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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARB17766, Application for Amend to License DPR-65,to Return Hydrogen Purge Sys to Former Classification of Being within Scope of Maint Rule Program,But Not as risk-significant Sys1999-09-23023 September 1999 Application for Amend to License DPR-65,to Return Hydrogen Purge Sys to Former Classification of Being within Scope of Maint Rule Program,But Not as risk-significant Sys B17832, Application for Amend to License DPR-65,removing Current Special Exception Which Precludes Applying Eighteen Month Functional Testing Surveillance to SG Hydraulic Snubbers1999-09-0707 September 1999 Application for Amend to License DPR-65,removing Current Special Exception Which Precludes Applying Eighteen Month Functional Testing Surveillance to SG Hydraulic Snubbers B17829, Suppl 1 to TS Change Request 1-1-99 for Amend to License DPR-21,revising Proposed Permanently Defueled TS Sections 5.6.1,5.7.2 & 5.7.3 & Adding Proposed Section 5.6.4 to Reflect ACs Contained in NUREG-14331999-08-25025 August 1999 Suppl 1 to TS Change Request 1-1-99 for Amend to License DPR-21,revising Proposed Permanently Defueled TS Sections 5.6.1,5.7.2 & 5.7.3 & Adding Proposed Section 5.6.4 to Reflect ACs Contained in NUREG-1433 B17799, Application for Amend to License NPF-49,incorporating Editorial Revs to TS Sections 3.8.3.2,4.6.2.1,4.6.2.2, 4.8.1.1,4.9.12 & Bases Sections B 3/4.3.2,B 3/4.4.11, B 3/4.6.1.2 & B 3/4.8.41999-08-0505 August 1999 Application for Amend to License NPF-49,incorporating Editorial Revs to TS Sections 3.8.3.2,4.6.2.1,4.6.2.2, 4.8.1.1,4.9.12 & Bases Sections B 3/4.3.2,B 3/4.4.11, B 3/4.6.1.2 & B 3/4.8.4 B17828, Application for Amend to License DPR-65,modifying TS by Increasing Action Requirement Time to Be in Mode If Temp of UHS Exceeds TS Limit of 75 F1999-07-16016 July 1999 Application for Amend to License DPR-65,modifying TS by Increasing Action Requirement Time to Be in Mode If Temp of UHS Exceeds TS Limit of 75 F B17772, Application for Amend to License DPR-65,relocating Selected TS Re Refueling Operations & Associated Bases to Plant TRM1999-07-16016 July 1999 Application for Amend to License DPR-65,relocating Selected TS Re Refueling Operations & Associated Bases to Plant TRM B17764, Application for Amend to License NPF-49,deleting Reference to ASME Code Paragraph Iwv 3472(b) Re Frequency of Leakage Rate Testing for Valves Six Inches Nominal Pipe Size & Larger Contained in TS 4.4.6.2.2.e1999-05-17017 May 1999 Application for Amend to License NPF-49,deleting Reference to ASME Code Paragraph Iwv 3472(b) Re Frequency of Leakage Rate Testing for Valves Six Inches Nominal Pipe Size & Larger Contained in TS 4.4.6.2.2.e B17621, Application for Amend to License DPR-21,reflecting Permanently Defueled Condition of Unit 1,Tech Specs Administrative Controls Section as Allowed by Guidance Contained in NRC Administrative Ltr 95-061999-04-19019 April 1999 Application for Amend to License DPR-21,reflecting Permanently Defueled Condition of Unit 1,Tech Specs Administrative Controls Section as Allowed by Guidance Contained in NRC Administrative Ltr 95-06 B17737, Mod to 990104 Application for Amend to License DPR-65, Changing Value for Turbine Driven Auxiliary Feedwater Pump Associated with Monthly Surveillance Testing of Various ESF Pump1999-04-0707 April 1999 Mod to 990104 Application for Amend to License DPR-65, Changing Value for Turbine Driven Auxiliary Feedwater Pump Associated with Monthly Surveillance Testing of Various ESF Pump B17343, Application for Amend to License NPF-49,revising TS to Support Spent Fuel Pool Rerack to Maintain Full Core Reserve Capability Approaching End of Ol.Proprietary & non- Proprietary Licensing Repts,Encl.Proprietary Rept Withheld1999-03-19019 March 1999 Application for Amend to License NPF-49,revising TS to Support Spent Fuel Pool Rerack to Maintain Full Core Reserve Capability Approaching End of Ol.Proprietary & non- Proprietary Licensing Repts,Encl.Proprietary Rept Withheld B16997, Application for Amend to License DPR-65,relocating Instrumentation TSs 3.3.3.2,3.3.3.3 & 3.3.3.4 to Mnps,Unit 2 Trm,Per GL 95-101999-03-19019 March 1999 Application for Amend to License DPR-65,relocating Instrumentation TSs 3.3.3.2,3.3.3.3 & 3.3.3.4 to Mnps,Unit 2 Trm,Per GL 95-10 B17658, Application