ML20150E462
| ML20150E462 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 06/15/1988 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20150E457 | List: |
| References | |
| 50-333-86-99, NUDOCS 8807150154 | |
| Download: ML20150E462 (54) | |
See also: IR 05000333/1986099
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ENCLOSURE
SALP BOARD REPORT
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
INSPECTION REPORT NO. 50-333/86-99
NEW YORK POWER AUTHORITY
JAMES A. FITZPATRICK NUCLEAR POWER PLANT
ASSESSMENT PERIOD: December 1, 1986 to April 30, 1988
BOARD MEETING DATE: June 15, 1988
8807150154 880707
DR
ADOCK 050
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TABLE OF CONTENTS
Page
I.
INTRODUCTION ....................................................
1
A.
Purpose and Overview .......................................
1
B.
SALP Board Members .........................................
1
II.
CRITERIA
2
.......................................................
III. SUMMARY OF RESULTS .............. ...............................
4
A.
Overall Facility Evaluation ................................
4
.
B.
Background .................................................
6
C.
Facility Performance Analysis Summary ...................
8
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D.
Unplanned Shutdowns, Plant Trips, and Forced Outages . . . . . .
9
IV.
PERFORMANCE ANALYSIS ..................... .....................
12
A.
O p e r a t i o n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
12
8.
Radiological Controls and Chemistry .......................
15
C.
Maintenance ...............................................
19
0.
Surveillance..............................................22
E.
Engineering and Technical Support .... .... ............ ..
25
F.
Security and Safeguards ............................... ...
28
G.
Emergency Preparedness ...................... .............
30
H.
Licensing .... ............. ......... ....................
32
1.
Assurance of Quality .......................... ...........
35
V.
SUPPORTING DATA AND SUMMARIES .. . ................ ... ........
39
A.
Investigations and A legations Summary .....
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39
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B.
Escalated Enforcement Actions .......
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39
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C.
Management Conferences ............
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TABLES
Tabl e 1 - In spec tion Hours Summa ry . . . . . . . . . . . . . . . . . . . . . . . . . ...
40
Table 2 - Enforcement Summary
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Table 3 - Licensee Event Reports
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I.
INTRODUCTION
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A.
Purpose and Overview
The Systematic Assessment of Licensee Performance (SALP) is an integrated
NRC staff effort to collect the available obsorvations and data on a
periodic basis and to evaluate licensee performance based upon this
information.
SALP is supplemental to normal regulatory processes used to
ensure compliance with NRC rules and regulations.
SALP is intended to be
sufficiently diagnostic to provide meaningful guidance to the licensee's
management to promote quality and safety of plant construction and
operation.
An NRC SALP Board, composed of the staff members listed below, met on June
.15, 1988, to review the collection of performance observations and data to
assess the licensee performance in accordance with the guidance in NRC
Manual Chapter DS16, "Systematic Assessment of Licensee Performance." A
summary of the guidance and evaluation criteria is provided in Section II
of this report.
B.
SALP Board Members
Board Chairman
W. Kane, Director, Division of Reactor Projects
Membey
H. Abelson, Project Manager JAF, NRR
R. Capra, Director, Project Directorate No. I-1, NRR
J. Durr, Chief, Engineering Branch, DRS
J. Johnson, Chief, Projects Section 2C, DRP
W. Johnston, Acting Director, Division of Reactor Safety, DRS
A. Luptak, Senior Resident Inspector, James A. FitzPatrick, DRP
M. Shanbaky, Acting Chief, Facilities Radiological Safety and Safeguards
Branch, DRSS
E. Wenzinger, Chief, Reactor Projects Branch 2, DRP
Attendees
N. Blumberg, Chief, Operational Programs Section, DRS
T. Dragoun, Senior Radiation Specialist, DRSS
G. Hunegs, Resident Inspector, Indian Poin
3, DRP
R. Keimig, Chief, Safeguards Section, DRSS
W. Lazarus, Chief, Emergency Preparedness Sec', ion, DRSS
R. Plasse, Resident Inspector, James A. FitzPatrick, DRP
W. Thomas, Radiation Specialist, DRSS
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II.
CRITERIA
Licensee performance is. assessed in selected functional areas, depending on
whether the facility is in a construction, preoperational, or operating
phase.
Functional areas normally represent areas significant to nuclear
safety and the environment, and are normal programmatic areas.
Special
areas may be added to highlight significent observations.
One or more of the following evaluation criteria were used to assess each
functional area.
1.
Management involvement and control in assuring quality.
2.
Approach to resolution of technical issues from a safety standpoint.
3.
Responsiveness to NRC initiatives.
4.
Enforcement history.
5.
Operational and Construction events (including response to, analysis
of, and corrective actions for).
6.
Staffing (including management).
7.
Training effectiveness and qualification.
Based upon the SALP Board assessment, each functional area evaluated is
classified into one of the three performance categories. The definitions
of these performance categories are:
Category 1 Reduced NRC attention may be appropriate.
Licensee management
attention and involvement are aggressive and oriented toward nuclear
safety; licensee resources are ample and effectively used so that a high
level of performance with respect to operational safety and construction
quality is being achieved.
Category 2 NRC attention should be maintained at normal levels.
Licensee
management attention and involvement are evident and are concerned with
nuclear safety; licensee resources are adequate and reasonably effective so
that satisfactory performance with respect to operational safety and
construction quality is being achieved.
Category 3 Both NRC and licensee attention should be increased.
Licensee
management attention or involvement is acceptable and considers nuclear
safety, but weaknesses are evident; licensee resources appear to be
strained or not effectively used so that minimally satisfactory performance
with respect to operational safety and construction quality is being
achieved.
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The SALP Board has also assessed each functional area to compare the
licensee's performance near the.end of the assessment period to that during
the entire period in order to determine the recent trend for functional
areas as appropriate.
The trend categories used by the SALP Board are as
follows:
Improving:
Licensee performance was determined to be improving near the
close of the assessment period.
Declining:
Licensee performance was determined to be declining near the
close of the assessment period.
A trend is assigned only when, in opinion of the SALP Board, the trend is
significant enough to be considered indicative of a like'y change in the
performance category in the near future.
For example, a classification of
"Category 2, Improving" indicates the clear potential for "Category 1"
performance in the next SALP period.
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III. SUMMARY OF RESULTS
A.
Overall Facility Evaluation
The FitzPatrick facility continues to be operated in a conservative and
safety conscious manner.
The site and corporate management have
demonstrated their commitment to plant safety and reliability through the
resources and programs directed at plant improvements.
These include new
training facilities, a new plant computer system, a corporate engineering
reorganization, and preventive maintenance programs.
Throughout the plant
staff, there exists a strong dedication, pride in ownership, and
accountability for performance.
Plant operations continues to be a strength.
The lack of operator errors
and the absence of plant trips caused by operators as well as a small
number of lit annunciators is indicative of the safety perspective and
conscientious approach taken by operators. The efforts to improve control
room decorum and professionalism are noteworthy.
In the radiation protection and chemistry areas significant program
improvements were noted this period.
Following an extremity overexposure
event early in the period (attributed to radiological program weaknesses),
program oversight and adherence to procedures showed marked improvement.
Program strengths noted were in the areas of respiratory protection and
training.
In the maintenance area licensee efforts to implement vendor manual updates
and a preventive maintenance program are showing slow progress.
Continued
emphasis for timely implementation is necessary.
Increased attention is
needed to improve work practices and procedural adherence in the maintenance
area.
The surveillance program satisfactorily implements a large number of test
requirements to assure reliable equipment operation. Weaknesses continue
to be noted in the administration of testing programs.
In particular, the
administrative controls for the Inservice Testing Program were found to be
deficient due to limited staffing and lack of management attention.
In the area of engineering supoort, limited staffing and lack of
coordination of engineering efforts have caused inconsistent performance.
Although actions have been taken to correct some of these deficiencies,
continued management attention is required.
The licensee continues to implement a strong and effective security
program.
The licensee's Emergency Preparedness continues to be of high
quality; however, weaknesses identified in the areas of audits and
protective action recommendations indicate a need for increased in manage-
ment attention.
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In the licensing area, significant improvements.have been noted. Manage-
ment-involvement has increased in this area and an improved attitude of
cooperation was noted.
Increased attention is required to correct long
- standing deficiencies in the plant's Technical Specifications and assuring
consistent technical quality of submittals.
A positive worker attitude and strong management commitment towards
assuring quality have maintained the FitzPatrick facility on a positive
performance trend. Principal areas which require increased attention are
engineering support, correcting discrepancies in Technical Specifications,
and emphasis in the area of procedural control and adherence
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B.
Background
1.
Licensee Activities
The licensee began the assessment period with the facility operating at 90%
power, conducting an end of_ cycle power coastdown. On January 15, 1987,
the plant was shut down for a scheduled three month refueling outage, which
lasted until April 22, 1987. During this outage, the licensee removed the
recirculation loop discharge bypass lines, replaced the residual heat
removal-reactor water cleanup tee connection, replaced 6 neutron monitoring
instrument dry tubes, replaced 18 power range neutron monitors, and
replaced 20 control rod blades.
Following testing, a plant startup
commenced April 22, 1987.
The plant returned to power operation on April
30, 1987.
From the refueling outage until the next scheduled maintenance outage,
normal power operation was interrupted by 6 unscheduled outages, lasting
between one and four days.
The plant also operated at reduced power during
various periods due to equipment problems, low condenser vacuum, and
restrictions while operating with 3 out of 4 main steam lines. On June 10,
1987, the reactor tripped from 100% power due to the loss of 'A'
reactor
feed pump. On July 10, 1987, power was reduced to near 70% to investigate
the 'A' reactor feedpump control circu't and returned to full power on July
12, 1987.
From July 13 - July 31, 1987, the plant operated at reduced
power (95-98%) due to vacuum restraints caused by high lake temperatures.
From August 1 - August 7,1987, the plant operated near 75*; due to the
availability of only 3 of the 4 main steam lines, due to a slow closing
time on one main steam isolation valve.
Power was raised to 88*; on August
7,1987, following analysis of 3 steam line operation. After approval of
an emergency Technical Specification Amendment, the plant returned to
normal 4 steam line operation on August 20, 1987, and subsequently returned
to full power operation.
