ML20149K165

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Insp Repts 50-254/97-06 & 50-265/97-06 on 970318-0505. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20149K165
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 07/07/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20149K149 List:
References
50-254-97-06, 50-254-97-6, 50-265-97-06, 50-265-97-6, NUDOCS 9707300027
Download: ML20149K165 (30)


See also: IR 05000254/1997006

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION ll1

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Docket Nos:

.50-254,.50-265'

License Nos:

DPR-28, DPR-30

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Report No:

50-254/97006(DR P), 50-265/97006(D RP) -

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Licensee:

Commonwealth Edison Company (Comed)

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Facility:

Quad Cities Nuclear Power Station, Units 1 and 2

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Location:

22710 206th Avenue North

Cordova, IL 61242

Dates:

March 18 - May 5,1997

Inspectors:

C. Miller, Senior Resident inspector

K, Walton, Resident inspector

- L. Collins, Resident inspector

R. Ganser, Illinois Department of Nuclear Safety

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Approved by:

Wayne J. Kropp, Chief

Reactor Projects Branch 1

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9707300027 970707

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EXECUTIVE SUMMARY

This inspection included aspects of licensee operations, engineering, maintenance, and

plant support. The report covers a 7-week period of resident inspection,

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Ooerations

Operators performed complex tasks, such as response to transients, unit startups and unit

shutdowns, well. However, several operator performance errors occurred during simple

tasks. Previous inspection reports also have discussed operator performance issues

(Sections 01.2 and 01.3).

Unit 2 fuel off-load activities were discontinued during the Unit 1 shutdown evolution to

reduce the potential for distraction. Overview personnelincluding site quality verification

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(SOV), operations, engineering and station management were present during startups and

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shutdowns (Section 01.2).

Operators appropriately responded to a loss of power on a reactor protection system (RPS)

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bus. Operators restored power to the RPS bus and reestablished shutdown cooling.

(Section 01.4).

Two violations were identified regarding document control. in one violation, operators

were using the wrong revision of a procedure which was obtained from a controlled set of

procedures. The second violation was issued regarding records where a master retention

schedule which lists required quality records and retention periods was'not maintained up-

to-date (Section 01.3 and 07.2).

Maintenance

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The inspectors observed lapses in worker attention to foreign material exclusion (FME) and

. personnelindustrial safety procedures. Radiation protection department monitoring and

control rod drive hydraulic control unit (CRD/HCU) overhaul work indicated the licensee's

continued emphasis on "as low as reasonably achievable"(ALARA) radiation dose

exposure principles (Section M1.1).

Longstanding problems with standby liquid control (SBLC) flow meters used to verify pump

operability led to a failed surveillance, entry into a limiting condition for operation (LCO),

and preparations for a unit shutdown. The adequacy of IST instrumentation is an

unresolved item (Section M2.4).

Enaineerina

The licensee's decision to expand invesselinspection activities based on information from

another nuclear facility, was both warranted and proactive (Section E1.1).

The NRC previously identified that engineering did not adequately trend or analyze room

cooler differential pressure for a period of time (see Deviation 50-254,265/96015-01).

The failure to analyze the degraded condition of the Unit 2 "B" core spray room cooler

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resulted in the licensee operating the facility for an extended period 'of time with a

potentially inoperable train of core spray (Section E2.1).

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The licensee identified on three separate occasions, broken auxiliary contact assemblies on

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4 kilovolt (kV) breakers which were planned to be installed in the facility. The licensee's

initial review of the importance of the issue was narrow in scope. However, subsequent

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breaker inspection, evaluation of the condition, and resultant shut down~of Unit 1 were

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appropriate (Section E2.3).

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Plant Sucoort '

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The first time efforts to decontaminate the Unit 2 torus suction header were partially

successful (Section R1.1).

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An incomplete understanding of the fire hazards analysis resulted in an untimely

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notification to the NRC (Section F4.1).

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Report Details

Summarv of Plant Status

Unit 1 started the period with operators decreasing load from full power to about

80 percent of full power operation due to equipment problems. During the period,

operators shut down and started up Unit 1 twice due to various equipment problems (see

chronology below) .

Unit 2 was shut down for refuel outage O2R14 on February 28,1997, and remained shut

down thr' ghout the period.

l. Ooerations

01

Conduct of Operations

01.1 General Colpments (71707)

Using inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

During the inspection period, several events occurred which required prompt

notification of the NRC pursuant to 10 CFR 50.72. The events and dates are listed

below.

March 19

A notification was made due to Unit 1 high pressure coolant injection

(HPCI) system being inoperable for about 75 minutes. Workers

identified a HPCI component power supply cable as degraded. The

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licensee later determined the cable was not connected.

March 21

A notification was made due to the Unit 2 "B" core spray room cooler

being inoperable due to fouling in parallel with the Unit 2 "A" core '

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spray system being inoperable due to emergency diesel generator

unavailability.

March 22

Operators shut down Unit 1 reactor due to unanticipated turbine

equipment problems requiring a longer repair time.

March 27

A notification was made due to nonconformance with a fire hazards

design requirement first identified on February 27,1996

(See Section E4.1).

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March 29

Operators startup and synchronize Unit 1 to the grid.

March 31

A notification was made due to an inadvertent start of the Unit 1

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emergency diesel generator.

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April 3

A notification was made due to the Unit 1 high pressure coolant

injection system being declared inoperable. Subsequent

troubleshooting identified the reason for the turning gear motor

failure.

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April 7-

A notification was made due to a failure of a single train safety

system. Operators received freon alarms indicating the refrigerant

compressor unit of Train B of control room ventilation had a leak.

The leak was later repaired.

April 7

A notification was made due to flow from both Unit 1 standby liquid

control pumps being less than the inservice inspection required flow

rates. Operations commenced shutdown of Unit 1 until the test

could be repeated with properly calibrated gauges.

April 9

Operators notified the NRC that Unit 1 was shutting down due to

concerns identified with cracked auxiliary switches in 4 kV breakers.

April 18

A notification was made due to loss of Unit 1 "B" reacter petection

systern bus. Unit 1 lost shutdown cooling for several hours due to

primary containment isolation system closing the suction valve to the

operating residual heat removal pump. Various other system

isolations occurred. (See Section 01.4).

May 1

A notification was made due to Unit 1 HPCI being declared inoperable

since a code required inspection of a valve was missed.

01.2 Control Room Observations

a.

Insnection Scone (71707)

Yhe inspectors reviewed the sequence of events recorder, operator logs, and spoke

to operators concerning the feedwater heater transient. The inspectors observed

two shutdowns and two subsequent startups associated with Unit 1.

b.

Observations and Findinas

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On March 19 during Unit 1 power ascension, control room operatois received

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annunciators indicating problems with the moisture separator drain tank (MSDT)

flows to the high pressure feedwater heaters. As required by annunciator response

procedures, operators quickly reduced reactor power from about 98 percent to

about 80 percent power. To effect feedwater heater repairs, the licensee removed

the turbine from service with the reactor critical. However, af ter removing the

turbine from service, the operators noted a second electrohydraulic control (EHC)

pump started unexpectedly. This required operators to shut down the reactor on

March 22 and perform additional repairs on the EHC system.

Unit 1 was returned to service on March 29. However, on April 5 operators again

were required to reduce Unit 1 reactor power due to problems associated with

feedwater heater level control valves. Maintenance personnel adjusted a feedwater

heater level controller and Unit 1 was returned to full power operation.

