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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML19345B9941980-11-26026 November 1980 RO 50-020/79-4A:supplemental Info Re Apparent Fuel Element Cladding Failure Originally Reported on 790702.Caused by Mfg Deficiency.Element Continously Monitored ML19312E6141980-05-27027 May 1980 Forwards Revised Page 2 of RO 50-20/80-2 Dtd 800523.Revision Corrects Second Paragraph of Section 7 Re Frequency of Blade Thickness Measurements & Clarifies Description of Electromagnetic Coupling of Blade ML19323G4221980-05-23023 May 1980 RO 50-20/80-02:on 800519,intermittent Binding of Shim Blade Number 1 Not in Accordance W/Tech Specs.Caused by Foreign Matl Impeding Motion.Electromagnet Containing Foreign Matl Replaced & Other Blades Checked ML19323D5081980-04-25025 April 1980 RO 50-20/80-1:on 800322,initial Rept Was Made Re Failure of Outer Door of Truck Airlock to Maintain Leak Rate of Bldg Containment Limits.Caused by Seal Leak in Outer Door. Door Will Not Be Routinely Opened Until Gasket Is Replaced ML19250C0681979-10-19019 October 1979 RO 50-20/79-5:on 791010,compiled 10-day Startup W/Only One Operable Nuclear Safety Channel Level Scram.Caused by Broken Resistor on Amplifier Circuit Board.Circuit Board Repaired 1990-03-22
[Table view] Category:LER)
MONTHYEARML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML19345B9941980-11-26026 November 1980 RO 50-020/79-4A:supplemental Info Re Apparent Fuel Element Cladding Failure Originally Reported on 790702.Caused by Mfg Deficiency.Element Continously Monitored ML19312E6141980-05-27027 May 1980 Forwards Revised Page 2 of RO 50-20/80-2 Dtd 800523.Revision Corrects Second Paragraph of Section 7 Re Frequency of Blade Thickness Measurements & Clarifies Description of Electromagnetic Coupling of Blade ML19323G4221980-05-23023 May 1980 RO 50-20/80-02:on 800519,intermittent Binding of Shim Blade Number 1 Not in Accordance W/Tech Specs.Caused by Foreign Matl Impeding Motion.Electromagnet Containing Foreign Matl Replaced & Other Blades Checked ML19323D5081980-04-25025 April 1980 RO 50-20/80-1:on 800322,initial Rept Was Made Re Failure of Outer Door of Truck Airlock to Maintain Leak Rate of Bldg Containment Limits.Caused by Seal Leak in Outer Door. Door Will Not Be Routinely Opened Until Gasket Is Replaced ML19250C0681979-10-19019 October 1979 RO 50-20/79-5:on 791010,compiled 10-day Startup W/Only One Operable Nuclear Safety Channel Level Scram.Caused by Broken Resistor on Amplifier Circuit Board.Circuit Board Repaired 1990-03-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20209C9331999-07-0808 July 1999 Vols 1 & 2 to SAR for Ma Institute of Technology Nuclear Reactor Lab ML20196K0331999-06-30030 June 1999 Quality Mgt Program for Generation of MITR-II Medical Therapy Facility Beams for Human Therapy, Reflecting Change to Provision 14 ML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20199H2371998-12-31031 December 1998 Revised SER for Fission Converter Facility ML20196B7541998-06-30030 June 1998 Mit Research Reactor Nuclear Reactor Lab Ma Inst of Technology,Annual Rept to Us NRC for Period 970701-980630. with ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20217G2181997-10-0303 October 1997 SER for Fission Converter Facility ML20198P8071997-06-30030 June 1997 Annual Operating Rept for Jul 1996 - June 1997 ML20137L5901997-04-0303 April 1997 Safety Evaluation Supporting Amend 30 to License R-37 ML20129B3201996-06-30030 June 1996 Annual Rept to Us NRC for Period 950701-960630 ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20092K2301995-06-30030 June 1995 Mit Research Reactor Annual Rept to NRC for Period Jul 1994 - June 1995 ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20072T3041994-06-30030 June 1994 Annual Rept for Mit Research Reactor for 930701-940630 ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20056G8011993-06-30030 June 1993 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for Period 920701-930630 ML20128P4371993-02-16016 February 1993 Safety Evaluation Supporting Amend 27 to License R-37 ML20073H1451992-12-0909 December 1992 Study of MITR-II Core Tank Aging for Relicensing Consideration ML20114D9261992-06-30030 June 1992 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for 910701-920630 ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20082L8451991-06-30030 June 1991 Mit Research Reactor Annual Rept to NRC for Jul 1990 to June 1991 ML20058N5741990-08-10010 August 1990 QA Program for MITR-II Spent Fuel Shipment ML20059G4331990-06-30030 June 1990 Mit Research Reactor Annual Rept to NRC for Jul 1989 - June 1990 