph

4.3.7 of EMP-002, the simplified documentation requirements of

EMP-002 would be invoked for this project since it satisfies the

technical requirements outlined in paragraph 4.1.1 of EMP-002.

What this memo basically did was invoke the " mini-mod" procedure

'

which streamlines the method of modification review and approval

by eliminating certain documents and reviews.

The inspector

4

reviewed the EDG Lube Oil Modification and the-mini-mod require-

ments discussed in EMP-002 paragraph 4.1.1 and determined that

this modification does not satisfy the stated technical require-

ments.

In discussions with GPUN Tech Functions management

regarding this discrepancy, it was concluded the Director-

Engineering and Design does not need to meet 4.1.1 requirements

to invoke the mini-mod process.

The licensee committed to revise

the standard memo used to invoke the m.ni-mod process to

eliminate confusion in the future.

l

The Project Sccpe Checklist stated no FSAR revision was

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i

required. A review of the modification package made it quite

clear, as well as did the Safety Evaluation, that a FSAR change

is required. Subsequent to inspector identification of this

discrepancy, the Project Scope Checklist was corrected.

--

Review of Fire Hazards Analysis FPE No. OC-402775-001 disclosed

that it did not evaluate the impact of the addition of the two

<

new motors. Subsequent to inspector identification of this

'

discrepancy, the licensee committed to amend the analysis to

<

include the two additional motors.

4

EMP-014 requires a Memorandum of Concurrence as a vehicle for

--

communicating the plant's concurrence with operability and main-

tainability of modification. A review of the documentation

.

files indicated no Memorandum of Concurrence (M of C) was

1

written. When the inspector pointed this out to the licensee,

he stated he believed that a M of C did exist and it would be

made available to the inspector for review.

Subsequent to this

statement, the licensee stated a M of.C was not required and,

therefore, was not written because the mini-mod process had been

invoked. A review of licensee procedures did not appear to

preclude the need for a M of C, especially in light of the fact

that a PEDR was conducted.

,

EP-008 discusses requirements for Comment . Resolution Forms.

--

These forms are to be used by each organization to transmit

their comments in the PEDR and OMCR review processes. Although

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the Comment Resolution Forms do not become pa'rt of the permanent

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23

plant records (except if PEDR is by mail), a review of the per-

manent and non permanent records indicated most organizations

involved in the PEDR and OMCR review processes had no comments

as evidenced by a lack of Comment Resolution Forms. The inspec-

tors asked the licensee if it was the intent that if a reviewing

organization had no comments they should so indicate on the

Comment Resolution Form and return it.

The licensee stated this

was not a requirement and was not generally done. Based on this

methodology for soliciting comments as part of the PEDR and OMCR

processes, the inspectors could not conclude that participating

organizations are actively taking part in the review process.

--

The controlling procedures for the Tech Functions review pro-

cesses do not specify what constitutes a quorum. The procedures

do require that specific organizations be invited to a PEDR and

mandatory attendance at the OMCR.

Reviews of the attendance

sheet for the combined PEDR/0MCR indicated that participation

was less than required by EMP-014. The inspectors asked the

licensee what constituted a quorum as not all required or in-

vitec participants attend the OMCR and PEDR meetings. The li-

censse stated that there was no quorum and that the chairman of

the meeting was responsible for cancelling the meeting if in-

sufficiently attended. The inspectors asked if a PEDR or 0MCR

meeting had ever been cancelled due to insufficient attendance.

The licensee stated they could not recall this ever happening.

Tha lack of enforcement of procedural requirements per EMP-014

fr.r mandatory attendance and the lack of a definition for a

q;orum, led the inspectors t.o conclude that the PEDR and OMCR

eview processes may not be as comprehensive as intended.

The inspector asked the licensee if, after completion of the EDG

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Lube Oil Modification, the lube oil system would be flushed.

The licensee stated they do not intend to flush the system but

will rely on Dermar,ent system filters to remove particulate left

from the construction activity.

Procedures LP-009 and EP-016 direct that the Responsible Techni-

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cal Review (RTR) be completed before the Safety Evaluation (SE)

is performed.

In the case of the EDG Lube Oil Mod, it appears

there were two RTRs -- one before and one after the SE.