On April 9 operations declared 4 kV breakers on safety-supporting electrical busses

as inoperable and shut down Unit 1 (See Section E2.3).

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With Unit 1 shut down on April 18, a loss of power to a reactor protection bus

resulted in a loss of shutdown cooling. This required operators to reset the reactor

protection system and reinitiate shutdown cooling operations (See Section 01.4).

The inspectors noted the control room atmosphere was quiet and controlled during

most evolutions. Communications and coordination efforts were conducted

smoothly with minimal distractions. A reduction in distractions was aided by the

licensee's recently implemented effort to strictly limit control room access, and to a

lesser degree, by reducing the number of phone calls to the control room.

The unit supervisors demonstrated good command and control of evolutions, and

conducted periodic briefings to ensure all operators received current information

concerning unit status. Operator communication with each other and with the unit

supervisor was good. Unit 2 fuel off-load activities were discontinued during the

Unit 1 shutdown evolution to reduce the potential for distraction. Overview

personnel including site quality verification (SOV), operations, engineering, and

station management were present during startups and shutdowns.

During one startup evolution, coordination of the nuclear station operators (NSOs)

was not commensurate with previous startups. This was primarily due to recent

reassignment of persons in key positions within the operating crew. Overall, crew

performance was adequate. All procedures were adhered to, and evolutions were

safely conducted. During a startup, the inspectors observed that operators

demonstrated professional demeanor in the conduct of unit startup evolutions. In

this example, communications, self-checking, and adherence to all procedures and

management expectations was excellent.

c.

Conclusions

Operators continued to be challenged by equipment problems requiring frequen'.

maneuvering of the units. The inspectors noted operators responded appropriately

to transients due to the equipment problems. - Unit 1 shutdowns and subsequer't

startups were well executed.

01.3 Operations Surveillances

a.

insnection Scooe (71707)

The inspectors observed operators performing surveillances and using operating

procedures during routine control room mocitoring. The inspectors discussed with

operators the errors that had occurred during the surveillance tests.

b.

Observations and Findinos

On March 31 prior to performance of a surveillance test, an operator over

rotated the Unit 1 EDG control switch. This resulted in an inadvertent start

of the EDG. The licensee documented this on Problem Information Form

(PlF) 97-1241. The licensee determined methods used by operators to

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operate a pistol-style grip switch were poor and initiated training for

operators (See Section 08.2).

On April 3 the inspectors observed an operator performing Quad Cities

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Operating Surveillance Procedure (OCOS) 2300-01, ."High Pressure Coolant

injection Periodic Test." The operator did not set the proper pump discharge

pressure as required by the surveillance test. An operations supervisor,

performing a peer check of the reactor operator setting discharge pressure,

concurred that the proper discharge pressure was set. However, before

proceeding with the test, a third operator identified and informed both

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operators that the incorrect discharge pressure was established. The proper

discharge pressure was established and the test proceeded.

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Previously, management suggested operating crews implement peer checks

to prevent undetected human errors from occurring. Peer checks were not

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required. The inspectors spoke to management about this issue. This issue

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was not documented on a PIF and the inspectors noted management missed

an opportunity to enforce expectations with the individuals involved.

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On April 9 the inspectors observed an operator realigning the 250 VDC

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system after performance of a battery discharge test. The operator used a

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copy of Guad Cities Operating Procedure (QOP) 6900-16, " Transfer of Bus

18 from MCC [ motor control center) 1 to MCC 2," Revision 8, from a

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controlled procedure book. During the procedure, operators in the plant

performed steps not recognized in the control room copy of the procedure.

The operator identified that the control room copy of.the procedure did not

have the proper revision. The operator stopped the procedure, reconciled

differences between the two revisions, and completed the procedure. This

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condition was documented on PlF 97-1540.

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Revision 9 to the procedure returned both 250 VDC buses 18 and 2A to

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their normal source. However, Revision 8 to the procedure only returned

250 VDC Bus 1B to the normal source. Bus 2A powered important safety-

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related components in Unit 2. However, Unit 2 was shut down at the time

of the event and components powered by Bus 2A were not required by

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Technical Specifications (TSs).

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The licensee acknowledged the failure of two barriers to prevent the use of

incorrect revisions of procedures. The operator did not ensure the proper

revision was in hand prior to performing the procedure and the wrong

procedure revision was included in the control room controlled procedures

book. The failure to maintain the proper revisions of operating procedures in

control room controlled procedure books and the failure to ensure the use of

the proper revision of the procedure was considered a Violation (50-

254:265/97006-01) of 10 CFR Part 50, Appendix B, Criterion VI,

" Document Control."

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On April 15 the inspectors observed control room operators during the

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performance of Quad Cities Operating Surveillance Procedure (OOS)

6500-03 "4 kV Bus 14-1 Undervoltage Functional Test." The surveillance

test was required to demonstrate the undervoltage relay operation and load'

shedding upon loss of voltage to Bus 14-1 and to verify that the Unit 1

diesel generator started and loaded in the required time. Bus 14-1 was a

safety-related 4 kV bus that supplied power to emergency core cooling

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pumps.

The procedure allowed for the prerequisite steps to be performed in any

logical order. Several of the prerequisite steps were performed by control

room operators on the night shift. The day shift operators continued the

procedure. Step C.1.t stated, Verify "At 901-8 Panel, BUSSES 14-1 and

24-1 TIE ACB is closed." The step was initialed as completed but the

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breaker remained in the open condition. One of the load shedding functions

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to be tested included the tie breaker between the Unit 1 Bus 14-1 and the

Unit 2 Bus 24-1. However, the test required that the tie breaker be closed

to verify that it opened properly during the undervoltage test. Immediately

after the undervoltage signal was introduced, the control room operator was

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required to verify that; the Unit 1 diesel generator automatically started,

Annunciator E3,4 kV Busses 13-1/14-1 low voltage alarmed, and the Bus

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14-1 and 24-1 tie breaker tripped. The operator could not verify that the tie

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breaker had tripped since it was already open. The failure to properly

implement the test procedure was a Violation (50 254:265/97006-02) of

TS 6.8. A.

Immediately af ter the discovery of the discrepancy, the operators generated

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PIF 97-1779 to document the error. The engineering staff wrote interim

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procedure 97-0057 to perform a modified version of the test to verify that

the tie breaker tripped on an undervoltage condition on Bus 14-1.

The cause was considered to be a procedural adherence failure.

Management recently emphasized the use of " peer check" for operators to

prevent such errors. In this case, peer check could have prevented the error

from occurring, but was not used. Another barrier to prevent such errors,

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the test briefing, failed to identify that the required test configuration did not

match the plant configuration.

c.

Conclusion

During this inspection period, the inspectors were concerned with operator errors,

and the effectiveness of the operator peer checks to prevent these errors. The

inspectors concluded that these errors were similar to those previously documented

in Inspection Report 50-254:265/96020 indicating a continuation of operator

performance errors.

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01.4 Loss of 1B Reactor Protection System Bus Causes Loss of Shutdown Coolina (PlF

97-1851)

a.

insoection Scooe (93702. 71707)

On April 18, the 182 electrical protection assembly (EPA) for RPS Bus 18 tripped

unexpectedly causing a loss of power to the 1B RPS bus. The loss of power

resulted in a loss of shutdown cooling and a partial primary containment isolation.

