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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217H2061999-10-12012 October 1999 Safety Evaluation Supporting Amend 106 to License DPR-22 ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205C1651999-03-19019 March 1999 Safety Evaluation Supporting Amend 105 to License DPR-22 ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198M8221998-12-24024 December 1998 Safety Evaluation Supporting Amend 104 to License DPR-22 ML20198M6901998-12-23023 December 1998 Safety Evaluation Supporting Amend 103 to License DPR-22 ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20151T0981998-08-28028 August 1998 Safety Evaluation Supporting Amend 101 to License DPR-22 ML20217E9611998-04-20020 April 1998 Safety Evaluation Supporting Amend 100 to License DPR-22 ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20198R3761997-10-29029 October 1997 Safety Evaluation Supporting Amend 99 to License DPR-22 ML20216H9171997-08-18018 August 1997 Safety Evaluation Denying Licensee 970818 Request for Exemption from Requirements of 10CFR50,App E, Section IV.F.2.c to Exercise Plant Offsite EP Plans W/State & Local Govt Authorities within Plant Planning Zone ML20137S5561997-04-0101 April 1997 Safety Evaluation Approving License Request for Transfer of Licenses for Monticello & Prairie Island,Units 1 & 2 Nuclear Generating Plants & Prairie Island ISFSI ML20117N5921996-09-17017 September 1996 Safety Evaluation Supporting Amend 97 to License DPR-22 ML20101Q1181996-04-0909 April 1996 Safety Evaluation Supporting Amend 96 to License DPR-22 ML20086J8171995-07-12012 July 1995 Safety Evaluation Supporting Amend 93 to License DPR-22 ML20073A1261994-09-15015 September 1994 Safety Evaluation Supporting Amend 92 to License DPR-22 ML20072U0761994-09-0909 September 1994 Safety Evaluation Supporting Amend 91 to License DPR-22 ML20072S6791994-09-0707 September 1994 Safety Evaluation Supporting Amend 90 to License DPR-22 ML20071F4501994-06-30030 June 1994 Safety Evaluation Supporting Amend 88 to License DPR-22 ML20065L4461994-04-15015 April 1994 Safety Evaluation Supporting Amend 87 to License DPR-22 ML20059C4051993-10-25025 October 1993 Safety Evaluation Re Inservice Testing Program Relief Requests GR-7 & RCIC-6 for Plant.Proposed Alternative to OM-1 Safety & Valve Relief Valve Requirements Authorized Based on Alternative Providing Acceptable Level of Quality ML20056D0921993-07-12012 July 1993 Safety Evaluation Supporting Amend 86 to License DPR-22 ML20045F8811993-06-29029 June 1993 Safety Evaluation Supporting Amend 85 to License DPR-22 ML20128E9991993-01-27027 January 1993 Safety Evaluation Supporting Amend 84 to License DPR-22, Respectively ML20096A9121992-04-16016 April 1992 Safety Evaluation Supporting Amend 81 to License DPR-22 ML20076E5071991-08-12012 August 1991 Safety Evaluation Supporting Amend 80 to License DPR-22 ML20065U4491990-12-19019 December 1990 Safety Evaluation Supporting Amend 76 to License DPR-22 ML20062B1891990-10-12012 October 1990 Safety Evaluation Supporting Amend 75 to License DPR-22 ML20043F1101990-06-0505 June 1990 Safety Evaluation Supporting Amend 74 to License DPR-22 ML20042F1951990-05-0101 May 1990 Safety Evaluation Supporting Amend 73 to License DPR-22 ML19327B9951989-11-0202 November 1989 Safety Evaluation Supporting Amend 72 to License DPR-22 ML20042F1651989-10-19019 October 1989 Safety Evaluation Supporting Amend 71 to License DPR-22 ML20248C3201989-09-28028 September 1989 Safety Evaluation Supporting Amend 70 to License DPR-22, Modifying Specs Having cycle-specific Parameter Limits by Replacing Values of Limits W/Ref to Core Operating Limits Rept ML20247P7271989-09-12012 September 1989 Safety Evaluation Supporting Amend 69 to License DPR-22 ML20247L5491989-07-14014 