On August 28, 1987, the reactor tripped following
a turbine trip due to a generator load reject caused by a generator field
ground fault. On September 7, 1987, the reactor tripped following a
turbine trip due to a generator load reject, similar to the August 28
event. On September 24, 1987, the reactor tripped due to a loss of the
'A'
reactor feed pump.
The plant restarted and operated near 60's power while
troubleshooting the 'A' feedpump and returned to full power operation on
October 11, 1987.
On November 5, 1987, the plant reduced power to near 60%
to allow repair to 'B' reactor feed pump.
In the process of increasing
power af ter completion of the repair, the reactor tripped from 80*4 power on
November 8, 1987.
The trip was due to a recirculation pump speed
controller failure. On December 9,1987, the reactor tripped from 100*;
power due to a false low reactor vessel level indication caused by
personnel error during surveillance testing.
The facility was shutdown from January 9, 1988, until January 23, 1988, for
a scheduled maintenance outage.
Major work accomplished during this outage
involved replacement of sixteen control rod drive mechanisms, inspection of
the torus coating, recirculation scoop tube modifications, and preventive
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maintenance on electrical equipment.
During the subsequent startup on
January 23, 1988, a drywell inspection at 500 psig reactor pressure noted
leakage from a reactor water cleanup (RWCU) system weld. The plant was
shut down, the RWCU system weld was satisfactorily repaired, and another
reactor startup was conducted January 26, 1988.
The plant was operated at
near full power ~throughout the remainder of the assessment period with a
reduction in power to near 60% from March 14 - March 18, 1987, to allow
repairs to 'B' reactor feed pump.
Section III.D provides a description (including NRC classification) of the
cause of all reactor trips and unscheduled plant shutdowns during this
assessment period.
2.
Inspection Activities
An NRC senior resident inspector was assigned for the entire assessment
period; an additional resident inspector was assigned in December 1987.
During a 17 month assessment period, the NRC expended a total of 3143
inspection hours equating to 2219 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.443295e-4 months <br /> on an annual basis.
Functional
area distribution of inspection hours is documented at the beginning of
each individual functional area.
During the period, three NRC team inspections were conducted in the
following areas:
a.
Health Physics Appraisal
b.
Environmental Qualification
c.
Design Change / Modification, Maintenance, and QA/QC
An NRC team also evaluated a routine, unannounced, full participation
emergency exercise performed on December 15, 1987.
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C.
Facility Performance Analysis Summary
Last Period Dates:
12/1/85 - 11/30/86
Present' Period Dates:
12/1/86 - 4/30/88
Category Last
Category This
Recent
Functional Area
Period
Perted
Trend
1.
Plant Operations
2, Improving
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Radiological Controls
2
2
3.
Maintenance
2
2
4.
Surveillance
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Engineering and Technical
2
2
Support **
6.
Security and Safeguards
1
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7.
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Declining
8.
Training and Qualification
2
N/A
Effectiveness *
9.
Licensing Activities
2, Declining
2
Improving
10. Assurance of Quality
2, Improving
2
Improving
During the previous assessment period, training and qualificaion were
discussed under a separate functional area.
During this a,sessment period,
training will be evaluated in the appropriate functional areas and will not
be considered as a separate area.
During the previous assessment period, this area combined Outage Management
and Engineering Support and was considered as a separate functional area.
During this assessment period, Outage Management will be evaluated in the
Maintenance functional area, and Engineering and Technical Support will be
evaluated as a separate functional area.
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D.
Unplanned Shutdowns, Plant Tr-
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forced Outages
Power
Functional
No.
Date
level
Description
Lause
Area
1.
06/10/87
100%
Equipment Failure /:
Engineering
due to reactor
Design Problem
Support
vessel low
Reactor Feed Pump
level.
(RFP) A tripped
(LER 87-08)
due to a seal
failure while
operating with the
scoop tube
positioners
locked up.
06/10/87
Startup
2.
08/28/87
100%
Initially Unknown:
N/A
due to turbine
Troubleshooting ar.d
trip caused by
discussion with
generator field
vendor could not
ground fault,
determine cause.
(LER 87-12)
Following second
event on 9/7, the
phenomena discussed
below was determined
to be the cause. The
ground was present
only when the
generator was on-line.
08/31/87
Startup
3.
09/07/87
100%
Equipment Failure:
N/A
due to turbine
A deposition of
trip caused by
material on the
generator field
teflon insulation
ground fault,
tube of the exciter
(LER 87-12)
rectifier bank for
the turbine
generator resulted
in a ground fault.
09/11/87
Startup
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UNPLANNED SHUTOOWNS, PLANT TRIPS AND FORCED OUTAGES
Power
Functional
No.
Date
Level
Description
Cause
Area
4.
09/24/87
100%
Equipment Failure /:
Engineering
due to reactor
_ Design Problem
Support
vessel low
Reactor Feed Pump
level.
(RFP) A tripped due
(LER 87-17)
to high vibration
while operating with
the scoop tube
positioners locked up.
09/25/87
Startup
5.
11/08/87
80%
Equipment Failure:
N/A
due to Average
High flux trip
Power Range
was initiated by
Monitor (APRM)
a sudden Reactor
.
High Flux Trip.
Water Recirculation
(LER 87-18)
System Pump speed
increase caused by
a random failure
in the pump speed
controller.
11/09/87
Startup
6.
12/09/87
100%
Reactor trip due Personnel Error:
Surveillance
to a reactor
While performing
vessel low
surveillance test
level signal.
I&C Technician
(LER 87-20)
trainee did not
fully close
reactor water
level inst:* ment
isolation valve,
resulting in a
false reactor water
Inw level transient.
12/10/87
Startup
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UNPLANNED SHUTDOWNS, PLANT TRIPS AND FORCED OUTAGES
Power
Functional
No.
Date
Level Description
Cause
Area
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01/23/88
0%
During a startup
Equipment Failure:
Engineering
from a scheduled
Installation
Support
maintenance outage deficiencies (within Construction
a leaking weld on
code requirements)
the Reactor Water
plus cyclic stresses
Cleanup System was were determined to
found requiring a
have caused a crack
plant shutdown to
in the weld.
repair.
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IV. PERFORHANCE ANALYSIS
A.
Operations (1001 hours0.0116 days <br />0.278 hours <br />0.00166 weeks <br />3.808805e-4 months <br />, 31.8%)
1.
Analysis
During the previous assessment period, this functional area was rated as
Category 2, improving. A marked improvement was noted in the plant
operations with no significant personnel errors occurring during the period
and two reactor trips from power. Other improvements were made in the area
of control room professionalism and event critiques.
Poor performance on
past replacement operator licensing exams was attributed to poor screening.
In addition, weaknesses were noted in the administration of the
requalification program; however, this did not adversely affect plant
operations.
Plant operations have continued to be a strength.
The operations staff
continues to exhibit a safe and conservative approach to plant operations.
Management attention is highly evident and control room operators continue
to demonstrate professionalism and dedication in the conduct of their
duties.
These are evidenced by the absence of plant transients caused by
operations personnel and the conscientious approach taken during plant
startups and other evolutions.
During this assessment, improvements continue to be made in this functional
area.
Policies have been implemented to require formalized pre-shift
briefings. Organization and control of work activities continue to be
improved through better operation of the Work Control Center, which
includes a computerized tagging system.
Changes to the control room, based
on the Control Room Design Review, were implemented to improve the control
room from a human factors standpoint.
These changes included new label
plates for all equipment, which standardized the labeling and nomenclature;
improved mimicking and demarkation of systems; and new annunciator windows,
which incorporate standard nomenclature and format.
These changes have
standardized the control room and have given it a more professional
appearance. A commendable effort to reduce the number of continuously
lighted annunciators in the control room has resulted in having normally 3
or 4 continually lit (out of a total of 800) in the control room. These
initiatives are indicative of the licensee's management commitment to
improving plant operations.
None of the scrams which occurred during this period were caused by plant
operators.
It was determined that the operators' actions to attempt to
prevent scrams due to equipment malfunction were timely and correct.
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Operators' actions during other operational events were also timely,
effective, and correct.
During the previous period, procedures and procedural adherence were noted
as being generally strong with minor exceptions that required plant
management attention. Although improvements have been - de, isolated cases
of inadequate procedures or lack of procedural compliar.e were noted.
Two
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examples involved a failure to follow procedures during radioactive liquid
f
discharge and an inadequate procedure resulting in a recirculation pump
trip during testing. Continued emphasis in this area is warranted by plant
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management.
The operations departmont, is staffed to its full complement, with a six
shift rotation; there has been a low staff turnover rate.
The operations
staff works closely with other departments in recognizing, troubleshooting,
and correcting deficiencies. A strong interface between departments
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provides for more efficient operations and good communications.
In
addition, operations personnel take active roles in the review of
modifications, implementation of inservice testing, and improvements in
training. Strong management involvement is evident throughout plant
operations. Mcnagers are involved in day-to-day operations, as well as
plant problems.
Examples of management irvolvement include the
identification of an unauthorized discharge during a log review and
on-shif t coverage during high activity periods, such as plant starbG
following maintecance outages.
During this appraisal period, LERs in general adequately described the
major aspects of each event, failures contributing to the event, and the
corrective actions to prevent recurrence.
The reports were thorough,
detailed, and easy to understand.
Sufficient details were givan to provide
a good understanding of the event,
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The licensee's review and corrective actions related to operational events
were generally thorough and adequate to prevent recurrence.
In particular,
the licensee displayed aggressive and conservative actions to test safety
relief valves following notification of a concern at another boiling water
reactor. Detailed reviews and troubleshooting were conducted following an
unusual main generator ground fault problem which included an extensive
startup testing phase to assure the cause had been identified following a
second trip. Additionally, a detailed review was conducted following
identification of a reactor water cleanup system weld leak to determine
possible causes or other cracks.
However, isolated examples of insufficient review or corrective actions
were noted.
These involved the failure to fully determine the cause of a
main steam isolation valve closure which occurred while the plant was shut
down and ineffective corrective action to prevent a repeat of an emergency
diesel generator actuatien during tra.isfer of house loads.
During this assessment period, improvements continued in the t aining area.
A new training complex was nearly completed at the end of this assessnent
period. A rigorous program for simulator verification is in progress.
