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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20137G3531985-04-18018 April 1985 RO 50-20/1985-1:on 850408,main Intake Valve Failed Light Test Maint Procedure.Caused by Excessive Wear of Valve Gasket.Gasket Replaced ML20081H8191983-09-15015 September 1983 RO 50-20/1983-2:on 830906,fission Product Gas Levels Rise from 2.8% Max Permissible Concentration in Jul 1983 to 4.57% in Aug Noted.Caused by Excessive Outgassing of Fuel Element MIT-08.Element Removed from Core ML20074A7521983-04-29029 April 1983 RO 50-20/1983-1:on 830419,main Intake Valve Closed & Could Not Be Reopened.Caused by Piston Rod Rupture Near Rod Eye, Leaving Valve in Closed Position.Defective Hydraulic Cylinder Shaft Replaced ML20063B9221982-08-17017 August 1982 Ro:On 820809,slight Increase Found in Levels of Fission Products in Reactor Primary Sys.Cause Under Investigation. Criterion for Operation W/Possible Faulty Core Element Per RO 50-20/79-4 Will Be Observed 1999-03-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20209C9331999-07-0808 July 1999 Vols 1 & 2 to SAR for Ma Institute of Technology Nuclear Reactor Lab ML20196K0331999-06-30030 June 1999 Quality Mgt Program for Generation of MITR-II Medical Therapy Facility Beams for Human Therapy, Reflecting Change to Provision 14 ML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20199H2371998-12-31031 December 1998 Revised SER for Fission Converter Facility ML20196B7541998-06-30030 June 1998 Mit Research Reactor Nuclear Reactor Lab Ma Inst of Technology,Annual Rept to Us NRC for Period 970701-980630. with ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20217G2181997-10-0303 October 1997 SER for Fission Converter Facility ML20198P8071997-06-30030 June 1997 Annual Operating Rept for Jul 1996 - June 1997 ML20137L5901997-04-0303 April 1997 Safety Evaluation Supporting Amend 30 to License R-37 ML20129B3201996-06-30030 June 1996 Annual Rept to Us NRC for Period 950701-960630 ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20092K2301995-06-30030 June 1995 Mit Research Reactor Annual Rept to NRC for Period Jul 1994 - June 1995 ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20072T3041994-06-30030 June 1994 Annual Rept for Mit Research Reactor for 930701-940630 ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20056G8011993-06-30030 June 1993 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for Period 920701-930630 ML20128P4371993-02-16016 February 1993 Safety Evaluation Supporting Amend 27 to License R-37 ML20073H1451992-12-0909 December 1992 Study of MITR-II Core Tank Aging for Relicensing Consideration ML20114D9261992-06-30030 June 1992 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for 910701-920630 ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20082L8451991-06-30030 June 1991 Mit Research Reactor Annual Rept to NRC for Jul 1990 to June 1991 ML20058N5741990-08-10010 August 1990 QA Program for MITR-II Spent Fuel Shipment ML20059G4331990-06-30030 June 1990 Mit Research Reactor Annual Rept to NRC for Jul 1989 - June 1990 ML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML20012C2771990-03-0909 March 1990 SER for BWR Coolant Chemistry Loop to Be Installed & Operated in Mitr ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20247H7041989-06-30030 June 1989 Mit Research Reactor Annual Rept for Jul 1988 - June 1989 ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20195K1161988-10-24024 October 1988 Suppl to PWR Loop Ser:Use of Large Circulating Pump ML20154J6221988-08-29029 August 1988 Revised Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20153F5591988-06-30030 June 1988 Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20151R7341988-04-19019 April 1988 Sser for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20237K6121987-06-30030 June 1987 Mit Research Reactor Annual Rept to NRC for Jul 1986 - June 1987 ML20151R7271987-02-13013 February 1987 SER for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20148B3011986-06-30030 June 1986 Mit Research Reactor Annual Rept to NRC for Period Jul 1985 - June 1986 ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20214R3811986-01-31031 January 1986 Rept of Educational & Research Activities for Academic/ FY84-85 W/Selected Data from Previous Yrs ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20133H4081985-06-30030 June 1985 Mit Research Reactor Annual Rept to Us NRC for Jul 1984 - June 1985 1999-07-08
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AN INTERDEPARTMENTAL CENTER OF %@{ig/
MASSACHUSETTS INSTITUTE OF TECHNOLOGY O K. HARLING 138 Albany Street Cambridge, Mass. 02139 L. CLARK, JR.
Director (617)253-4211/4202 Director of Reactor Operations November 6, 1986 Dr. Thomas E. Murley, Administrator Region I U.S. Nuclear Regulatory Commission Attn: Mr. D. Haverkamp, Project Engineer 631 Park Avenue King of Prussia, PA 19406
Subject:
Reportable Occurrence 50-20/1986-3, License R-37 Mechanical Interference with a Shim Blade Gentlemen:
Massachusetts Institute of Technology hereby submits this ten-day report of an occurrence at the MIT Research Reactor in accordance with paragraphs 7.13.2(d) and 1.15.3 of the Technical Specifications. An initial report was made by telephone to Mr. Robert Sommers of Region I on 28 October 1986.
The format and content of this report are based on Regulatory Guide 1.16, Revision 1.