for Amend to License DPR-65,revising TSs 3.5.2, 3.7.1.7 & 3.7.6.1 Re ECCS Valves,Atmospheric Steam Dump Valves & CR Ventilation Sys.Associated Bases Will Be Modified as Necessary to Address Proposed Changes1999-03-17017 March 1999 Application for Amend to License DPR-65,revising TSs 3.5.2, 3.7.1.7 & 3.7.6.1 Re ECCS Valves,Atmospheric Steam Dump Valves & CR Ventilation Sys.Associated Bases Will Be Modified as Necessary to Address Proposed Changes ML20207J6201999-03-15015 March 1999 Application for Amends to Licenses NPF-49 & NPF-86, Transferring Control of Licenses to Reflect Change in Upstream Economic Ownership of Parent Company of Nep,Vols I & Ii.Pages 48,49 & Annual Rept 1996 Pages 2 & 3 Omitted B17566, Application for Amend to License NPF-49,proposing Amend to TS 3/4.7.4, SW Sys, by Adding AOT for One SW Pump Using Duration More in Line with Significance Associated with Function of Pump1999-03-0202 March 1999 Application for Amend to License NPF-49,proposing Amend to TS 3/4.7.4, SW Sys, by Adding AOT for One SW Pump Using Duration More in Line with Significance Associated with Function of Pump B17669, Suppl to Application for Amend to License DPR-65,revising DG Action Statements & Surveillance Requirements1999-02-11011 February 1999 Suppl to Application for Amend to License DPR-65,revising DG Action Statements & Surveillance Requirements B17004, Application for Amend to License NPF-49,revising TS Table 3.7-6, Area Temp Monitoring & Revising FSAR to Describe Full Core off-load Condition as Normal Evolution.Proprietary Rev 2 to HI-971843,encl.Proprietary Info Withheld1999-01-18018 January 1999 Application for Amend to License NPF-49,revising TS Table 3.7-6, Area Temp Monitoring & Revising FSAR to Describe Full Core off-load Condition as Normal Evolution.Proprietary Rev 2 to HI-971843,encl.Proprietary Info Withheld B17623, Application for Amend to License DPR-65,changing TS 3.6.1.2, Containment Sys - Containment Leakage1999-01-18018 January 1999 Application for Amend to License DPR-65,changing TS 3.6.1.2, Containment Sys - Containment Leakage ML20199L0631999-01-18018 January 1999 Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into TS 3/4.2.2, Heat Flux Hot Channel Factor-FQ(Z), 6.9.1.6.a & 6.9.1.6.b, Colr B17590, Application for Amend to License DPR-65,removing TS 3/4.6.4.3, Containment Systems,Hydrogen Purge Sys, from Plant TS1999-01-18018 January 1999 Application for Amend to License DPR-65,removing TS 3/4.6.4.3, Containment Systems,Hydrogen Purge Sys, from Plant TS B17517, Application for Amend to License DPR-65,incorporating Changes to ESF Pump Testing Contained in TSs 3.5.2,3.6.2.1, 3.7.1.2,3.7.3.1 & 3.7.4.11999-01-0404 January 1999 Application for Amend to License DPR-65,incorporating Changes to ESF Pump Testing Contained in TSs 3.5.2,3.6.2.1, 3.7.1.2,3.7.3.1 & 3.7.4.1 B17519, Application for Amend to License DPR-65,revising Loss of Normal Feedwater (Lonf) Analyses to TS 2.2.1.Addl TS Bases Change to Floor Value for Thermal Margin Low Pressure Reactor Trip & Proposed FSAR Changes,Included1998-12-28028 December 1998 Application for Amend to License DPR-65,revising Loss of Normal Feedwater (Lonf) Analyses to TS 2.2.1.Addl TS Bases Change to Floor Value for Thermal Margin Low Pressure Reactor Trip & Proposed FSAR Changes,Included B17542, Application for Amend to License DPR-65,requesting Review & Approval to Plant Fsar,Per 10CFR50.90.Changes to Plant FSAR Pages,Encl1998-12-10010 December 1998 Application for Amend to License DPR-65,requesting Review & Approval to Plant Fsar,Per 10CFR50.90.Changes to Plant FSAR Pages,Encl B17342, Application for Amend to License NPF-49,proposing Rev to TS 4.7.10.e to Eliminate Need to Cycle Plant & Components Through SD-startup Cycle by Allowing Next Snubber Surveillance Interval to Be Deferred1998-12-0404 December 1998 Application for Amend to License NPF-49,proposing Rev to TS 4.7.10.e to Eliminate Need to Cycle Plant & Components Through SD-startup Cycle by Allowing Next Snubber Surveillance Interval to Be Deferred B17546, Application for Amend to License DPR-21,requesting NRC Approval of Certified Fuel Handler Training & Retraining Program & Request for Exemption from Requirements of 10CFR50.54(m)(2)1998-12-0404 December 1998 Application for Amend to License DPR-21,requesting NRC Approval of Certified Fuel Handler Training & Retraining Program & Request for Exemption from Requirements of 10CFR50.54(m)(2) B17498, Application for Amend to License DPR-65,revising FSAR Due to Increase in Radiological Consequences Caused by Changes in Assumptions Used in Updated Dose Consequences Analysis of Sgtr.Rvised FSAR Pages Encl1998-11-13013 November 1998 Application for Amend to License DPR-65,revising FSAR Due to Increase in Radiological Consequences Caused by Changes in Assumptions Used in Updated Dose Consequences Analysis of Sgtr.Rvised FSAR Pages Encl B17492, Application for Amend to License DPR-65,modifying TSs 3.3.1.1 & 3.3.2.1 to Restrict Time That Reactor Protection or ESF Actuation Channel Can Be in Bypass Position to 48 H, from Indefinite Period of Time1998-11-10010 November 1998 Application for Amend to License DPR-65,modifying TSs 3.3.1.1 & 3.3.2.1 to Restrict Time That Reactor Protection or ESF Actuation Channel Can Be in Bypass Position to 48 H, from Indefinite Period of Time B16951, Application for Amend to License DPR-65,changing TS 3.3.2.1, Instrumentation - ESFAS Intrumentation, 3.4.9.3, RCS - Overpressure Protection Sys & ECCS - ECCS Subsystems - Tavg 300 F1998-10-22022 October 1998 Application for Amend to License DPR-65,changing TS 3.3.2.1, Instrumentation - ESFAS Intrumentation, 3.4.9.3, RCS - Overpressure Protection Sys & ECCS - ECCS Subsystems - Tavg 300 F B17417, Application for Amend to License DPR-65,re Separation Requirement in FSAR of Six Inches,Which Is Applied to Redundant Vital Cables,Internal Wiring of Redundant Vital Circuits & Associated Devices1998-09-28028 September 1998 Application for Amend to License DPR-65,re Separation Requirement in FSAR of Six Inches,Which Is Applied to Redundant Vital Cables,Internal Wiring of Redundant Vital Circuits & Associated Devices B17413, Application for Amend to License DPR-65,revising TS Sections 3.3.2.1,3.4.6.2,3.4.8,3.6.2.1,3.6.5.1,3.7.6.1 & 3.9.15 as Result of Revised MSLB Analyses & Revised Determinations of Radiological Consequences of MSLB & LOCA1998-09-28028 September 1998 Application for Amend to License DPR-65,revising TS Sections 3.3.2.1,3.4.6.2,3.4.8,3.6.2.1,3.6.5.1,3.7.6.1 & 3.9.15 as Result of Revised MSLB Analyses & Revised Determinations of Radiological Consequences of MSLB & LOCA B17381, Application for Amend to License DPR-65,changing TS Definitions 1.24,1.27,1.31,TSs 3.0.2,4.0.5,3.2.3,3.3.2.1, 3.4.1.1,3.4.11 & Adding TS 3.0.61998-09-0909 September 1998 Application for Amend to License DPR-65,changing TS Definitions 1.24,1.27,1.31,TSs 3.0.2,4.0.5,3.2.3,3.3.2.1, 3.4.1.1,3.4.11 & Adding TS 3.0.6 ML20237B2691998-08-12012 August 1998 Application for Amend to License DPR-65,updating List of Documents Describing Analytical Methods Specified in TS 6.9.1.8b.Rev 1 to EMF-98-036,encl ML20236Y4951998-08-0606 August 1998 Application for Amend to License NPF-49,revising TS Surveillance 4.4.5.3.a Re SG Tube Insp Interval B16902, Application for Amend to License DPR-65,changing TS 3.7.1.3, Plant Sys - Condensate Storage Tank & Adding TS 3.7.1.7, Plant Sys - Atomspheric Steam Dump Valves1998-08-0404 August 1998 Application for Amend to License DPR-65,changing TS 3.7.1.3, Plant Sys - Condensate Storage Tank & Adding TS 3.7.1.7, Plant Sys - Atomspheric Steam Dump Valves B17310, Application for Amend to License DPR-65,changing TS Bases 3/4.9.1,3/4.1.1.1,3/4.7.1.6,3/4.7.7,3/4.5.4 & 3/4.3.3.10 by Resolving Miscellaneous Condition Repts1998-07-30030 July 1998 Application for Amend to License DPR-65,changing TS Bases 3/4.9.1,3/4.1.1.1,3/4.7.1.6,3/4.7.7,3/4.5.4 & 3/4.3.3.10 by Resolving Miscellaneous Condition Repts B17046, Application for Amend to License NPF-49,clarifying Administrative Controls for RHR Isolation Valves When RHR Sys Is in Svc for Core Cooling1998-07-30030 July 1998 Application for Amend to License NPF-49,clarifying Administrative Controls for RHR Isolation Valves When RHR Sys Is in Svc for Core Cooling B17190, Application for Amend to License DPR-65,changing Tech Specs 2.1.1, Safety Limits - Reactor Core, 2.2.1, Limiting Safety Sys Settings - Reactor Trip Setpoints & 3.3.1.1, Instrumentation - Reactor Protective Instrumentation1998-07-21021 July 1998 Application for Amend to License DPR-65,changing Tech Specs 2.1.1, Safety Limits - Reactor Core, 2.2.1, Limiting Safety Sys Settings - Reactor Trip Setpoints & 3.3.1.1, Instrumentation - Reactor Protective