ML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML20012C2771990-03-0909 March 1990 SER for BWR Coolant Chemistry Loop to Be Installed & Operated in Mitr ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20247H7041989-06-30030 June 1989 Mit Research Reactor Annual Rept for Jul 1988 - June 1989 ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20195K1161988-10-24024 October 1988 Suppl to PWR Loop Ser:Use of Large Circulating Pump ML20154J6221988-08-29029 August 1988 Revised Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20153F5591988-06-30030 June 1988 Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20151R7341988-04-19019 April 1988 Sser for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20237K6121987-06-30030 June 1987 Mit Research Reactor Annual Rept to NRC for Jul 1986 - June 1987 ML20151R7271987-02-13013 February 1987 SER for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20148B3011986-06-30030 June 1986 Mit Research Reactor Annual Rept to NRC for Period Jul 1985 - June 1986 ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20214R3811986-01-31031 January 1986 Rept of Educational & Research Activities for Academic/ FY84-85 W/Selected Data from Previous Yrs ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20133H4081985-06-30030 June 1985 Mit Research Reactor Annual Rept to Us NRC for Jul 1984 - June 1985 1999-07-08
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! NUCLEAR REACTOR LABORATORY
, , - AN INTERDEPARTMENTAL CENTER OF
. MASSACHUSETTS INSTITUTE OF TECHNOLOGY
' o.K, HARLING 138 Albany Street, Cambridge, Mass. 02139 ~ J.A. BERNARD, JR.
Diroc'or Telefax No. (617)253-7300 Director of Reactor Operations '
Telex No. 92-1473-MIT CAM Tel. No. (617) 253-421 t/4202 -
March 22,1990 s
U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Attn: Document ControlDesk -
Subject:
Reportable Occurrence 50-20/1990-1, Incorrect Calculation of Estimated Critical
..v, Position '
Gentlemen:
Massachusetts Institute of Technology hereby submits this ten-day report of an occurrence'at the MIT Research Reactor in accordance with paragraph 7.13.2(d) of the ~
Technical Specifications. An initial report was made by telephone to Region I (Dr. P. K.
' Eapen) on 13 March 1990.
The format and content of this report are based on Regulatory Guide 1.16, .
Revision 1.
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- 1. ' Report No.: 50-20/1990-l' 2a.- Reoort Date: 22 March 1990
< 2b. Date of Occurrence: 12 March 1990
?. " Facility: MIT Nuclear Reactor Laboratory 138 Albany Street Cambridge, MA' 02139
- 4. Identification of Occurrence:
During a reactor startup on 12 March 1990, the MIT Research Reactor was briefly operated on an unusually short reactor period. - As a result, an automatic safety system shutdown occurred.' No technical specifications were violated and all safety system equipment functioned properly. The o;3eration in this period range was not in accordance 1with internal operating procedures in t 1at a dynamic period of 10.4 seconds was attained -
while that allowed by normal operating procedure is 30.0 seconds with allowance for l
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shorter periods during special tests. The technical specification for the limiting safety ,
system setting is 3 seconds.
- 5. : Conditions Prior to Occurrenc_e:
The reactor had been operated normally the previous week and, following a
- weekend shutdown,'was being started up in accordance with the standard operating procedures, f
af 6.' Description of Occurrence:
, As part of the routine reactor startup procedure, an estimated critical position (ECP) ,
is calculated. This is done by first determmmg the net reactivity change that has occurred since the last startup. For example, allowance is made for such factors 'as refuelings, sample changes, primary temperature, and xenon. Once this figure is obtained, it is added (or subtracted as the case may be) to the critical data recorded from the most recent, previous, xenon-free startup to obtain the anticipated critical position for the present startup. For the startup on 03/12/90 a trainee, the console operator, and the reactor supervisor each independently calculated the net reactivity change, which is the first part of the pmcess of determining the ECP. All three did the~ calculation correctly. However, for the second part of that process, both the operator and the supervisor relied on the traince's s , calculation. Unfortunately, the trainee used critical data from a xenon-equilibrium.
l' condition when that for a xenon free (or near xenon-free) condition should have been used.