July 1989 Safety Evaluation Supporting Amend 68 to License DPR-22 ML20245G3481989-06-19019 June 1989 Safety Evaluation Supporting Amend 67 to License DPR-22 ML20246L7191989-05-10010 May 1989 Safety Evaluation Supporting Amend 64 to License DPR-22 ML20245F7281989-04-18018 April 1989 Safety Evaluation Supporting Amend 63 to License DPR-22 ML20248G0001989-03-29029 March 1989 Safety Evaluation Supporting Amend 61 to License DPR-22 ML20235X4781989-02-28028 February 1989 Safety Evaluation Supporting Amend 60 to License DPR-22 ML20235S0851989-02-16016 February 1989 Safety Evaluation Supporting Amend 59 to License DPR-22 ML20237C1761987-12-11011 December 1987 Safety Evaluation Supporting Amend 56 to License DPR-22 ML20236V2721987-11-25025 November 1987 Safety Evaluation Supporting Amend 54 to License DPR-22 ML20236V3151987-11-25025 November 1987 Safety Evaluation Supporting Amend 55 to License DPR-22 ML20236V4571987-11-19019 November 1987 Safety Evaluation Supporting Amend 53 to License DPR-22 1999-08-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2061999-10-12012 October 1999 Safety Evaluation Supporting Amend 106 to License DPR-22 ML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With 05000263/LER-1999-007, :on 990610,HPCI Test Return Valve Was Unable to Close Against Max Expected Differential Pressure.Caused by Failure to Accurately Predict Valve Performance.Procedure Revised.With1999-07-0909 July 1999
- on 990610,HPCI Test Return Valve Was Unable to Close Against Max Expected Differential Pressure.Caused by Failure to Accurately Predict Valve Performance.Procedure Revised.With
05000263/LER-1999-006-01, :on 990602,during Quarterly Surveillance Hcpi Was Declared Inoperable.Caused by Drain Pot Alarm.Revised HPCI Surveillance Test Procedure.With1999-07-0202 July 1999
- on 990602,during Quarterly Surveillance Hcpi Was Declared Inoperable.Caused by Drain Pot Alarm.Revised HPCI Surveillance Test Procedure.With
ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With 05000263/LER-1999-005, :on 990508,personnel Inserted Manual Scram When Pressure Transient Closed Air Ejector Suction Isolation Valves & Tripped off-gas Sys.Caused by Recombiner Catalyst Migration.Catalyst Was Removed.With1999-06-0707 June 1999
- on 990508,personnel Inserted Manual Scram When Pressure Transient Closed Air Ejector Suction Isolation Valves & Tripped off-gas Sys.Caused by Recombiner Catalyst Migration.Catalyst Was Removed.With
ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With 05000263/LER-1999-004-01, :on 990422,low Reactor Water Level Scram,Group 2 & 3 Isolations & Subsequent HPCI Became Inoperable.Caused by Feedwater Controller Power Supply Failure.Three Power Supplies Replaced & Connections Cleaned.With1999-05-24024 May 1999
- on 990422,low Reactor Water Level Scram,Group 2 & 3 Isolations & Subsequent HPCI Became Inoperable.Caused by Feedwater Controller Power Supply Failure.Three Power Supplies Replaced & Connections Cleaned.With
05000263/LER-1999-003-01, :on 990412,HPCI & Division 1 ECCS Equipment Were Declared Inoperable Due to Svc Water Pump Failure.Pump Shaft Was Mechanically Freed,Check Valve Was Repaired & Pump Was Successfully Tested.With1999-05-12012 May 1999
- on 990412,HPCI & Division 1 ECCS Equipment Were Declared Inoperable Due to Svc Water Pump Failure.Pump Shaft Was Mechanically Freed,Check Valve Was Repaired & Pump Was Successfully Tested.With
05000263/LER-1999-002-01, :on 990329,event Sequence That Results in Available ECCS Being Reduced to Less than That Assumed in Current Safety Analysis.Caused by Failure of Edg.Plant Operating Procedures Revised.With1999-05-11011 May 1999
- on 990329,event Sequence That Results in Available ECCS Being Reduced to Less than That Assumed in Current Safety Analysis.Caused by Failure of Edg.Plant Operating Procedures Revised.With
ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20205C1651999-03-19019 March 1999 Safety Evaluation Supporting Amend 105 to License DPR-22 ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 05000263/LER-1999-001-02, :on 990215,HPCI High Steam Flow Isolation During Quarterly Surveillance Test Was Noted.Caused by Inadequate Surveillance Procedure.Revised Surveillance Procedure.With1999-03-17017 March 1999
- on 990215,HPCI High Steam Flow Isolation During Quarterly Surveillance Test Was Noted.Caused by Inadequate Surveillance Procedure.Revised Surveillance Procedure.With
ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198M8221998-12-24024 December 1998 Safety Evaluation Supporting Amend 104 to License DPR-22 ML20198M6901998-12-23023 December 1998 Safety Evaluation Supporting Amend 103 to License DPR-22 ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv 05000263/LER-1998-005-01, :on 980921,HPCI Was Removed from Service to Repair Steam Leak in Drain Trap by Pass.Caused by Localized Erosion of Valve Body.Valve Was Declared Inoperable & Was Replaced with Manual Valve1998-10-21021 October 1998
- on 980921,HPCI Was Removed from Service to Repair Steam Leak in Drain Trap by Pass.Caused by Localized Erosion of Valve Body.Valve Was Declared Inoperable & Was Replaced with Manual Valve
05000263/LER-1998-004-02, :on 980909,manual Scram Was Inserted Following Pressure Transient Closed Air Ejector Suction Isolation Valves & Trips Offgas Recombiners,Occurred.Caused by Seat Leakage.Leaking Valve Seat Was Reworked1998-10-0909 October 1998
- on 980909,manual Scram Was Inserted Following Pressure Transient Closed Air Ejector Suction Isolation Valves & Trips Offgas Recombiners,Occurred.Caused by Seat Leakage.Leaking Valve Seat Was Reworked
ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20151T0981998-08-28028 August 1998 Safety Evaluation Supporting Amend 101 to License DPR-22 ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant 05000263/LER-1998-003-01, :on 980417,transgranular Stress Corrosion Cracking Was Identified in Control Rod Drive Lines.Caused by chloride-induced Transgranular stress-corrosion Cracking. Affected Sections of Two Lines Replaced1998-05-14014 May 1998
- on 980417,transgranular Stress Corrosion Cracking Was Identified in Control Rod Drive Lines.Caused by chloride-induced Transgranular stress-corrosion Cracking. Affected Sections of Two Lines Replaced
05000263/LER-1998-002-02, :on 980415,main Steam Isolation Valve Position Setpoint Outside Allowed Range,Was Found.Caused by Previous Testing Technique & Use of Particular Switch Model.Eight New Position Switches W/Less Deadband Installed1998-05-14014 May 1998
- on 980415,main Steam Isolation Valve Position Setpoint Outside Allowed Range,Was Found.Caused by Previous Testing Technique & Use of Particular Switch Model.Eight New Position Switches W/Less Deadband Installed
ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant 05000263/LER-1998-001-02, :on 980323,discovered Containment Isolation Valve Leakage Exceeded TS Limit.Caused by Foreign Matl Found on Valve Seat.Repaired Subject Valves & Developed Process to Ensure Cleanliness of Testing Equipment1998-04-22022 April 1998
- on 980323,discovered Containment Isolation Valve Leakage Exceeded TS Limit.Caused by Foreign Matl Found on Valve Seat.Repaired Subject Valves & Developed Process to Ensure Cleanliness of Testing Equipment
ML20217E9611998-04-20020 April 1998 Safety Evaluation Supporting Amend 100 to License DPR-22 ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant 1999-09-30
[Table view] |
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LAFETY EVA1.UA110N BY THE OFFICE OF NUCLEAR REACTOR REGULATION A
RELATED TO AMENDMENT NO.