Instrumentation B16537, Application for Amend to License DPR-65,modifying DG Testing Requirements by Incorporating Recommendations Contained in GLs 84-15,93-05 & 91-041998-07-17017 July 1998 Application for Amend to License DPR-65,modifying DG Testing Requirements by Incorporating Recommendations Contained in GLs 84-15,93-05 & 91-04 B17280, Application for Amend to License DPR-65,revising Section 9.7.2, Svc Water & Section 9.4 Reactor Bldg Closed Cooling Water, Affected by Change.Attachment 1 Provides Discussion of Proposed Changes1998-07-0202 July 1998 Application for Amend to License DPR-65,revising Section 9.7.2, Svc Water & Section 9.4 Reactor Bldg Closed Cooling Water, Affected by Change.Attachment 1 Provides Discussion of Proposed Changes B17308, Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into Chapter 12 of Millstone Unit 3 FSAR1998-06-10010 June 1998 Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into Chapter 12 of Millstone Unit 3 FSAR B17276, Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into Chapters 6,9 & 15 of Millstone Unit 3 FSAR1998-06-0606 June 1998 Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into Chapters 6,9 & 15 of Millstone Unit 3 FSAR B17288, Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into Chapter 15 of Millstone,Unit 3 FSAR1998-06-0505 June 1998 Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into Chapter 15 of Millstone,Unit 3 FSAR B16186, Application for Amend to License DPR-65,modifying TSs 3.3.1.1 & 3.3.2.1 to Restrict Time Most Reactor Protection or Esfa Channels Can Be in Bypass Position to 48 Hours,From Indefinite Period of Time1998-05-14014 May 1998 Application for Amend to License DPR-65,modifying TSs 3.3.1.1 & 3.3.2.1 to Restrict Time Most Reactor Protection or Esfa Channels Can Be in Bypass Position to 48 Hours,From Indefinite Period of Time ML20247J1131998-05-0707 May 1998 Application for Amend to License NPF-49,incorporating Attached Proposed Rev Into Chapter 15 of Unit 3 FSAR B17210, Application for Amend to License NPF-49,revising TS 3/4.5.4 Re Refueling Water Storage Tank Min Boron Concentration1998-05-0101 May 1998 Application for Amend to License NPF-49,revising TS 3/4.5.4 Re Refueling Water Storage Tank Min Boron Concentration B17112, Application for Amend to License DPR-65,replacing Two low- Range Pressurizer transmitters,PT-103 & PT-103-1 Which Will Identify That Two low-range Pressurizer Pressure Instrument Channels Are Independent & Redundant Only1998-04-29029 April 1998 Application for Amend to License DPR-65,replacing Two low- Range Pressurizer transmitters,PT-103 & PT-103-1 Which Will Identify That Two low-range Pressurizer Pressure Instrument Channels Are Independent & Redundant Only B17194, Application for Amend to License NPF-49,changing TS Bases Section 3/4.3.3.5 to Add Wording to Clarify Calibration of Intermediate Range Neutron Amps Channel Associated W/Remote Shutdown Instrumentation1998-04-23023 April 1998 Application for Amend to License NPF-49,changing TS Bases Section 3/4.3.3.5 to Add Wording to Clarify Calibration of Intermediate Range Neutron Amps Channel Associated W/Remote Shutdown Instrumentation B17144, Application for Amend to License NPF-49,assuring That PORVs Will Be Capable of Automatic Cycling as Well as Manual Cycling When in TS Action Statements That Allow Indefinite Continued Operation1998-04-14014 April 1998 Application for Amend to License NPF-49,assuring That PORVs Will Be Capable of Automatic Cycling as Well as Manual Cycling When in TS Action Statements That Allow Indefinite Continued Operation ML20216J5141998-04-13013 April 1998 Application for Amend to License DPR-65,adding TS 3.5.5, ECCS - Trisodium Phosphate B17028, Application for Amend to License NPF-49,revising TS 3/4.4.3 by Replacing Pressurizer Max Water Inventory Requirements W/ Pressurizer Level Requirement1998-04-0707 April 1998 Application for Amend to License NPF-49,revising TS 3/4.4.3 by Replacing Pressurizer Max Water Inventory Requirements W/ Pressurizer Level Requirement ML20216C0401998-04-0606 April 1998 Application for Amend to License DPR-65,changing TSs 3.4.4, RCS - Pressurizer, 3.6.1.5, Containment Sys - Air Temp & 3.7.1.5, Plant Sys - Msli Valves. Info Will Be Added to Bases of Associated TSs to Address Proposed Changes 1999-09-07
