ML20141A239

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Insp Rept 50-333/97-04 on 970413-0525.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20141A239
Person / Time
Site: FitzPatrick 
Issue date: 06/13/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20141A231 List:
References
50-333-97-04, 50-333-97-4, NUDOCS 9706200189
Download: ML20141A239 (36)


See also: IR 05000333/1997004

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U.S. NUCLEAR REGULATORY COMMISSION

Region I

l.icense No.:

DPR-59

Report No.:

97-04

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Docket No.:

50-333

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Licensee:

New York Power Authority

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Post Office Box 41

Scriba, New York 13093

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Facility Name:

James A. FitzPatrick Nuclear Power Plant

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Dates:

April 13,1997 through May 25,1997

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Inspectors:

G. Hunegs, Senior Resident inspector

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R. Fernandes, Resident inspector

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K. Cotton, Project Manager

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J. McFadden, Radiation Specialist

W. Schmidt, Senior Resident inspector

R. Skokowski, Resident inspector

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Approved by:

John F. Rogge, Chief, Projects Branch 2

Division of Reactor Projects

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9706200189 970613

PDR

ADOCK 050LJ333

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EXECUTIVE SUMMARY

James A. FitzPatrick Nuclear Power Plant

NRC Inspection Report 50-333/97-04

Operations

On May 17, the licensee commenced a downpower to take the generator off line in

order to make repairs to a 345 KV line bolted connection in the switch yard. The

licensee's decision to take the unit off line to conduct repairs demonstrated a sound

thought process with a solid safety focus. Operators demonstrated good control of

the plant during the evolution.

The process to control operator workarounds appeared to be functioning well and

received good management attention.

The licensee is in the process of completing licensed operator requalification

examinations. On May 21,1997, the inspector observed simulator scenarios

conducted for an operating crew examination and noted that licensed operators

demonstrated solid performance.

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An NRC team inspection was conducted to evaluate the effectiveness of licensee

controls in identifying, resolving, and preventing issues that degrade the quality of

plant operations or safety. These licensee controls include safety review

committees, root-cause analysis programs, corrective action programs, self

assessment programs, and other processes that provide for incorporation of

operating experience feedback.

The licensee implemented an effective problem identification and corrective action

program. The Plant Operation and Safety Review Committees provided an

appropriate level of oversight and the well supported Quality Assurance audits were

considered to be a strength. Additionally, licensee management was actively

involved in the self-assessment and corrective action process.

Based on interviews, the licensee has increased their awareness of human

performance issues and recently implemented semo programs to reverse the past

negative trends in human performance.

Maintenance

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Both the technical issue report and the maintenance rule processes appear to be

working hand-in-hand to allow proper management attention to system performance

issues. System engineers understood the problems of their particular systems.

However, based on equipment performance, it appeared that the licensee's previous

corrective actions taken to address emergency service water and primary

containment isolation valve issues were not fully effective.

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Executive Summary (cont'd)

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An anonymous concern about the quality of maintenance performed by a valve

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maintenance contractor during the 1996 outage was brought to the licensee's

employee concern program through a handwritten report. The licensee's initial

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review, followed up with a subsequent review of valve operating history, provided

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an acceptable level of confidence that valve maintenance performed by the vendor

was adequate and had not contributed to system performance issues. Although

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there were several valve maintenance performance issues identified during the

outage, those issues were addressed through the licensee's corrective action

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program.

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The inspectors considered the strong operations background of the work week

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managers to be a positive attribute of the work control organization. Corrective

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actions associated with identified work control process weaknesses have been

effectively implemented and an improved questioning attitude was noted. The

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weekly and special evolution critiques were a good tool for the identification and

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correction of problems within the work control process.

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Overall, good management oversight of the temporary modification program was

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evident. The older temporary modifications appear to lack engineering support but

are not safety significant. The number of temporary modifications has been

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consistent over the past two years and does not appear to adversely impact plant-

operations.

The licensee's response and planned corrective actions to the nonconforming scram

solenoid pilot valves demonstrated a good safety focus.

Plant Sucoort

Overall, the licensee's corrective action program for the radiological protection

program was acceptable. Identification and characterization of deviations and

events were also acceptable, however, weaknesses were identified in review for

extent of condition and in response to repetitive problems. Also, the evaluation and

documentation of each identified deviation and event for generic implications was

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considered to be a weakness. The elevation of identified deviations and events to a

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proper level of management was adequately addressed. Self-identification of

problems by front-line personnel and their willingness to do so seemed to be

increasing,

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Executive Summary (cont'd)

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Two separate incidents concerning improper entry into a radiological controlled area

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occurred on April 16,1997. Also, in December,1996, two radiation workers did

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not adhere to the radiation work permit, disregarded radiological posting

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requirements and one worker improperly used the portal monitor. These failures of

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radiation workers to comply with radiation protection instructions are a violation.

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As there have been several other cases where mistakes have been made concerning

radiation protection requirements, it appears that corrective actions for previous

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similar licensee findings were not fully effective.

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TABLE OF CONTENTS

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EXEC UTIVE S U MM A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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TA B L E O F CO NT E NTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v

Summ a ry of Pla nt Statu s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. O P E R AT I O N S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01

Conduct of Operations . . . . . . . . . . . .. . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 General Comments

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01.2 345 KV Boited Connection Repair . . . . . . . . . . . . . . . . . . . . . . . 1

01.3 Operational Safety Verification . . . . . . . . . . . . . . . . . . . . . . . . . 2

01.4 Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

O2

Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 4

O2.1 Engineered Safety Feature System Walkdowns

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Operator Training and Qualification . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

05.1 Licensed Operator Requalification Training . . . . . . . . . . . . . . .

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Quality Assurance in Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

07.1 Corrective Action Program Overview . . . . . . . . . . . . . . . . . . . . 5

07.2 Problem Identification and Corrective Action

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07.3 Plant Operations Review Committee . . . . . . . . . . . . . . . . . . . . . 6

07.4 Safety Review Committee (inspector Followup Item 50-

3 3 3 /9 7 0 04-01 ) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

07.5 Quality Assurance Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

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07.6 Self Assessment Program . . . . . . . . . . . . .

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07.7 Human Performance

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11. M A I NT E N A N C E . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

M1

Conduct of Maintenance

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M 1.1 General Comments

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M1.2 General Comments on Surveillance Activities . . . . . . . . . . . . . . 12

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M1.3 Conclu :ons on Conduct of Maintenance . . . . . . . . . . . . . . . . . 13

M3

Maintenance Procedures and Documentation . . . . . . . . . . . . . . . . . . . 13

M7

Quality Assurance in Maintenance Activities

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M7.1 Valve Maintenance Performed by a Contractor . . . . . . . . . . . . . 14

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M7.2 Work Control

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M8

Miscellaneous Maintenance issues

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M8.1 (Closed) Unresolved item 50-333/95001-01

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M8.2 (Closed) LER 5 0-3 3 3 /9 5 00 8 . . . . . . . . . . . . . . . . . . . . . . . . . . 17

M8.3 (Closed) LER 5 0-3 3 3 /9 601 1 . . . . . . . . . . . . . . . . . . . . . . . . . . 17

M8.4 (Closed) Violation 50-3 3 3/9 600 2-01 . . . . . . . . . . . . . . . . . . . . 18

111. E N G I N E E RI N G . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

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Conduct of Engineering

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E1.1

Control of Temporary Modifications

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Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . 19

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Table of Contents (cont'd)

E2.1

Nonconforming Scram Solenoid Pilot Valves

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Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

E8.1

(Closed) Violation 5 0-3 3 3/9 500 6-02 . . . . . . . . . . . . . . . . . . . . 20

E8.2 (Closed) LER 50-333/96-005

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E8.3 (Closed) Inspector Followup Item (IFI) 50-333/92014-01

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E8.4 (Closed) Unresolved item 50-333/95002-01

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I V. PL A NT S U PPO RT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

R7

Quality Assurance in Radiological Protection and Chemistry (RP&C)

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Activities

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R7.1

Effectiveness of Licensee Controls in Identifying, Resolving,

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and Preventing Problems

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R7.2 Improper RCA Entry by Escorted Visitors (Violation 50-

3 3 3 /9 7004-0 2 ) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

R8

Miscellaneous RP&C lssues (VIO 50-33 3/97004-02) . . . . . . . . . . . . . . 25

R8.1

(Closed) Unresolved item 50-333/95002-02 and EA 96-096 . . . 25

R8.2 (Closed) Unresolved item 50-333/96008-03

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Miscellaneous Fire Protection issues . . . . . . . . . . . . . . . . . . . . . . . . . 25

F8.1

(Closed) Enforcement (EA) 50-333/95-142

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V. MANAGEMENT MEETINGS

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X1

Exit Meeting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

X2

Review of UFSAR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

X3

Pre-Decisional Enforcement Conference Summary

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Report Details

Summarv of Plant Status

The unit began this inspection period at 100 percent power. On May 17, the unit was

taken off line to effect repairs to a bolted connector on the 345 KV line. The plant was

returned to 100 percent power on May 19. On May 24, the number 3 turbine control

valve failed open. As the valve is normally full open, all pre-transient plant parameters

remained normal. The licensee began a plant shut down to make repairs. Originally, the

licensee intended to shut the valve manually, however, the valve would not operate. At

70 percent reactor power, the licensee inserted a manual reactor scram and tripped the

main turbine. Shutdown cooling was entered on May 25 and the licensee implemented a

short forced outage.