A report was made to the NRC via the emergency notification system (ENS). The

inspectors observed the restoration of shutdown cooling and followed up on the

root cause investigation and initial operator response to the event. The inspectors

reviewed the Unit 1 logbook and spoke with operators to understand the sequence

of events,

b.

Observations and Findinas

The loss of power to the RPS Bus 18 occurred at 7:27 a.m. central standard time,

when the 182 EPA deenergized unexpectedly. Two EPAs in series are designed to

protect the RPS bus from an undervoltage, over voltage, or under frequency

condition. The loss of the B RPS bus caused some valves in the primary

containment isolation system to close. As a res alt, the reactor water cleanup

(RWCU) system, which was controlling reactor watcr level, and the residual heat

removal (RHR) system, which was removing decay heat. isolated.

Prior to the event, shutdown cooling was in service and the initial reactor water

temperature was recorded as 150 degrees Fahrenheit. Operators responded to the

event and entered Quad Cities Operating Abnormal Procedure (QCOA) 1000-2,

" Loss of Shutdown Cooling," and Quad Cities Operating Abnormal Procedure (OOA)

7000-1,"120 VAC Reactor Protection Bus Failure." Per OOA 7000-1, an operator

was dispatched to the RPS bus to determine the cause of the bus deenergizing. No

obvious reason for the condition was identified. Electricians were called to assist in

checking the status of the 1B bus prior to reenergizing per QOP 70001, " Reactor

Protection System MG Sets." i9o problems were identified and the 1B RPS bus

was reenergized at 8:55 a.m. At 8:58 a.m. operators restored the RWCU system

and at 9:17 a.m. RHR shutdown cooling (SDC) was placed in operation. The

highest recorded reactor water temperature was 175.5 degrees Fahrenheit, an

increase of about 25 degrees Fahrenheit during the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and

50 minute period that SDC was off.

Based on discussions with operators, the inspectors found the first 70-80 minutes

were used for troubleshooting the 182 EPA and the 1B RPS bus to determine the

cause of the EPA trip and that the actual time spent to restore power and return

RWCU and SDC to service was approximately 30-40 minutes.

Operators considered a band of 130 to 180 degrees Fahrenheit as an administrative

limit for reactor water temperature during normal shutdown cooling operations.

The inspectors did not find any procedures that referenced these administrative

temperature limits. A review of Unit 1 plant data and log books showed that

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operators generally maintained temperature around 150 degrees Fahrenheit, but the

temperature fluctuated between 140 and 170 degrees Fahrenheit. The inspecto s

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questioned operations management about the wide temperature band and

concluded that the_130 to 180 degree temperature band was a widely understood

but informal operating range. At the end of the inspection period, operators were

reviewing past practices and procedural guidance for maintaining a temperature

band while in shutdown cooling and planned to enhance existing controls.

The failed breaker was last calibrated on April 12,1997, with satisfactory results.

Testing after the failure revealed that the breaker was tripping prematurely and

could not be reset. The breaker was replaced. The licensee reviewed five years of

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data on the EPAs and found one spurious trip of the 182 EPA had occurred in

1996. The licensee planned to upgrade the remaining EPAs with new breakers and

upgraded circuit boards. The failed breaker was sent off site to the materials

engineering group (MEG) for additional failure analysis.

c.

C_qn, clusion

The inspectors reviewed the initial operator response to the loss of shutdown

cooling event and concluded that operators followed the appropriate procedures to

restore power to the RPS bus and restore RWCU and RHR SDC. However, the

control of the limit for reactor water temperature during normal shutdown cooling

operations was not procedural defined and sometimes varied from shift to shift.

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Quality Assurance in Operations

07.1 Premature Event Screenino Committee Event Closures

The inspectors attended an event screening committee (ESC) meeting. The ESC

evaluated the quality of corrective actions and disposition of events. The licensee

has recently been using the ESC to disposition and close PIFs at an early stage to

help reduce the number of open PIFs. The inspectors found that PIF 97-1295

which involved plant oversight review committee (PORC) members not being

qualified for their function (specifically, the chairman) was closed with no corrective

action taken. The items covered during the PORC were not reboarded because the

licensee said that the function of the chairman was not critical enough to invalidate

the results in addition, no action to ensure a repeat of the failure to operate with

qualified members was called for and no action was initiated to review past

meetings for qualified members was initiated. Although PORC is not required at

Quad Cities, management has relied upon PORC as tte key organization to review

the quality cnd effectiveness of plant decisions. The inspectors concluded that ESC

decisions to close the PlF were not based on good corrective actions commensurate

with the importance of the function of PORC.

Another PIF (971243) was closed which dealt with a potential degraded condition

of fan noise on the shared EDG ventilation fan. The ESC committee closed the PIF

with the understanding that the problem occurred once and had not repeated, and

that an action request for the fan would be worked in September 1997. The nature

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of the root cause analysis, the effect of the fan's failure on EDG operability, and the

effect of the operable but potential degraded condition on the Unit 2 startup were

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not discussed. The inspectors concluded that the decisions made by the ESC about

the EDG PlF were not based on the criticalimportance of the shared EDG.

07.2 Quality Records Manaaement

a.

Insoection Scooe (39701)

The inspectors reviewed the licensee's process for identifying quality records and

specifying the required retention period in accordance with 10 CFR Part 50,

Appendix B, Criterion XVil and the Site Quality Assurance Manual. The inspectors

questioned operations, site quality verification, and office support personnel to

determine how completed procedures were documented as quality records.

b.

Observations and Findinas

The Site Quality Assurance Manual stated that the quality records program included

those record types, controls, and provisions for storage and preservation contained

in Nuclear Quality Assurance (NOA) -1, Supplement 17S-1 and that records were

administered through a system which included an index of record type, retention

period, and storage location.

The Quality Assurance Program Requirements for Nuclear Facilities outlined in

NOA 1, Supplement 17S-1, covered receipt control of records. This supplement

states that as a minimum the receipt control system shallinclude a method for

designating the required records. The receipt control section also stated that each

receipt control system shall be structured to permit a current and accurate

assessment of the status of records during the receiving process.

The inspectors reviewed UFSAR Section 13.7 covering records. The UFSAR stated

that control room record retention period was specified on the Commonwealth

Edison Record Retention Schedule forms for each record.

The inspectors reviewed the master retention schedule which was the document

intended to ipecify retention requirements for various plant procedures. The

retention schedule did not specify whether the records were considered to be

quality documents. Additionally, the retention schedule was not up to date. The

inspectors identified that outdated procedures were listed and that some currently

required surveillances were not listed. Also, new required surveillances since the

implementation of the upgraded TS in September 1996 had not been added to the

master retention schedule to designate the required retention period. The station

procedure, Quad Cities Administrative Procedure (OCAP) 1200-1, " Station

Records," stated that the responsible department records custodian shall update the

master retention schedule when a new record is created. The custodian was

responsible for determining if the record was a quality document. The inspectors

found that the procedure was recently implemented and that the department

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records custodian was not following the procedure. The operations department

records custodian told the inspectors that the custodians did not regularly review

new procedures to determine if the procedures created quality records.