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARB17766, Application for Amend to License DPR-65,to Return Hydrogen Purge Sys to Former Classification of Being within Scope of Maint Rule Program,But Not as risk-significant Sys1999-09-23023 September 1999 Application for Amend to License DPR-65,to Return Hydrogen Purge Sys to Former Classification of Being within Scope of Maint Rule Program,But Not as risk-significant Sys ML20212A7211999-09-10010 September 1999 Amend 174 to License NPF-49,revising TS 4.4.6.2.2 Re Leak Testing of Reactor Coolant Sys Pivs.Rev Replaces Surveillance Interval & Frequency of Leakage Rate Testing as Outlined in ASME Code,Section Xi,Paragraph IWV-3427(b) B17832, Application for Amend to License DPR-65,removing Current Special Exception Which Precludes Applying Eighteen Month Functional Testing Surveillance to SG Hydraulic Snubbers1999-09-0707 September 1999 Application for Amend to License DPR-65,removing Current Special Exception Which Precludes Applying Eighteen Month Functional Testing Surveillance to SG Hydraulic Snubbers B17829, Suppl 1 to TS Change Request 1-1-99 for Amend to License DPR-21,revising Proposed Permanently Defueled TS Sections 5.6.1,5.7.2 & 5.7.3 & Adding Proposed Section 5.6.4 to Reflect ACs Contained in NUREG-14331999-08-25025 August 1999 Suppl 1 to TS Change Request 1-1-99 for Amend to License DPR-21,revising Proposed Permanently Defueled TS Sections 5.6.1,5.7.2 & 5.7.3 & Adding Proposed Section 5.6.4 to Reflect ACs Contained in NUREG-1433 ML20210U0781999-08-13013 August 1999 Amends 239 & 173 to Licenses DPR-65 & NFP-49,respectively, Relocating Certain TS Section 6.0 Administrative Controls to NRC Approved Northeast Utilities QAP TR IAW NRC Administrative Ltr 95-06 ML20210Q1291999-08-12012 August 1999 Amend 238 to License DPR-65,revising Surveillance Requirements for ECCS Atmospheric Steam Dump Valve Requirements to Focus on Steam Release Path Instead of Individual Valves B17799, Application for Amend to License NPF-49,incorporating Editorial Revs to TS Sections 3.8.3.2,4.6.2.1,4.6.2.2, 4.8.1.1,4.9.12 & Bases Sections B 3/4.3.2,B 3/4.4.11, B 3/4.6.1.2 & B 3/4.8.41999-08-0505 August 1999 Application for Amend to License NPF-49,incorporating Editorial Revs to TS Sections 3.8.3.2,4.6.2.1,4.6.2.2, 4.8.1.1,4.9.12 & Bases Sections B 3/4.3.2,B 3/4.4.11, B 3/4.6.1.2 & B 3/4.8.4 B17828, Application for Amend to License DPR-65,modifying TS by Increasing Action Requirement Time to Be in Mode If Temp of UHS Exceeds TS Limit of 75 F1999-07-16016 July 1999 Application for Amend to License DPR-65,modifying TS by Increasing Action Requirement Time to Be in Mode If Temp of UHS Exceeds TS Limit of 75 F B17772, Application for Amend to License DPR-65,relocating Selected TS Re Refueling Operations & Associated Bases to Plant TRM1999-07-16016 July 1999 Application for Amend to License DPR-65,relocating Selected TS Re Refueling Operations & Associated Bases to Plant TRM ML20209G2991999-07-13013 July 1999 Amend 237 to License DPR-65,relocating TSs Sections 3.3.3.2, Instrumentation,Incore Detectors, 3.3.3.3 & 3.3.3.4 to Plant,Unit 2 Technical Requirements Manual ML20209D6431999-07-0202 July 1999 Amend 172 to License NPF-49,revising MP3 Licensing Basis Associated with Design Basis SG Rupture Accident Analysis Described in Chapter 15 of MP3 FSAR to Address Unreviewed Safety Question ML20196H1551999-06-29029 June 1999 Amend 236 to License DPR-65,changing TSs 3.5.2,3.6.2.1, 3.7.1.2,3.7.3.1 & 3.7.4.1 & Bases for Associated TSs ML20207G6321999-06-0303 June 1999 Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49, Respectively,Replacing Specific Titles in Section 6.0 of TSs for All Three Millstone Units with Generid Titles B17764, Application for Amend to License NPF-49,deleting Reference to ASME Code Paragraph Iwv 3472(b) Re Frequency of Leakage Rate Testing for Valves Six Inches Nominal Pipe Size & Larger Contained in TS 4.4.6.2.2.e1999-05-17017 May 1999 Application for Amend to License NPF-49,deleting Reference to ASME Code Paragraph Iwv 3472(b) Re Frequency of Leakage Rate Testing for Valves Six Inches Nominal Pipe Size & Larger Contained in TS 4.4.6.2.2.e ML20206N6441999-05-10010 May 1999 Amend 170 to License NPF-49,modifying TS 3/4.2.2 to Be IAW NRC-approved Westinghouse Methodologies for Heat Flux Hot Channel Factor - Fq(Z) B17621, Application for Amend to License DPR-21,reflecting Permanently Defueled Condition of