1. OPERATIONS

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Conduct of Operations'

01.1 General Comments

The inspectors conducted frequent reviews of ongoing plant operations. In general,

operations were conducted well. Specific events and noteworthy observations are

detailed in the sections below.

01.2 345 KV Bolted Connection Repair

a.

Inspection Scope

The main generator provides power through transformers which step up the voltage

to 345 KV for distribution to the electrical grid. The licensee had been monitoring a

345 KV bolted connection located in the switchyard which was showing signs of

degradation. Due to a rapid increase in a thermography reading, the licensee

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elected to take the unit off line to conduct repairs. The inspector reviewed the

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work package and discussed the activity with operations and engineering personnel.

b.

Observations and Findinas

On May 17, the licensee commenced a downpower to take the generator off line in

order to make repairs to a 345 KV line bolted connection in the switch yard. The

licensee performs routine predictive maintenance on the bolted connections using

thermography. Inspection showed that the bolted connection was not tight, which

caused increased resistance and a higher temperature. The connection was cleaned

and reassembled using guidance provided by the manufacturer. Other connections

on the 345 KV line were checked and were satisfactory. The cause for the

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connector degradation was indeterminate, but the licensee stated that it was

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' Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized

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reactor inspection report outline. Individual reports are not expected to address all outline

topics.

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possibly due to less than optimum original installation which caused slow

degradation over time.

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The licensee had evaluated performing the repair wit.i the unit "n line. However

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due to the nature of and risks associated with the job, the licensee concluded that it

was more prudent to take the unit off line to conduct the repair.

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Conclusions

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The licensee's decision to take the unit off line to conduct the repair demonstrated a

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sound thought process with a solid safety focus. Operators demonstrated good

control of the plant during the evolution.

01.3 Operational Safety Verification

The inspectors observad plant operation and verified that the facility was operated

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safely and in accordance with procedures and regulatory requirements. Regular

tours were conducted of the plant with focus on safety related structures and

systems, operations, radiological controls and security. Additionally, the operability

of engineered safety features, other safety related systems and on-site and off-site

power sources was verified. No safety concerns were identified as a result of these

tours.

The inspection activities during this report period included inspection during normal,

backshift and weekend hours. Regular tours were conducted of the following plant

areas:

control room

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secondary containment building

radiological control point

electrical switchgear rooms

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emergency core cooling system pump rooms

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security access point

protected area fence

intake structure

diesel generator rooms

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Control room instruments and plant computer indications were observed for

correlation between channels and for conformance with technical srecification (TS)

requirements. Operability of engineered safety features, other safety related

systems and onsite and offsite power sources wt > varified. The inspectors

observed various alarm conditions and confirmed .r.:.t operator response was in

accordance with plant operating procedures. Compliance with TS and

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implementation of appropriate action statements for equipment out of service was

inspected. Plant radiation monitoring system indications and coolant stack traces

were reviewed for unexpected changes. Logs and records were reviewed to

determine if entries were accurate and identified equipment status or deficiencies.

These records included operating logs, turnover sheets, system safety tags, and

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temporary modifications. Control room and shift manning were compared to

regulatory requirements and portions of shift turnovers were observed. The

inspectors found that control room access was properly controlled and that a

professional atmosphere was maintained. Daily supervisor meetings were attended

to assess personnel focus on risk significant items and plant priorities.

Specific plant issues which were followed up on included control rod drive hydraulic

control unit TS issues,345 KV line maintenance, fire protection hoso station

storage, uninterruptible power supply (UPS) motor generator (MG) set maintenance.

a low lube oil pressure alarm on "D" emergency diesel generator (EDG) and licensed

operator requalification training. These issues were managed effectively by the

licensee.

01.4 Operator Workarounds

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a.

Inspection Scone

The inspectors revievied the licensee's program used to identify and track operator

workarounds and also discussed the status of workarounds with plant operator and

maintenance personnel,

b.

Observations and Findinas

The licensee uses a quarterly surveillance test (ST) 99H, Operator Workarounds

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Assessment, to document the workaround, the procedures affected and the

compensatory measure in place. The procedure provides a good format for

identification and dc4cumentation of workarounds and the evaluation criteria for

workarounds appeaied to be well organized, enabling operators to assess the

impact on plant operations. The licensee defines an operator workaround as any

deficiency that would require compensatory operator actions in the execution of

normal operating prc,cedures, abnormal operating procedures, emergency operating

procedures, or annunciator response procedures.

Equipment issues appear to be tracked well and compensatory measures appeared

adequate. Additionally, the inspectors found that the list of workarounds received

good management attention, in part through routine discussions at morning

meetings.

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Conclusions

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The process to control operator workarounds appeared to be functioning well and

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received good management attention.

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Operational Status of Facilities and Equipment

O2.1 Engineered Safety Feature System Walkdowns

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The inspectors performed a walk down of accessible portions of the following

systems and performed general area tours:

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eemergency diesel generator

eintake structure

eemergency service water

oresidual heat removal service water

ehigh pressure coolant injection

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Equipment operability, material condition and housekeeping conditions were good.

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Operator Training and Qualification

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05.1 Licensed Operator Requalification Training

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a.

Inspection Scope

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The licensee is in the process of completing licensed operator requalification

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examinations. On May 21,1997, the inspector observed simulator scenarios

conducted for an operating crew examination. The inspector discussed training

with instructors including simulator fidelity, training requirements and training

initiatives and attended the post scenario critique.

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b.

Observations and Findinas

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During the exercises observed, the inspector noted good use of peer checking to

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validate decision making, good use of appropriate procedures including alarm

response procedures, abnormal operating procedures, emergency operating

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procedures and the emergency plan and good use of three point communications by

operators.

The evaluator's critique provided constructive criticism of the crews performance

using specific evaluation criteria.

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Conclusions

Licensed operators demonstrated solid performance during recent licensed operator

requalification examinations which were observed.

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Quality Assurance in Operations

07.1 Corrective Action Program Overview

An NRC team inspection was conducted to evaluste the effectiveness of licensee

controls in identifying, resolving, and preventing issues that degrade the quality of

plant operations or safety. These licensee controls include safety review

committees, root-cause analysis programs, corrective action programs, self

assessment programs, and other processes that provide for incorporation of

operating experience feedback.

To assess the ability of the FitzPatrick management and staff to identify and correct

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problems at the site, the inspectors conducted structured interviews of plant

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personnel. The team reviewed the deficiency event report (DER) process,

equipment performance trending and use of the maintenance rule, operator

workarounds, activities of oversight committees including the plant operations

review committee (PORC) and the safety review committee (SRC), the involvement

of the Quality Assurance (QA) organization and the use of self-assessment.

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Further, based on several recent operational events and radiological control

problems, the inspectors specifically reviewed the identification of issues and

corrective actions taken in the areas of human performance, work control and

radiological controls.

07.2 Problem Identification and Corrective Action

a.

insoection Scope

Procedures which implement the problem identification end corrective action

program were reviewed and a sample of DERs were evaluated to assess program

effectiveness.

b.

Observations and Findinas

The licensee has developed several procedures to govern the problem identification

and corrective action program. These procedures included: Administrative

Procedure (AP)-03.02, Deviation and Event Reporting; AP-03.03, Deviation and

Event Analysis; AP-03.08, Action and Commitment Tracking System; ORG-SO-

03.02, Deviation and Report Screen:ng. The procedures address the identificction,

evaluation and corrective actions process for plant deficiencies. The procedures

provided controls for tracking, trending, and closure. Causal screening levels varied

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from A (most severe) through D (least severe) and were used to screen deviations

and events based both on degree of risk of recurrence and on significance.

Deficiency and Event Report (DER) evaluation types, included root cause analysis,

team root cause analysis, post transient review, critique, equipment failure

evaluation, written response, and none (trend only). All evaluations shall, as a

minimum, include extent of condition when appropriate.

