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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20137G3531985-04-18018 April 1985 RO 50-20/1985-1:on 850408,main Intake Valve Failed Light Test Maint Procedure.Caused by Excessive Wear of Valve Gasket.Gasket Replaced ML20081H8191983-09-15015 September 1983 RO 50-20/1983-2:on 830906,fission Product Gas Levels Rise from 2.8% Max Permissible Concentration in Jul 1983 to 4.57% in Aug Noted.Caused by Excessive Outgassing of Fuel Element MIT-08.Element Removed from Core ML20074A7521983-04-29029 April 1983 RO 50-20/1983-1:on 830419,main Intake Valve Closed & Could Not Be Reopened.Caused by Piston Rod Rupture Near Rod Eye, Leaving Valve in Closed Position.Defective Hydraulic Cylinder Shaft Replaced ML20063B9221982-08-17017 August 1982 Ro:On 820809,slight Increase Found in Levels of Fission Products in Reactor Primary Sys.Cause Under Investigation. Criterion for Operation W/Possible Faulty Core Element Per RO 50-20/79-4 Will Be Observed 1999-03-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20209C9331999-07-0808 July 1999 Vols 1 & 2 to SAR for Ma Institute of Technology Nuclear Reactor Lab ML20196K0331999-06-30030 June 1999 Quality Mgt Program for Generation of MITR-II Medical Therapy Facility Beams for Human Therapy, Reflecting Change to Provision 14 ML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20199H2371998-12-31031 December 1998 Revised SER for Fission Converter Facility ML20196B7541998-06-30030 June 1998 Mit Research Reactor Nuclear Reactor Lab Ma Inst of Technology,Annual Rept to Us NRC for Period 970701-980630. with ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20217G2181997-10-0303 October 1997 SER for Fission Converter Facility ML20198P8071997-06-30030 June 1997 Annual Operating Rept for Jul 1996 - June 1997 ML20137L5901997-04-0303 April 1997 Safety Evaluation Supporting Amend 30 to License R-37 ML20129B3201996-06-30030 June 1996 Annual Rept to Us NRC for Period 950701-960630 ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20092K2301995-06-30030 June 1995 Mit Research Reactor Annual Rept to NRC for Period Jul 1994 - June 1995 ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20072T3041994-06-30030 June 1994 Annual Rept for Mit Research Reactor for 930701-940630 ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20056G8011993-06-30030 June 1993 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for Period 920701-930630 ML20128P4371993-02-16016 February 1993 Safety Evaluation Supporting Amend 27 to License R-37 ML20073H1451992-12-0909 December 1992 Study of MITR-II Core Tank Aging for Relicensing Consideration ML20114D9261992-06-30030 June 1992 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for 910701-920630 ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20082L8451991-06-30030 June 1991 Mit Research Reactor Annual Rept to NRC for Jul 1990 to June 1991 ML20058N5741990-08-10010 August 1990 QA Program for MITR-II Spent Fuel Shipment ML20059G4331990-06-30030 June 1990 Mit Research Reactor Annual Rept to NRC for Jul 1989 - June 1990 ML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML20012C2771990-03-0909 March 1990 SER for BWR Coolant Chemistry Loop to Be Installed & Operated in Mitr ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20247H7041989-06-30030 June 1989 Mit Research Reactor Annual Rept for Jul 1988 - June 1989 ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20195K1161988-10-24024 October 1988 Suppl to PWR Loop Ser:Use of Large Circulating Pump ML20154J6221988-08-29029 August 1988 Revised Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20153F5591988-06-30030 June 1988 Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20151R7341988-04-19019 April 1988 Sser for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20237K6121987-06-30030 June 1987 Mit Research Reactor Annual Rept to NRC for Jul 1986 - June 1987 ML20151R7271987-02-13013 February 1987 SER for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20148B3011986-06-30030 June 1986 Mit Research Reactor Annual Rept to NRC for Period Jul 1985 - June 1986 ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20214R3811986-01-31031 January 1986 Rept of Educational & Research Activities for Academic/ FY84-85 W/Selected Data from Previous Yrs ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20133H4081985-06-30030 June 1985 Mit Research Reactor Annual Rept to Us NRC for Jul 1984 - June 1985 1999-07-08
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MASSACHUSETTS INSTITUTE OF TECHNOLOGY O.K. HARLING 138 Albany Street Cambridge, Mass. 02139 L. CLARK, JR.
Dir:ctor (617)253- 4 21 1 Directorof Reactoroperations Sep tember 15, 1983 Dr. Thomas E. Murley, Acting Administrator Region I U.S. Nuclear Regulatory Commission Attn: Mr. W. Kinney, Reactor Inspector 631 Park Avenue King of Prussia, PA 19406 Subject : Reportable Occurrence 50-20/1983-2, License R-37 Increase in Outgassing of a Fuel Element Gentlemen:
Massachusetts Institute of Technology hereby submits the 10-day report of an occurrence at the MIT Research Reactor, in accordance with paragraph 7.13.2(d) of the Technical Specifications. An initial report of this occurrence was made by telephone to Region I on Sept. 7, 1983.
The format of this report is based on Regulatory Guide 1.16, Revision 1.
