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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20137G3531985-04-18018 April 1985 RO 50-20/1985-1:on 850408,main Intake Valve Failed Light Test Maint Procedure.Caused by Excessive Wear of Valve Gasket.Gasket Replaced ML20081H8191983-09-15015 September 1983 RO 50-20/1983-2:on 830906,fission Product Gas Levels Rise from 2.8% Max Permissible Concentration in Jul 1983 to 4.57% in Aug Noted.Caused by Excessive Outgassing of Fuel Element MIT-08.Element Removed from Core ML20074A7521983-04-29029 April 1983 RO 50-20/1983-1:on 830419,main Intake Valve Closed & Could Not Be Reopened.Caused by Piston Rod Rupture Near Rod Eye, Leaving Valve in Closed Position.Defective Hydraulic Cylinder Shaft Replaced ML20063B9221982-08-17017 August 1982 Ro:On 820809,slight Increase Found in Levels of Fission Products in Reactor Primary Sys.Cause Under Investigation. Criterion for Operation W/Possible Faulty Core Element Per RO 50-20/79-4 Will Be Observed 1999-03-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20209C9331999-07-0808 July 1999 Vols 1 & 2 to SAR for Ma Institute of Technology Nuclear Reactor Lab ML20196K0331999-06-30030 June 1999 Quality Mgt Program for Generation of MITR-II Medical Therapy Facility Beams for Human Therapy, Reflecting Change to Provision 14 ML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20199H2371998-12-31031 December 1998 Revised SER for Fission Converter Facility ML20196B7541998-06-30030 June 1998 Mit Research Reactor Nuclear Reactor Lab Ma Inst of Technology,Annual Rept to Us NRC for Period 970701-980630. with ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20217G2181997-10-0303 October 1997 SER for Fission Converter Facility ML20198P8071997-06-30030 June 1997 Annual Operating Rept for Jul 1996 - June 1997 ML20137L5901997-04-0303 April 1997 Safety Evaluation Supporting Amend 30 to License R-37 ML20129B3201996-06-30030 June 1996 Annual Rept to Us NRC for Period 950701-960630 ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20092K2301995-06-30030 June 1995 Mit Research Reactor Annual Rept to NRC for Period Jul 1994 - June 1995 ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20072T3041994-06-30030 June 1994 Annual Rept for Mit Research Reactor for 930701-940630 ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20056G8011993-06-30030 June 1993 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for Period 920701-930630 ML20128P4371993-02-16016 February 1993 Safety Evaluation Supporting Amend 27 to License R-37 ML20073H1451992-12-0909 December 1992 Study of MITR-II Core Tank Aging for Relicensing Consideration ML20114D9261992-06-30030 June 1992 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for 910701-920630 ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20082L8451991-06-30030 June 1991 Mit Research Reactor Annual Rept to NRC for Jul 1990 to June 1991 ML20058N5741990-08-10010 August 1990 QA Program for MITR-II Spent Fuel Shipment ML20059G4331990-06-30030 June 1990 Mit Research Reactor Annual Rept to NRC for Jul 1989 - June 1990 ML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML20012C2771990-03-0909 March 1990 SER for BWR Coolant Chemistry Loop to Be Installed & Operated in Mitr ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20247H7041989-06-30030 June 1989 Mit Research Reactor Annual Rept for Jul 1988 - June 1989 ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20195K1161988-10-24024 October 1988 Suppl to PWR Loop Ser:Use of Large Circulating Pump ML20154J6221988-08-29029 August 1988 Revised Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20153F5591988-06-30030 June 1988 Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20151R7341988-04-19019 April 1988 Sser for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20237K6121987-06-30030 June 1987 Mit Research Reactor Annual Rept to NRC for Jul 1986 - June 1987 ML20151R7271987-02-13013 February 1987 SER for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20148B3011986-06-30030 June 1986 Mit Research Reactor Annual Rept to NRC for Period Jul 1985 - June 1986 ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20214R3811986-01-31031 January 1986 Rept of Educational & Research Activities for Academic/ FY84-85 W/Selected Data from Previous Yrs ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20133H4081985-06-30030 June 1985 Mit Research Reactor Annual Rept to Us NRC for Jul 1984 - June 1985 1999-07-08
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MASSACHUSETTS INSTITUTE OF TECHNOLOGY O.K. HARLING 138 Albany Street Cambridge, Mass. 02139 L. CLARK. JR.