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The inspectors determined that the DER process was effectively used to identify

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and document issues at a proper level for resolution and operability /reportability

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reviews appeared to be acceptable. The equipment failure evaluations (EFEs) and

root cause analyMs enclosures to the DER procedure were well developed and

provided good ger, err' formats and guidance for conducting such evaluations. EFEs

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and root caun ane ysis completed for several DERs in the last year were of good -

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quality and effec +.ive corrective actions were identified.

Several minor program weaknesses were identified including the fact that

procedures do not provide for the ideltification of repeat problems, although,

personnel who review DERs have an informal process to identify repeat problems.

Additionally, documentation did not always indicate that an extent of condition

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review was completed. Although the licensee stated that an extent of condition

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consideration is always performed, the lack of documentation of this evaluation was

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considered a weakness. The licensee's QA department has previously identified

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this concern and several other issues, and correctivs actions were in process.

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c.

Conclusions

The licensee implemented an effective problem identification and corrective action

program. DER tracking was conducted well; specific reviews specified by

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procedures and the associated corrective actions generally appeared good. Several

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areas for improvement including the identification and documentation of repeat

problems and the documentation of extent of condition reviews were identified.

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07.3 Plant Operations Review Committee

a.

Inspection Scoce

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The inspectors assessed the Plant Operations Review Committee (PORC) activities

and verified that selected PORC activities were performed in accordance with the

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TS. A PORC meeting was attended, applicable procedures and PORC meeting

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minutes were reviewed and six members of PORC were interviewed.

b.

Observations and Findinas

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The inspectors reviewed Procedures AP-01.01, " Plant Operating Review

Committee," Revision 7, and ORG-SO-03.03, "PORC Administration," Revision 0,

and verified that TS requirements pertaining to PORC were adequately included.

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The inspectors attended PORC Meeting 97-18 held April 1,1997. The inspectors

verified that the quorum requirement was met, and that the meeting was

accomplished in accordance with the approved procedures. Although the meeting

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briefly discussed issues related to the overall safe operation of the plant, the

meeting was focused on a review of open PORC action items. These were ACTS

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items opened during PORC meetings that PORC tracks for closure. Of the 14 PORC

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action items due for closure, only one item was closed, and the remaining 13 were

extended. The PORC members seemed aware of the issues associated with each

item. However, only one item was challenged to ensure there was no safety

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concern that should prevent the extension. In general, the PORC members seemed

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cognizant of the issues discussed.

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Based on the large percentage of PORC action items extended during the April 1,

1997, meeting, the inspectors reviewed previous PORC meeting minutes to

determine the extent to which PORC action items have been extended in the past.

Of the 16 PORC items closed in 1997, eight were closed on their original due date.

The inspectors reviewed the items extended in detail and identified no safety

concerns with the extensions. The inspectors discussed the issue of PORC action

item extensions with several members of the PORC and ascertained that, routinely

due dates are selected prior to the expected completion of the work to provide

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PORC with a working status of the item. Additionally, the PORC members

expressed that other items were extended due to more significant emergent issues,

which required the planned work to be delayed. Although a large percentage of

PORC action item due dates have been extended, no safety concerns were

identified with the extensions.

PORC recently changed the controlling procedure to include requirements to discuss

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the " Broad Assessment of the Safe Operation of the Plant" during each meeting.

According to the PORC Chairman, this section was adde, to ensure the PORC was

looking at the " big picture" during each meeting. The information for discussion

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was to be provided by the PORC members on an impromptu basis. The inspectors

reviewed PORC minutes for eight meetings held after the incorporation of this new

requirement. Although two of the eight meeting minutes reviewed indicated no

discussion in tNs area, the minutes for the other six meetings indicated a wide

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range of discussion topics that t,enefited PORC. For example, PORC Meeting 9713

discussed the impact of tne recent loss of engineers from personnel resignations.

c.

Conclusions

In general, the PORC members seemed cognizant of the issues discussed. Although

a large percentage of PORC action item due dates have been extended, safety

appeared to have been appropriately considered in the extensions. PORC's initiative

to routinely discuss the broad assessment of the safe operation of the plant

enhanced PORC's ability to identify potential problems.

07.4 Safety Review Committee (Inspector Followup Item 50-333/97004-01)

a.

Insoection Scope

The inspectors assessed the Safety Review Committee (SRC) oversight activities

and verified that selected SRC activities were performed in accordance with the TS.

Applicable procedures and the scheduled SRC meeting minutes since January 1,

1996, were reviewad and the plant manager was interviewed regarding SRC

activities.

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b.

Observations and Findinas

The inspectors reviewed Procedures SRCP1, " Charter," Revision 12, SRCP8,

" Reviews," Revision 8, and SRCP9, " Audits," Revision 10, and verified that the TS

requirements pertaining to the SRC were either met or exceeded.

The inspectors reviewed the minutes for the six scheduled SRC meetings completed

in 1996, and determined that the SRC provided an appropriate level of oversight on

corrective actions for significant issues, as evidenced by the tracking of "significant

areas of risk." During 1996, the SRC was tracking three "significant areas of risk"

at Fitzpatrick, including Radiological and Environmental Services (RES) human

performance, corrective action programs and engineering rigor. The areas of

significant risk were discussed during each SRC meeting until the issue was closed.

In addition to the "significant areas of risk," the inspectors noted that problems

pertaining to human performance and engineering performance appeared repeatedly

in the SRC meeting minutes.

SRC was tracking RES human performance and corrective action programs as

"significant areas of risk" prior to 1996. The concern associated with RES human

performance gained SRC's attention as a result of numerous deficiencies in the RES

area. This "significant area of risk" was closed in November 1996, following

indication of adequate corrective actions through the Fall 1996 refueling outage.

The concerns associated with the corrective action program related to corrective

action implementation and the assessment of whether these actions were effective.

Based on progress made in DER evaluation timeliness and management's focus on

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the corrective action timeliness, SRC closed this "significant area of risk" for the

licensee in July 1996. The updates regarding RES human performance and

corrective actions programs provided to the SRC, as described in the meeting

,

minutes, were thorough and provided adequate information for the SRC to evaluate

the situations,

Engineering rigor was added as a "significant area of risk" in November 1996,

based on four NRC violations described in Inspection Report (IR) 50-333/96007,

with the purpose of monitoring the thoroughness and timeliness of engineering

processes, evaluations and response to events. Prior to classification as a

"significant area of risk," the SRC discussed engineering-related concerns on several

i

occasions. These discussions were based on other NRC Inspection Reports and QA

Audit A96-04J. This QA audit identified particular concerns with ineffective

corrective actions for past engineering-related deficiencies. Therefore, based on the

concerns raised by the QA audit, previous NRC inspection findings, and the

untimely completion of engineering-related corrective actions described in Section

07.5 (QA), the adequacy of the er rrective action program for engineering issues is

'

considered an inspector followup item (IFI) (50-333/97004-01).

c.

Conclusions

The SRC provided an appropriate level of oversight on corrective actions to

significant issues during 1996, as evidenced by the tracking of "significant areas of

risk." The updates provided to the SRC, as described in the meeting minutes were

thorough, and p;ovided adegaate information for the SRC to evaluate the situations.

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The SRC's perception of the licensee appeared to be consistent with the indications

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provided in DERs, audits, self-assessments and trending reports. Concerns

associated with the timeliness and adequacy of the corrective actions for

engineering issues is considered an inspector followup item.

07.5 Quality Assurance Activities

a.

Inspection Scope

The inspectors assessed the licensee's OA Department's ability to identify problems

and adverse trends in performance. Also assessed was the timeliness, quality and

effectiveness of the licensee's actions taken in response to QA findings. The

inspectors reviewed selected QA audits, surveillances, procedures, and QA-initiated

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Deviation / Event Reports (DERs) and Action / Commitment Tracking System (ACTS)

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items, and applicable licensee trending reports. The inspectors also interviewed

licensee personnel, including QA management and QA auditors.

b.

Observations and Findinas

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The inspectors discussed the QA function with QA management and staff. The -

inspectors ascertained that the QA organization was staffed with individuals having

strong operations, engineering and maintenance experience. The inspectors found

this experience evident in the depth of the auditor's findings.

The inspectors reviewed all, or portions, of the following QA audits and

surveillances:

Audit Report A96-11J, "Results of Actions Taken to Correct Deficiencies,"

dated July 17,1996;

)

Audit Report A96-20J, "JAF (James A. Fitzpatrick] Results of Actions Taken

]

to Correct Deficiencies," dated January 27,1997;

Audit Report A96-09J, " Maintenance Activities Program Audit," dated

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June 18,1996;

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Audit Report A96-04J, " Design Control," dated April 12,1996; and

Surveillance 1913, " Management Controls PORC [ Plant Operations Review

Committee]/SRC [Sofety Review Committeel Activities," dated October 15,

1996.