In
addition, the licenset is incorporating recent detailed control room design
review improvements, made to the main control room, into the simulator
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during construction. The delivery of the simulator is scheduled for the
summer of 1988. An NRC requalification examination was administered to 10
operators to evaluate the requalification program based on previous
,
weaknesses.
Six out of seven Senior Reactor Operators and one out of three
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Reactor Operators passedLtheir respective requalification written
examinations. All six Senior Reactor Operators and two out of three
Reactor Operators passed their respective requalification operating
examinations. Based on the NRC criteria, the licensee requalification
program is' considered marginal, having six cut of ten operators pass all
portions of the examination.
No generic weaknesses were identified. The
licensee implemented corrective actions to address the specific
deficiencies identified during the examination.
The good.operatirig record
of the plant.is indicative of an effective requalification program.
One Fire Protection inspection was conducted during this SALP period. The
licensee's Fire Protection program, including administrative controls, fire
brigade organization, staff training, and surveillance and maintenance of
Fire Protection equipment were found satisfactory. Associated records were
well organized and were easily retrievable.
Licensee audits of the station
Fire Protection activities were conducted by trained and qualified
individuals.
Concerns identified in the aud'.s were properly dispositioned
in a timely manner.
Housekeeping and material condition, in general, was considered above
average.
Plant cleanliness was very good; however, equipment storage,
scaffolding control, and control of equipment deors and covers were noted
as needing improvement.
In summary, plant operations continue to be a strength. Operations
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personnel are knowledgeable, dedicated, and highiy motivated toward safe
operations.
Licensee management promotes a safety conscious attitude and
accountability for performance.
They are committed to improving plant
performance as demonstrated by the importance placed in new training
ficilities and by improvements made to the ccntrol room.
2.
Conclusion
Rating:
1
3.
Board Recommendations
None
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'B.
Ra'diolog'ical Control's and Chemistry (504 hours0.00583 days <br />0.14 hours <br />8.333333e-4 weeks <br />1.91772e-4 months <br />,'16.0%)
1.~
Anal sis
.Durin'itha' previous SALP assessment period,' the radiological controls area
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'was rated as Category 2.-
Weaknesses included delayed responses to NRC
findings 'and lack of management attention relative toJconforming to
radiation protection. pro.cedures.
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During(thisassessmentperiod,onehealthphysicsappraisal'andthree
routine inspections were conducted.
Resident inspectors reviewed this area
t
on a' continuing basis.
Three' violations related to locked high radiation
area controls and audits.were cited.
In addition five violations related
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to an extremity overexposure were cited.
Ra'diation Protection
Program weaknesses f aentified during the previous assessment period
continued to exist and impacted performance during the early part of this
assessment period.
The licensee's inadequate supervision of radiation
protection activities'during the.beginning of this assessment period may
have ontributt:d'to 'several instances of personnel failing to follow
-procedures, and the extremtty overexposure of-an empioyee. .This
overexposure occurred when a worker threw a piece of highly irradiated
material back into the spent fuel pool when it was inadvertently remond
during cutting of. instrument dry tubes.
Immediate program improvements
were noted in this' area after the overexposure incident.
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Th'e' radiological protection program is staffed with qualified. personnel.
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Previous problems associated with the lack of an health physics general
. supervisor were corrected near the beginning of thir assessment period by
-the appointment of.a well qualified and knowledgeable individual to this
position.
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The -licensee has shown increased responsiveness to NRC concerns during this
. ass _essment period.
Programmatic and equipment weaknesses identified in NRC
inspection reports early in the assessment period were generally resolved
by the end of the~ assessment period.
A' notable exception _ continues to be
the radiological survey instrument controls and calibration facility.
Although the facility is adequate to support normal plant operation, it is
severely taxed during outage conditions.
During this assessment period the individual f;isking units located within
the radiation controlled area were removed from service due to concerns
~
expressed by NRC i.nspectors concerning high background count rates in the
frisker areas. These were replaced with seven IPM-7 complete personnel
, contamination monitoring systens installed at the access control points.
These monitors are state-of-the-art instruments arm should facilitate
detection of personnel contami.iation.
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radiological and environmental services personnel was found to'be very
-good. An initial . training program.has been established for all personnel
-
and a continuing training program has been established for. radiological and
Lenvironmental. technicians. ?These. training' programs'have received'INPO
.
. accredi tation'-duringithi s l period.
LThe ALARA' program is well_ organi.
with good management support and
represents a program. strength.
A_.AA reviews of planned work,. completed
work, and continuous _ exposure evaluation of work in progress are good.
,
Major projects that are in place or planned which will reduce. exposure
>
include. source term reduction through a complete primary system
.
, decontamination, installation of. removable. lagging, use of.high radiation
area video mapping, use of a drywell closed. circuit television system, and
use of_'~a tele-dose monitoring system.
During the course of two inspections
during this assessment period, the ALARA program was examined and found to
be of consistently good quality.
TheD11censee's ALARA person-rem exposure goal for the site was 950
person-rem for'1987,:a refueling year. Actual exposure accumulated was 940
person-rem which continues to be high. Although the ALARA section.was'able
to. plan and control many jobs well, inspectors observed instances of
non productive work involving the very large contracted work force.
For
example, approximately 25 personnel were. observed standing at the refuel
,
-guard ' rail in a 25 mr/hr area and watching the decontamination of the-
cavity.. Also', controls of work involving exposure were lax during the
refueling outage (i.e. contamination of personnel during cavity
decontamination, unmarked containers with radioactive material contributing
to personnel- unplanned exposure, and poor radiological controls of dry tube
cutting operation). .However, exposure goals for 1988 and beyond indicate a
<
much more aggressive' approach to ALARA. By 1990, the licensee's goal is
500 perso'n-rem for a three year average.
This is ambitious considering the
age and h.istory of the plant.
.The program for external and internal exposure control, after the
over-exposure incident, reflects an increased commitment to safety.
'
Following the over-exposure event, increased attention has been placed on
strict adherence to radiation work procedures and radiation work permits.
The respiratory protection program continues to be of high quality.
It is
apparent that the licensee has placed a high priority on this program as
evidenced by effective respirator selection, training, issue, use, and
-maintenance practices.
Licensee quality assurance audits of the radiation erotection program were
found to be technically sound and thorough.
The NRC identified one
deficiency regarding the lack of audits of the qualifications of radiation
protection supervisors below the level of the Radiological and
Environmental Services Superintendent, which was promptly corrected.
Audit
findings were resolved in a timely manner.
, . . _ . . .
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17
..
Chemistry / Radiochemistry
An extensive plant chemistry upgrade program was noted during the
assessment period indicating a management commitment to improve performance
.in this area. Corporate involvement in, and support for, the program were
clearly evident. Technically sound and thorough approaches to improve
sampling and measurement capabilities, introduction of hydrogen water
chemistry and monitoring for control of intergranular stress corrosion
cracking demonstrated a clear understanding of the issues.
Chemistry
staffing at the facility was adequate, fully cognizant of their duties and
responsibilities, and knowledgeable of the licensee's sampling and analyses
procedures.
State-of-the-art analytical capabilit,es were provided.
Analytical capability intercomparisons showed the licensee's analyses to be
adequate with all results within agreement of NRC values.
Technicians
demonstrated both theoretical and practical knowledge of the operation of
the equipment while attempting to resolve disagreements with NRC
measurements. Adequate radiochemical capabilities were demonstrated by the
licensee during a measurements intercomparison with NRC-supplied
radioactivity standards.
Radioactive Waste Management
The licensee's radioactive waste management program was generally adequate.
The liquid and gaseous waste systems meet 10 CFR 50, Appendix I design
objectives but the ' censee takes a more conservative approach treating all
liquid waste before release and requiring the offgas treatment system to be
operational virtually at all times when the plant is operating.
The
licensee has adequate procedures for handling and discharging liquid and
gaseous effluents.
Procedures address, as appropriate, valve line-ups,
sampling and analys's, alarm and isolation setpoints and tracking of
releases to ensure compliance with technical specification limits. In
response to self-identified weaknesses, the licensee has initiated a
-program to improve the Offsite Dose Calculation Manual and related
,
procedures to better address the Radiological Effluent Technical
i
Specifications.
Summary
Several radiological program weaknesses noted early in this assessment
period may have contributed to an extremity overexposure of a worker.
However, significant program improvements in the areas of program oversight
and adherence to procedures were later achieved during this assessment
period.
Increased responsiveness to NRC concerns, a good radiation
protection training and qualification program, and further improvements in
the ALARA program were noted.
Supervisory staffing levels were appropriate
to ensure program oversight and effective implementation.
Subsequent to
the extremity overexposure incident, there exists an increased commitment
to safety and strict adherence to radiation work permits and procedures.
i
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18
Programs for the control o' plant chemistry and radioactive wastes are
effective and indicate' strong site and corporate management support for
these two programs,
2.
Conclusion
Rating:
2
3.
Board Recommendation
None
.
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C.
Maintenance (571 hours0.00661 days <br />0.159 hours <br />9.441138e-4 weeks <br />2.172655e-4 months <br />, 18l2%)~
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-During'the. previous assessment period, the maintenance functionalLarea was
rated as Category 2.
Improvements were noted in this area withLthe absence
of personnel errors and proficiency in properly completing work. . Progress
.was generally good in implementing improvement: programs.
Procedural
compliance 'and root cause analysis were areas where attention.was :
. +
warranted.
~*
~
The area of outage management was combined with engineering support during
.the previous assessment period.
This area was rated as Category 2.with
improvements noted in the planning'and managing of two short outages (24
days total). During this assessment period, outage management and
maintenance are-addressed under one functional area.
During this period, three routine inspections were conducted covering
activities assor.iated with outage maintenance.
In addition,throughout the
assessment period, the resident inspector frequently reviewed' activities in
this area.
The licensee continued to make progress implementing the extensive'
improvement programs already begun. Although progress.is slow, the scope
and thoroughness of the programs and large volume of information needed
makes this a difficult task. The Master Equipment List (MEL) was completed
during this. period, and is the first key to the comprehensive preventive
maintenance program.
The licensee gathered all pertinent data
(manufacturer, drawings, nameplate) and assigned safety classification
(including basis) for 36,000 components. The next significant portion of
the program begun was the determination of preventive maintenance
requirements. As part.of this effort, the licensee began a program to'
'
validate all of the vendor-technical manuals.
