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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARGO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With 05000397/LER-1984-027, Revised LER 84-027-01:on 840322,main Steam Relief Valve Solenoids Failed Due to Grounding in Solenoid Coils.Voltage Spike Suppression Diodes Installed Across Each Solenoid Circuit.Ge Conducting Review of Failures1984-07-19019 July 1984 Revised LER 84-027-01:on 840322,main Steam Relief Valve Solenoids Failed Due to Grounding in Solenoid Coils.Voltage Spike Suppression Diodes Installed Across Each Solenoid Circuit.Ge Conducting Review of Failures 05000397/LER-1984-008, Revised LER 84-008-01:on 840128,suppression Pool Level Indicator & Pool Level Fell Below Tech Spec Limits.Caused by Simultaneous Loss of Control Room Indication & Operation of Loop a of RHR Sys.Indication Reenergized1984-07-19019 July 1984 Revised LER 84-008-01:on 840128,suppression Pool Level Indicator & Pool Level Fell Below Tech Spec Limits.Caused by Simultaneous Loss of Control Room Indication & Operation of Loop a of RHR Sys.Indication Reenergized 05000397/LER-1984-026, Revised LER 84-026-01:on 840419 & 27,water Found in Train B of Standby Gas Treatment Sys.Caused by Pressure Surges in Preaction & Deluge Portions of Fire Protection Sys.Design Change in Progress1984-05-18018 May 1984 Revised LER 84-026-01:on 840419 & 27,water Found in Train B of Standby Gas Treatment Sys.Caused by Pressure Surges in Preaction & Deluge Portions of Fire Protection Sys.Design Change in Progress 05000397/LER-1983-003, Updated LER 83-003-01:on 831222,walk Down Revealed Fire Dampers Not Meeting Fire Rating Requirements,Violating Tech Specs.Caused by Personnel Error.Defective Dampers Replaced1984-03-28028 March 1984 Updated LER 83-003-01:on 831222,walk Down Revealed Fire Dampers Not Meeting Fire Rating Requirements,Violating Tech Specs.Caused by Personnel Error.Defective Dampers Replaced 05000397/LER-1984-010, Supplemental LER 84-010-00 Providing Corrective Actions Inadvertently Omitted from Original Ler.All Five Excess Flow Check Valves Removed,Modified & Reinstalled.Drawings Revised Indicating Water or Gas Svc1984-03-28028 March 1984 Supplemental LER 84-010-00 Providing Corrective Actions Inadvertently Omitted from Original Ler.All Five Excess Flow Check Valves Removed,Modified & Reinstalled.Drawings Revised Indicating Water or Gas Svc 1999-10-01
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
LER-2084-008, Revised LER 84-008-01:on 840128,suppression Pool Level Indicator & Pool Level Fell Below Tech Spec Limits.Caused by Simultaneous Loss of Control Room Indication & Operation of Loop a of RHR Sys.Indication Reenergized |
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UCENSEE EVENT REPORT (LER) 00CEST seveW4R 623 #88E '3
, ACsLITY *taast f11 Washington Nuclear Plant - Unit 2 o1510101o13 9 17 1 loFl0 13 TirL. .A.
Suppression Pool Level Outside Technical Specification Limits
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Revision 0 to LER 008, issued on February 24, 1984, reported a failure of a suppression pool level indicator (CMS-LR/PR-4) and the subsequent determination that suppression pool level was below the Technical Specification limits.
The purpose of this supplemental report is to address the loss of water in the suppres-sion pool during the event due to an inadequate valve lineup. As previously reported, Technical Specifications (4.5.3.1) requires the suppression pool level to be maintained at a minimum of 30 feet 9-3/4 inches. Actual level was determined to be approximately 30 feet 5 inches and was verbally reported to the NRC pursuant to 10CFR50.72(2)(iii)(D).
i (It should be noted that the original report incorrectly stated that the Plant was in mode 5 at the time of the event. The Reactor vessel head was tensioned on January 26, 1984, two days preceding the event, and the nede switch was transferred from refueling to shutdown.)
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- 8407260033 840719 PDR ADOCK O$000397 5 PDR p,,. .
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4eC Form Je6A , U.S. NUCLEAll EEGULATO3Y COMMIS6JON
- ' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION movio ous =o mo-om EXPtRES. 8/31/85 4
FAcluTV NAME lu DOCKET NUMSER (21 ggn gyuggR (6, PAGE138 TEAR M*M'b :
$"e Washinaton Nuclear Plant - linit 2 0 ls j o lo lo I 31917 81 4 Ol0l 8 -
Of 1 d2 F Ol 3 Plant Operating Conditions l
_.a). Power Level -
0%
b) Operating Mode -
4 (Prior to Initial Plant Heatup)
Event During normal shutdown conditions prior to initial power operation, only one channel of suppression pool level indication was available. The suppression pool level recorder was ~ inadvertently de-energized when the 120 VAC power supply breaker feeding it was I opened at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on January 27, 1984. The Control Room recorder was not noted as out of service until 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> on January 28, 1984. The level decrease occurred during this 20 hour2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> period. The NRC was notified at 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br /> on January 28, 1984 pursuant to ,
10CFR50.72(2) (iii )(D) . '
When pool level indication was returned to service it was noted that condensate had ac-cumulated in the reference leg of the transmitter causing an incorrect level indication in the Control Room. The cause of the violation was the result of a simultaneous loss of suppression pool level indication in the Control Room and the operation of the ' A' loop of the Residual Heat Removal (RHR) system in shutdown cooling while the 'B' loop was also lined up for shutdown cooling but was not in service. This configuration of the Residual Heat Removal system, as specified in the then existing plant procedure, provided a flow path to remove water from the wetwell through the inactive loop and inject it into the vessel where normal Reactor vessel level control actions discharged the water to the condenser hotwell. The flow path resulted from an incorrect cross-tie t valve lineup which allowed suppression pool water to flow through the waterleg pump, RHR-P-3, to the discharge of RHR-P-2B back through the discharge check valve, RHR-V-31B, to the pump suction and into the A RHR system when RHR pump B shutdown cooling suction valve RHR-V-6B was left open. This lineup produced insufficient differential pressure to adequately backseat the RHR B discharge check valve.