The surveillance and audits were completed in accordance with the licensee's

Procedures, QAP 18.2 (J), " Quality Assurance Surveillance Program," Revision 1,

and QAP 18.1-J, " Quality Assurance Audit Program," Revision 4. The inspectors

found issues identified in these audit and surveillance reports consistently well

supported.

A review of the Quarterly Integrated Self-Assessment Trend Reports indicated that,

,

over the last six quarters, an average of 11 % of all DERs initiated for the station

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were initiated by QA. The inspectors reviewed a list of those DERs initiated by QA

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since January 1,1996, and, based on this list, the inspectors considered the

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percentage and type of DERs identified by QA to be reasonable.

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The inspectors reviewed the weekly Corrective Action Monitoring Program Reports

issued by QA for the weeks of March 26 through April 9,1997. The reports

provided trend information regarding QA-initiated DERs issued, closed, and overdue

over the last 12 months; and corrective action QA ACTS itemr, open, overdue, and

pending QA review. Additionally, the reports described, in detail, the open QA

i

ACTS items greater than a year old, and listed all the open QA ACTS items with

selected information, such as the issue date, due date, the number of times the due

date had been extended, and the number of times the proposed corrective actions

had been rejected by QA. The inspectors considered these reports to be a good

tool to keep plant management abreast of long-standing issues.

The April 2,1997 Corrective Action Monitoring Program Report documented that

the due dates for 85 of the 151 open QA ACTS had been extended. The large

percentage of corrective action ACTS items being extended had been identified in

1

the last two QA audits of the licensee's corrective actions program. QA Audit 96-

11J indicated that " extension requests appear to be the norm, rather than the

)

exception," and QA Audit 96-20J indicated similar concerns. Although the practice

of extending ACTS items appeared excessive, no negative consequen :es were

)

identified from these extensions. Furthermore, as of the week of April 14,1997, all

extension requests for QA-related ACTS items greater than one year old were to be

reviewed by the plant manager.

The April 2,1997, Corrective Action Monitoring Program Report indicated that

13 of 21 QA-related ACTS items open for greater than one year were the

responsibility of design engineering. Additionally, of these 13 ACTS items, two

were associated with ineffective corrective actions. Further discussion regarding

engineering-related corrective actions is provided in Section 07.4 of this report.

Also, during the review of the April 2,1997, report, the inspectors noted that 11 of

the 151 open QA ACTS items had the associated corrective actions rejected by QA.

The corrective actions for one ACTS item were rejected three times. The inspectors

discussed the rejection rate with QA management and ascertained that since the

beginning of the year,10 out of 464 (appropriately 2.16%) proposed ACTS item

corrective actions reviewed by QA were rejected. The inspectors considered the

rejection rate to be rersonchte, and an indication of a good balance between

adequate corrective actions and adequate QA acceptance reviews.

c.

Conclusions

The strong industry experience of the QA auditors was evident in the depth of their

findings. Audit reports findings were consistently well supported. The weekly QA

Corrective Action Monitoring Provam Reports were considered a good tool to keep

plant management abreast of long t.tandicg issues. Although the practice of

extending ACTS items apreared excessa, no negative consequences were

identified from these enensions. The rocently implemented plant manager review

of all extension reques:s for QA-related ACTS items greater than one year old

indicated increased ma.vgement attention to long-standing issues. The QA

rejection rate of reviewed proposed corrective actions appeared reasonable, and

indicated a good balance between adequate corrective actions and adequate QA

acceptance reviews.

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07.6 Self Assessment Program

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a.

Insoection Scope

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The inspector reviewed department self-assessments, documented management

observations and the performance enhancement review committee meeting minutes

and interviewed personnel. Operation review group (ORG) quarterly reports for

,

1996 and 1997 were also reviewed.

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b.

Observations and Findinas:

<

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The licensee has a formal self assessment program as described in various licensee

"

internal audit procedures. The inspectors reviewed several self assessment reports

and found that these reports were self-critical and thorough.

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ORG quarterly reports were considered to be an excellent resource for plant

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managers to trend the overall and departmental performance. The report

statements were generally concise and provided specific insight into past

i

performance problems.

,

c.

Conclusions

,

,

Licensee management was actively involved in the self-assessment and corrective

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action process. The evaluation of a sampling of the departmental self-assessment

,

findings showed consistency with previous inspecuon findings as well as other third

party audits. ORG quarterly trend reports were considered to provide a valuable

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,

summary of plant performance.

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07.7 Human Performance

a.

Inspection Scope

,

i

The inspectors reviewed a recently completed licensee human performance report

l

and interviewed licensee personnel. The inspectors attended a Performance

!

Enhancement Review Committee (PERC) meeting and reviewed several meeting

minutes and the associated lessons learned that had been generated,

b.

Observations and Findinas

!

Due to several significant human performance errors, the licensee developed a

human performance team to examine human performance and develop

t

recommended corrective actions. The inspector reviewed the report and corrective

actions recommended and considered that the report provided a good appraisal of

the licensee's performance in this area. Through interviews, the inspector

determined that the awareness of human performance issues has increased greatly

i

since this effort.

The PERC is a committee which meets on a regular basis to review personnel errors

in an effort to improve human performance. In reviewing the committee, the

inspectors found that DERs were properly screened for PERC review if personnel

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12

performance was possibly an issue. The inspector attended a meeting and noted

that the meeting was conducted well. The PERC reviewed severalissues regarding

an unauthorized exit of the radiologically controlled area. In this case, the PERC

focused on what corrective actions may be appropriate to prevent such an event in

the future. Meeting minutes were incorporated into DER packages for tracking and

trending purposes. However, there was an example where the corrective actions

specified by PERC were not documented on the DER form, although through other

document review, it was clear that some actions had in fact been taken.

The inspector noted that the licensee has also recently implemented several new

observation programs (Worker for a Day, Coach of the Day, and Coach of the

Week), in an effort to improve human performance at FitzPatrick.

c.

Conclusions

Based on interviews, the licensee has increased their awareness of human

performance issues and recently implemented some programs to reverse the past

negative trends in human performance. The PERC program was a generally

effective process to investigate human performance issues.

II. MAINTENANCE

M1

Conduct of Maintenance

i

M 1.1 General Comments

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a.

Inspection Scooe

The inspectors observed all or portions of the following work activities:

  • WR 97-02992 RCIC steam admission valve 13 MOV 131 repair
  • WR 97-02901 Uninterruptible power supply
  • WR 97-02431345 KV bolted connection repair

b.

Observations and Findinas

The inspectors found the work performed under these activities to be professional

and thorough. Technicians were experienced and knowledgeable of their assigned

task.

M1.2 General Comments on Surveillance Activities

a.

Inspection Scoce

The inspectors observed selected surveillance tests to determine whether approved

procedures were in use, details were adequate, test instrumentation was properly

calibrated and used, technical specifications were satisfied, testing was performed

by knowledgeable personnel, and test results satisfied acceptance criteria or were

properly dispositioned.

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The inspectors observed portions of the following surveillance activities:

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eST 24A reactor core isolation cooling pump test

eST 20C control rod operability

eST 8C emergency service water motor operated valve test

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b.

Observations and Findinas

The licensee conducted the above surveillance activities appropriately and in

I

accordance with procedural and administrative requirements. Good coordination

and communication were observed during performance of the surveillance activities.

M1.3 Conclusions on Conduct of Maintenance

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Overall, maintenance and surveillance activities were well conducted, with good

adherence to both administrative and maintenance procedures.

M3

Maintenance Procedures and Docurnentation

a.

Inspection Scoce

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The inspectors reviewed the methods used to track equipment problems and failures

>

including the technical issues report (TIR) and maintenance rule (MR)

'

implementation. To assess maintenance rule implementation related to the

identification and tracking of system performance, the inspectors reviewed the high

pressure coolant injection system, safety relief valves, emergency service water

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(ESW) and primary containment isolation valves (PCIV) and discussed the issues

with the applicable system engineer.

b.

Observations and Findinos

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The TIR appeared to be a good way of focusing emphasis on specific plant

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equipment issues. For each item listed, the report contained a problem statement,

plant impact, corrective actions, and a place to note any particular problems in the

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resolution. For systems categorized as (a)(1) under the maintenance rule, the report

also included a statement on when the system would be returned to an (a)(2) status

I

under the maintenance rule. The inspectors noted good tracking of equipment

failures and identification of systems to be placed in (a)(1) status. The recovery

1

plans for (a)(1) systems were detailed and provided good insight into past problems

'

and the plans for addressing performance concerns.

I

c.

Conclusions

Both the TIR and the maintenance rule processes appear to be working hand-in-hand

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to allow proper management attention to system performance issues. System

engineers understood the problems of their particular systems. Based on equipment

]

performance, it appeared that the licensee's previous corrective actions taken to

address ESW and PCIV issues were not fully effective.