This effort is designed to
ensure that the licensee's technical manuals are up to date with the
~
- vendor's latest revision and any other information, plus gather information
i
concerning recommended maintenance. spare parts, and drawings.
In 1983 (Generic Letter 83-28), the NRC requested that all licensee's
upgrade or confirm their MEL and validate their vendor supplied
information, including the appropriate technical manuals.
The NYPA efforts
described above, although slow and indicative of limited resources, are
responsive to these issues.
The licensee is committed to completing the
update of vendor manuals by December 1988.
During this period, maintenance personnel continued to exhibit a good
safety perspective concerning the potential impact of their activities on
plant operation. This is evidenced by the absence o' plant transients or
equipment failures attributed to personnel error during maintenance.
Maintenance personnel generally exhibit pride and professionalism in the
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conduct of their activities. Management involvement in and control of the
.
quality. of maintenance was evident by adequate planning and prioritization
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of maintenance activitiesLincluding ample QA/QC coverage for these
activities. .'Individua_l-responsibilities and authorities are well~ defined.
- for control'of Jaaintenance' activities. . Maintenance. staffing is. adequate
'
to perform _the existing work load, with a very low turnover rate. :During-
the 1987 refueling o_utage, three maintenance supervisors, thirty-four craft
/pers'onnel, and' containment integrated. leak rate testing consultants were
,
added to support the maintenance activities'.
Generally, maintenance personnel conduct work: activities in a quality
manner, as noted during replacement of an emergency diesel generator
turbocharger,' calibration-of instrumentation, and during the generator
ground l troubleshooting. .However, several examples of. poor workmanship or
practices.were'noted.- These involved inadequate troubleshooting.which-
failed to recognize a low. control oil pressure and corrective maintenance
which damaged ~a valve operating cylinder of a High Pressure Coolant
' Injection system,. insufficient testing of_ reactor :ooca switch in all modes,
failure to tighten fasteners for a Limitorque valve operator switch-
component,:and continuing' maintenance problems for reactor feed pumps.
Although these are considered isolated occurrences, they indicate'a need
for more effective supervision. -In addition, although the licensee's
program implementation for control of measuring and test equipment is
generally, satisfactory, three instances of not recording test instrument
usage were-found. Although some improvement in procedural adherence was
observed,'centinued emphasis should be placed in this area.
Two examples
of_ inattention to procedures were noted during Standby Liquid Control pump
'
maintehance involving system tagout recommendations and inattention to the
' expiration date.of the procedure.
During this pericd, a refueling outage of 105 days and a planned outage for
plant maintenance of 14 days were conducted. This was the first refueling
outage under the recently established Planning and Contract Services
Department and Work Control Center.
Improvements were evident in the
_ planning, -scheduling, and control of activities under these newly-
-established programs. Work progressed smoothly and problems were
effectively communicated and resolved.
The_ licensee took prompt corrective
action following an overexposure incident on the refuel floor, and
conducted extensive analysis and review of a missing Control Rod Blade
-roller guide ball, and the failure of bolts in the High Pressure Coolant
Injection Turbine.
During the 1987 refueling outage, it was observed that the licensee made a
-concerted effort to produce quality welds by training welders in the use of
the automatic welding equipment.
However, review of other welding
activities indicated poor judgment or lack of technical support for not
properly evaluating the adequacy of the welding requirements involving
dissimilar metal joints.
This is indicative of a need for more supervisory
oversight in this area.
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21
Improvements continue to be made in training of personnel.
Benefits from
implementation of'the four year apprentice training program are, in
general, evident in the conduct of work activities.
The licensee
effectively utilizes mock-ups of equipment in training personnel.
INP0
accreditation was received in December 1987 for the maintenance training
program. Management's commitment to improvements in performance is-
evidenced by the emphasis placed in the training of personnel.
In summary, the maintenance program is adequately staffed with well-trained
and experienced personnel.
Slow, steady progress is being made on a very
comprehensive maintenance program, although continued emphasis is required
to ensure timely completion. Management attention should be focused on
improving supervisory oversight to ensure proper workmanship and procedural
compliance.
2.
Conclusion
Rating:
2
3.
Board Recommendations
Licensee: Expedite upgrading the preventive maintenance program
including validation of vendor nanuals.
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22
D.
Surveillance (406 hours0.0047 days <br />0.113 hours <br />6.712963e-4 weeks <br />1.54483e-4 months <br />, 12.9%)
1.
Analysis
During the previous assessment period, this functional area was rated as
Category 2.
A strength noted was the lack of personnel errors during
testing.
Improvements were noted in the procedures which fall under the
inservice testing (IST) program, including providing for a thorough review
of data by the operator and the addition of the acceptable values. However
review of data by plant performance personnel was, at times, excessively
slow.
Increased management attention was warranted in the area of program
administration, as evidenced by three missed surveillance tests.
During the current assessment period, inspections were conducted in the
areas of containment local leak rate testing (LLRT), containment integrated
leak rate testing (CILRT), and inservice testing of pumps and valves. The
resident inspectors reviewed routine surveillance activities regularly.
The licensee surveillance program is, in general, technically adequate and
sufficiently controlled. Each department is responsible for scheduling,
tracking, and performing their own surveillance testing. Approximately
5000 surveillance tests were completed during this assessment period.
The
scheduling and tracking of surveillance tests utilizes computerized
systems.
Procedures generally are clearly written and sufficiently
detailed for effective implementation.
One reactor scram and three Engineered Safety Feature (ESF) actuations
occurred while conducting surveillance testing during this assessment
period.
The cause of the scram was mainly due to personnel error in that
an instrument isolation valve was not tightly shut.
Following shutting of
the valve by the technician trainee, a very small amount of valve movement
(approximately 1/16th of a turn) was found by a supervisor, during initial
l
review of the scram. During followup investigation of the trip, this
occurrence was verified.
Contributing to this event is the fact that these
valves are original plant equipment and require a slightly larger amount of
torque to fully close, due to years of operation.
Two of the three ESF
actuations were reactor core isolation cooling system isolations; both
involved personnel error.
The third ESF actuation involved a core spray
system and emergency diesel generator start during integrated leak rate
testing; this occurred due to a procedural inadequacy involving lifted
In addition, isolated cases were identified, by the NRC, where
surveillance test procedures were in error or confusing. These were
promptly corrected by the licensee.
In general, operators and technicians
readily identify and correct surveillance test inadequacies during
l
performance of testing activities.
I
Training of Instrument and Control (I&C) Technicians, who are involved in a
large portion of the surveillance testing, is considered to be a strength
as indicated by the small number of plant transients or equipment failures
l
caused by surveillance testing.
Improvements were made in this area
!
throughout the assessment period.
Implementation of the four year
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' apprentice,' training program has' improved the' technicians overall
pe rformance .' Except asinoted above, the I&C department on-the-job training
for'te_chnicians involved in surveillance' testing assures personnel are
adequately. trained prior to becoming responsible for. conducting testing,
Plant management';s'. increased attention'and emphasis on training indicate a
,
commitment-to improved! performance.
>
During the previous assessment period, three surveillance tests were missed
.or late; two of which~were missed due to surveillance test scheduling
~
. inadequacies.
Following these missed surveillances,'the licensee took
prompt action to. strengthen their administrative controls through increased
audits and improved tracking programs.
In this period, two Technical
<
.
Specification surveillance test requirements were identified by the
licensee as being missed.
These surveillance test problems were of little
or no safety significance.
One involved the failure to calculate d ywell
leak rate during one four-hour period. This' occurred while the plant was.
..
shut down preparing for.a reactor startup.and instrumentation was operating
12 '
.to detect'any abnormal leak rate.
The second missed surveillance test was
a TS required. test of the standby gas treatment system during secondary
leak rate te'sts-(normally once per cycle). This requirement had been
overlooked and had never been scheduled at the plant because these tests
have also been performed on a six month interval as required. Although
'
these two examples of missed surveillance tests occurred,.overall
improvement in' the scheduling and tracking of required surveillance tests
was noted.
Administrative controls for LLRT were good. Positive aspects of this
control included individual acceptance criteria for valves, good record
keeping of LLRT results, and a good tracking system for valve maintenance.
Management involvoment and control of LLRT activities, and response to NRC
concerns and initiatives were satisfactory, which was reflected through the
licensee's effective performance.of the control rod drive removal hatch
seal test and LLRT.
However, it was observed that, although the QA
personnel had conducted LLRT'surveillances,-no evaluation of the LLRT
program was performed.
The licensee recognized the concern and instituted
an LLRT effectiveness audit.
In the area of CILRT, the licensee's technical staff demonstrated good
knowledge and competency in CILRT methodology and test performance.
The
licensee hired a CILRT consultant who collected test data, analyzed the
test results and provided technical assistance.
The progress of CILRT
preparation and execution were discussed daily by the licensee management
and technical staff.
However, administrative control of the test and its
related activities appeared weak in some areas. The test director did not
have complete control over test preparation or containment access prior to
the test.
The operations and I&C departments worked independently of the
test director and he was not apprised of the status of such preparations as
CILRT sensor installation and operability, and valve lineup.
In one
instance, the I&C department accessed the containment to check a dewcell
and upon exiting could not secure the equalization valves properly.
This
led to large leakage during pressurization.
This lack of adainistrative
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' pressurization for the test'when incorrect leadswere lifted which actuated'
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emergency diesel generators land the core spray system.-
.
.
7
1
During the previous period,.the review of. data by"plant? performance
personnel following. the t'est was,' at times, excessively slow.
Administrative controls have adequately addressed this concern, however,
continued' ineffective control and: implementation _.of the.IST program
indicate poor' management oversight of the program.
Lack of proper
~
allocation ofiresources,-including _ staffing, and' lack of attention to
details and review of.the test activities.were' identified.
Test
documentation and corrective action were also inadequate. . Two specific
concerns were' identified:'(1) failure to follow IST procedures,-and (2)
failure to verify and document -the acceptability of. the new High Pressure
Coolant' Injection pump reference data, per ASME Section XI.
These
..
instances-indicated inconsistency in data recording and general program
implementation,'which were attributable to the lack of formal-methodology
to generate and retain test data, and inattention to details by the
-cognizant-test reviewer. -Many of the IST-program implementation related
changesLwere made on-the-spot without appropriate safety committee review
and attention to details. This contributed to lack of reference to
differential pressure -in the test program, -lack of incorporation of ' Alert-
-and Required Action values in the test reports, and existence of various
transposition errors in the; test reports, including stroke times, valve
designation, and white-out of test data. These deficiencies indicate a
lack of management attention to the IST program.