The inspectors identified several surveillances and other quality records that were

not listed or were listed incorrectly on the master retention schedule including:

OCAP 0230-07, " Operability Determination"

OCCP 1200-2, " Post LOCA Hydrogen and Oxygen Monitoring System"

OCIS 2400-1, "Drywell Radiation Monitor Calibration and Functional Test"

OCOS 1600-4, " Weekly Primary Containment Oxygen Concentration"

The licensee told the inspectors that these records were properly retained even

though they were not listed on the retention schedule. The licensee was in the

process of upgrading the records management program, including the master

retention schedule, but no completion date for the project was available. The

inspectors concluded that records were not accurately identified as quality records,

and that the station was not controlling quality records in accordance with the

station procedure, the quality assurance manual and 10 CFR Part 50, Appendix B.

The failure to identify quality records and to establish retention requirements was

considered a Violation (50-254:265/97006-03) of 10 CFR Part 50, Appendix B,

Criterion XVil, " Quality Assurance Records."

c.

Conclusion

Over time, the licensee failed to ensure that the master retention schedule was

updated to include newly created quality records. The inspectors identified that

some TS required surveillances were not listed on the retention schedule and were

not designated as quality records. This was considered to be a violation of 10 CFR Part 50 Appendix B, Criterion XVil, " Quality Assurance Records."

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Miscellaneous Operations issues (92700)

08.1 (Closed) Insoector Follow-uo item (50-254:265/96006-04): Inattentive Test

Director. The inspectors observed a test director in the control room in an

inattentive state and brought this to the attention of the shift engineer. The

licensee conducted an investigation. The individual was disciplined. The inspectors

reviewed the investigation results and consider the item closed.

08.2 (Closed) Licensee Event Reoort (LER) (50-254:265/97007): Unit 1 EDG Mar! Due

to Personnel Error. A r.oet room operator over-rotated a pistol grip stya EC'G

control switch. As a r69 ult, the Unit 1 EDG inadvertently started. The operator

was counseled and an operations supervisor provided direction to operators on

proper operation of pistol grip switches. The inspectors considered this a violation

of adherence to the surveillance procedure OCOS 6600-01, "EDG Monthly Load

Test," since the switch was to be moved to the stop position instead of the start

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position. This licensee-identified and corrected violation is being treated as a

Non-Cited Violation (50-254:265/97006 04), consistent with Section Vll.8.1 of the

NRC Enforcement Policy. This LER is closed.

08.3 (Closed) Violation 50-254:265/95005-02: Failure to Maintain the RHR Room

Watertight Door Closed in Accordance with TSs. As corrective action the licensee

developed procedure OCAP O250-06, " Control of In-Plant Watertight Submarine

Doors." This procedure provided adequate guidance for control of the watertight

doors. Several PlFs have been generated since the violation was written. Problem

Identification Form 95-2542 was written to address a worker leaving a door open

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long enough to retrieve a tool. The worker was unaware that the procedure did not

allow this practice. The licensee coached the individual on the correct use of the

procedure. Problem Identification Form 961780 was written to address an

incident where a door was found latched but not dogged. The licensee did not

determine the person responsible; however, narrowed it down to a specific work

group. As follow-up action, the licensee addressed the issue through tailgate

meetings. The licensee's vigilance and attention to maintaining the integrity of

watertight doors has been increased since June 1995 when the initiating violation

was identified. This item is closed.

08.4 (Closed) Licensee Event Reoort 50-265/95007: Unit 2 HPCI Turning Gear Motor

Failed to Start as the Turbine Coasted to a Stop. Following this event, the licensee

suspected a failure of the turning gear to properly reset. The licensee performed a

series of tests on an accelerated schedule; however, they were unable to reproduce

the failure. One of the accelerated tests resulted in a turning gear engagement

-

failure due to gear abutment; however, the license"3 procedures addressed this

condition. There were two turning gear related wcurrences on the Unit 1 HPCI

since this LER. The licensee has shown that neither of these was related to the

event on the Unit 2 HPCI. This item is closed based on adequate follow-up action

by the licensee.

11. Maintenance

M1

Conduct of Maintenance (62707)

M 1.1 Observation of Maintenance Activities Durina Refuel Outaae 02R14

a.

Insoection Scone

Maintenance activities observed during this inspection period included: movement

of emergency core cooling system (ECCS) suction strainers to the Unit 2 torus,

Unit 2 turbine overhaul work, turbine stop valve HO 2-5699-MSV1 actuator rebuild,

electrical maintenance department (EMD) switch replacement work on the 2202-20

panel for hydraulic control unit (HCU) banks three and four, CRD HCU overhaul

work, snubber testing, preparation for chemical decontamination of the Unit 2

recirculation system, tube lance on the 18 control room heating ventilation and air

conditioning (HVAC) heat exchanger, electrical maintenance department (EMD)

inspection of 4 kV breaker auxiliary contact assemblies, penetration sealing and

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duct repair of the control room emergency ventilation system, and planned -

inspection and maintenance of the 2B recirculation system motor generator (MG)~

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set slip rings and commutator.

b.

Observations and Findinos

When workers attempted to lower the first of the new type ECCS suction

.

4

. strainers through the floor opening into the Unit 2 torus, there was

i

insufficient clearance due to interference from a section of structural steel.

Lack of adequate planning and pre-measurement caused some lost time and

j

unnecessary radiation exposure during this first attempt. All other aspects

of this effort observed by the inspectors were satisfactory.

The inspectors observed contract workers perform overhaul work on a

'e

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Unit 2 turbine stop valve actuator HO 2-5699-MSV1, in accordance with

j.

work package WR 960076977. Work procedures were conducted

j

adequately, with the exception that foreign material exclusion (FME) controls

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were somewhat lax. The inspectors observed that there were items in a

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zone 2-work area that were not logged in on the FME log sheet, specifically

some tape and gloves. The inspectors brought this to the attention of the

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workers, who did not appear to have a clear understanding of the FME

i

requirements. The workers removed the non-controlled items from the FME

5

zone. The workers discussed the procedures with the immediate supervisor

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to understand the FME requirements. The work package was current and

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workers adequately documented the work steps when completed.

!

Overhaul work on CRD/HCUs was well coordinated. Radiation protection

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personnel were assigned full time to this job to coordinate work movement

and to assure radiation exposure to workers was maintained ALARA. The

- total radiation exposure for the entire effort was approximately 55 percent of

the amount allotted. This dose savings was due to job planning and worker

diligence in minimizing dose, and by workers consistently remaining in the

lowest possible dose areas throughout the entire job.

e

The inspectors observed three scaffolding workers standing on high scaffold

elevations in the Unit 1 turbine building who were wearing fall protection

harnesses but were not hooked up to an anchor point. The inspectors

questioned the acting foreman about the safety requirement for fall

protection. The foreman reminded the workers of the safety requirement.

Later in the shift the tr.spectors verified that all of the workers were correctly

adhering to the safety procedure. The inspectors discussed these

observations with site safety engineers the following day.

The inspectors observed EMD workers following a procedure in preparation

for chemical decontamination of the Unit 2 reactor recirculation system. The

project manager for the decontamination crew accompanied the EMD

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workers and was closely involved in the activity. The inspectors observed

that the projact manager and the workers observed good self-checking and

second party verification (peer checking) techniques.

c.

Conclusions

in general, plant workers were attentive to radiation and personnel safety

requirements, with only minor exceptions. Workers used approved procedures to

perform work and contributed constructive suggestions to help minimize radiation

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exposure. Work areas were kept orderly and free of clutter. Job coordination in

!

. busy work areas was good.

