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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20137G3531985-04-18018 April 1985 RO 50-20/1985-1:on 850408,main Intake Valve Failed Light Test Maint Procedure.Caused by Excessive Wear of Valve Gasket.Gasket Replaced ML20081H8191983-09-15015 September 1983 RO 50-20/1983-2:on 830906,fission Product Gas Levels Rise from 2.8% Max Permissible Concentration in Jul 1983 to 4.57% in Aug Noted.Caused by Excessive Outgassing of Fuel Element MIT-08.Element Removed from Core ML20074A7521983-04-29029 April 1983 RO 50-20/1983-1:on 830419,main Intake Valve Closed & Could Not Be Reopened.Caused by Piston Rod Rupture Near Rod Eye, Leaving Valve in Closed Position.Defective Hydraulic Cylinder Shaft Replaced ML20063B9221982-08-17017 August 1982 Ro:On 820809,slight Increase Found in Levels of Fission Products in Reactor Primary Sys.Cause Under Investigation. Criterion for Operation W/Possible Faulty Core Element Per RO 50-20/79-4 Will Be Observed 1999-03-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20209C9331999-07-0808 July 1999 Vols 1 & 2 to SAR for Ma Institute of Technology Nuclear Reactor Lab ML20196K0331999-06-30030 June 1999 Quality Mgt Program for Generation of MITR-II Medical Therapy Facility Beams for Human Therapy, Reflecting Change to Provision 14 ML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20199H2371998-12-31031 December 1998 Revised SER for Fission Converter Facility ML20196B7541998-06-30030 June 1998 Mit Research Reactor Nuclear Reactor Lab Ma Inst of Technology,Annual Rept to Us NRC for Period 970701-980630. with ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20217G2181997-10-0303 October 1997 SER for Fission Converter Facility ML20198P8071997-06-30030 June 1997 Annual Operating Rept for Jul 1996 - June 1997 ML20137L5901997-04-0303 April 1997 Safety Evaluation Supporting Amend 30 to License R-37 ML20129B3201996-06-30030 June 1996 Annual Rept to Us NRC for Period 950701-960630 ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20092K2301995-06-30030 June 1995 Mit Research Reactor Annual Rept to NRC for Period Jul 1994 - June 1995 ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20072T3041994-06-30030 June 1994 Annual Rept for Mit Research Reactor for 930701-940630 ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20056G8011993-06-30030 June 1993 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for Period 920701-930630 ML20128P4371993-02-16016 February 1993 Safety Evaluation Supporting Amend 27 to License R-37 ML20073H1451992-12-0909 December 1992 Study of MITR-II Core Tank Aging for Relicensing Consideration ML20114D9261992-06-30030 June 1992 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for 910701-920630 ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20082L8451991-06-30030 June 1991 Mit Research Reactor Annual Rept to NRC for Jul 1990 to June 1991 ML20058N5741990-08-10010 August 1990 QA Program for MITR-II Spent Fuel Shipment ML20059G4331990-06-30030 June 1990 Mit Research Reactor Annual Rept to NRC for Jul 1989 - June 1990 ML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML20012C2771990-03-0909 March 1990 SER for BWR Coolant Chemistry Loop to Be Installed & Operated in Mitr ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20247H7041989-06-30030 June 1989 Mit Research Reactor Annual Rept for Jul 1988 - June 1989 ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20195K1161988-10-24024 October 1988 Suppl to PWR Loop Ser:Use of Large Circulating Pump ML20154J6221988-08-29029 August 1988 Revised Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20153F5591988-06-30030 June 1988 Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20151R7341988-04-19019 April 1988 Sser for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20237K6121987-06-30030 June 1987 Mit Research Reactor Annual Rept to NRC for Jul 1986 - June 1987 ML20151R7271987-02-13013 February 1987 SER for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20148B3011986-06-30030 June 1986 Mit Research Reactor Annual Rept to NRC for Period Jul 1985 - June 1986 ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20214R3811986-01-31031 January 1986 Rept of Educational & Research Activities for Academic/ FY84-85 W/Selected Data from Previous Yrs ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20133H4081985-06-30030 June 1985 Mit Research Reactor Annual Rept to Us NRC for Jul 1984 - June 1985 1999-07-08
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- NUCLEAR REACTOR LABORATORY AN INTERDEPARTMENTAL CE NT ER OF MASS ACHUSE*TS INSTITUTE OF TECHNOLOGY k.h7
- - - -..--- - - - - - - .. - -. - - - - ..~ .. - .~.. . -
O K. HARLING 138 Albany Street, Camtitdge. Mass 02139 J A BERNARD. JR.