In summary, the licensee continues to implement an adequate surveillance
^
program. Although improvements have been made in some areas, weaknesses
continue in program administration.
These are noted by inadequate staffing
in.the IST program area and deficiencies in the management involvement and
' administrative control of the IST and CILRT programs.
Personnel are well
qualified :and conscientious;-however, continued emphasis needs to be placed-
in. procedural control and adherence.
2.
Conclusion
Rating:
2
3.
Board Recommendation
Licensee:
Review IST program and evaluate reasons for continued
ineffectiveness in program administrations.
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E.
Engineering and Technical Support (323 hours0.00374 days <br />0.0897 hours <br />5.340608e-4 weeks <br />1.229015e-4 months <br />, 10.3%)
'
'1.
Analysis
t
This area was notfevaluated as a. separate functional area in the previous
v
-assessment,'but was discussed under the functional area-of Outage.
.
Management and Engineering ~Suppor.t.. In the. previous period, this area was
..
rated-as_a~ Category 2.
Although the engineering support group generally
. performed well in. assuring technical. adequacy of modifications,. several
'
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inadequacies noted-required-the need-for increased management attention.
DuringLthis assessment period, this functional-area addresses the adequacy
of' technical and engineering support for all plant activities, including
design of plant modifications and engineering support for operations,
outages, maintenance, and surveillance.
The angineering; support evaluation for this period is based on four
o -
inspections which covered the licensee's Equipment Qualification (EQ)
-
- progra..i. implementation, evaluation of the pipe supports per NRC Bulletin 79-14, plant de' sign changes and modification activities, and drawing
control activities. .In addition, the resident inspector reviewed this area-
throughout the assessment period.
,
The plant technical services department is responsible for reviewing and
designing modifications,; resolving plant engineering problems,
- administering the-EQ program, and supplying engineering support as needed.
The major modifications installed in the plant for most of this period were
originated and controlled from the utility's corporate office in White
Plains, New York. .In addition, an Operations and Maintenance Support group
located in the corporate office assists in providing engineering support to
the fa ility.
During this assessment period, the performance in this area was
inconsistent.
The-technical services department continues to be staffed
with dedicated, knowledgeable, and industrious personnel. This department
is actively involved in significant improvement programs, wSich include the
(Master Equipment List, procurement programs, motor operated valve
performance enhancement, and development and implementation of new design
change control program procedures from a corporate level.
The engineering
support organization demonstrates the ability to adequately control major
modifications, complete minor plant modifications, and provide support on
.an as-needed basis.
Examples of timely and effective completion of
modifications include: installation of the new plant computer system and
piping removal and replacement.
In addition, numerous modifications in the
radioactive waste systems and main control room (recorders and
. instrumentation) were effectively implemented.
In support of plant
problems, noteworthy performance was demonstrated in review of operation
with 3 of 4 steam. lines, analysis of a reactor water cleanup system cracked
weld, and follow up and analysis of plant trips and transients.
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'However, ins'tances:where the licensee's: design and engineering were not
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, properly reviewed a'nd-coordinated and. analyses which lacked depth or proper-
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documentation were'also noted- , Numerous deficiencies were noted in the
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modification-to. upgrade the automatic.depressurization. system pneumati.c
'
supply, tExamples where the flicensee's ' analysis or documentatjon lacked -
,
Jdetails' included determining' effects on the residual heat removal system
2
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components.due to missing check valve internals, documenting the test
'
,
pressure of a hydrostatic test of the core . spray. system, and analysis of
p
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pitting:on the. core spray system-piping.
-In addition, some 'l'ong-standing engineering problems have been slow to be
4
resolved.' In.particular, a problem with the recirculation pump speed ~
control circuit contributed to 2 scrams during this period.
This problem
has. existed since 1979; several fixes were attempted since that time,
_
- howeser, they had been unsuccessful.
In September, 1986, an engineering
. review, which made.use of'information from other sites, identified a
'3 ,.
modification to correct-the problem. This modification was in2talled in
January-1988 and has corrected the speed control problem.
In Jan'uary'1988,.a, licensee reorganization took place to strengthen the
engineering organization.
Portions of the previous Engineering and Design
group were placed under the nuclear generation department.
This change was
made so-that all activities, including engineering, will fall under the
cognizance'of one-department and are intended to improve communications,
management,- and control of the activities at the_ nuclear facilities.
In
,
addition, a new field engineering group was added at_ the FitzPatrick site
'
which reports to the corporate office.
Their role is to assist in the
- engineering of major plant modificat' ions which originate from the corporate
' office. . This group is staffed with 4 engineers, who previously worked for
the plant's. technical services department and 4' contractor engineers; it
provides the interface'and work area for engineers from the corporate
office during their site visits.
Their main function is to review and
assist in major modifications and provide an interface with the plant,
assuring the modifications accurately reflect the as-built plant and input
any operating experience.
This group!s efforts has allowed the technical
services engineers to focus their efforts in supporting minor modifications
and day-to-day support of plant activities.
.The EQ inspection identified a lack of active site management involvement
to address and resolve EQ issues.
In addition, limited staffing and
expertise were available to properly review, evaluate and comply with the
EQ requirements in a timely fashion. The technical service department,
.which has the responsibility for the EQ program, astigned three
individuals, including the department supervisor, to establish and
implement the EQ program and maintain station equipment qualification
within the guidelines of 10 CFR 50.49.
Several concerns were identified.
The licensee could not establish qualification of several EQ related
.
components prior to the November 30, 1985 deadline, and did not provide an
caerability statement (justification for continued operation).
The
licensee relied heavily on consultants to respond to the NRC concerns; EQ
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files;chnsisted.~of the consultant's review of specific EQ components.
This
_
-resulted inJa lack of self-sufficiency'and an~ inability to resolve the
plant-specific EQ concerns on their own.
'
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In the area of drawing control, improvements have been noted in reducing
.the backlog .of drawings, awaiting update,to final as-built conditions.
However,. examples of drawings not y'et updated where the modifications had
'been completed over.two years ago still exist. Additionally,, minor
discrepancies-are continuing to be identified in the. control of drawings.
'
.Although. improvements have been made and discrepancies found are-of minor
significance, continued attentionLis warranted in-the control of drawings.
In. summary, station engineering support has been adequate.
Deficiencies
have been noted in the quality of modification packages; however, the
e
corporate management has takaa measures to improve:the communication and
control of engineering fro.i the' corporate level .
From the site engineering
group,-performance has been inconsistent; this appears to be due to heavy,
workload of on-site. engineers. . Efforts 1should be continued to improve the
. effectiveness of1the engineering support organization.
-
2.
. Conclusion
Rating:
2
3.
Board-Recommandations
Licensee: Eval 6 ate the adequacy and use of site staff in the
engineering support arsa to ensure a high level of
performance.
no
NRC:
Perform followup inspection of EQ-program open issues
including the licensee oversight of the program.
J
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'
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_ . _ _
_
_
__ ._
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4
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,
4
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,
F.
Security ' and ~ Safeguards' (126 hours0.00146 days <br />0.035 hours <br />2.083333e-4 weeks <br />4.7943e-5 months <br />, 4.0%)'
_
1.
Analysis-
c
During the, previous'SALP, the licensee's performance in this area was
' Category l'. . That rating was influenced by the licensee's responsiveness'to
NRC concerns,. initiatives to review the effectiveness-of the program,
1
?
acquisitions;of' state-of-the-art systems and equipment, and' continued
support for the program'from corporate and site management.-
c
During this assessment period, two routine. unannounced physical security
'in.pections were condu'cted.
Routine inspections by-the resident inspector
continued throughout the. period.
One violation was identified during the
period.
Corporate security. management continued to be actively involved in all site
security program-matters, including visits to the site by the corporate
staff.to provide assistance, program appraisals and direct support in the
budgeting and planning processes affecting program modifications, upgrades
- and program plan' changes.
Security management personnel are also actively
involved-in the Region I Nuclear Security Association and other industry
groups engaged in nuclear plant. security matters. This demonstrates
program support from upper level management.
- As in past SALP periods,'the licensee continues to utilize a self-appraisal
program which is independent of NRC's required annual security program
review. This licensee initiative. allows management to identify potential
problems early and take action to prevent their occurrence.
This program,
combined.with the licensee's annual program review, is a contributing
factor in the success of the program and reflects management's commitment
to a .high quality and effective program. ' The annual review of the security
program, performed by the licensee's quality assurance group, was made more
comprehensive in scope and depth than previous reviews at the licensee's
initiative; it placed more emphasis on the detailed requirements of the NRC
approved Security, Contingency, and Training and Qualifications Plans.
Corrective actions on deficiencies identified during the annual reviews
were prompt and effective with adequate follow-up to ensure their proper
,
implementation.
There were no security events that required reporting under 10 CFR 73.71
.during the assessment period. Review of the licensee's event reporting
procedures found them consistent with the NRC'; revised regulation (10 CFR
- 73.71) and implemented by personnel knowledgeable of the reporting
requirements.
As during the previous SALP periods, management and training of the
proprietary security force continued to be effective, as evidenced by a low
personnel error rate, low turnover rate, high morale and a professional
- attitude toward job performance by members of the security force.
Staffing
of the security management organization and the security force is adequate
as indicated by the limited use of overtime.
The security force training
.-
. ..
. . ~ . - -
. -
,. . . . - . - . -
- , - - - - - - . - ,,
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- p
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.
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-
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a'nd requalification program is well developed.and effectively administered.
'
This is apparent from the excellent jobLknowledge' demonstrated by members!
..
of,the security: force during interviews:by NRC personnel.
In addition to
20
theiinitial and requalification training, a self-appraisal prog' ram measures
,the retention and ~ proficiency. of individuals with regards to generaliand;
,
46
- specific:securi+vLprogram requirements between-qualification periods.
,
'
I
lThe licens~ee also conducted numerous' Safeguards Contingency-PlanLdrills
,
during. this~ assessment. period to exercise members of the security force in
emergency' procedures, however there was very little_ indication of
participation from.the operations organization'. :When'this was brought to
the. licensee's attention, plans were promptly made' to' conduct joint-drills -
'
for' contingency events.