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M2

Condition of Facilities and Equipment

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M2.1 Miscellaneous Material Condition issues (71707)

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The inspectors noted continued equipment problems affected reactor operations,

and resulted in two forced shutdowns for Unit 1 during the period. Listed below

are material condition issues that affected Unit 1 operations:

Breakers installed in safety-related electrical switchgear were identified as having

- auxiliary contact switches prone to cracking. This resulted in operations declaring

the breakers inoperable and required shutdown of Unit 1 (See

Section E2.3).

Repairs were made to an inoperable intermediate range monitor (IRM) -15. During

startup of Unit 1, IRM-15 acted erratically. Operators declared the IRM inoperable

again. The licensee subsequently replaced the IRM detector and declared IRM 15

operable. IRM-15 operated properly during subsequent startup of Unit 1.

During the shutdown of Unit 1, a valve on a hydraulic control unit exhibited leakage

from a body to bonnet joint. The valve was cut out and replaced. A laboratory

later determined the valve was missing a body to bonnet gasket due to

maintenance performed a year previously.

Refuel bridge locked up twice due to problems with an electrical cable. The

licensee later identified the cable was improperly manufactured. The cable was

replaced and Unit 2 reactor defueling continued.

The normal drain valves from the moisture separator drain tanks to the high

pressure feedwater heaters on Unit 1 were degraded and resulted in a plant

transient. The licensee shut down Unit 1 to effect repairs to the system. The

licensee historically has had problems operating the feedwater heating system. The

licensee's investigation identified the valves were undersized by industry standards,

air leaks existed on valve actuators, and the system had been prone to fouling by

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material from inside the system. Engineering determined the system was not

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periodically tested, there were no existing preventive maintenance items for the

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system, and existing predictive maintenance activities were not adequate to trend

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valvo performance. The licensee identified these issues and others, and panned to

implement corrective actions.

During the shutdown of Unit 1, operators noted increased flow through the turbine

electrohydraulic control system. Engineers noted excessive seat leakage through

spool valves in both intercept and stop valves manifolds. Spool valves in ten

actuators were replaced.

i

c.

Conclusion

in each of the above cases, the inspectors reviewed the licensee's investigations

(when performed) and corrective actions. The inspectors noted initial work on the

IRM did not correct the condition. The inspectors noted work performed on the

HCU introduced a problem which was not identified during post maintenance

testing. The inspectors deemed the licensee's corrective actions appropriate to the

circumstances.

M2.3 250 Volts Direct Current Batterv Testina

a.

Insnection Scone

The inspectors observed portions of the Unit 2 modified performance test for the

250 volts direct current (VDC) safety-related battery (Quad Cities Technical Staff

Procedure [OCTS] 0240-06). The inspectors reviewed the load duty cycle of the

battery, the TS requirements for testing, and the UFSAR.

b.

Q_bservations and Findinos (61726)

The modified performance discharge test was allowed by TS 4.9.C.5 to satisfy

both the service test and the performance test. The modified performance

discharge test was perforrned once every 60 months and was used to verify the

battery's ability to meet the critical period of the load duty cycle and to measure

the battery's capacity. The UFSAR (Section 8.3.2.1) stated that the battery was

sized to start and carry the normal direct current (DC) loads required for safe

shutdown on one unit, and the operational loads required to limit the consequences

of a design basis event on the other unit, for a period of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> following loss of

all alternating current (AC) sources. The 250 VDC battery systems are cross-tied

such that each unit's battery feeds the high pressure coolant injection system

(HPCI) system for that unit and the reactor core isolation cooling system (RCIC)

system on the opposite unit in addition to several other DC loads.

The licensee had recently updated the electricalload profile and determined that the

most severe transient on the 250 VDC battery had changed from an intermediate

loss of coolant accident to a steam line break outside of containment. The

inspectors observed portions of the test and verified that the load applied to the

battery conformed to the licensee's documented load profile for the steam line

break scenario. The inspectors reviewed the completed procedure and verified that

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the calculated battery capacity of 100.7 percent was greater than the minimum

.

acceptable battery capacity and that the TS requirement was satisfied.

The inspectors reviewed in detail the electricalload profile for the steam line break

t.

)

scenario and asked the system engineer to clarify several of the assumptions made

. in the calculation. The load profile based on Unit 1 assumed that Unit 1 HPCI and

j

Unit 2 RCIC were in the test configuration when the steam line break and loss of

offsite power occurred. The inspectors questioned why this configuration was

more limiting than the HPCI system starting at the initiation of the accident since

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the operation of the injection valve, the auxiliary oil pump, and the steam supply

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valve were significant loads on the battery. The inspectors also questioned the

1

system engineer if the HPCI suction path transfer from the contaminated

condensate storage tank (CCST) to the suppression pool and any cycling of HPCI

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. on and off was considered in the load profile. Additionally, the inspectors asked

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the system engineer to identify which Unit 2 safe shutdown loads were included in

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the load profile. This issue is an Inspector Follow up item (50-254:265/97006-05).

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c.

Conclusions

The modified performance discharge test for the 250 VDC battery was performed

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successfully and appeared to meet TS requirements. The inspectors had some

follow-up questions concerning assumptions made in identifying the limiting

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electricalload profile for the 250 VDC battery system.

M2.4 Standby Liauid Control System Testina

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a.

Inspection Scooe(93702. 61726)

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The inspectors observed portions of OCTS 0340-01, " Standby Liqu'd Control

j.

System Outage Surveillance" performed on Unit 2. The inspectors attended a pre-

job briefing and observed operators in the field. The inspectors also followed up on

an NRC ENS notification on April 7,1997, when the SBLC system on Unit 1 was

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' declared inoperable due to low system flow during quarterly surveillance testing.

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b.

Observations and Findinas

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The outage surveillance tested portions of the SBLC system that could not be

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routinely tested during reactor operations. The inspectors attended the pre-job

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briefing and noted good communication among operators. One equipment operator

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specifically asked for an additional operator to assist in " peer check." The

inspectors observed the portion of the test designed to verify the pump suction

lines from the storage tank were not plugged. The test results were satisfactory.

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The. inspectors reviewed the test requirements against the TSs and noted that the

test was designed to satisfy surveillance requirements for SBLC system specified in

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TS 4.4.A.4 and for isolation actuation specified in TS 4.2.A. The initiation of SBLC

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causes the isolation of the RWCU. The inspectors verified that the procedure

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tested the isolation function. However, this portion of the test was not identified

under the performance acceptance criteria section or under the discussion section

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which listed the TS requirements which were satisfied by the procedure. The

licensee recently performed an audit of TS surveillance requirements and had also

noticed the deficiency and planned to fix the procedure.

On April 7,1997, operators declared Unit 1 SBLC system inoperable when the

j

measured flow for each of the pumps was in the required action range of the

inservice test (IST) program criteria. The TS flow requirement of 40 gpm was

satisfied. The IST program baseline for the Unit 1 pumps was established at

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44 gpm with the required action range either greater than 48.4 gpm or less than

40.9 gpm. The measured flow for each pump during the surveillance was 40 gpm.