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M7

Quality Assurance in Maintenance Activities

M7.1 Valve Maintenance Performed by a Contractor

a.

Insoection Scoce

An anonymous concern about the quality of maint'enance performed by a valve

maintenance contractor during tne 1996 outage was brought to the licensee's

employee concern program through a handwritten report. The individual's key point

was that work, particularly documentation and use of procedures, performed by the

contractor was of poor quality. Additionally, a stripped stud was left in place rather

than replaced and valve bolting torque requirements were questioned. Concerns

with specific salves and valve maintenance requirements were not documented.

The individual also wrote to " turn over this report to the NRC."

The inspectors reviewed the licensee's investigation reports of the concern,

reviewed work history for applicable valves including post work and rework and

discussed the issue with the licensee. Additionally, a sample of valves were

inspected.

b.

Observations and Findinas

The inspector determined that the contractor repaired or performed preventive

'

maintenance on 114 valves and valve operators, primarily in the condensate

domineralizer system.

The licensee conducted a review of the contractor's work as documented in a

licensee memo dated January 8,1997. The review included a sample of

maintenance packages which the licensee found to be acceptable, although several

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administrative errors were identified and corrected. The licensee also noted that the

maintenance valve engineer provide oversight of the contractor during the outage

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and a QA surveillance report no. 96-0005 dated December 11,1996 also

documented good performance by the contractor.

The licensee conducted an additional review of the operating history including work

requests and deficiencies of all valves worked on by the valve contractor and

conducted walkdowns of a sample of valves. Results of that review were

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documented in a licensee memorandum dated May 13,1997. The licensee

i

identified no adverse condition existed with valve operation based on the

maintenance history review and valve walkdown and concluded that sufficient time

had elapsed during which the applicable systems had been in service to provide an

opportunity for problems to surface.

c.

Conclusions

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The licensee's initial review, followed up with a subsequent review of valve

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operating history, provided an acceptable level of confidence that valve

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maintenance performed by the vendor was adequate and had not contributed to

system performance issues. Although there were several valve maintenance

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performance issues identified during the outage, those issues were addressed

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through the licensee's corrective action program.

M7.2 Work Control

a.

Lnsoection Scope

Due to recent events which had contributing causes related to the work control

process, the inspectors assessed the ability of the work control department to

identify and correct problems. To complete this assessment, the inspectors

reviewed a sample of DERs related to work control and work planning initiated

within the last nine months, and evaluated the root causes and corrective actions.

The inspectors also reviewed internal critiques performed by work control staff and

,

the actions taken to address identified concerns. Applicable procedures were

reviewed and work control management, supervisors, planners and work week

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managers were interviewed.

b.

Observations and Findinas

The inspectors discussed the work control process and organization with work

control management and staff. The inspectors ascertained that the work control

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organization was staffed with severalindividuals having strong operations

backgrounds. For example, three of the four work week managers were either

reactor operator or senior reactor operator qualified. The inspectors considered the

i

strong operations background of the work week managers to be a positive attribute

of the work control organization.

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Through discussion with a work control supervisor, the inspectors ascertained that

since January 1,1997, approximately 3100 work requests have been implemented.

~

Of those work requests, there have been five cases where DERs were written

related to deficient plant impact evaluations. In addition, the inspectors reviewed a

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list of DERs issued since January 1,1997. Of the 348 DERs liated, six were

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associated with the work control program and 19 had an apparent cause related to

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planning.

i

On September 16,1996, during the performance of a relay calibration, two

terminals were inadvertently shorted together, resulting in a main turbine trip and

subsequent reactor scram. The details associated with this event were described in

NRC IR 50-333/96006. The inspectors reviewed the work control-related corrective

actions contained in DER 96-1060 associated with the scram. The corrective

)

actions included changes to Procedure AP-10.03, " Work Control Planning," to

j

provide more detailed requirements regarding the pre-job walkdown of the work site

i

to assess the potential impact from equipment in the vicinity of the work to be

accomplished. Other corrective actions identified in DER 96-1060 were to reinforce

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the need for technicians to protect adjacent equipment when working on energized

i

equipment, to reinforce the need for technicians not to become complacent or over-

confident in their work, and to stop work in situations when they identify a plant

impact not noted within the work package. The inspectors considered these

corrective actions associated with the work control process to be appropriate.

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The effectiveness of the corrective actions for the September 1996 scram was

assessed by reviewing subsequent DERs associated with either the work control

process or that had an apparent root cause associated with work planning. Seven

DERS were reviewed, four of which were written for items where one or more of

the barriers in the work control process had f ailed, but the discrepancies were

identified prior to actualimplementation of work. In at least three cases, the

discrepancy was identified by the technicians. The three remaining DERs,

associated with discrepancies not identified until after the work was initiated,

related to missed administrative requirements or poor scheduling issues with little -

impact on plant safety. The inspectors reviewed the proposed or completed

corrective actions for these seven DERs and considered them to be appropriate.

The three DERs initiated for cases where the technician stopped work when

discrepancies were identified, indicated an improved questioning attitude.

The inspectors reviewed the corrective actions for DER 97-106 regarding the

January 23,1997, simultaneous removal of two traveling screens from service,

which contributed to plant shutdown when a large influx of fish clogged the screen.

The details associated with this event were described in NRC IR 50-333/97001.

Traveling screens were normally removed from service and inspected weekly under

minor maintenance controls. Minor maintenance activities required less review than

those activities performed under the work request process. The apparent causes

for the simultaneous removal of two traveling screen, as described in the DER,

included:

A lack of communications between work control and operations,

poor decision on operations part to take both screens out of service

simultaneously, and

a new requirement associated with the protective tagging process.

The proposed corrective actions were reviewed and found to appropriately address

the root causes. Furthermore, during the inspectors' review of DERS initiated over

i

the last nine months, no additional problems were identified regarding the minor

maintenance process.

Through discussion with various members of the work control organization, the

inspectors ascertained that, although work control had not performed a formal self

assessment, the organization routinely critiques the completed work week activities

and special evolutions. The inspectors reviewed a random sample of four weekly

critiques and the critique of the March 22,1997, down-power. The weekly

critiques provided statisticalinformation pertaining to schedule adherence and

shortcomings within the quality of the work packages and scheduling. When

appropriate, the weekly critiques provided recommendations to address the

identified shortcomings. The down-power critique was extensive; areas for

improvement and recommendations were identified. Discussions with the work

control supervisor indicated that the recommendations from the weekly and special

evolution critiques were normally incorporated into the schedule preparation

checklist. The inspectors verified that several previously identified

recommendations were in-f act added to the checklist. The inspectors considered

the weekly and special evolution critiques to be a good tool for the identification

and correction of problems within the work control process.

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c.

Conclusions

The inspectors considered the strong operations background of the work week

managers to be a positive attribute of the work control organization. The corrective

actions associated with the work control process initiated as a result of the

September 1996, scram were effectively implemented, and the proposed or

completed corrective actions for other DERs associated with the work control

process were appropriate. In addition, the three DERs initiated f r cases where the

technician stopped work when discrepancies were identified inucated an improved

questioning attitude. The weekly and special evolution critiques were a good tool

for the identification and correction of problems within the work control process.

M8

Miscellaneous Maintenance issues

M8.1 (Closed) Unresolved item 50-333/95001-01: Reactor pressure vessel (RPV) nozzle

examinations. During the review of inservice inspection (ISI) data, the inspector

identified a concern regarding the need for additional attention to procedural quality

and adherence. The licensee completed several action commitment tracking system

(ACTS) items to address the specific concerns identified in NRC inspection reports-

50-333/95001 and 95-400. In NRC inspection report 50-333/96-07 dated

December 13,1996, an NRC Region I non-destructive examination (NDE) technician

reviewed the licensee's ISI program and concluded that the program was well

documented, controlled and implemented. The documentation supporting the

examinations was accurate and readily available for review. Additionally, an ISI

program checklist was provided which was an improvement over previous controls

and that the licensee demonstrated good oversight of the NDE subcontractor and

NDE examinations. Based on the licensee's completion of the ACTS items to

address the specific concerns and a subsequent ISI program review by the NRC, the

issues identified in the URI have been addressed.

i

M8.2 (Closed) LER 50-333/95008: High Pressure Coolant Injection (HPCI) System Trip on

Overspeed Due to Procedure Deficiency. On March 26,1995, while conducting

post refuel outage testing, the HPCI turbine tripped on overspeed when a cold quick

start test was attempted. The licensee determined that the system flow controller

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output current limit circuit adjustment was not included in the calibration procedure

1

and therefore, not properly adjusted following replacement during the refuel outage.