The

reason for sequencing the SE after the'RTR is to provide a total

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picture to the individual doing the SE. The-procedures do not

address updating the SE if a RTR held af terwards results in

comments.

Procedure LP-009 states that revisions to SEs are not

appropriate.

It is not clear what constitutes a revision, but

it wo.ild seem appropriate that if a RTR held after the SE

resulted in comments, that the individual who performed the SE

would be informed to determine if there was any impact on his SE.

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This was not accomplished for this med in that the first RTR and

the SE were dated nearly three weeks before the second RTR (PEDR)

and there was no evidence of a subsequent SE by the reviewer.

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The above concerns contain examples of failure of the licensee to follow

procedures.

In summary the licensee failed to:

(1) Follow the requirements of EMP-014 by not issuing a M of C in

two of the four packages reviewed.

(2) Assign a PEDR chairman who was independent of the engineering

or managing of the design package as required by EMP-014 for

the transformer fan cooling modification.

(3) Enforce the mandatory attendance requirements for the OMCR as

required by EMP-014.

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(4) Properly schedule the RTR prior to the SE as required by LP-009

and EP-016 for the EDG Lube Oil Modification.

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These four examples of failure to follow procedures are contrary to the

requirements of Criterion V of 10 CFR 50 Appendix B and represent a

single violation.

(219/86-06-06)

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The inspectors were also concerned with the substantial time delay between

identification of the need for a modification and final implementation.

Although the licensee appears convinced that the delays are unavoidable,

the fact remains that six years would appear excessive.

The synergistic effects of a group review of modifications is obviously

appreciated and intended as demonstrated by the procedural requirements

governing the process. However, the lack of total participation would

seem to detract from the licensee's goal.

10. Management Meeting

A nanagement meeting was held to discuss the present status of work as-

sociated with IE Bulletin 79-02 and 79-14 on April 1, 1986 in the NRC

Regional office. GPUN Technical Functions Division presented information

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providing the status of 79-02 and 79-14, schedule and plans for future

work to be conducted, and analysis regarding current system operability.

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The licensee stated they had deleted the requirement from their inspection

program to determine as found torque on concrete expansion' anchor bolts.

The licensee is going to submit meeting minutes to the regional office for

Concurrence.

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11. Observation of Physical Security

During daily tours, the inspectors verified access controls were in

accordance with the Security Plan, security posts were properly manned,

protected area gates were locked or guarded, and isolation zones were

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.free of obstructions.

The inspectors examined vital area access points

to verify that they were properly locked or guarded and that access

control was in accordance with the Security Plan.

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A portion of the security system was taken out of service because of an

equipment malfunction. Although compensatory measures were taken, they

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were not in accordance with Security Plan requirements. The discrepancy

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was self-identified by the licensee a short time later and corrected.

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After identification of the problem, a search of various areas of the

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plant was conducted to ensure no security breeches occurred. The inspec-

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tors reviewed licensee response to the event and corrective action to

preclude recurrence. No concerns were identified.

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During this report period, the licensee implemented a drug and alcohol

control program.

It is based on a random sampling technique for most

employees and a 100% check on certain critical employees.

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12. -Unusual Event: Bomb Threat

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At 4:35pm on March 24, 1986 the plant telephone operator reported receiving

a bomb threat on an outside line.

The licensee declared an Unusual Event

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at 4:54pm and responded appropriately in accordance with their procedures.

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A search of the site and plant spaces was completed prior to ending the

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Unusual Event.

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13.

Briefings

During this inspection period, the resident inspectors attended briefings

on the following topics:

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Powershape Monitoring system-

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Quality Assurance Annual Review

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Inservice Inspection schedule for cycle 11 refueling outage

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Work Management System

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The inspectors found the briefings to be informative.

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14. Exit Interview

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A summary of the results of the inspection activities performed during

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this report period were made at meetings with senior licensee management

at the end of the inspection. ..The licensee stated that, of the subjects

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dhscussedattheexitintervf'ew,noproprietaryinformationwasincluded.

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During the telephone exit with, Technical Functions, the licensee indicated

that he might be able to provide additional information.or documentation

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to alleviate some of the concerns in Detail 9.

Upon receiving no ad-

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ditional documentation or pertinent information af.er ten days, the inspec-

tor' reconfirmed to the licensee the disposition of the findings.

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