Once the pumps were declared inoperable, operators entered the action statement

for TS 3.4.A.1 which required at least one pump be restored in 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or the unit

to bo in hot shutdown in the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

1

The licensee immediately suspected the flow meter which was in-line to the test

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tank since there were past problems associated with the meter. Under work

request 970040020-01, instrument maintenance mechanics adjusted the zero

reference for the flow meter. The flow test for the pumps was then successfully

performed. The inspectors reviewed the calibration history for the flowmeters and

found that the meters were sent offsite for calibration once a year. The inspectors

reviewed the calibration data and found that the flow meter was often found to be

out of tolerance during the as-found testing. The system engineer was aware of -

the problems with this particular type of flow meter and had identified a new style

flowmeter to use. However, the modification packago initiated in 1995 had not yet

been approved. The inspectors found that the margin between the established

baseline flow rate of the pump and the IST and TS limits was small which increased

the importance of accurate flow rate measurements. Additionally IST limits were

calculated down to the tenth of a gpm (e.g.,40.9) and the installed gauge was in

increments of 2 gpm. The inspectors reviewed several completed surveillances and

found the operators were recording the flow in whole numbers and not attempting

to read the gauge to meet the IST criteria. In this event, longstanding problems

with the flow meter caused entry into an LCO and required operators to begin a

reactor shutdown.

The vendor manual for the meter stated that a check and adjustment of the

indicator should be performed at an interval established by the customer and that

indicator response should be checked every six months. The inspectors asked

instrument maintenance staff if these checks were performed and found that

adjustment of the indicator was performed during the annualinstallation of the flow

meter and that indicator response was checked during performance of the flow

test.

c.

Conclusion

Longstanding problems with the SBLC flowmeters used to verify SBLC pump

operability led to a failed surveillance, entry into a limiting condition for operation,

and preparations for a unit shutdown. The installed gauge did not allow the

operator to read the flow measurement with the precision required by the IST

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limits. Accurate flow measurement was particularly important in the SBLC system

since little margin existed between the required flow and reference flow of the

pumps. This issue is an unresolved item pendinp NRC review of IST

instrumentation requirements. (URI 50 256:264/97006-06)

4

Ill. Enaineerino

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Conduct of Engineering

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E1.1

Exoansion of Invessel Insoection Activities

4

Based on information received from another nuclear station, the licensee decided to

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expand the scope of interior reactor vessel weld inspections to include core shroud

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vertical welds. The vertical weld inspections added about three days to the outage

schedule. The licensee performed both visual and ultrasonic inspections of four of

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4

the six welds. (The other two welds were considered inaccessible.) These

inspections did not identify any rejectable indications on the welds. The inspectors

considered the addition of this inspection activity to be both warranted and

proactive.

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E2

' Engineering Support of Facility and Equipment

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E2.1

Inocerable Core Sorav Room Cooler Due to Foulina

1

a.

Insoection Scooe (71707. 37551)

The inspectors spoke to system engineering, reviewed room cooler trend charts,

and reviewed the licensees response to Deviation 50-254:265/96015-01. The

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inspectors reviewed Section 3.11.4, 6.3.2.1, and 9.5.5 of the UFSAR and an NRR

safety evaluation related to comer rcom cooler heat removal capability.

s

b.

Observations and Findinas

!

On March 21,1997, with Unit 2 in a refueling outage, the licensee opened and

inspected the "B" core spray room cooler. The licensee found 10 of 18 tubes that

were completely plugged with erosion and corrosion products. Six additional tubes

were significantly plugged. Operations declared the room cooler incperable.

System engineering reviewed room cooler monthly differential p. essure

'

measurements, and concluded the condition existed since abotit June of 1996. In

addition, the shared emergency diesal annerator was inoperable a total of about

]

nine days resulting in the "A" core spray pump room cooler not having an

2

emergency source of elec%ical power.

4

The licensee attributed the blockage of the room cooler to a previous attempt to

hydrolaze upstream service water piping during the refuel outage in Spring of 1995.

This resulted in loosening debris, and later, required disassembly of the room cooler

to remove erosion and corrosion products. The room cooler was placed back in

service.

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In October 1996,in NRC Inspection Report 50-254;265/96015, the inspectors

identified that the licensee had not implemented a 1992 LER commitment te trend

and analyze residual heat removal room cooler differential pressure. Data recorded

by QCOS 5750-09, "ECCS Room and DGCWP [diesei generator cooling water

pump] Cubicle Cooler Monthly Surveillance Test," was not evaluated by the

cognizant system engineer. In 1994, the licensee had removed the acceptance

criteria for the cooler flow surveillance from the procedure, relying on engineering to

trend and analyze the data. In response to the deviation, the licensee evaluated

ECCS room cooler d/p in October 1996. At that time, system engineering identified

2 "B" core spray room cooler had exceeded the maximum criteria .in June 1996.

The room cooler d/p periodically exceeded the maximum criteria and showed an

increasing d/p trend during the operating cycle. System engineering noted this

condition and commented the cooler would be cleaned during the upcoming outage.

This condition was not documented on a PlF and the condition was not evaluated

for operability. In addition, there were no attempts to clean and inspect the room

cooler during plant operation.

The licensee attributed this event to inadequate flushing of the 2 "B" core spray

room cooler after hydotazing, and a personnel error by the system engineer for not

trending and analyzing the room cooler performance. Engineering could not

determine the heat removal capebilities of the degraded "B" core spray room

cooler.

The inspectors noted the shared EDG was inoperable with both units at power from

October 21 to October 27,1996, and from January 15 to January 18,1997. The

shared EDG provided emergency power to Unit 2 "A" core spray equipment. The

emergency source of power to the Unit 2 "A" core spray room cooler was

unavailable and the Unit 2 "B" core spray room cooler was inoperable since

June 1996. The inspectors consider this to have been potentiaHy significant as

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TS 3.5.A.1 required both core spray systems to be operable with Unit 2 in

operation.

During the outage, the licensee also opened and inspected all the other ECCS roorn

coolers except the 2 "B" RHR room cooler. (The 2 "B" RHR room cooler was

planned to be inspected later in the outage.) Flow through the Unit 2 HPCI room

cooler was previously determined to be degraded but not inoperable. The licensee

found pieces of zebra mussel shells plugging scme of the room cooler tubes. In all

cases, the room coolers were cleaned prior to beng returned to service.

c.

Conclusions

The NRC previously identified that engineering did not adequately trend or analyze

room cooler differential pressure for a period of time (see Deviation

50-254:265/96015-01). The system engineer had an opportunity to document,

and evaluate the degraded condition upon responding to the deviation in

October 1996. Missed opportunities to identify, document and analyze the

degraded condition of the core spray room cooler resulted in the licensee operating

a train of core spray for an extended period of time with a cooler in a degraded

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condition without evaluating its effect on operations. Failure to take timely

corrective action for a condition adverse to quality was a violation of 10 CFR,

Appendix B, Criterion XVI " Corrective Action" (VIO 50 254:265/96006-07).

E2.2 Facility Adherence to the UFSAR

While performing the inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors reviewed plant practices, procedures and/or parameters to that described

in the UFSAR and documented the findings in this inspection report. The inspectors

reviewed the following sections of the UFSAR:

IR Section

UFSAR Section

Aoolicability

07.2

13.7

Reccrds

M2.3

8. 3. 2.1

250 VDC System

E2.1

3.11.4, 6.3.2.1, 9.5.5

CS room cooler

For the sections reviewed, no issues with plant configuration or UFSAR accuracy

were identified.

E2.3 Unit 1 Shut Down Due to Dearaded Auxiliary Switches in 4 Kilovolt (kV) Breakers

a.

Insoection Scone (71707,37551)

The inspectors observed licensee inspection of 4 kV breakers and attended

engineering action meetings and plant operations review committee meetings to

evaluate the degraded condition of the breakers. The inspectors monitored

operators during the Unit 1 shutdown.

b.