Corrective actions included proper adjustmerit of the flow controller and satisfactory

retest of the HPCI turbine. The reactor core isolation cooling (RCIC) flow controller

)

was also verified by the licensee to be properly set. The calibration procedures for

the flow controllers were revised to include the requirement to adjust the current

limit circuits. The inspector verified that corrective actions had been completed and

reviewed subsequent quick start surveillance testing of HPCI and RCIC systems for

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similar problems.

M8.3 (Closed) LER 50-333/96011: Both Standby Liquid Control Subsystems

inoperable Due to Inoperable Pump Discharge Pressure Relief Valves. On

October 29,1996, while in cold condition for refueling the licensee

'

determined that both standby liquid control (SLC) system pump discharge

relief valves were found with lift setpoints below the technical specification

required range of 1400 to 1490 psig. Relief valve 11SV-39A lifted at 1380

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psig and 11SV-39B lifted at 1310 psig. Corrective actions included replacing

one valve and adjusting the relief setpoint for the second valve. In addition,

the licensee completed an equipment failure evaluation and test interval

evaluation as the B side relief valve had failed during the previous test. The

licensee determined the setpoint drift of the relief valves to be the result of

cyclic pressure spikes from the operation of the reciprocating positive

displacement SLC pumps. Additional corrective actions included increased

frequency of bench testing baseo on setpoint drift data and evaluating the

reinstallation of the hydraulic accumulators which were part of the original

system design.

M8.4 (Closed) Violation 50-333/96002-01: Foreign material exclusion (FME) controls.

Requirements to maintain system cleanliness while performing maintenance on the

pressure relief system were not met. The licensee programmatic corrective actions

included additional training, assessment of the effectiveness of the corrective

actions, review of refueling outage work packages and changes to the

administrative procedure for maintaining system and component cleanliness. The

inspector reviewed training records, procedural changes, licensee program

assessment and audit documentation, and recent plant deficiency report history for

FME issues. Licensee corrective actions appear to have been effective.

lli. ENGINEERING

E1

Conduct of Engineering

E1.1

Control of Temporary Modifications

a.

Insoection Scope

The inspector reviewed the temporary plant modification control program

including procedures, performance indicators and implementation.

Additionally, specific temporary rnodifications were also assessed.

b.

Observations and Findinas

Historically, the average number of temporary modifications has been about

34 over the past two years. The current number is 37, with the oldest two

involving modifications to enhance the chemistry of the service water system

which are scheduled for permanent installation. There are currently 16 non-

outage temporary modifications and 21 which require an outage to address.

Six of the " outage required" temporary modifications are scheduled for the

next forced outage. The inspector determined that five temporary

modifications were for additional plant performance monitoring, four were

equipment enhancements waiting permanent installation, and 28 were the

result of equipment deficiencies. Ten temporary modifications involved

system leakage, seven of which are steam leak repairs on non-safety related

equipment. Twenty-five of the temporary modifications to correct equipment

deficiencies were on balance-of-plant components and not safety significant.

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The inspector reviewed the status of the temporary modifications following the

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completion of last refueling outage and noted that of the six open temporary

modifications, four were installed on start-up as a result of equipment deficiencies,

one was of a housekeeping nature and one lacked engineering support.

Modification 95-098, which lacked engineering support, could have been done

during the outage but was not. The modification involved the installation of

.

capacitors on several reactor manual control system (RMCS) relays which had

contributed to some previous RMCS timing problems during the previous cycle.

Although the problem has not repeated itself to date, no clear explanation was

available as to why the permanent modification was not completed during the

outage.

~

The inspector also reviewed deficiency event reports for the last year which

documented problems with the temporary modification program. In general,

J

the inspector noted that problems were of an administrative nature and were

being addressed by the licensee,

c.

Conclusions

Temporary modifications were being effectively managed and all temporary

'

modifications were scheduled for removal or permanent installation. The

older temporary modifications appear to lack engineering support, but are not

,

safety significant. The number of temporary modifications has been

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consistent over the past two years and does not appear to adversely impact

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plant operations. Overall, good management oversight of the temporary

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I

modification program was evident.

)

E2

Engineering Support of Facilities and Equipment

E2.1

Nonconforming Scram Solenoid Pilot Valves

4

a.

Insoection Scope

On May 5,1997, the licensee was notified by General Electric that an

>

investigation into observed air leakage past the core disc in the scram

solenoid pilot valves (SSPV's) at another facility was caused by incorrect

!

core disc elastomer material supplied with some valves. The NRC was

notified through the Emergency Notification System in accordance with

-

10 CFR Part 21 of the potential safety related problem. The inspector reviewed the

licensee's response to the issue and reviewed the justification for continued

operation (JCO) completed by the licensee,

b.

Observations and Findinos

l

The safety function of the scram solenoid pilot valves is to ensure rapid

insertion of the control rods during an automatic or manual scram. To

perform this, the core disc in the SSPV has to isolate the air system from the

scram valves when the SSPV is de-energized. The vendor had determined

!

that some of the SSPVs it had provided to various licensees had nitrile

(BUNA-N) vice the intended material, fluorocarbon (Viton). The concern

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20

involved the susceptibility of the BUNA-N to harden due to thermal stresses

from elevated temperatures, and subsequently lack the ability to provide a

good seal. The licensee received 50 of the suspected SSPVs and determined

that 24 had been installed in the plant. As each control rod drive unit

contains two SSPVs, the installed group encompassed 18 control rod drive

units.

The licensee determined, based on vendor information, that the drives were

operable. The basis for the decision was focused on the vendor's

information that the disc have a service life of three to four years. The

SSPVs were shipped to the licensee in October of 1994. Corrective actions

by the licensee includes replacing the suspected SSPVs by October 17,1997

and development of augmented leakage testing as suggested by the vendor,

c.

Conclusions

The licensee's response and planned corrective actions to the nonconforming

SSPV demonstrated a good safety focus.

E8

Miscellaneous Engineering issues

E8.1

(Closed) Violation 50-333/95006-02: Fire protection program procedures not

maintained. On March 19,1995, Carbon Dioxide was inadvertently discharged into

the relay room during a surveillance test. The cause was that the surveillance test

was not changed to include a portion of a logic change modification. The causes

for the condition were that the engineering design organization did not identify the

logic change and the review of the surveillance test procedure for implementation of

the modification change was inadequate. To address these causes, the licensee's

engineering department developed a system to review major modifications including

procedure changes and their impact on operations and maintenance and developed

an adequacy review process to ensure that all changes are reflected on modification

documents and affected procedures. The licensee implemented their corrective

'

actions through a new procedure, Site Engineering Standing Order (SESO)-11,

Modification Teams and Adequacy Review Process, implemented on October 2,

1995, to formalize a modification team concept. The procedure provides

instructions and a framework to minimize the amount of design and personnel

errors. Attachments to the procedure include system drawing markup guidance and

a modification adequacy review checklist. The checklist provides a list of key

modification requirements which were overlooked on past modifications, issues

j

identified through the licensee's corrective action process and items from

modification critiques. Additionally, the inspector verified that the commitments

documented in the licensee's response to the Notice of Violation dated June 8,

l

1995 were completed.

E8.2 (Closed) LER 50-333/96-005: Error in Safety Limit Minimum Critical Power

Ratio Calculation. On April 16,1996 General Electric (GE) informed the

4

licensee that preliminary recalculation of the cycle specific safety limit

minimum critical power ratio (SLMCPR) may be more limiting than

determined by the original calculations. Subsequently the licensee was

notified by GE that the cycle 12 SLMCPR in the technical specifications,

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1.07, was incorrect and should be 1.08, which was a non-conservative

.

error. The licensee reviewed the operating records for the cycle and

determined that the fraction of the operating limit MCPR had at no time

exceeded 0.98 and therefore there was no potential that the new SLMCPR

would have been violated in the event of a limiting abnormal operating

'

occurrence. In addition the SLMCPR for cycle 13 was verified to be correct

and an Operating License amendment request for the cycle 12 SLMCPR was

submitted. The inspector reviewed the Technical Specification change

request and the administrative controls that were put into place at the time

of the event. The corrective actions were complete and no other concerns

were identified.