- 1. Report No: 50-20/1986-3 2a. Report Date: 6 November 1986 2b. Date of Occurrence: 27 October 198C
- 3. Facility: MIT Nuclear Reactor Laboratory 138 Albany Street Cambridge, MA 02139
- 4. Identification of occurrence:
Mechanical interference with shim blade #6 at the full-out position such that this blade could not have been operated, at the full-out position, in accordance with Technical Specification 3.9.3, which requires that the time from the initiation of a scram signal to 80% of full insertion be less than 1.0 second.
It should be noted that Technical Specifications 3.9.2 and
- 3. II.2(c) allow operation of the reactor with one control blade inope rable if that blade can be maintained at or above the aver-age shim bank position.
8611170305 DR 861106 I ADOCK 05000020 I
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s 1 Dr. Thomas E. Murley Paga 2
- 5. Conditions Prior to Occurrence:
The reactor had been shut down over the weekend. Full power mechanical and ins trument startup checklists had been completed in preparation for the usual Monday-Friday operating week. Reac-tor startup had not yet begun.
- 6. Description of Occurrence:
The reactor was being prepared for startup in accordance with approved operating procedures. A blade drop time test was con-ducted on shim blade #6. After the signal initiation for the blade drop time test, the blade was observed not to drop until its drive was driven in for about one-half inch. This test was repeated three more times on blade #6 with the same result each time. Drop tests were subsequently performed on all the remain-ing control blades with no abnormality found. A visual inspec-tion was then made of blade #6. A mechanical interference was found between the guide rod which was connected to the absorber section of blade #6 and the tube which houses the proximity
. switch for blade #6. This tube had moved out of its slot, with the resul t that it mechanically prevented the guide rod of blade
- 6 from dropping if that blade were withdrawn more than 20.5 inches from the fully inserted position. (Note: Allowable range of blade travel is 0.0"-21.0".) On receipt of the initiation signal from the rod drop timer, the drive moved in and pushed the blade to below the height of interference. The blade then dropped freely to the fully inserted position.
- 7. Description of Apparent Cause of Occurrence:
This occurrence was apparently caused by the misalignment of the blade #6 proximity switch tube. The misalignment evidently occurred on 20 October 1986 when, as part of a scheduled proce-dure, the proximity switch for blade #6 was replaced. During the installation of the new switch, a evagelock fitting was tightened l onto the proximity switch tube. The torque generated from the I tightening of this fitting evidently caused the tube to twist out l
of its slot. (Note: The tube cannot normally be twisted because it is tackwelded to a mounting bracket which is bolted to the core tank. The tack weld on the bracket of the blade #6 proximi-ty tube was either broken or broke while the switch was being replaced.)
Tests were done following the installation of the new proxim-ity switch on 20 October to verify its operation. However, these tests did not require that the blade be taken to its full-out position. Blade #6 was never operated at a position higher than 14.05 inches throughout the week and was therefore always fully operable prior to the occurrence.
Each control blade is attached by a webbed of fset plate to a weighted guide rod that moves vertically in a guide tube machined
, to a 1/16 in. clearance (see Figure 1). An armature, with a flat upper surface, sits atop the guide rod. The blade may be raised l
a a Dr. Thomas E. Murley )
Paga 3 I or lowered by mating the armature to the lower surface of an electromagnet that is connected to the drive mechanism. Control blade position is indicated by a magnetically actuated proximity switch at the fully inserted position. Continuous indication of blade position is provided by signals taken f rom the drive mecha-nism. The proximity switch indicates only the fully inserted position of the absorber section of the control blade.
Subsequent to the determination that the tack weld on the support bracket of the blade #6 proximity tube was not holding the tube securely, all tack welds on the support brackets for the other blades were inspected. They were found to be holding the tubes properly.
- 8. Analysis of Occurrence:
The reactor was operated for one week in a condition in which blade #6 could not have satisfied Technical Specification 3.9.3 if it were withdrawn to 20.5 inches or higher. The furthest withdrawn position for blade #6 during that week was 14.05 inches. Blade #6 was therefore always fully operable and would have dropped to its full-in position in less than the required time of one second if it had been required to do so.
The shutdown margin in excess of that required by the Technical Specificaitons for the week of 20 October was 2.27 beta, which is more than the integral worth of blade #6. Therefore blade #6 could have been declared as inoperable with sufficient shutdown margin remaining in accordance with Technical Specifications 3.9.2. and 3.11.2(c). No damage to the reactor has or could have resulted from this occurrence.
- 9. Corrective Action:
The corrective action consisted of:
a) Performance of drop-time tests on the other five shim bl ade s . All data were within specifications.
b) Inspection of the tack welds on the support brackets of the proximity tubes for the other five shim blades. All tubes were found to be securely held.
c) Removal and leak testing of the proximity switch tube for blade #6, fitting, tack-welding the tube onto the bracket securely, again leak testing, and reinstalling the tube properly.
d) Es tablishment of a requirement to perform a blade drop time test after the replacement of a proximity switch.
e) Evaluation of other maintenance items which may cause simi-lar interference to control blades. Magnet and control rod drive change procedures were identified, but both already have detailed checklists which require mul tiple drop times after each drive or magnet change.
.r Dr. Thomas E. Murley Page 4
- 10. Failure Data: There have been no previous instances of blade inter-ference caused by a proximity switch tube. However, as discussed in ROR-80-2, a shim blade did previously become stuck in its slot due to foreign material.
Sincerely, Kwan S. Kwok
'C Assistant Superintendent Reactor Operations L M d W '-
Lincoln Clark, Jr.
Director of Reactor Operations KSK/LC:DKE cc: MITRSC USNRC-0MIPC USNRC-DMB
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