Observations and Findinas

On February 11,1997, during breaker testing observed by a Quad Cities engineer

at the manufacturer, an auxiliary contact assembly (ACA) on a 4 kV breaker was

found broken. The manufacturer replaced the ACA. On March 5, the licensee

identified a similarly broken ACA on another spare 4 kV breaker. The condition was

documented on PlF 97-0822. On April 1,1997, the licensee identified a third

broken phenolic auxiliary contact assembly (ACA) mounted on a 4 kV breaker prior

to installation in a safety-related bus (PlF 97-1276). The failure resulted in the ACA

physically separating from the support mount. The ACA provided ci itacts for both

local and remote, indication and operation of the breaker. The licensee .nspected

similar spare breakers and identified 12 of 14 breakers with similarly cracked, but

not broken, ACA. The licensee removed and replaced two residual heat removal

service water pump (RHRSWP) breakers in Unit 1 due to finding cracked ACAs. All

of the inservice electrical breakers' ACAs were identified as being intact.

The licensee used Merlin-Gerin breakers in safety-related applications. These

breakers supplied normal power to safety-related busses and power to the

RHRSWPs. Engineering concluded that the breakers installed could not be deemed

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operable based on conditions identified on both installed and spare breakers. The

licensee had not experienced any failures to operate with the installed breakers.

The breakers could be operated locally. However, the licensee declared the

RHRSWP breakers inoperable and commenced shut down of Unit 1 on April 9,

1997, as required by TSs. (Unit 2 was already in a refuel outage when the

deficient condition was identified.)

The licensee tested and implemented a interim repair to the cracked ACAs. The

tests were observed by the inspectors and NRR personnel (see below paragraph).

After the repairs to the ACAs, the affected breakers were considered operable for a

limited number of cycles. The licensee planned to implement random weekly

surveillances to ensure the breaker modification was monitored. The licensee

considered the modification to the breaker as a potential long term repair and

planned to continue testing the modification at an offsite laboratory. The licensee's

long term corrective actions will be tracked by LER 254/97-011.

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c.

Conclusions

The inspectors noted the licensee had prior opportunities to identify the degraded

ACAs condition and effect repairs prior to April 1. Similarly, the inspectors noted

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the PlF 97-0822 was marked by the events screening committee as not being a

potential Part 21 notification. The inspectors considered the licensee's initial

evaluation of PlF 97-0822 to be narrow in scope. Subsequent engineering

evaluation of the ACAs condition resulted in the licensee viewing the condition on a

wider perspective, including Part 21 aspects. The licensee subsequently decided to

declare the breakers inoperable and shut down Unit 1 due to the unknown status of

the electrical breaker ACAs. The additional surveillances to rnonitor the condition

of the ACAs in the affected breakers was deemed by the inspectors to be an

acceptable interim measure untillong term testing of the repair was completed.

E2.4 Modification to Auxiliarv Switch in Merlin-Gerin (M-G) Circuit Breakers

a.

Scope

On April 14,1997, inspectors from NRC headquarters Office of Nuclear Reactor

Regulation (NRR) met with the licensee's staff at the System Materials Analysis

Department (SMAD) and reviewed the actions taken by the licensee to determine

the root cause of the cracking of auxiliary switches installed in 4.16 kilovolt (kV),

M G circuit breakers at Dresden and Quad Cities. The inspectors also examined

some of the failed breakers from Quad Cities and reviewed the licensee's proposed

interim corrective action and development of permanent corrective action in

consultation with the breaker supplier and the manufacturer. On April 15,1997,

the inspectors observed testing of one of the failed M-G breakers at Dresden 2.

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b.

Observations and Firdinas

Root Cause Evaluation

To investigate the cause of the cracks on the switches, SMAD assembled

engineers from Dresden and Quad Cities, representatives from M-G, Square D

Company (M-G's U.S. distributor), and Pacific Breaker Systems (the current

supplier) and modifier of the M-G breakers for General Electric (GE) (Magne-Blast

switchgear). SMAD evaluated numerous possible contributing factors and showed

the inspectors the high-speed videos which captured the motion of the switches

during the opening and closing of the breaker.

SMAD identified two potentially significant factors that distinguished the M-G

breakers at Dresden and Quad Cities from those at other U.S. installations and

abroad: The type of switch wiring connections and the spring discharge feature.

To meet a licensee wiring requirement, the wires to the breaker auxiliary switches

for Quad Cities and Dresden were connected using ring-tongue terminals . screwed

onto the switch terrninals; whereas, all other installations used spado connectors.

In addition, the inspectors pointed out that connecting the wires after the switches

were mounted could subject the switch mounting slots to extra stress during the

tightening of the terminal screws.

The spring discharge safety feature in the Dresden and Quad Cities breakers,

specified by ANSI /IEEE Std C37.04 for U.S. nuclear plants, was unique among all

other installations of the affected type of M-G breakers because those facilities are

the only U.S. nuclear plants with M-G breakers. The spring discharge feature,

actuated by a mechanical rackout interlock for personnel safety, subjects the

breaker to a complete closing and opening cycle in rapid succession every time the

i

breaker is racked out. This feature, with its associated significant increased stress

on the switches (vibration and shock loading), was being considered as a possible

contributing factor to the cracking of the auxiliary switches.

The upper auxiliary switch shaft is the fulcrum for the operating levers which

operate the upper auxiliary switch, the bottom auxiliary switch and the open/close

indicating flag. If the tabs of the mounting slots (which are molded into the

phenolic switch body segments) crack and break off, the mounting T-bolts can

come out of the slots and the switch will break away from its mounting bracket.

However, the switch remained attached to the operating levers by its shaf t and

thus will hang down, typically about 1/4 inch below the mounting bracket. Thus

far, cracks have been found only on the upper switch.

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Failure Effects

Specifically, if the auxiliary switch broke loose as the breaker closed, the breaker

may not have opened electrically (automatic trips, or local or remote hand switches)

unless the upper auxiliary switch changed state. If the auxiliary switch broke loose

'

as the breaker opened, the breaker may not have closed electrically unless the

switch changed state.

Prooosed interim Corrective Action

The licensee's proposed interim corrective action was to replace all upper auxiliary

switches that are broken or have visible pieces missing (but not ones that only have

visible cracks) and then secure all the switches with nylon cable tie (ty-wrap), with

Tygon tubing as chafing gear, as a backup to their regular mounting system. To

test this proposed fix, the licensee cycled a breaker 225 times with the ty-wrap

installed, the rear mounting slot tabs completely broken off and with the nuts

removed from the T-bolts that normally attach the switch to its mounting bracket.

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No failures occurred during this testing. This interim fix was also being seismically

tested at Wyle Laboratories.

Testina of the Bus 23 Feeder Breaker at Dresden.

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On April 15,1997, the inspectors observed the Dresden 2 operating tests of its

Bus 23 M-G feeder breaker (from Bus 23-1). The intent was to demonstrate the

prior operability of this closed breaker, whose local mechanical position indicator

flag was stuck in an intermediate, nearly open position. Control room personnel

opened and closed the breaker successfully several times accompanied by proper

operation of the local and remote indicating lights. However, when the breaker was

opened, the position indicating flag on the breaker would go almost fully closed and

when the breaker was closed, the flag would return to its intermediate, mostly-open

position. When the technicians removed the front cover of the breaker mechanism

enclosure, the inspectors observed that the auxiliary switch was detached from its

mounting bracket and was hanging down about 1/2 inch.

c.