E8.3 (Closed) Inspector Followup Item (IFI) 50-333/92014-01: Relay room Carbon

Dioxide (CO2) discharge test. NRC inspection report 50-333/92014 section 6.6.3

documented the performance of a discharge or an acceptable National Fire

l

Protection Association (NFPA) code test on the relay room carbon dioxide system.

i

The test performed identified significant problems with the relay room and control

I

room ventilation system and the licensee developed an action plan to address the

issues. NRC inspection report 50-333/92023 provided a detailed review of the

licensee's action plan and concluded that the plan was acceptable for unit restart

and power operation. Specifically, the proposed modification to the relay room

ventilation system and the subsequent CO2 full discharge verification testing

appeared to be appropriate and that no additional or immediate safety concerns

remained. The licensee installed a modification which consisted of altering the relay

'

room ventilation system to isolate prior to a CO2 discharge, relocating the relay

room CO2 vent path and replacing a fire door to minimize leakage into the control

room. in lieu of performing a full CO2 discharge test, an alternate test methodology

~

was utilized. The alternate test was an enclosure integrity test and tracer gas air-

exchange test. In NRC inspection report 50-333/95002, the inspector witnessed

i

the performance of a relay room CO2 test as a follawup. The purpose of the test

was to collect data for a subsequent engineering analysis and confirmation of the

relay room es a carbon dioxide protected enclosure. IFl 50-333/92014-01 remained

open pending review of the results of the test. In NRC inspection report 50-

333/95006, the completion of the relay room CO2 system modification and

subst,quent testing was determined to satisfy the licensee's commitment to the

'

NRC to return the relay room CO2 fire suppression system to an operable status

prior to startup from the 1994-95 refueling outage. However, the inspector

questioned the adequacy of alternate trace gas CO2 fire suppression system testing

j

in meeting requirements.

Alternate CO2 fire suppression system testing is discussed in NRC Information Notice (IN) 92-28, Inadequate Fire Suppression System Testing, dated April 8,

1992. The IN documents that full discharge testing of CO2 fire suppression

i

systems may present certain hazards at operating nuclear power plants and that

some licensees have used alternative testing methods which avoid these hazards.

The alternate testing is an enclosure integrity test and tracer gas air exchange test

which is acceptable per NFPA standards. Data is obtained from the tests for use in

an engineering analysis.

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The inspector reviewed the engineering analysis and discussed the issue with the

fire protection engineer. The inspector noted that the engineering analysis, using

the data from alternate tracer gas testing, demonstrated that an adequate

concentration of fire suppression agent for the required soak time was available.

E8.4 (Closed) Unresolved item 50-333/95002-01: Discrepancies with containment spray

system. During the performance of a containment spray header and nozzle air test,

the licensee identified that one of the spray nozzles had no air flow due to an

internally instz!Ied plug. A subsequent engineering review of the condition

determined that this condition was acceptable and that the system was operable.

However, several engineering aspects of the issue were still under review at the end

of the inspection period. Specifically, the reason the nozzle was plugged had not

been determined and drawing and design basis documentation did not reflect the as

found condition.

The inspector reviewed design basis document (DBD)-010, Residual Heat Removal

System, and verified that the design basis document was updated to reflect the

actual condition concerning the number of drywell spray header nozzles.

Additionally, the inspector noted that a design document open item (DDOI) had

been initiated to revise applicable drawings to indicate the actual configuration. The

1

licensee determined that there were no modifications which would have installed

the plug. However, it was determined that the plug was internally installed, which

was most likely from original construction.

IV. PLANT SUPPORT

R7

Quality Assurance in Radiological Protection and Chemistry (RP&C) Activities

R7.1 Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

a.

Inspection Scope

t

To determine the effectiveness of licensee controls in identifying, resolving and

preventing problems in the radiological protection area, the inspector reviewed the

licensee's corrective action program including procedures, documentation, root

cause analysis performed and discussed the program with RP&C personnel.

Additionally, walkdowns of the radiological controlled area (RCA) were performed.

b.

Observations and Findinas

The licensee's Quarterly Integrated Self-Assessment and Trend Report for the

Fourth Quarter of 1996 noted that the number of DERs written in the Radiation

Protection functional area during the fourth quarter of 1996 was more than three

times the average number written during previous outage quarters. Of the seventy-

five DERs generated, fifty-two were for personnel contaminations, and nine others

were for contamination control issues. The licensee characterized this three-fold

increase as an improving trend based on the increased willingness and instruction

for self-identification of problems by plant personnel at the worker level rather than

by management, the quality assurance organization, or external organizations. Plant

.

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personnel at the worker level identified 87.2% of the DERs written for this period.

The licensee stated that their review of outage personnel contaminations, triggered

by the large documented number, was an example of escalation of characterization

and evaluation type required for a DER. Their review concluded that most of the

contaminations were unrelated and of low safety significance. Findings in NRC

Inspection Reports 50-333/96007 and 97001 documented similar low safety

significance concerning the personnel contaminations. The licensee also pointed

out that a DER (97-0427) was written on April 17,1997, which would escalate the

characterization and the type of evaluation required for recurring non-adherence to

radiological safety postings at RCA boundaries. However, the fact that this

escalation and subsequent effective corrective action intended to prevent recurrence

did not occur eallier in time was considered a weakness in this area.

The evaluation of each identified deviation and event for generic implications

(extent of condition) was not apparent. Procedure AP-03.03, Deviation and Event

Analysis, provided the methodology for evaluating deviations and events, identifying

their causes, and recommending corrective action to prevent their recurrence.

Section 8.3.3.E stated, in part, that all evaluations shall, as a minimum, include

extent of condition when appropriate. A large number of inspector-reviewed DERs

did not include any documented statement concerning extent of condition.

Although the licensee stated that an extent nf condition consideration is always

performed, the lack of documentation of this evaluation and the evaluation's basis

was considered a weakness.

The elevation of identified deviations and events to a proper level of managemes,t

appeared to be adequately addressed. Responses to DERS required two levels of

management approval before submittal to the ORG. To track action items

generated to resolve DERS to completion, Procedure AP-03.08, Action and

Commitment Tracking System (ACTS) was used. ACTS items associated level A

and B DERS required two levels of management approval before closure. ACTS

items associated with lesser level DERS required at least one level of management

approval before closure.

c.

Conclusions

l

Overall, the licensee's corrective action program for the radiological protection

program was acceptable. The adequacy and timeliness of corrective actions were

acceptat,

axcept that the corrective actions for non-adherence to radiological

safety postings at the boundaries of radiologically-controlled areas (RCAs) was

found to be inadequate. Identification and characterization of deviations and events

were also acceptable, but evaluation of extent of condition and corrective actions of

possibly recurrent deviations and events in appropriate situations were not evident

in the documentation and therefore considered to be weaknesses. Also, the

evaluation and documentation of each identified deviation and event for generic

,

i

implications was considered to be a weakness. The elevation of identified

deviations and events to a proper level of management was adequately addressed.

i

Self-identification of problems by front-line personnel and their willingness to do so

seemed to be increasing.

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R7.2 Improper RCA Entry by Escorted Visitors (Violation 50-333/97004-02)

a.

Insoection Scoce

On April 16,1997, two licensee-identified events occurred concerning improper

RCA entry. The inspector reviewed the events, past performance in RCA access

controls and discussed licensee corrective actions with RP&C management.

b.

Observations and Findinas

April 16 and 17,1997, had been designated career days during which parent

employees were allowed to bring and si ow their children around their workplace.

On April 16,1997, at approximately 9:45 a.m., with the plant operating at

approximately 100% power, the licensee discovered that, in two separate incidents

at times earlier that morning, minor visitors (two children by one parent employee

and one child by another parent employee) were escorted inadvertently into a RCA

(the cable tunnell by their parent employees without authorization for RCA entry.

The two parent employees were both currently trained radiation workers and

qualified to be visitor escorts. The visitors were not authorized or monitored for

radiation exposure as required by procedure. The access point used was posted

with a yellow and magenta Caution Radioactive Material posting, which stated that

the area was an RCA, that only authorized personnel were to enter, and that a TLD

was required for entry. This area was not controlled with a radiation work permit

(RWP). The licensee had posted the area because the condensate piping and

chemical drain piping in the area were internally contaminated with small amounts

of radioactive material and because this radioactive contamination resulted in low

gamma dose rates external to the piping.

The dose consequences to the visitors involved in these events were calculated to

be negligible. A licensee survey of general area dose rates in the cable tunnel

shortly after the incident indicated that

the maximum and average exposure rates were 0.3 and approximately

i

0.1 millirem / hour, respectively. A documented dose evaluation by the licensee for

thesc two incidents indicated that the maximum transit time in the cable tunnel was

6 minutes, that the maximum individual dose to the unmonitored individuals was

O.03 millirem, and that the calculated individual dose is less than the minimum

l

reportable dose of 10 millirem for the licensee's personnel TLD radiation badge.

The area was scheduled to be surveyed for removable contamination on a quarterly

basis due to its low potential for such contamination to exist. Quarterly surveys of

this area on February 13,1997 and on April 23,1997 indicated that general area

removable radioactive contamination was less than 1000 disintegrations per 100

square centimeters. The visitors exited the protected area through radiation portal

monitors in the security access building without exceeding the alarm setpoint of the

monitors. These latter facts indicated that there was no significant removable

'

contamination in the cable tunnel area.