Darrctor (617)2534211 Director of Reactor Operations April 29, 1983 Mr. James M. 'Allan, Acting Administrator Region 1 U.S. Nuclear Regulatory Commission Attn: Mr. W. Kinney, Reactor Inspector 631 Park Avenue King of Prussia, PA 19406
Subject:
Reportable Occurrence 50-20/1983-1, License R-37 Failure of Ventilation Valve Actuator Gentlemen:
Massachusetts Institute of Technology hereby submits the 10-day report of an occurrence at the MIT Research Reactor, in accordance uith paragraph 7.13.2(d) of the Technical Specifications. An initial report of this occurrence was made by telephone to Region 1 on April 20, 1983.
The format of the following report is based on Regulatory Guide 1.16, Revision 1.
- 1. Report No: 50-20/1983-1 l 2a. Report Date: 29 April 1983 l
2b. Occurrence Date: 19 April 1983
- 3. Facility: MIT Nuclear Reactor Laboratory 138 Albany Street Cambridge, MA 02139
- 4. Identification of Occurrence:
The penetrations for the ventilation system of the reactor containment building are sealed by the closing of two 30 inch hydraulically-actuated butterfly valves which form gas-tight seals with rubber gaskets. During a series of routine checks of containment isolation prior to a scheduled reactor startup the main intake valve was closed and could not be reopened.
Inspection of the operating mechanism showed that the piston rod of the hydraulic cylinder on this valve had ruptured near its rod eye, leaving the valve in the closed position.
8305160043 830429 ne DR ADOCK 050 g
Mr. James M. Allan April 29, 1983 Page 2
- 5. Conditions Prior to Occurrence:
As is normally the case, the reactor had been shutdown for the previous weekend. The sh'utdown extended through Monday 18 April since that day was a holiday in Massachusetts. The failure occurred when the reactor was being prepared for startup in accordance with the standard full power startup checklists. The reactor was shut down at the time of the occurrence.
- 6. Description of the Occurrence:
A portion of the full power startup checklist requires that the four effluent monitors in the ventilation exhaust plenum be tested to assure that the ventilation isolation valves will close automatically in the event of abnormal amounts of airborne radioactive material in the effluent. The test consists of lowering the trip setting to the background level indicated by the monitor, acknowledging the alarm, checking that the valves both close, resetting the trip, and finally reopening the valves. Three out of the four plenum monitors had been tested successfully using the above procedure. The last monitor was tested and it was found that the ventilation valves closed successfully but one could not be reopened. The valve in question was the main intake damper. It had failed in the closed position. Investigation of the operating mechanism revealed that the 1-3/8" diameter piston rod of the valve's hydraulic cylinder had ruptured where its diameter reduces to 7/8".
The fracture occurred approximately 1/4" from where it is threaded so that it can be connected to the rod eye. (See attached diagram.)
- 7. Description of Apparent Cause of Occurrence:
The failure occurred in the piston rod of a hydraulic cylinder manu-factured by the Miller Fluid Power Division of Flick-Reedy Corp. , Bensenville, Illinois. The failed cylinder was a Model H81B with the following nameplate data: bore 3-1/4", stroke 10", 3000 psi severe service, 5000 psi moderate service, serial no. 76163872. It had been installed new in September of 1976 and is estimated to have operated in the vicinity of 4000 complete cycles (i.e., extend plus retract.) Virtually all these cycles were for test purposes.
The piston rod is screwed into a rod eye which is in turn connected to the valve lever arm as shown in the attached diagram. The force from the hydraulic pressure is transmitted via the piston rod and the rod eye to the valve lever which rotates 90* from the OPEN position to the CLOSED position.
The valve lever is attached to the shaf t of the valve by means of a hub and a 1/2" key. The isolation valve is a steel butterfly valve with a diameter of thirty inches. It is'five inches thick where it is attached to the shaft.
A steel lever attached to the end of the shaft of the isolation valve operates two micro-switches which indicate the true position of the valve in the control room independently of the operating mechanism. A gas-tight seal
Mr. James M. Allan April 29, 1983 Page 3 is formed by a rubber gasket which is held on by bolts along the perimeter edge of the butterfly valve. The actuating oil pressure is 1200 psi and the valve rotates from the fully open position to the fully closed position in less than a second.
The manufacturer's catalogue data show that the piston rod is made of steel with a yield strength of 90,000 to 110,000 psi. The piston rod is turned down from 1-3/8" diameter to 1" diameter at the end to allow for -
1"-14 thread. A distance of about 1/4" between the 1-3/8" main diameter and the 1" threaded diameter is undercut to a 7/8" diameter. A rod eye piece -is pinned to the isolation valve lever arm and the threaded end of the piston rod is screwed into the rod eye. The rupture occurred at the transition from 1-3/8" to 7/8" diameter.