Unit 1,Tech Specs Administrative Controls Section as Allowed by Guidance Contained in NRC Administrative Ltr 95-061999-04-19019 April 1999 Application for Amend to License DPR-21,reflecting Permanently Defueled Condition of Unit 1,Tech Specs Administrative Controls Section as Allowed by Guidance Contained in NRC Administrative Ltr 95-06 ML20205S5281999-04-16016 April 1999 Amend 169 to License NPF-49,incorporating Alternative Insp Requirements Into TS SR 3/4.4.10, Structural Integrity, for Rc Pump Flywheel ML20205Q9781999-04-14014 April 1999 Amend 234 to License DPR-65,revising TS 3.6.1.2 & Related TS Bases & FSAR Sections.Rev Relate to Changes in Secondary Containment Bypass Leakage ML20205N3521999-04-12012 April 1999 Amend 233 to License DPR-65,removing TS 3/4.6.4.3 from TS & Allowing Downgrading Sys to non-safety-related Sys ML20206B4191999-04-0808 April 1999 Amend 232 to License DPR-65,revising TS 2.2.1 to Reflect Revised Loss of Normal Feedwater Flow Analyses & Authorizes Changes to FSAR B17737, Mod to 990104 Application for Amend to License DPR-65, Changing Value for Turbine Driven Auxiliary Feedwater Pump Associated with Monthly Surveillance Testing of Various ESF Pump1999-04-0707 April 1999 Mod to 990104 Application for Amend to License DPR-65, Changing Value for Turbine Driven Auxiliary Feedwater Pump Associated with Monthly Surveillance Testing of Various ESF Pump B17343, Application for Amend to License NPF-49,revising TS to Support Spent Fuel Pool Rerack to Maintain Full Core Reserve Capability Approaching End of Ol.Proprietary & non- Proprietary Licensing Repts,Encl.Proprietary Rept Withheld1999-03-19019 March 1999 Application for Amend to License NPF-49,revising TS to Support Spent Fuel Pool Rerack to Maintain Full Core Reserve Capability Approaching End of Ol.Proprietary & non- Proprietary Licensing Repts,Encl.Proprietary Rept Withheld B16997, Application for Amend to License DPR-65,relocating Instrumentation TSs 3.3.3.2,3.3.3.3 & 3.3.3.4 to Mnps,Unit 2 Trm,Per GL 95-101999-03-19019 March 1999 Application for Amend to License DPR-65,relocating Instrumentation TSs 3.3.3.2,3.3.3.3 & 3.3.3.4 to Mnps,Unit 2 Trm,Per GL 95-10 B17658, Application for Amend to License DPR-65,revising TSs 3.5.2, 3.7.1.7 & 3.7.6.1 Re ECCS Valves,Atmospheric Steam Dump Valves & CR Ventilation Sys.Associated Bases Will Be Modified as Necessary to Address Proposed Changes1999-03-17017 March 1999 Application for Amend to License DPR-65,revising TSs 3.5.2, 3.7.1.7 & 3.7.6.1 Re ECCS Valves,Atmospheric Steam Dump Valves & CR Ventilation Sys.Associated Bases Will Be Modified as Necessary to Address Proposed Changes ML20205G0041999-03-17017 March 1999 Amend 168 to License NPF-49,revising Plant Unit 3 FSAR by Adding New Sump Pump Subsystem to Address Groundwater Inleakage Through Containment Basemat ML20207J6201999-03-15015 March 1999 Application for Amends to Licenses NPF-49 & NPF-86, Transferring Control of Licenses to Reflect Change in Upstream Economic Ownership of Parent Company of Nep,Vols I & Ii.Pages 48,49 & Annual Rept 1996 Pages 2 & 3 Omitted ML20205G4731999-03-12012 March 1999 Amend 231 to License DPR-65,revising Certain DG Action Statements & SR to Improve Overall DG Reliability & Availability ML20205G8631999-03-11011 March 1999 Amend 230 to License DPR-65,resolving Several Previously Identified TS Compliance Issues ML20205G4381999-03-10010 March 1999 Amend 229 to License DPR-65,allowing Implementation of Change to FSAR Re Post LOCA Long Term Core Cooling ML20204E7411999-03-10010 March 1999 Amend 228 to License DPR-65,allowing Implementation of Revised Main Steamline Break Analysis & Revised Radiological Consequences ML20207L2581999-03-0505 March 1999 Amend 104 to License DPR-21,changing TSs for Staffing & Training Requirements to Allow Use of Certified Fuel Handlers to Meet Plant Staffing Requirements B17566, Application for Amend to License NPF-49,proposing Amend to TS 3/4.7.4, SW Sys, by Adding AOT for One SW Pump Using Duration More in Line with Significance Associated with Function of Pump1999-03-0202 March 1999 Application for Amend to License NPF-49,proposing Amend to TS 3/4.7.4, SW Sys, by Adding AOT for One SW Pump Using Duration More in Line with Significance Associated with Function of Pump B17669, Suppl to Application for Amend to License DPR-65,revising DG Action Statements & Surveillance