Director TeMax No. 10171253 7300 Deector of Reactor Operrions Telen No 92-1473 MIT CAM Tel No (617)253 4211/4202 March 2,1992
)
U.S. Nuclear Rcgulator/ Commission Washington, D.C. 20555 Attn: Document Control Desk
Subject:
Reportable Occurrence 50-20/1992-1, Improper Increase of Reactor Power Causing a Brief Excessive Power Level 1 Gentlemen:
Massachusetts Institute of Technology hereby submits this ten-day report of an ocentrence at the MIT Research Reactor (MITR) in accordance with paragraph 7.13.2(d) of the Technical Specifications. An initial report was made by telephone to NRC Region I (Mr. Thomas F. Dragoun) on February 21,1992. A telephone report was also made to NRC lleadquaners, Mr. Alexander Adams, on the same day. These telephone reports were delayed beyond the normal 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> because this occurrence was not identified by the MITR's u:nior staff until late on February 20,1992. This is further discussed in the
The format and content of this report are based on Regulatory Guide 1.16, Revision 1.
- 1. Reoort No.: 50-20/1992-1 2a. Repon Date: 2 Man:h 1992 2b. Date of Occunencc: 18 February 1992
- 3. Facility: MIT Nuclear Reactor Laboratory 138 Albany Street.
Cambridge,MA T139
(' gn o rup f 920306o3e3 92o3o2 PDR S
ADOCK 05000020
/
PDR W.' '
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Reportable Occurrence 50-20/921 Page 2
- 4. Idsgifcation of Oc' . xnce:
Impmper t>erformance of an inc* case in reactor power so that as a result of manual withdrawat of individual shim blades, the reactor's neutronic power att'dned 5.25 MW. The control devices were then inserted with the result that the total time for which the neutronic power exceeded 5.0 MW was about 22 s *1 his occurred at 1921 on 18 February 1992. The reactor's thermal power, which is continuously computed by a calorimetric balance and recorded, never exceeded 4.69 MW.
S. Conditions Prior to Occurrence:
The reactor was on analog automatic control at steady-state with the shim bank at 15.40 inches, The regulatin;; rod which was connected to the analog 3 controller was at 7.04 inches. Channei #7, the linear flux channel, was indicating 84.8 p.a which contsponds to 4.8 MW. TR reactor had been at this power level for about 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and had not yet attained thermal equilibrium. As a result, the thermal power was 4.69 MW. Several experiments were in propess, including one which required a near-constant temperature envimnment. This in turn meant that the power level had to be maintained constant.
- 6. Descriotion of Occunence:
The performance of reactor power increases at the MIT Rescamh Recctor is governed by written pmcedures that have been reviewed and approved by the MIT Reactor Safeguards Committee (MITRSC). These procedures rec uire, among other things, that (1) reactor power be increased on a period that is ..onger than 100 s whenever power is within 80% of the demanded level and (2) that two licensed operators, one of whom holds a senior license, be present in the control room during any power increase of more than 10%.
At approximately 1921 on February 18,1992, a malfunction occurred in the reactor's analog controller with the result that the regulating rod was continuously inserted until it reached its near-in limit. This caused the reactor's neutronic power,-
as indicated by channel #7, to decrease to 33.0 pa (1.87 MW). The console operator, a licensed senior operator, then took manual control of the reactor and notified the Duty Shift Supervisor and the Reactor Superintendent of the problem.