Technical Specification 6.11 states that procedures for personnel radiation

protection shall be prepared and adhered to for all plant operations. Procedure

i

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AP-07.00 (Rev. 0), Radiation Protection Program, in Section 6.1.5, states that

radiation workers shall comply with written and oral Radiation Protection (RP)

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25

instructions. The inspector noted that, during the last six months, there had been

four similar incidents involving non-adherence to radiological safety postings at the

boundaries of RCAs, including an incident on December 7,1996, involving a non-

licensed operator who improperly exited the RCA. It appears that past corrective

actions concerning RCA access were not fully effective. The failure of radiation

workers to comply with posted RCA access instructions resulted in minors entering

a posted RCA and is a violation (VIO) (50-333/97004-02),

c.

Conclusions

The two separate incidents on April 16,1997 constituted two examples of failure to

,

comply with written instruction (i.e., postings) since the escorted visitors had not

been provided TLDs and had not been authorized for entry into a RCA. Corrective

actions for previous similar licensee findings were not effective in preventing these

incidents.

R8

Miscellaneous RP&C issues (VIO 50-333/97004-02)

R8.1

(Closed) Unresolved item 50-333/95002-02 and EA 96-096: Improper dosimetry

use by a visitor. The licensee determined that a visitor entered the RCA using

dosimetry not issued to him by the site dosimetry office. Additionally, the

contractor supervisor had the visitor log into and out of the RCA using a different

persons name. The NRC Office of Investigations (01) reviewed the event and a

violation concerning this willful act was issued in a letter to the licensee dated

May 2,1996. The licensee's response dated May 31,1996 documented corrective

,

actions including changes to dosimetry control procedures to provide more stringent

administrative control and the conduct of pre-outage briefings to discuss the

violation and station requirements. The inspector verified that the licensee's

corrective actions have been completed. Additionally, the inspector reviewed DERs

and discussed the event with licensee personnel and determined that there have

been no similar events.

R8.2 (Closed) Unresolved Item 50-333/96008-03: Improper radiation worker practices

by a non-licensed operator. This item documented that there were several

radiological control barriers and radiation worker practices which were not adhered

to by two workers which resulted in one worker becoming contaminated. These

requirements which were not met included the failure to obtain a radiation control

brief, not adhering to the radiation work permit, wearing inadequate anti-

contamination clothing, disregarding radiological postirg requirements and improper

use of the portal monitor. The deficient radiation wo'ker practices are similar to the

event described in paragraph R.7.2 above in that inJividuals exhibited poor radiation

j

worker practices. Accordingly, this Unresolved item is closed based on including

this issue as an example of violation 50-333/97004-02.

F8

Miscellaneous Fire Protection issues

F8.1

(Closed) Enforcement (EA) 50-333/95-14'2: Unauthorized approval of combustion

control permit. On February 3,1995, the licensee informed the NRC that results of

an internal investigation of a combustible control permit (CCP) authorization

identified that a fire protection supervisor / fire inspector inappropriately used the Fire

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I

(

Protection System Engineer's signature on a permit. On July 27,1995, the NRC

issued a violation of NRC requirements set forth in 10 CFR 50.9. In the cover letter

'

to the violstion, the NRC recognized that significant corrective actions had been

taken, including comprehensive review of all current and previously issued / closed

combustion control permits to identify any further discrepancies; conduct of a

i

formal critique of the unauthorized CCP and related events, training to reemphasize

procedure compliance and procedure revisions. The licensee responded to the

Notice of Violation in a letter dated August 28,1995 and committed to completion

of a Quality Assurance assessment of the fire protection program. The inspector

verified that the corrective actions documented in the licensee's response had been

'

completed and reviewed the Quality Assurance audit report A 95-15W, Annual and

Biennial Fire Protection Audit. The audit identified weaknesses in the area of

management attention to address human performance errors, the need to sirnplify

the combustible control permit procedure, development of trending in fire protection

and review of fire protection documents. The licensee addressed the issues

i

identified in the OA audit,

j

V. MANAGEMENT MEETINGS

X1

Exit Meeting Summary

The inspectors presented the inspections results to members of the licensee management

at the conclusion of the inspection on June 10,1997. The licensee acknowledged the

findings presented.

J

'

The inspectors asked the licensee whether any materials examined during the inspection <

should be considered proprietary. No proprietary information was identified.

The preliminary results of the team inspection were discussed with licensee management

on April 18,1997 and an exit meeting with licensee management was conducted on

April 24,1997.

l

1

X2

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner contrary a the Updated

Final Safety Analysis Report (UFSAR) description highlighted the need for a special focused

review that compares plant practices, procedures and/or parameters to the UFSAR

,

'

description. While performing the inspections discussed in this report, the inspector

reviewed the applicable portions of the UFSAR that related to the areas inspected. The

inspector verified that the UFSAR wording was consistent with the observed plant

practices, procedure and/or parameters.

X3

Pre-Decisional Enforcement Conference Summary

On May 8,1997, a pre-decisional enforcement conference was held in the NRC Region I

office, to discuss potential enforcement issues identified in Inspection Report 50-333/

97-003. The issues related to a March 3,1997 inadvertent control rod withdrawal event,

j

Results of the enforcement conference including slides used in the presentation at the

I

conference are included with the letter to the licensee under EA No.97-118.

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I-

PARTIAL LIST OF PERSONS CONTACTED

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Licensee

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J. Bracy, Administrative Coordinator (RES)

i

J. Maurer, General Manager, Support

,

A. McKeen, Manager, Radiological and Environmental Services (RES)

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E. Mulcahey, General Supervisor, Radiological Engineering

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P. Policastro, Radiological Supervisor

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C. Sherman, Radiological Technician

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R. Steigerwald, Acting Manager, Operational Review Group

S. Wisla, General Supervisor, Health Physics

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None

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INSPECTION PROCEDURES USED

l

37551

Onsite Engineering

40500

Effectiveness of Licensee Controls in identifying, Resolving, and

Preventing Problems

62707

Maintenance Observations

61726

Surveillance Observations

71707

Plant Operations

l

71750

Plant Support

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92902

Maintenance Followup

92903

Engineering Followup

92904

Plant Support Followup

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-333/97004-01

IFl

adequacy of corrective action program for engineering issues

50-333/97004-02

VIO

failure to comply with radiation control requirements, two

examples

,

Closed

50-333/92014-01

IFl

relay room Carbon Dioxide (CO2) discharge test

j

l

50-333/95001-01

URI

reactor pressure vessel (RPV) nozzle examinations

50-333/95002-01

URI

discrepancies with containment spray system

i

50-333/95002-02

URI

(E 95-005) improper dosimetry use by a visitor

l

50-333/95006-02 VIO

fire protection program procedures not maintained

'

50-333/96002-01

VIO

foreign material exclusion controls and the pressure relief

system

50-333/96008-03

URI

improper radiation worker practices by a non-licensed operator

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50-333/95-142

ENF

Unauthorized approval of combustion co..tol permit.

50-333/95008

LER

HPCI System Trip on Overspeed Due to Procedure Deficiency.

50-333/96-005

LER

Error in Safety Limit Minimum Critical Power Ratio Calculation.

50-333/96011

LER

Both Standby Liquid Control Subsystems Inoperable Due to

j

inoperable Pump Discharge Pressure Relief Valves

Discussed

None

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LIST OF ACRONYMS USED

ACTS

Action and Commitment Tracking System

AP

Administrative Procedure

CCP

Combustible Control Permit

DBD

Design Basis Document

DDOI

Design Document Open item

DER

Deviation and Event Report

EDG

Emergency Diesel Generator

EFE

Equipment Failure Evaluations

ESW

Emergency Service Water

HPCI

High Pressure Coolant injection

IN

Information Notice

ISI

Inservice Inspection

JCO

Justification for Continued Operation

MG

Motor Generator

NDE

Non-Destructive Examination

NFPA

National Fire Protection Association

NRC

Nuclear Regulatory Commission

01

Office of Investigations

ORG

Operational Review Grcup

l

PCIV

Primary Containment Isolation Valves

PERC

Performance Enhancement Review Committee

PORC

Plant Operations Review Committee

QA

Quality Assurance

RCA

Radiological Controlled Area

RCIC

Reactor Core isolation Cooling

RES

Radiological & Environmental Services

j

RMCS

Reactor Manual Control System

RP

Radiation Protection

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RP&C

Radiological Protection and Chemistry

RPV

Reactor Pressure Vessel

RWP

Radiation Work Permit

SESO

Site Engineering Standing Order

SLC

Standby Liquid Control

SLMCPR

Safety Limit Minimum Critical Power Ratio

SRC

Safety Review Committee

ST

Surveillance Test

TIR

Technical Issues Report

TS

Technical Specification

UPS

Uninterruptible Power Supply