Requirements1999-02-11011 February 1999 Suppl to Application for Amend to License DPR-65,revising DG Action Statements & Surveillance Requirements ML20203J3081999-02-10010 February 1999 Amend 227 to License DPR-65,allowing Licensee to Prevent Automatic Start of Any High Pressure Safety Injection Pump When Shutdown Cooling Sys in Operation ML20199H9091999-01-20020 January 1999 Amend 224 to License DPR-65,approving Previously Implemented Rev to Final Safety Analysis Rept Section 8.7.3.1 That Changed Certain Electrical Separation Requirements from 12 Inches to 6 Inches B17590, Application for Amend to License DPR-65,removing TS 3/4.6.4.3, Containment Systems,Hydrogen Purge Sys, from Plant TS1999-01-18018 January 1999 Application for Amend to License DPR-65,removing TS 3/4.6.4.3, Containment Systems,Hydrogen Purge Sys, from Plant TS ML20199L0631999-01-18018 January 1999 Application for Amend to License NPF-49,by Incorporating Attached Proposed Rev Into TS 3/4.2.2, Heat Flux Hot Channel Factor-FQ(Z), 6.9.1.6.a & 6.9.1.6.b, Colr B17004, Application for Amend to License NPF-49,revising TS Table 3.7-6, Area Temp Monitoring & Revising FSAR to Describe Full Core off-load Condition as Normal Evolution.Proprietary Rev 2 to HI-971843,encl.Proprietary Info Withheld1999-01-18018 January 1999 Application for Amend to License NPF-49,revising TS Table 3.7-6, Area Temp Monitoring & Revising FSAR to Describe Full Core off-load Condition as Normal Evolution.Proprietary Rev 2 to HI-971843,encl.Proprietary Info Withheld B17623, Application for Amend to License DPR-65,changing TS 3.6.1.2, Containment Sys - Containment Leakage1999-01-18018 January 1999 Application for Amend to License DPR-65,changing TS 3.6.1.2, Containment Sys - Containment Leakage B17517, Application for Amend to License DPR-65,incorporating Changes to ESF Pump Testing Contained in TSs 3.5.2,3.6.2.1, 3.7.1.2,3.7.3.1 & 3.7.4.11999-01-0404 January 1999 Application for Amend to License DPR-65,incorporating Changes to ESF Pump Testing Contained in TSs 3.5.2,3.6.2.1, 3.7.1.2,3.7.3.1 & 3.7.4.1 B17519, Application for Amend to License DPR-65,revising Loss of Normal Feedwater (Lonf) Analyses to TS 2.2.1.Addl TS Bases Change to Floor Value for Thermal Margin Low Pressure Reactor Trip & Proposed FSAR Changes,Included1998-12-28028 December 1998 Application for Amend to License DPR-65,revising Loss of Normal Feedwater (Lonf) Analyses to TS 2.2.1.Addl TS Bases Change to Floor Value for Thermal Margin Low Pressure Reactor Trip & Proposed FSAR Changes,Included ML20198E0461998-12-17017 December 1998 Amend 221 to License DPR-65,reducing Frequency of Surveillance Interval for Boron Concentration of SITs in TS Section 4.5.1.d from Once Per 31 Days to Once Every 6 Months B17542, Application for Amend to License DPR-65,requesting Review & Approval to Plant Fsar,Per 10CFR50.90.Changes to Plant FSAR Pages,Encl1998-12-10010 December 1998 Application for Amend to License DPR-65,requesting Review & Approval to Plant Fsar,Per 10CFR50.90.Changes to Plant FSAR Pages,Encl B17546, Application for Amend to License DPR-21,requesting NRC Approval of Certified Fuel Handler Training & Retraining Program & Request for Exemption from Requirements of 10CFR50.54(m)(2)1998-12-0404 December 1998 Application for Amend to License DPR-21,requesting NRC Approval of Certified Fuel Handler Training & Retraining Program & Request for Exemption from Requirements of 10CFR50.54(m)(2) B17342, Application for Amend to License NPF-49,proposing Rev to TS 4.7.10.e to Eliminate Need to Cycle Plant & Components Through SD-startup Cycle by Allowing Next Snubber Surveillance Interval to Be Deferred1998-12-0404 December 1998 Application for Amend to License NPF-49,proposing Rev to TS 4.7.10.e to Eliminate Need to Cycle Plant & Components Through SD-startup Cycle by Allowing Next Snubber Surveillance Interval to Be Deferred B17498, Application for Amend to License DPR-65,revising FSAR Due to Increase in Radiological Consequences Caused by Changes in Assumptions Used in Updated Dose Consequences Analysis of Sgtr.Rvised FSAR Pages Encl1998-11-13013 November 1998 Application for Amend to License DPR-65,revising FSAR Due to Increase in Radiological Consequences Caused by Changes in Assumptions Used in Updated Dose Consequences Analysis of Sgtr.Rvised FSAR Pages Encl B17492, Application for Amend to License