84 T0 FACILITY QPERATING LI WESE NO. DPR-22 HORTHERN STATES POWER COMPANY MONTICELLO NUCLEt,R GENERATING PLANT
@CKET NO. 50-263_
5 1.0.11(11QDUCT10N By letter dated September 16, 1992, as supplemented November 3, 1992, the Northern States Power Company (the licensee) requested an amendment to the Technical Specifications (TS) appended to facility Operating License No. DPR-22 for the Monticello Nuclear Generating Plant.
The proposed amendment approves 15 changes to permit implementation of an expanded operating domain resulting from maximum extended load line limit analysis (MELLLA) and increased core flow (ICF).
The November 3,1992, submittal provided clarifying information that did not i
change the initial proposed no significant hazards determination.
2.0 EVALVATION 2.1 D G R E110N OF PROPOSED TS CHANGES Averaae Pnwer Ranae Monitqr (APRM) Flow-Biated Scram Set Point - TS 2.3. A. and Table LL1:
The proposed amendment would change the flux scram lines on the power / flow map and establish a new two loop APRM flux scram line of 0.66W +
70%.
The existing two-loop APRM flux scram function is 0.58W + 624.
The single-loop line would remain at 0.58(W-5.4) + 62%.
(Note:
"W i s the -
percentage of drive flow required for 100% core flow.) This change would allow higher power operation when core flow is below 87%.
In addition, a high flow clamp of 120% rated power would be added to the APRM scram specifications.
The Updated Safety Analysis Report-(USAR), Section 7.3.5.2.2 indicates that the 120% clamp instrumentation is currently-installed.
Ayarjao Power Ranae Monitor flow-Biased Rod Block Set Point - Table 3.2.31 The proposed amendment would similarly change the rod block monitor (RBM) set point requirements, establishing a two-loop set point function of 0.66W + 58%,
and a high flow clamp of 108% rated power.
The present two-loop operation rod block set point function is 0.58W + 50%. The proposed changes maintain the same maximum set points (120% for APRM scram.and 108% for rod block) as currently approved. The changes also maintain the same margin (12%) between 9302110202 930127 ADOCK0500g3--
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t the APRM scram and rod block set points as provided in the current Technical Specifications. As for the scram function, the single-loop operation requirement would not be changed.
Ihe Bases (LJ. A) and Core Operal.ing Limits Report fC01H)_Reportina Ets kements (15 6.7.a):
Ine Bases sections of the 15 would be revised to reflect the changes to affected Limiting Safety System Settings and Limiting Conditions for Operation.
References to supporting analyses would be included in the revised Bases. Also, reporting requirements for the COLR would be changed to require that the COLR for each reload include a power / flow map.
2.2 EYALu&II.03 The proposed amendment affects safety system set points for two protective functions, (1) the APRM flow-biased scram, and (2) the RBM trip.
Both functions utilize the APRM neutron monitoring system.
The function of the slope and bias circuits of the APRM flow-biased scram is to account for-the decreasina mar vith reduced recirculation flow. gin to fuel damage at a given power-level The function of the RBM is to prevent rod withdrawal under conditions that could initiate a rod withdrawal error event leading to local fuel damage.
Operation with the proposed changes implemented on these protective functions has been analyzed for limiting accidents, transients, and thermal-hydraulic stability.
The results of the Monticello analyses are reported in (a) NEDC-31849P
" Maximum Extended Load Line Limit Analy>is for Monticello Nuclear Generating Plant Cycle 15," (b).NEDC-31849P-1, " Maximum Extended Load Line Limit Analysis for Monticello Nuclear Generating Plant Cycle 15, Supplement 1," and (c) NEDC-31778P " Safety Review for Monticello Nuclear Generating Plant Increased Core Flow Operation Throughout Cycle 14."