During the period when a vital area door was found in an unlocked condition
by the NRC, immediate. compensatory measures were taken and the corrective-
' actions.were' prompt and extensive.
Even though, in the case cited, the
-
dete: tion aid was still operable,-the1 licensee took the initiative to
,
change'all'vitalEarea door locks to a type that will prevent recurrence of-
F
.the problem. - This is' further evidence of the licensee's desire to
11mplement and maintain an effective high quality security program.
,
There were four revisions to the licensee's security. program plans
submitted ~toLthe NRC under 10 CFR 50.54(p) during this assessment period.
The' plan changes were clear'and concise, with detailed ' explanations of the
< .
-reasons.for change._ This is indicative of knowledgeable' personnel and
adequate management oversight of submittals~to the NRC.
,
'In. summary,'the . licensee continues to manage and implement a security
program that is effective and goes_beyond regulatory requirements and
.
^
- -
security plan commitments. Licensee initiatives, responsiveness to NRC
concerns, and support for the program were readily apparent during the
' assessment period and combined to provide evidence of a high quality
program.
'2.-Conclusion:
Rating:
1
3. Board Recommendation:
o
None
i
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-
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-
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30
)
' i '
'G.
Emergency Preparedness (212 hours0.00245 days <br />0.0589 hours <br />3.505291e-4 weeks <br />8.0666e-5 months <br />, 6.8%)-
1.D Analysis
E
~
'
Ouring the previous assessment period, the' licensee was rated Category 1 in
this area,; based on information. gathered during observation of a partial
' parti.cipation exercise,. review of the. Emergency Preparedness (EP) training
program, and support of off-site emergency activities.
During this assessment period, the e were two unannounced, routine, safety
inspections and observations of the annual _ exercise. 'Ouring the.
. inspections,-it was noted that Emergency Response Facilities (ERFs) were
.
adequately maintained and Emergency Preparedness procedures, equipment,
.
f~
training and training records were current. About 85% of the 550 full
'
~
time, on site NYPA-personnel are qualified for one or more of the emergency
' response organization' positions.
Three or four full activation drills.are
conducted annually in addition to a number of partial activation drills.
During requalification' training, licensed operators are given eight
a
_ classroom hours of EP instruction, plus another eight hours on simulator.
The effectiven'ess of this training was demonstrated by the results of
twalk-throughs with licensed, senior < operators qualified as Emergency
Of rectors (ED). These' operators were well trained and capable of
'
' discharging ED responsibilities correctly.
-
Communications and computer systems were functional. The Safety Parameter
Display Systems (SPOS) was installed and used during the last exercise. A
-
/
new, dedicated Emergency Operations Facility (E0F) was' built, having an
a ea of about 2500 square feet, and is located beyond the ten mile
Emergency Planning Zone (EPZ).
NRC review of the findings of independent reviews / audits required by 10 CFR 50;54(t) disclosed that EP. personnel gave the auditors their exercise
observation ' assignments 'and tracked their findings, which is contrary to
.the requirement for independence of the auditor. Additionally, the
auditors reviewed off-site interfaces for adequacy but failed to notify the
County of results until this was called to their attention by the NRC.
~
'
- During this assessment period, the' licensee reduced staffing support in the
EP area by one technical position. The site emergency planning coordinator
is supported by one professional and one administrative assistant. This
reduction'has the potential to negatively impact performance and
coordination in this area.
Observations of an unannounced, off-rormal hours, ful', participation,
-
exercise indicated that, although the licensee could implement the
emergency plan and implementing procedures adequately, performance was not
as strong as in previous exercises.
Observations indicated protective
action recommendations (PARS) were sometimes in error, or reviewed after
transmittal to the State and County.
This is attributed to a lack of
leadership within the Health Physics group at the Emergency Operations
! 5
.
.
.
31
Facility (E0F). Otherwise, there was good command and control as well as
communication within and among Emergency Response Facilities (ERFs).
activation was timely.
Emergency worker doses were well controlled.
In summary, while the licensee maintains commitments to Emergency
Preparedness resulting in an adequate program, weaknesses identified above
indicate a reduction in management attention to this area.
2.
Conclusion
Rating: 1
Trend:
Declining
3.
Board Recommendations:
Licensee: Improve administration of protective action recommendations
including dose assessment.
-__
x
.'
T
'
f
- N'
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32
'
H".'
LICENSING
,
1.
Analysis'
In the previous SALP assessment, a Category 2 rating with a declining trend
~
,
,
-
swas given to;this functional area.
Communications and spirit of
~
cooperation with the NRC were noted.as the principal-areas where licensee
'
improvement was needed.
1
'
During the current assessment' period, a more active participation on the
part of corporate. management has been evident in the area of licensing.
Management has been cognizant of_the status and priorities of current.and
anticipated licensing actions, both licensee-initiated.and NRC-initiated,
'
and utilizes an expanded, automated commitment tracking system to assist in
their' oversight. JAdditionally, there has been increased communication
during this-period between the licensee and NRC at the corporate
Vice-President level concerning licensing activities.
In December 1986,_
-
the licensee completely revised its procedure concerning the preparation,
review, and control of submittals to the NRC. As a result, the licensing
< '
staff has _been given increased authority to assign . work to other
organizations and to better control its adequacy and timeliness. Also,
under a.recent management reorganization, the engineering and design
function ~ for FitzPatrick has been assigned to the Nuclear Generation
Department. As a result, resolution of problems occurring between the
1
s
licensing. staff and the engineering / design staff, which previously needed
to be handled interdepartmentally, is now simplified,
t
- In the previous SALP evaluation, it was _ noted that corporate and station
.
. management had not directed sufficient attention toward correcting e'rrors
and upgrading some confusing sections of Technical Specifications (TS).
During.the current SALP period, no significant progress has been made in
this area. - Although a large number of TS errors were identified by the
licensee early in the rating period, an amendment request to eliminate
these errors has_not yet been submitted. A majority of the errors are
- typographical in nature; however, there are several cases where TS' are
ambiguous, inconsistent, or have wording which does not clearly reflect
'their intent. Though none of the identified problems, per se, represents a
-
-direct or immediate_ safety concern, this situation may complicate the
day-to-day implementation of the TS by operating personnel.
During this
~
assessment period, examples of inadequate TS concerning minimum Emergency
-Core and Containment Cooling System availability while shut down,
- conflicting TS in the case of spiral offload, and inattention to TS
,
surveillance requirements involving standby gas treatment system were also
'
' identified.
In addition, several longstanding inadequacies including the
TS table concerning containment isolation valves and containment integrated
leak rate test acceptance criteria continue to go uncorrected.
Although in the final few months of this rating period, the level of
activity devoted to rectifying this situation has increased, these problems
demonstrate a lack of sensitivity to the accuracy and clarity of TS from a
licensing standpoint.
However, the plant operating staff has been
attentive in implementing TS requirements.
,
.:.:, ,
-
, .-.
. - - , -
. . . . - - . .
. . _ - , - , , . . . - . . . - . , - _ _ - - .. - -_-.,
.
.
.
33
A second area where additional management attention is needed is in
assuring consistency in the technical quality of licensing submittals
Evaluation of the licensee's approach to the resolution of the technical
issues, as related to licensing _ activities, is based on an assessment cf
the technical quality of various licensing documents submitted, as well as
on the licensee's priorities for scheduling these submittals.
During the
current rating period, variability in the technical quality.of licensing
submittals has been evident.
For the most part, the licensee has presented
clear and substantive descriptions and evaluations of the relevant issues,
thus minimizing the need for requests for additional information and
resubmittals.
Examples of high quality submittals include the reload TS
amendment request and the Intergranular Granular Stress Corrosion Cracking
(IGSCC) evaluations submitted in support of the 1987 refueling outage.
In certain instances, however, the licensee has not provided adequate
technical justification to suoport its position.
System / component
reliability data, based on pl&nt operating history, which would have
clarified the licensee's arguments, were not utilized.
Examples are the TS
regarding operability of the control room emergency filtration system, and
the responses concerning the recirculation pump trip aspect of the
anticipated transient without scram (ATWS) rule.
Additionally, there were
several cases where weak justification was provided far the licensee's no
significant hazards determinations. An example of this is the analysis
submitted as part of the amendment request regarding license conditions for
handling nuclear material. With respect to setting priorities for
resolving safety-significant issues, the licensee's performance has been
satisfactory overall .
Notwithstanding the need for increased attention to TS improvement and
assuring the technical quality of submittals, licensee management has
exhibited a greater involvement in managing and directing licensing
activities during this rating period than in the past.
In the past three SALP evaluations, it was noted that improved performance
was sought concerning the licensee's responsiveness to NRC initiatives.
During the current rating period, the licensing staff has exhibited notable
improvement in its cooperation with the NRC. As a result, there have been
fewer impediments to conducting day-to-day business.
The licensee has
shown a greater willingness to provide schedules for licensing submittals,
has kept the staff better informed on the progress of various activities,
and has responded to requests for information in a more timely manner.
1
Additionally, submittals required to support refueling outages or other
major activities have, in general, been timely and have been discussed with
the NRC in advance.
There have been isolated cases, however, where
submittals were significantly delayed.
A case in point is the additional
information required to support an amendment request regarding containment
purge / vent valves.
Staffing levels for the licensing group are adequate and have remained
,
l
constant (at nine persons) from the beginning of the rating period until
L
l
.
_
..
.
.
.
.. - - - - - - -
s
.
.
"
34
January 1988, when one engineering position became vacant following a
reorganization. The licensee plans to fill this position in the near
future.
Presently, the entire licensing staff is situated at headquarters.
Ccmmunications between the licensing staff and the plant appear strong,
with frequent project meetings held on site and a morning conference call
held daily.
During this rating period, adequate resources have been allocated to
training of the licer. sing group.
In addition to annual requalification
training, ALARA training, computer software training, and training in
writing and communications, certain members of the licensing staff received
more specialized technical training. This included a 3-day Probabilistic
Risk Assessment course, a one-week simulator course, and EQ training.
In
addition, during the last refueling outage, two licensing engineers were
sent to the site for a two-month period to assist in refueling operations.
In summary, during this rating period, licensee management has demonstrated
a more active involvement in-licensing activities and generally.
satisfactory performance in resolving technical issues.