Conclusions

The inspectors concluded that the root cause investigation was proceeding

satisfactorily although not completed. The licensee appeared to be effectively

utilizing its contractors and the contractors were providing adequate support.

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IV Plant Support

R1

Radiological Protection and Chemistry Controls

R 1.1 Torus Suction Header Decon1mination Efforts

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a.

Insoection Scoce (71707)

The inspectors spoka with Radiological Protection and Chemistry Controls (RPC)

staff and reviewed the results of the torus suction header decontamination efforts.

b.

Observations and Findinas

The radiation levels in the torus suction header had historically resulted in the

reactor building basement being treated as a high radiation area. During the recent

Unit 2 refuel outage, the licensee removed the emergency core cooling system

(ECCS) suction strainers and used a robot to clean the torus suction header. This

effort had previously not been used and was considered experimental.

Consequently, equipment problems and schedule slippage resulted in cleaning only

eleven of the sixteen bays. For the areas cleaned, post decontamination surveys

showed doses decreased by up to 50 percent and some areas showed an increase

in dose of up to 20 percent due to redeposition of fine particles.

The licensee intended to incorporate lessons learned from this effort to ensure the

entira torus suction header would be decontaminated during the upcoming Unit 1

refuel octage.

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c.

Conclusio 13.

The inspectors concluded the torus decontamination efforts were good. However,

first time use of equipment resulted in the torus suction ring header

decontamination efforts not being fully completed.

F4

Fire Protection Staff Knowledge and Performance

F4.1

Delinauent Reoortina of Event

On March 27,1997, the licensee identified a previously corrected condition that

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was not reported in accordance with 10 CFR 50.72 requirements. The licensee's

fire hazards analysis report required protection of low pressure piping frem high

pressure systems. The licensee identified that during a postulated fire, no

procedures were in place to ensure low pressure portions of the reactor water

cleanup piping would be protected from the high pressure recirculation system.

This condition was documented on PlF 97-1132 and LER 50-254/97008. The

licensee attributed this event to an incomplete understanding of the licensee's safe

shutdown analysis. The licensee revised a procedure to correct the condition by

May 28,1996, but did not report the condition until March 27,1997.

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The licensee did not report the condition as being outside the design basis until ten

months later. Failure to report the condition is considered a violation of 10 CFR 50.73. However, this licensee-identified and corrected condition was Non-Cited

Violation (50-254:265/97006-08), consistent with Section Vll.B.1 of the

j.

Enforcement Policy.

V. Manaaement Meetinas

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X1

Exit Meeting Summary

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The inspectors presented the inspection results to members of licensee management at the

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conclusion of the inspection on May 2,1997. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

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should be considered proprietary. No proprietary information was identified,

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PARTIAL LIST OF PERSONS CONTACTED

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Licensee

B. Pearce, Station Manager

D. Cook, Operations Manager

F. Famulari, Site Quality Verification Director

J. Hutchinson, Site Engineering Manager

J. Kudalis, Support Services Director

J. Purkis, Work Control Supervisor

B. Svaleson, Radiation Chemistry Superintendent

M. Wayland, Maintenance Superintendent

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 39701:

Records Program

IP 61726:

Surveillance Observations

IP 62706:

Maintenance Rule Inspection Procedure

IP 62707:

Conduct of Maintenance

IP 71707:

Plant Operations

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

IP 93702:

Prompt Onsite Response to Events at Operating Power Reactors

ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

50-254;265/97006-01

VIO

failure to maintain the proper revisions of

operating procedures

50-254:265/97006-02

VIO

failure to properly implement test procedure

50-254:265-97006-03

VIO

failure to identify quality records and to establish

retention requirements

50-254;265/97006-04

NCV Unit 1 EDG start due to personnel error

50-254:265/97006-05

IFl

250 volts direct current battery testing

50-254:265/97006-06

URI

IST instrumentation requirements

50-254;265/97006-07

VIO

Core spray room cooler clogged and degraded

50-254:265/97006-08

NCV delinquent reporting of event

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failure to maintain the RHR room watertight door

closed in accordance with TSs

50-254:265/96006-04

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inattentive test director

50 254:265/97006-04

NCV Unit 1 EDG start due to personnel error

50-254i265/97006-08

NCV delinquent reporting of event

50-265/95007

LER

Unit 2 HPCI turning gear motor failed to start as

the turbine coasted to a stop

-50-254:265/97007

LER

. Unit 1 EDG start due to personnel error

Discussed '

50 254:265/97002-07

URI

Maintenance Rule issues

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LIST OF ACRONYMS AND INITIALISMS USED

AC

Alternate Current

ACA

' Auxiliary Contact Assembly

ALARA

As Low As Reasonably Achievable

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ANSI

American National Standards institute

ASME

American Society of Mechanical Engineers

CAM

Containment .^tmosphere Monitor

CCST-

Contaminated Condensate Storage Tank

CFR

Code of Federal hegulations

CRD

Control Rod Drive

d/p

differential pressure

DC

Direct Current

DGCWP

Diesel Generator Cooling Water Pump

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EHC

Electrohydraulic Control

EMD

Electrical Maintenance Department

ENS

Emergency Notification System

EPA

Electrical Protection Assembly

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ESC

Event Screening Committee

FME

Foreign Material Exclusion

GE

General Electric

GL

Generic Letter

HCU

Hydraulic Control Unit

HPCI

High Pressure Coolant Injection System

HVAC

Heating Ventilation and Air Conditioning

(DNS

tilinois Department of Nuclear Safety

IFl

Inspector Follow-up Item

IRM

Intermediate Range Monitor

IST

inservice Test

kV

Kilovolt

LCO

Limiting Condition for Operation

LER

Lice ~nsee Event Report

LOCA

Loss-of-Coolant Accident

MCC

Motor Control Center

MEG

Materials Engineering Group

MG

Motor Generator

MPFF

Maintenance Preventable Function Failure

MRFF

Maintenance Rule Functional Failure

MSDT

Moisture Separator Drain Tank

NCV

Non-Cited Violation

NOA

Nuclear Quality Assurance

NSO

Nuclear Station Operator

PDR

Public Document Room

PIF

Problem Identification Form

PORC

Plant Oversight Review Committee

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QCAP-

Quad Cities Administrative Procedure

OCCP <

Quad Cities Chemistry Procedure

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Quad Cities Instrument Surveillance

OCOA

Quad Cities Operating Abnormal Procedure

QCOS

Quad _ Cities Operating Surveillance Procedure

QCTS-

Quad Cities Technical Staff Procedure

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OOA

. Quad Cities Operating Abnormal Procedure

OOP

Quad Cities Operating Procedure -

QOS-

Quad Cities Operating Surveillance Procedure

RCIC

Reactor Core Isolation Cooling System

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RG'

Regulatory Guide

RHR

Residual Heat Removal

RHRSWP

Residual Heat Removal Service Water Pump

RPC

Radiological Protection and Chemistry Controls

RPS-

Reactor Protection System

RWCU

Reactor Water Cleanup

.SBLC

Standby Liquid Control

SDC

Shutdown Cooling

, SIL .

Service Information Letter

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Site Quality Verification

TS-

Technical Specification

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UFSAR

Updated Final Safety Analysis

.VDC

Volts Direct Current

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VIO

Violation

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