These documents provide the results of new analyses and evaluations supporting HELLLA and ICF operation and discussions providing the basis for not reanalyzing certain events.
Events addressed in these reports include:
A.
Transients:
(1) Feedwater Controller Failure with Maximum Demand (MELLLA and ICF)
(2) Turbine Trip w uh Bypass failure (MELLLA and ICF)
(3) Loss of Feedwater Heating (MELLLA)
(4) Closure of One Turbine Stop Valve at 100% Power and 75% Flow (MELLLA)
(4) Transfer to Backup Pressure Regulator (MELLLA)
(5) Slow Flow Runout (MELLLA)
(6 Main Steam Isolation Valve Closure With Flux Scram (MELLLA and ICF)-
(7 Rod Withdrawal Error Event (MELLLA and ICF)
(8 Rod Drop Accident (ICF) 8.
Design Basis Accident (DBA)
(1) DBA-LOCA Containment Pressure Response and containment dynamic loads (MELLLA)
(2) DBA-LOCA Peak Clad Temperature (MELLLA and-lCF)
I- '
C.
Analysis of effect of acoustic loads and flow-induced loads on reactor internals (MELLtA and ICF)
D.
Analysis of effects on flow-induced vibration (MELLLA and ICF)
E.
AnticipatedTransientsWithoutScram[ATWS)(MELLLA)
TransieAta: Analysis rasults for the turbine trip with bypass failure and feedwater controller failure to maximum demand for 100A power and 75% core flow initial conditions resulted in peak vessel pressures, peak neutron flux and heat flux, and delta-Critical Power Ratios (CPRs) less than the corresponding values for the transient with 100% power and 100% core flow initial conditions.
The peak vessel pressure for the HSIV closure with flux scram event initiated from 100% power and 75% core flow was slightly less than the corresponding values for the transient with 100% power and 100% core flow initial condition.
For the closure of one turbine stop valve event and for the transfer to backup pressure regulator event, the peak neutron flux values for the 100% power and 75% core flow initial condition were well below the 120% rated power APRM clamp.
The slow flow runout event was analyzed due to the fact that the power increase for this event occurs along a steeper rod line. Reanalysis was performed for various. flow conditions down to 30% rccirculation pump speed, i
with each flow condition on the maximum possible rod line.
The analysts demonstrated that results are acceptable using current flow dependent minimum critical power ratio (MCPR,) and flow dependent maximum average planar linear heat generation rate factor (MAPFAC,) limit curves.
Pod Withdrawal Error (RWE1:
The RWE analysis for the Extended Load Line Limit Analysis (ELLLA) region (Amendment 29) bounds the RWE for-the MELLLA and ICF regions.
Desian_ B_giis Accidents - Peak Clad Temperature (PCT):
SAFER /GESTR and 10 CFR Part 50, Appendix K calculations for a 102% power and 80% core flow initial condition indicate a PCT of 1623*F. This is less than the 1769'F PCT calculated based on the 102% power and 105% initial flow condition.
This indicates that for a 75% flow initial condition, the PCT would be expected to be close to that calculated for the 80% flow initial condition, considerably under the 2200*F limit.
For ICF operation, the initial core heatup will be lessened, but the core uncovery duration is increased resulting in.a slightly increased PCT, on the order of 10'F, which is insignificant.
-Desian Basis Accidents - Cont 11nment-Pressure Response:. The'DBA-LOCA short--
term containment response for initial conditions in the HELLLA region was found to be bounded by the current USAR analysis limiting value-of 42 psig which is below the containment design value of 56 psig. -Long-term containment-response is unaffected by initial flow.
Containment dynamic loads, including pool swell, condensation oscillation, chugging, and vent clearing are also not impacted by ooeration in the MELLLA region.