In addition, the
licensing group is adequately staf fed and trained and has exhibited an
improved attitude of cooperation with the NRC. Additional management
attention, however, should be directed toward TS improvement and assuring
consistent hlgh quality submittals.
2.
Conclusion
Rating: 2
Trend:
Improving
3.
Board Recommendations
None
!
I
_ _ - _ _ _ _ _ _
-
h
4
s
..
35
.
'
.I h
Assurance of Quality
~ 1) Analysis
hssurance of Quality is a summary assessment of management oversight and
effectiveness in_ implementation of the-quality-assurance program and
administrative controls affecting quality. This functional. area Lis not an
assessment:of the quality assuranr- M artment alone, but is an overall
- evaluation of the_ licensee's_ initiatives, programs, and policies which
'
~ ffect or assure quality.
It also~ assesses the attitude and performance of
a
plant staff personnel.
'
This functional area was rated as Category 2, improving, during the.
previous assessment period.
Strengths noted were the active role of the
Quality Assurance Department in assuring quality at the facility and the
aggressive attitude _ displayed by plant management in improving the quality
at the_' facility. ' Weaknesses noted were the slowness in implementing
- "
programs and corrective actions, and lapses in the requalification training
program, root.cause~ analysis, and procedural adherence.
,-
Various aspects of this area were routinely reviewed as part of the NRC
routira inspections.
In addition, an NRC team inspection assessed the
effecti.veness of the licensee's quality verification activities.
The
licensee has maintained a high emphasis on quality throughout all levels.of
J
~~
the organization.
This is exemplified by the plant management's continuing
efforts to improve communications throughout the site organization.
Efforts. include: meetings with all station personnel- to discuss plant and
industry problems and promote a_quali.ty conscious attitude; training
sessions for all station-personnel which have improved overall radiological
practices; implementing an employee feedback program; and conducting
routine meetings between supervisors and department staff. Although
additional attention needs to be focused in some areas (as noted in the
s
particular- furctional areas) and isolated problems occur, an excellent
worker attitude and approach to performance of duties is evident by the
lack of personnel errors.
Corporate and plant management continue to strive for excellence and foster
improvement in performance throughout the organization.
For example, more
n equent and better quality critiques of events are being performed with
more worker involvement in the critique. Approximately 30 individual plant
goals have been set with these goals extending over a 3 year period to
track long term improvement.
Individual tasks have been developed to help
achieve these goals. Many of these goals are tracked on a monthly basis
with some posted for all personnel to review.
The above actions are aimed
at making long lasting improvements through increasing the awareness and
pride of ownership through each individual.
Management has also demonstrated their commitment towards plant improvement
in other areas.
The completion of a new training complex, including plant
specific simulator, installation of a new plant computer, reduction of the
number of lit control room annunciators, implementation of Hydrogen Water
.
4
.
a
'
36
Chemistry program, significant efforts to detect and mitigate IGSCC,
equipment upgrade for local leak rate improvements, motor operated valve
performance enhancement programs, improvement in the procurement area, and
planned construction of a new warehouse and maintenance facilities are
examples of this commitment.
Reorganization of the corporate engineering
staff is indicative of management's active role in identifying and taking
action to correct weaknesses.
Progress, .although slow, has been noted on some of the licensee's long term
improvement programs.
In particular, the Master Equipment List has been
completed and training conducted on use of the computerized system, and the
vendor manual validation program has begun. Although these are
longstanding concerns, the licensee is following an extensive and detailed
planned maintenance program approach.
This approach includes developing
detailed procedures for establishing component classification, closely
monitoring of the vendor to assure the desired product is achieved, and
conducting extensive material history reviews and equipment reliability
studies to formulate a preventive maintenance schedules.
The licensee is
expending a large amount of effort to ensure the job is done right the
first time to assure a quality product with long term benefits.
Management involvement has also been demonstrated by increasing the effort
to get supervisors into the plant, providing oversight by assigning
management coverage of outage activities and plant startups, and
implementing lessons learned, throughout the organization, from an
overexposure incident.
The Plant Operations Review Committee (PORC) continues to take an active
role in reviewing plant events and safety evaluations.
Noteworthy
performance was identified during review of the personnel overexposure,
generator field ground problems, and the reactor water cleanup system
cracked weld.
Safety evaluations for plant modifications were found to
adequately address the basis for determining whether an unreviewed safety
question existed.
However, two examples were noted where a formal safety
evaluation was not written for changes made to the facility.
In these
examples the PORC had considered the safety impact of the changes made.
The site quality assurance (QA) organization has continued to play an
active role in assuring quality at the plant.
The QA department has
established open lines of communications with plant management and all
levels of the plant staff and interacts daily with these individuals.
During regional based inspections, management support to assure quality in
the area of inspection and examination was found to be satisfactory.
This
was evidenced by the addition of contracted QC personnel who more than
tripled the site QC staffs.
In addition to the regular QC inspection, the
licensee has introduced another level of OC overview, monitoring of
safety-related activities.
The QC overview was further enhanced by an
on going update of the QA audit program. A liberal use of technical
specialists is a noteworthy feature of this audit program.
l
l
-.
-
J ;
3
7;
a
37
j
t,
O
The licens'ee's warehouse controls and conditions are satisfactory.
The'
l
enveloping of other than. large items in a porous transparent wrap is an
example 1of the licensee's action to improve quality of' storage.
~
,_
'
Concurrently,.the procurement-has also improved as evidenced by'
strengthened. controls.
The requirements, as established in.the source
documents such as FSAR, the plant Technical Specifications, and industry
standards, are~. incorporated-in the procurement document.
-In the, area;of LLRT-and CILRT, QA/QC interfaces have been good. .A
Q
-provided extensive coverage of the test program, including preparation,
. initiation and. performance of the tests. The test personnel and QA
individuals were knowledgeable of test methodology and demonstrated
conscientious, efforts _to complete the test professionally. The QA
department communicated effectively with the cognizant test groups to
resolve QA findings, including general procedural compliance and tagging of
, the containment isolation vains.
The above are f riicative of an improvement in the licensee's QA/QC
interfaces in th areas'of audits, inspection, and testing.
.0verall, the' site.and co porate management is doing an effective job of
identifying and correc'.ing problems and programmatic weaknesses as
,
t
described above. As discussed in each of the appropriate functional areas,
attention is' warranted in improving performance.in the review of and
corrective actions for events, improvements of Technical Specifications,
and: surveillance program administration. _In t ;dition, efforts should
4
.
continue to be placed in resolving long stanu ng problems'and concerns,
such as NRC open -items, and the implementation of minor plant
modifications.
A professional' and conscienticus attitude is displayed by all members of
the plant staff.
Free and open communications are encouraged with outside
organizations, including the NRC.
The licensee takes a very self-critical
and conservative approach towards their activities and performance.
This
,
was demonstrated by testing of Safety Relief Valves, on their own
initiative, following problems identified at another facility and the
E.
prompt and extensive corrective actions following the overexposure
incident.
In stmmary, there exists a sensitivity to Assurance of Quality throughout
management and plant staff personnel of the FitzPatrick facility.
The
management has demonstrated a conservative approach to operation and
instituted numerous improvement programs.
Continued attention is warranted
in the areas of engineering support and Technical Specifications.
.-
..
.-
'.
.
38
2.
Conclusion
Rating: 2
Trend: l Improving
3.
Board Recommendations
None
,
,
.
.
c
.
.
,
.
'
39
V.
SU? PORTING DATA AND SUMMARIES
A. Investigations and Allegations Summary
During this assessment period, a total of three allegations were received
and reviewed by tha NRC. One was directed towards the Department of Labor
and unsubstantiated. Of the remaining two, one was unsubstantiated and the
other partially substantiated.
B.
Escalated Enforcement Actions
An Enforcement Conference was held on March 25, 1987, to discuss numerous
violations identified from the event on February 13, 1987, leading to the
occupational extremity radiation exposure of a co-tract worker in excess of
NRC quarterly limits. A Notice of Violation was issued on March 11, 1987,
detailing five instances of violations, citing an aggregate Severity Level
III and cumulative $75,000 civil penalty.
C.
Management Conferences
The management meeting for the previous SALP period was held on April 15,
1987, in the NRC Region I Office, King of Prussia, PA.
On January 29, 1988, a meeting was held at the NRC Region I Office, King of
Prussia, PA, at the licensee's request to discuss plant performance and
programs, future plans, and a recent reorganization of the corporate
engineering department.
..
.
-.
'
40
TABLE 1
INSPECTION HOURS SUMMARY
AREA-
HOURS
% OF TIME
Operations
1001
31.8%
Radcon/ Chemistry _
504
16.0%
Maintenance /0utages
571
18.2%
Surveillance
406
12.9%
Engineering
323
10.3%
Sec/ Safeguards
126
4.0%
212
6.8%
Licensing
Assurance of Quality
---
__
TOTALS:
3143
100%
Hours expended in the area of assurance of quality are included in
other functional areas, therefore, no direct inspection hours are
given for these areas. Operator licensing activities are not included
with direct inspection effort statistics.
Hours expended in facility licensing activities are net included in
direct inspection effort statistics.
,-
-
,
..
.g
-
~
41
TABJ.E 2
ENFORCEMENT SUMMARY
A. Violations Versus Functional Area By Severity Level
Functional
No. of Violations in Each Severity Level
Area
LI*
V
IV
III
II
I
Total
Plant Operations
1
2
3
Radiological Controls
2
1**
3
Maintenance and Outages
1
1
Surveillance
2
1
1
4
0
Security and Safeguards
1
1
Assurance of Quality
3
3
Licensing
0
Engineering and
1
3
4
Technical Support
TOTALS
3
r
10
1
0
0
19
- LI - Licensee Identified Violations (10 CFR 2, Appendix C)
- 5 violations in aggregate were considered to be a severity level
III violation.
'
.
.
42
TABLE 3
LICENSEE EVENT REPORTS
Cause Determined by SALP Board
An assessment bas been conducted to determine the root cause of each evene from
the perspective of the NRC.
The causes fell into the following categories and
sub-categories.
Personnel Errors (PE)
1.
Lack of Knowledge (LK) - the individual was not properly trained or
provided with' instructions from supervision.
2.
Inattention to Detail (IC) - the individual failed to pay proper
attention to a task and was careless.
3.