The immediate cause of failure was found to be an interference, which developed over time under normal usage, between the valve lever arm and the rod eye. Evidence of contact between the above two parts was found when disassembling the failed mechanism. The interference is believed to have been caused by the normal wear and tear of the valve gasket. The valve lever arm has to travel further to form a tight seal as the rubber gasket becomes worn. It is probably because of this extra throw which is required to close the damper tightly that the interference occurred. The damper is designed with gasket adjustment clamps which can be tightened to push a i section of the rubber gasket out further from its channel to form a round tight seal. These gasket adjustment clamps can be adjusted to insure that sufficient clearance exists between the valve lever arm and the rod eye.
The rupture surfaces were examined under optical microscopes and two distinct zones were fo"nd. The central zone has a very coarse texture which is indicative of a very high strain rate rupture mechanism. The circumferential zone has a fine texture which indicates that it was caused i by one of the fatigue failure mechanisms. Slight discoloration, but not l heavy oxidation or corrosion, was also found in this zone. This observa-tion shows that the surfaces had not been exposed to air for too long but nevertheless long enough to accumulate some initial oxidation which shows up as discoloration. In addition, the texture in this zone is not fine enough to be classified as high cycle fatigue. Low cycle fatigue is, therefore, the mechanism that is responsible for the surface in the circum-ferential zone. The transition from the circumferential zone to the central zone is abrupt and distinctive. Brittle rupture is the failure mechanism
~
that formed the coarse texture in the central zone.
In conclusion, the interference between the valve lever arm and the rod eye produces a bending moment and a shear force in the piston rod.
The transition of the rod diameter from 1-3/8" to 7/8" where the radius of curvature of the surface is the minimum, is where the stress concentra-tion is at its maximum. The tensile stresses in the top half of the piston rod, which were a direct result of the bending moment induced by the inter-ference, coupled with the shear stress initiated a micro-crack normal to e
f L
- d Mr. James M. Allan April 29, 1983 Page 4 the surface of the rod at this transition point. The crack grew and propa-gated along the circumference of 'the rod due to the fatigue cyclic loadings.
This circumferential fatigue zone continued to progagate toward the center of the rod until the strength of the rod had decreased to the point that the rupture stress was reached. The rod finally failed by brittle rupture and the central zone formed.
- 8. Analysis of the Occurrence:
The main ventilation isolation valves are backed up by auxiliary valves which vill close automatically within ten seconds af ter a high radiation sig-
, nal from any one of the plenum effluent monitors if the corresponding main isolation valve has failed to close. The auxiliary valves can also be operated manually at the valve location and remotely in the control room.
Operability of thu auxiliary valves is tested at least monthly and the delay time for automatic closing is measured at least annually. The autematic closing function of the auxiliary intake valve was tested shortly af ter the failure of the main intake valve and the interlock was found to function satisfactorily.
The main intake valve was failed in the closed position although whether the valve was sealed tightly enough to meet the containment leak rate requirement is not known. Given the redundant protection provided by the auxiliary isolation valves and the unlikely release of dangerous amounts of radioactive materials within the containment, the probability of a potential hazard to the general public from failure of an isolation valve in the manner experienced is extremely low.
- 9. Corrective Action:
The immediate corrective action was to replace the defective hydraulic cylinder's shaft, test its operation, and verify,using standard procedures, that the valve was sealing. (Note: Replacement of the cylinder's shaft did not affect the degree to which the valve sealed. A recently completed Containment Building Pressure Test had shown that leakage from the building, and hence from this valve, was well within specification.)
Once the failed mechanism had been studied, further corrective action 3
was taken. This consisted of adjusting the gasket on the isolation valve, shortening the throw on the valve lever arm, and relieving the rod eye by i
1/16" to insure sufficient clearance between the rod eye and the valve
, lever arm. Given that these repairs might have affected the degree to which the valve sealed, a pressure test was performed after the repair in order to verify the proper adjustment of the throw on the valve lever arm and the valve gasket. The test was conducted in accordance with previously established standard procedures. It showed that the Icakage through the repaired valve was well within the specified limits. In addition, specific steps have been added to the standard maintenance procedures to check that the clearance between the rod eye and the valve lever arm is sufficient when the isolation valve is in the closed position.
Mr. James M. Allan April 29, 1983 Page 5
- 10. Failure Data:
A similar failure occurred on 30 August 1976 and was reported as ROR 50-20/1976-4.
Sincerely, Kwan Kwok Q
Assistant Superintendent w: / /
Lincoln Clark, Jr.
Director of Reactor Operations KK/gw xc: MITRSC USNRC-0MIPC l
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