2 4
Desian Basis Accidents - Effect on Reactor Vessel Internals:
Pressure differential forces on fuel assemblies and vessel internals for DBAs (the main
^
steam line (MSL) break upstream of flow restrictors is the worst case) initiated from the MELLLA region are bounded by the values for higher flow operation. Reanalysis was performed for ICF operation and stresses were found to be within allowable values.
For the MELLLA region and ICF, flow-induced vibrations and acoustic loads are evaluated with particular attention on the shroud, separator assembly, jet sumps, and incore housing and control rod guide tubes.
It was concluded t1at balanced recirculation loop operations in the MELLLA region and ICF operations up to 105% rated core flow are acceptable.
(Note:
The licensee is currently evaluating test results from a series of jet pump tests which were conducted as a result of cracking in a jet pump upper riser brace.
Data indicates that riser brace harmonic frequencies may exist at certain pump speeds.
Pending completion of full scale tests and analysis of findings, the licensee is restricting operation of the recirculation pumps in the area of concern.
The lower riser braces at Monticello are capable of c
providing the required jet pump support and the upper bc :es are considered-unnecessary.
The potential effects of loose parts resu: cing from upper riser brace f ailure have been analyzed by the vendor and licensee, and found to result in no safety concern.)
. Thermal-Hydraulic Stability:
Thermal-hydraulic stability reanalysis was not necessary in support of MELLLA/ICF.
Stability performance of GE fuel, which is used exclusively at Monticello, is generically demonstrated in NEDE-22277-P-1 " Compliance of GE BWR fuel Designs to Stability Licensing Criteria." This NEDE-22277-P-1 has been incorporated as part of the GESTAR 11 methodology, This methodology utilizes calculations to show that individual channels are as-stable or more' stable than the core, thus indicating the core-wide limit cycle oscillations will not occur.
AM:
The limiting ATWS event (MSIV Closure with one safety relief valve out of service, recirculating pumps trip and alternate rod insertion) was reanalyzed for the 100% power and 75% flow initial condition in the MEl,LLA region.
Analysis results of peak vessel pressure, peak containment. pressure, and peak suppression pool bulk temperature were within applicable design guidelines.
Summary:
The new and earlier analyses encompass and bound the range of effects on accidents and transients resulting from-the expanded MELLLA/ICF operating regime.
The areas examined are the same areas examined in previous MELLLA-ICF reviews such as that for Fermi-2 reported in the staff's Safety Evaluation of May 15, 1991, supporting Amendment 69 to Operating License NPF-43.
Based on the results'of the analyses and evaluations riescribed in the --
report, maximum extended lohe line operation will not result in significantly reduced fuel thermal margins and will n9t compromise the structural integrity of the containment or of the reactor vessel or its internals.
Based on the findings, the proposed amendment is acceptable.
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The analyses conducted in support of HELLLA and ICF operation are cycle specific and will be reanalyzed for each reload as necessary.
However, the associated TS changes encompass anticipated future reloads.
The addition of the cycle dependent Power to flow Hap to COLR as described in TS 6.7.a is a clarification and therefore, the staff finds it acceptable.
3.0 AIA11_C.0MLIAT10B In accordance with the Commission's regulations, the Minnesota State official was notified of the proposed issuance of the amendment. The state official had no comments, 4,0 ENVIRONMENTAL CONSIDEPAIl0B The amendment changes a requirement with respect to the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20.
The staff has determined that the amendment involves no significant increase in the amounts and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration and there has been no public comment on such finding (57 FR 48823). Accordingly, the amendment meets the aligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9),
Pursuant to 10 CFR 51.22(b), no environmental impa::t statement or environmental assessment need be prepared in connection with the issuance of the amendment.
5.0 CONCLUSION
The staff has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the pro 30 sed manner. (2) such activities will be conducted in compliance wit 1 the Commission's regulations, and (3) the issaance of the amendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributors:- William Long, A. H. Hsia Date: January 27, 1993
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