Poor Judgement (PJ) - the individual failed to make the correct
assessment with the proper amount of training and attention to fac'.s.
Equipment Malfunction / Failure (EM/F)
1.
Random (R) - isolated component problem not of generic concern.
2.
Design Deficiency (DD)
poor design was the cause cf the
malfur.ction/ failure.
3.
Construction Deficiency (CD) - improper installation during
construction / modification caused or could have causec the malfunctirn
failure.
4.
Maintenance Deficiency (MD) - improper preventive or corrective
maintenance.
Procedural Error (PROE)
The procedure failed to provide adequate instruction, was coorly worded or
was not properly reviewed for use.
Ineffective Corrective Action (ICA)
Action was not taken by management or the action taken on a previously
identified item was not timely or did not correct the roct cause ard
allowed this occurrence.
__.
_
_
____ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _
.
.
..
' ' '
43
'
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
,
Cau:es As Determined By The Licensee
The licensee i's required to include cause codes in the reports.
These codes are
only required when equipment malfunction or failure is determined to be the
cause of the occurrence. -The following codes are used:
A - Personnel Error
8 - Design, Manufacturing, Construction or Installation
C - External Cause
0 - Defective Procedures
E - Component Failure
X - Other
.,
p.
- - -
__
,-
.
.
..-
...
.e
$
'
44
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
Summary of Cause Determined by SALP Board by Functional Areas
CAUSE
RAD
MAINT
SURV
ENG/TS
SEC
TOTAL
P E/'_K
1
1
PE/ID
1
1
5
7
PE/PJ
0
EM/F/R
2
3
5
EM/F/DD
1
2
3
.EM/F/CD
1
1
EM/F/MD
4
4
PROE
2
1
1
4
1
2
3
TOTAL
4
1
10
7
4
2
28
Summary of Cause of Equipment Malfunctions / Failure Determined by. Licensee
Area
A
B
C
D
E
X
TOTAL
Assurance of Quality
1
1
Surveillance
1
1
Maintenance
2
1
5
8
Operations
2
2
TOTALS
1
2
0
1
0
8
12
. - _ _ _ _ _ _ _ -
.,
.
' .s
's'
TABLE 3 (Cont'd)
.
LICENSEE EVENT REPORTS
LER Number /
Cause Cetermined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
86-19 **
11/12/86
Automatic
PE/ID - Technician
Surveillance
Actuation of
failed to check test
an Engineered equipment readiness
Safety
before commencement
Feature
of activities.
(Reactor
Core
Isolation
Cooling
Isolation).
86-20
12/21/86
TS Violation:
PE/ID - Radwaste
Operations
Unauthorized
operator did not
release of
ensure discharge
radioactive
permit requirements
liquid,
were met prior to
commencing
'
discharge.
86-21
12/23/86
High Pressure EF/DD - Battery
Engineering
Coolant
Motor Control
Support
Injection
Center was not
System
water tight
allowing intrusion
due to water
of water,
intrusion
into Battery
Motor Control
Center.
87-01
01/18/87
Excessive
EF/MD - Cause of
Maintenance
X
leakage of
failures was
Primary
attributed to wear,
Containment
licensee is
1 solation
developing program
Valves during to review failures
LLRT.
and maintenance
histories of the
failed components
to develop preventive
maintenance
recommendations.
,
-
--
-
'
,
j
..
.
.a
46
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
LER Number /
Cause Determined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
87-02
02/13/87
TS Violation:
PE/ID - Deficiencies
Rad. Control
Extremity
included inadequate
radiological surveys,
training, poor
pre-job planning
failure to follow
procedure.
87-03
02/19/87
High Pressure EF/MD - Failure
Maintenance
B
Coolant
mechanism of the
Injection
bolts caused by
Turbine
high bolt hardness
throttle
and contributed by
valve bolts
pitting due to use
broken,
of copper antiseizure
compound.
87-04
02/04/87
Three of six
EM/0D - No apparent
Maintenance
X
Main Stem
reason for setpoint
Safety Relief drift other than
Valves
sticking of one of
setpoints
the pilot valve disc,
found out of
tolerance.
87-05
04/01/87
EM/MD - Stem packing
Maintenance
X
Line
leakage from main
Isolation.
steam differential
pressure isolation
valves allowed
instrument
depress _rization
creating a simulated
high steam flow
resulting in PCIS
actuation.
.- .
c.-
.'
.
,
' i '.
t
47
TABLE 3(Cont'd)
LICENSEE EVENT REPORTS
LER Number /-
Cause Determined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
87-06
04/07/87
PROE - Procedure did
Surveillance
and Emergency not give adequate
Diesel
instructions to
Generator
ensure proper
Automatic
electrical leads
Actuation due were lifted.
to procedure
deficiency.
87-07
04/09/87
Reactor
EM/CD - During
Assurance of
A
Vessel Head
construction
Quality
vent piping
supports were not
inoperability installed as
due to
required by plant
missing pipe
drawings.
supports.
87-08
06/10/87
Low reactor
Engineering
vessel water
caused by operating
Support
level scram
with scoop tube
due to
positioners locked
Reactor Feed
up, losing the
Pump Trip,
ability to receive
while
an auto recirculation
operating
system runback on a
with scoop
loss of feed pump,
tube
positioners
locked up.
87-09
06/11/87
Emergency
EM/DD - During
Engineering
Diesel
transfer of loads
Support
Generator
voltage drop
start due to
sufficient to
temporary
activate
degraded
protective system
voltage
before operator
!
cot.di tion
action could correct
during bus
voltage.
transfer.
!
!
!
.o
.-
?4
- C'
' '
48
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
LER Numbur/
Cause Determircd
Functional
Cause Code *
Event Date
Description
SALP Board
Area
87-10
07/23/87
High Pressure EF/R - Auxiliary
Maintenance
B
Coolant
oil pump bearing
Injection
failed resulting
in lower discharge
due to
pressure. Cause of
Auxiliary
failure was not
Oil Pump
determined.
low pressure.
87-11
07/28/87
PROE - Previous
Assurance
Electrical
procedures for
of
inspection of fire
Quality
Seals not
barriers failed to
installed.
contain
unscheduled
87-12
08/28/87
Reactor Trips EF/R - Teflon
Maintenance
09/07/87
due to Main
insulation tubes had
a cupric oxide layer
caused by
buildup which under
generator
certain electrica'
field ground.
conditions becomes
fully conductive.
87-13
09/05/87
Reactor Core
EF/R - The trip
Operations
X
Isolation
unit and transmitter
Cooling
were replaced.
Vendor
System
analysis could not
Isolations
determine a cause
due to
of the spurious trips.
spurious
Analog
Transmitter
Trip Unit
trip.
87-14
09/12/87
Emergency
ICA - Corrective
Operations
Diesel
actions taken to
Generator
prevent recurrence
start due to
of this event were
temporary
inadequate (see
degraded
LER 87-09).
voltage during
bus transfer.
. _ -
i
.-
,
- c o
49
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
LER Number /'
Cause Determined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
87-15
09/16/87
High Pressure EM/MD - Malfunctional Maintenance
X
Coolant
because of foreign
Injection
material deposits
on internal float
due to
mechanism,
unstable
suppression
chamber level
switch.
87-16
09/16/87
High Steam
PE/ID - Operator
Surveillance
flow
failed to follow
Isolation
prescribed sequence
of Reactor
of surveillance
Co ,*e
test procedure.
Isolation
Cooling
System due
to operator
error.
87-17
09/24/87
Reactor low
Engineering
level scram
caused by operating
Support
following
with scoop tube
feed pump
positioners locked
trip on
up, losing the
high
ability to receive
vibration,
an auto recirculation
system runback on loss
of feedpump.
1
l
l
"
l
,
&=
'
50
i
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
LER Number /
Cause Determined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
87-18
11/8/87
High Flux
EF/R - Recirculation
Operations
X
System Speed Controller
due to
malfunctioned;
reactor water suspected cause was an
recirculation age effect, controller
system pump
was replaced with a
sudden speed
spare unit.
increase.
87-19
12/7/87
TS Violation:
PE/IO - Responsible
Maintenance
Failure to
supervision did not
perform
ensure that the
Standby Gas
specified
Treatment
surveillance test
Surveillance
was performed as
Test as
required.
required.
87-20
12/9/87
PE/LK - Technician
Surveillance
X
from low
failed to fully
water level
close an isolation
actuation
valve prior to
caused by
valving in test
personnel
equipment.
error
during
surveillance
test.
87-21
12/13/87
Reactor Water PROE - Bolt
Maintenance
Cleanup
torquing
Isolation
procedure
on High
was inadequate,
temperature
causing improper
due to
flange makeup,
inadequate
resulting in a
procedure,
steam leak which
resulted in system
isolation on high
room temperature.
a
-
e
51
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
LER Number /
Cause Determined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
87-22
12/20/87
TS Violation:
PE/ID - Operators
Surveillance
Failure to
failed to perform
perform
surveillance test
drywell
at required
leakage rate
frequency.
surveillance
at required
frecuency.
88-01
03/10/88
High Pressure PROE - Maintenance
Maintenance
D
Coolant
precedure did not
Injection
include evaluation
System
of relubrication of
of the valve stem
due to motor
and stem nut during
operated
maintenance causing
valve failure motor operated valve
as a result
failure due to
procedure
excessive current.
deficiency.
88-02
03/10/88
Reactor Core
PE/ID - I&C
Surveillance
Isolation
technician petforming
Cooling
the assigned task did
Automatic
not follow the
Isolation
prescribed procedure;
during
there was no copy of
Surveillance
the procedure
Testing as a
utilized, which led
result of
to the wrong trip
personnel not unit placed in test.
following
procedures.
I
,
_
_ _ _ _ _ _ ,
t
%
3,
52
TABLE 3 (Cont'd)
LICENSEE EVENT REPORTS
LER Number /
Cause Determined
Functional
Cause Code *
Event Date
Description
SALP Board
Area
88-03
04/18/88
Engineered
EF/R - The relay coil
Operations
X
Safety
is normally energized
Feature
and had oeen in
Actuations
service for thirteen
due to loss
years.
No similar
of Reactor
problems with this
Protection
type relay.
System power
supply caused
by relay
failure.
Indicates licensee's cause code for equipment failures only.
Event occurred during previous assessment period.
.
I
- "
i
,