- 1. Report No: 50-20/1983-2 2a. Report Date: 15 Sept. 1983 2b. Occurrence Date : 6 Sept. 1983
- 3. Facility: MIT Nuclear Research Reactor 138 Albany Street Cambridge, Massachusetts 02139
- 4. Identification of Occurrence:
A steady increase in the fission product gas release over a period of several weeks to approximately 5% of the maximum permissible concentration (MPC) was interpreted as an indication of a possible fuel element cladding failure. It was decided that the best means to investigate this possibility was to both " sip" and visually inspect fuel elements during scheduled shut-downs. The sipping process consists of collecting and counting one liter coolant samples drawn through the fuel element. This procedure, coupled with visual inspection using alternately light and the Cerenkov radiation to illuminate the plates, would permit determination of whether or not any particular element had either a higher fission product gas release than what normally dif fuses through the aluminum cladding or a blister. The 8311070593 0 #
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Dr. Thomas E. Murley September 15, 1983 Page 2 reactor was then operated at low power, approximately 1 Kw, for several hours for training while the water samples were being anelyzed. MIT-08 was identi-fled as having an abnormally high rate of outgassing. The reactor was then shutdown and preparations for refueling initiated.
- 5. Conditions Prior to Occurrence:
Element MIT-08 was first inserted in the reactor's B-Ring on 23 Feb.
1981. It remained in-core continuously until 18 Jan. 1982 when it was removed and placed in the fuel storage ring for subsequent reuse. This pattern is standard and has been followed for almost all of the MITR fuel elements . Element MIT-08 was placed in-core again on 27 June 1983. A slow, but steady increase in fission product gas levels was observed several weeks later.
- 6. Description of Occurrence:
The fission product gas levels obtained in accordance with standard sampling procedures rose from approximately 2.8% of MPC in July 1983 to approximately 4.57% one month later. In addition, spiking of the core purge monitor by a factor of about 1.5 for about one minute following reactor startups for the three preceding weeks was observed.
- 7. Description of Apparent Cause of Occurrence:
The apparent cause of this occurrence is excessive outgassing of fuel element MIT-08. Visual examinations of the element (under water) have been performed. What may be a blister is barely visible. It is located on the third plate of the element, counting plates radially outward from the core center. It appears to be about 0.5 inch in diameter, appears to invade the coolant channel by only a small amount, is only on one side of the plate, and is about 5"-6" from the top of the element. The exact mode of failure can not be determined without the use of hot cells and special facilities not available at MIT.
- 8. Analysis of Occurrence:
Quality assurance records on the manufacture of element MIT-08 do not indicate any deviations from the MITR element specifications. The forma-tion of the blister probably occurred in July-Aug. 1983. Element MIT-08 had been in-core while 22,600 MWH of energy were produced. It has 447 grams of its original 506 gram loading of U-235 remaining. It is standard MITR policy to both rotate and invert fuel elements in order to maximize b urnup . Neither of these operaitns had been performed on MIT-08 because it was not yet sufficiently advanced in the fuel cycle. Power production in the upper portions of the MIT Reactor is, by design, kept low through the use of fixed poison plates. As a result, while the point of peak
Dr. Thomas E. Murley September 15, 1983 Page 3 burnup on MIT-08 was 32.7% of the allowed fission density (1.810 fissions /cc),
the area where the blister occurred was in the low power region and only at 17.7% of the limit. Primary coolant chemistry is carefully monitored. The three parameters measured (pH, chloride, conductivity) have generally been as specified. The few deviations that have occurred were too brief and of too low a magnitude to have caused this occurrence.
Relative to effluent releases, the combination of standard sampling pro-cedures and the existence of procedures for handling any abnormalities in the sampling results means that the problem was quickly diagnosed, identified, and corrected. No significant release occurred.
- 9. Corrective Action:
The immediate corrective action consisted of removing element MIT-08 from the core. Fission product gas levels subsequently decreased and are currently only slightly up (3.3% MPC) over what was measured prior to the occurrence. All other in-core "MIT" series elements have been " sipped" and no abnormalities were found. MIT-08 was also again sipped at this time and the abnormally high fission product release rate was confirmed.
- 10. Failure Data:
A cladding failure occurred to a "4M?' series element in June 1979.
Refer to ROR #50-20/79-4 dated 2 July 1979. The current failure was far less severe than that one. Also, it occurred in a "MIT", not a "4W',
series element. ("MIT" series fuel was made by Atomics International.
The "4M" series by Gulf Atomic.) The existence of a gradual and slight increase in the fission product levels in the NETR's primary coolant was reported to Region I as a matter of information on 17 Aug.1982. One element, MIT-21, was identified as being suspect at that time. MIT-08 was i not in the core during most of 1982 and there does not appear to be any l
connection between the possible problem described in the letter of 08/17/82 and this occurrence.
Operating experience with fuel from both manufacturers has been good, except as noted below. Of 43 elements made by Gulf Atomic, 26 elements (390 plates) have been permanently discharged from the core after peak burn-up approached the license limit. 16 other elements (290 plates) are still in use and have peak fission densities in the range 0.5-1.3 x 10 2t f/cc.
Average burnups in the above cases range from 14% to 35%. One failed in 1979 as reported earlier, at an average burnup of 32.5%.
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Dr. Thomas E. Murley September 15, 1983 Page 4 Of24elementsmadebyAIandnowinuse,greeelements (45 plates) have peak fission densities exceeding 1.37 x 10 f/cc, average burnup 33%.
21 other elements now in use (315 plates) have peak fission densities in 21 the range 0.1-0.5 x 10 f/cc.
On the basis of the above experience, the two failures are very likely fabrication defects and not generic problems.
Sincerely, M b John A. Bernard Superintendent y
{ -. -- 4$ { r-Lincoln Clark, Jr.
N Director of Operations JB/gw cc: MITRSC USNRC-0MIPC USNRC-DMB
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