, Immediate Corrective Action j
The Control Room indication was reenergized, a local measurement of the suppression pool level was taken, water was drained from the reference leg of the tre.nsmitter to provide l i accurate level indication and water level was restored in the suppression pool.
Further Corrective Action The cause of the water loss was not identified until a similar event occurred approxi- !
mately two weeks later. The corrective action taken after the recurrence was to close ,
the Residual Heat Removal Pump suction cross-tie valve for the inactive loop when both !
loops are lined-up for ' shutdown cooling. A subsequent revision to the RHR system pro-cedure was issued to specify the correct valve lineup. When not in the shutdown cooling mode, the Residual Heat Removal trains are maintained in their normal Low Pressure Cool-ant Injection mode lineup.as required by Plant procedure.
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l mac rem asea *' u s. muctsan macutaroav commission I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION areaovio ove No. siso-oto. I Expints. 8'3115 FACIL&TY NAME 118 OOCKET NUMSER (28 (gg gygggR 168 PAGE 431
"^a ".?t*JJt' .: *tt*3:
Washinaton Nuclear Plant - Unit 2 o ls j o l0 j o I 319 I 7 814 -
0 l0 l 8 -
01 1 0l3 F Ol 3 TEXT t# #iore apoco a regered, ese esseoriet #Ac Arm JsM'sJ ith To eliminate the level indication complication, the suppression pool level recorders were marked to show Technical Specification upper and lower level limits. A list of loads receiving power from each circuit breaker is being developed and the suppression pool level transmitter's reference legs are periodically drained.
Safety Significance There were no safety consequences as a result of this event. The reactor was in cold shutdown condition with the fuel having an insignificant fission product inventory.
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r Washington Public Power Supply System P.O. Box 968 3000GeorgeWashingtonWay Richland, Washington 99352 (509)372-5000 Docket No. 50-397 July 19,1984 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO. 84-008-01
Dear Sir:
Transmitted herewith is Licensee Event Report No. 84-008-01 for WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and provides supplemental information to LER 84-008, Rev. O.
Very truly yours, J. D. Ma n (M/D 927PI)
WNP-2 Plant Manager JDM:mm
Enclosure:
Licensee Event' Report No. 84-008-01 cc: Mr. John B. Martin, Adninistrator Region V, Office of Inspection and Enforcement -
U.S. Nuclear Regulatory Commission 1450 Maria Lane Walnut Creek, California 94596 Mr. A. D. Toth, NRC Resident inspector (901 A)_ .
Ms. Dottie Sherman American Nuclear Insurers
.The Exchange Suite 245 270 Farmington Ave.
Farmington, CT 06032 4
+W 4
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05000397/LER-1984-008, Revised LER 84-008-01:on 840128,suppression Pool Level Indicator & Pool Level Fell Below Tech Spec Limits.Caused by Simultaneous Loss of Control Room Indication & Operation of Loop a of RHR Sys.Indication Reenergized | Revised LER 84-008-01:on 840128,suppression Pool Level Indicator & Pool Level Fell Below Tech Spec Limits.Caused by Simultaneous Loss of Control Room Indication & Operation of Loop a of RHR Sys.Indication Reenergized | | 05000397/LER-1984-010, Supplemental LER 84-010-00 Providing Corrective Actions Inadvertently Omitted from Original Ler.All Five Excess Flow Check Valves Removed,Modified & Reinstalled.Drawings Revised Indicating Water or Gas Svc | Supplemental LER 84-010-00 Providing Corrective Actions Inadvertently Omitted from Original Ler.All Five Excess Flow Check Valves Removed,Modified & Reinstalled.Drawings Revised Indicating Water or Gas Svc | | 05000397/LER-1984-026, Revised LER 84-026-01:on 840419 & 27,water Found in Train B of Standby Gas Treatment Sys.Caused by Pressure Surges in Preaction & Deluge Portions of Fire Protection Sys.Design Change in Progress | Revised LER 84-026-01:on 840419 & 27,water Found in Train B of Standby Gas Treatment Sys.Caused by Pressure Surges in Preaction & Deluge Portions of Fire Protection Sys.Design Change in Progress | | 05000397/LER-1984-027, Revised LER 84-027-01:on 840322,main Steam Relief Valve Solenoids Failed Due to Grounding in Solenoid Coils.Voltage Spike Suppression Diodes Installed Across Each Solenoid Circuit.Ge Conducting Review of Failures | Revised LER 84-027-01:on 840322,main Steam Relief Valve Solenoids Failed Due to Grounding in Solenoid Coils.Voltage Spike Suppression Diodes Installed Across Each Solenoid Circuit.Ge Conducting Review of Failures | |
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