At 1100, the console operator and the supervisor commenced a reactor startup on
. the assumption that criticality would be attained at about 11.04 inches on the reactor's shim bank. In reality, the correct ECP was 8.60 inches. As the startup progressed, the operator g observed an increasingly short period but attributed it to noise on the instrument channels.
The operator and supervisor also failed to recognize the significance of several other 4
- indicators of approaching criticality including'the need to upscale both the startup channels i and an audible count rate meter. Also, they might have predicted the approach to criticality if they had taken heed of the changes in count rate level on the startup channels.
At 1120, the reactor was automatically shut down by the safety system. The reactor l- supervisor reported the cause of the shutdown as instmment noise and obtained approval for a restart from the Reactor Superintendent. At 1135, the restart began. At 1150 the operator and supervisor again observed an increasingly short period. This time they g recognized it as a true signal and immediately made the reactor suberitical in accordance with existing written procedures that cover an error in the ECP calculation. The
- Superin endent was agam notified, the reactor was shut down, and the Director of Reactor Operations was notified.
L 7.- Dgscriotion of Apparent Cause of Occurrence:
This occurrence was the result of several factors. These were as follows:
.y a) The console operator and reactor supervisor did not check the second
[ portion of the ECP calculation which had been performed by an individual L; m traimng.
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b) Excessive reliance was placed on the ECP as the means of identifying -
criticality, c) The console operator and supervisor did not take notice of the indications that the reactor was approachmg cri;icality. These included the earlier-than-usual upscaling of the mstrumentation and the response of the reactor period -
to contml blade motion.
~ d). The existence f L actual short period was' attributed to instrument noise.
Each of the above involves a human error. It should be noted that all equiament functioned properly. However, in the startup range, some _' noise' on some of the c iannels has becc observed in the past. -
- 8. Analysis of Occurrence:
This occurrence resulted solely in a violation ofinternal operating procedures. No technical specification violations occurred. Following the occurrence, the trip points of the -
three period channels in the safety system were verified. They were found to trip at 10.5, 10.3, and 10.4 seconds. The specification is 10-11 seconds. The limiting safety system
, setting for period is 3 seconds. The excess tractivity present at the time of the automa'.ic shutdown was estimated to be 325 mbeta which corresponds to a steady period of 16 seconds. (Holn: The dynamic effect of blade withdrawal is sufficient to create an.
Instantaneous 10.4 second period given a steady one of 16 seconds.) The reactor neutronic power at the time of the scram was 340 watts. The reactor's heat removal system had been configured for 5 MW, the licensed operating level. Hence, at all times the reactor _was safely within the limiting conditions for operation.
- 9. Conective Action:
The following corrective actions have been taken:
a) Reponed the occurrence to the Chairman and to several members o'f the MIT.
, Reactor Safeguards Committee (MITRSC). ,
b) Held a meeting with alllicensed personnel on 03/19/90 to discuss both the occurrence and , roper operating practice. Both the MITRSC Chairman and the Director of t le NRL attended and spoke at the meeting stressing the need to give attention to the details of safe operation.
n c) Modified the reactor startup procedure to require two independent calculations of the ECP by licensed operators. (Previously, it was required ,
that the calculation only be reviewed by the supervisor. It is now required that the console operator and supervisor each do the calculation separately.
. Action' implemented via temporary directive 03/19/90. Action to be L complete 05/31/90).
d) Stressed to all operators the importance of sound operating practices including not to rely on trainees and to thoroughly investigate all abnormal instrument readings.
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kl e) ~ Directed electronics personnel to investigate noise effects on the reactor !
startup instrumentation. ,
L p 10.- Failure Data:
here have been no related occurrences.
.l
. Sincerely, o Kwan S. Kwok .
.s Superintendent .
MIT Research Reactor
.k o ' d< !
ohn 'A. Bernard, Ph.D.
. Director of Reactor. Operations
' MIT Research Reactor r.
1-JAB /CRH 1
cc: MITRSC -
USNRC -- Region I- Chief, . ,
_ Reactor Projects Section 3B P- -
USNRC - Region I Project Engineer,-' -;
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Reactor Projects Section 3B -
L USNRC - Senior Resident Inspector, . -
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- Pilgrim Nuclear Station :
USNRC - Project Manager, .s B - Standardization and Non-Power Project Directorate -
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