Permission was given for a return to the i mal operating power. The operator was anxious to minimize the temperature perturbation to the on-going experiment and therefore, instead of waiting for the Duty Shift Supervisor to reach the control -
room, asked another operator, who was in the immediate area, to witness the power increase. This was an acceptable practice except that the increau was imtiated before the second operator had fully reviewed the situation. The console operator sequentially raised each of the reactor's six shim blades by several tenths of an inch so as to create a positive period and to maintain a uniform bank height, This was in accordance with the governing procedure, except that enough reactivity was inserted to create a reactor period of about 50 s tnd, contrary to the approved procedure, the operator maintained this period until approaching the desired pow -
level. He then began to insen the shim blades sequentially, but was unable to negate completely the positive period because the differential reactivity worth of an
' individual blade at a height of about 16.00 inches is not sufficient to immediately_
i
+
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J
Reportable Occurrence 50-2092-1 Page 3 offset the reactivity associated with a 50-s period. As a result, an overshoot of the neutronic power occurred. This is shown in the attached figure which is the strip-chart reco~iing oflinear flux channel #7. (Nag: Once it was a aparent thr.t the power would overshoot, the operator drove one of the silm blades in continuously.) An error in judgment was then made in that the console operator did not notify the Reactor Supenntendent of the overshoot. As a result, the occurrence was not identified by the MITR's senior staff until the evening of February 20, 1992.
- 7. Description of Apparent Cause of Otcunence:
'Ihe apparent cause of this occurrence was operator error in that the operator performed a power increase on a period shorter than 100 s while tne power was within RO% of the dernanded level. L
- 8. Analysis of Occena:
The reactor's neutronic power, as measured by the trace recorded on the strip chart for channel #7 (the linear flux channel) cached 5.25 MW and was above 5.0 MW for 22 s. The reactor safety system is set to activate at 5.5 MW and this level was not reached. Reactor power, as recorded on the thermal power strip chart, did not exceed 4.69 MW It should be noted that the MITR-II Facility Operating License is written in terms of thermal power and hence no limiting condition for operation was exceeded.
It is not expected that an excursion to the 5.25 MW neutronic power level reached in this case, which is well below the authorized limiting safety system setting of 6 MW, would in any way cause any damage to the reactor. Nevertheless, ,
analyses were made of the primary coolant. No abnormalities were identified. The core purge gas monitor was norraal and a subsequent visual inspection of the reactor core revealed no abnormalities. These actions confirmed that no damage -
7 occurred to the n: actor.
t
- 9. Corrective Action:
The following corrective actions have been :aken:
(a) This occurrence was reviewed verbally with the operator in question with emphasis on the proper conduct of power increases.
(b) The Senior Review Board met to discuss the occurrence and decided to require tha' the operator involved complete a special review of the procedures and principles that govern power increases. (Action to be completed by 13 March 1992.)
(c) The Senior Review Board also decided that the protocol for information exchange between operators, the details of this occurrence, and the criteria for notifying the senior MITR stat'f of occurrences be reviewed by all
. licensed operators. (Action to be completed by 30 April 1992.)
t . . . .
. 4 Reportable Occurrence 50-20921 Page 4 L .
(d) Investigated and repaired analog automatic control system. (Temporary repair completed 25 February 1992 Permanent trpair is still pending.)
- 10. Failure Data:
An improper reshim that resulted in an overshoot of the neutronic power occurred on 19 November 1987, (See ROR #50-2Qfl987-2.)
Sinenrely,
(
Kwan S. Kwok, h6h. k Superintendent i
.k CL !
John A, Best ud, Ph.D. ~
Director of Reactor Operations MIT Research Reac'or JAB:CRH
Attachment:
Figure One cc: MITRSC USNRC- Region I- Chief,' , .
Reactor Projects Se; tion No. 3A USNRC - Region I- Reactor Engineer, Reactor Projects Section Nn. 3A USNRC- Project Manager, Standardization and Non-Power Reactor lioject Directorate USNRC - Region I - Chief, . .
Effluents Radiation Protection Branch .
1 I I
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- - - _ - - _ - _ - _ - - _ - - _ - - - _ - - - - - --- n
Reportable Oxurrerne 5420921 Page5 i
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g5 5.'25 MW i 1.87 MW Period of -50 s - '
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