DPR-65,modifying TSs 3.3.1.1 & 3.3.2.1 to Restrict Time That Reactor Protection or ESF Actuation Channel Can Be in Bypass Position to 48 H, from Indefinite Period of Time1998-11-10010 November 1998 Application for Amend to License DPR-65,modifying TSs 3.3.1.1 & 3.3.2.1 to Restrict Time That Reactor Protection or ESF Actuation Channel Can Be in Bypass Position to 48 H, from Indefinite Period of Time B16951, Application for Amend to License DPR-65,changing TS 3.3.2.1, Instrumentation - ESFAS Intrumentation, 3.4.9.3, RCS - Overpressure Protection Sys & ECCS - ECCS Subsystems - Tavg 300 F1998-10-22022 October 1998 Application for Amend to License DPR-65,changing TS 3.3.2.1, Instrumentation - ESFAS Intrumentation, 3.4.9.3, RCS - Overpressure Protection Sys & ECCS - ECCS Subsystems - Tavg 300 F B17417, Application for Amend to License DPR-65,re Separation Requirement in FSAR of Six Inches,Which Is Applied to Redundant Vital Cables,Internal Wiring of Redundant Vital Circuits & Associated Devices1998-09-28028 September 1998 Application for Amend to License DPR-65,re Separation Requirement in FSAR of Six Inches,Which Is Applied to Redundant Vital Cables,Internal Wiring of Redundant Vital Circuits & Associated Devices B17413, Application for Amend to License DPR-65,revising TS Sections 3.3.2.1,3.4.6.2,3.4.8,3.6.2.1,3.6.5.1,3.7.6.1 & 3.9.15 as Result of Revised MSLB Analyses & Revised Determinations of Radiological Consequences of MSLB & LOCA1998-09-28028 September 1998 Application for Amend to License DPR-65,revising TS Sections 3.3.2.1,3.4.6.2,3.4.8,3.6.2.1,3.6.5.1,3.7.6.1 & 3.9.15 as Result of Revised MSLB Analyses & Revised Determinations of Radiological Consequences of MSLB & LOCA 1999-09-07
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4 NORTHEAST UTILf7BES cenerai ott ces semen street. Be+n. connect' cut c
j 2 ) 665 5 October 25, 1990 h
Docket No. 50-423 B13510 Re:
10CFR50.90 U.S. tuclear Regulatory Commission Attention:
Document Control Desk Washington, DC 20555 Gentlemen:
Millstone Nucler Power Station, Unit No. 3 Proposed Revision to Technical Specifications L:
Residual Heat Removal (RHR) System Autoclosure Interlock (ACl)
Introduction Northeast Nuclear Energy Company (NNECO) hereby proposes to remove the auto-closure interlock (ACl) function from the Millstone Unit No. 3 residual heat removal (RHR) system si:ction valves.
There are three motor-operated valves in
' series in each of the two RHR pump suction lines from the reactor coolant system (RCS) hot legs.
Two valves in series (Train A suction-valves--
3RHS*MV8701 A & B, Train B suction valves--3RHS*MV8702 A & B) located close to the. containment walls, one inside containment and one outside containment, are provided with interlocks.
The third valve (Train A--RHS*MV87010 and Train B--RHS*87020) in each train is located inside containment and is closed and deepergized at the motor control center (MCC) during power. operation.
No interlocks are provided to this third valve.
The proposed modification will
=
remove the ACI feature of the RHR suction valves 3RHS*MV8701 A & B and 3RHS*MV8702 A & B.
The function of this interlock is to automatically isolate the RHR system from the RCS when the RCS pressure exceeds 750 psig.
- Instead, p
an alarm will be added on these valves to warn the operators if the RCS pressure is high (exceeds 440 psig) when the suction valves are open.
Removal of the RHR ACI function
-? dresses Commission concerns regarding the potential for failure of the ACI
.rcuitry to cause inadvertent isolation of the RHR system with subsequent los: of RHR capability during cold shutdown and refueling operation.
In addition, this proposed change is consistent with the recommendations of Generic Letter 88-17, " Loss of Decay Heat Removal."
The proposed removal of ACI features will result in a char.ge in the Millstone Unit No. 3 Technical Specifications.
Therefore, pursuant to 10CFR50.90, NNEC0 hereby proposes to amend its operating license, NPF-49, by incorporating the change identified in Attachment 1 into the Technical Specifications of Millstone Unit-No. 3.
9011080085 903o23 i
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u
U.S. Nuclear Regulatory Commission B13510/Page 2 October 25, 1990 Backcround For Millstone Unit No. 3, the RHR system transfers heat from the RCS to the reactor plant component cooling water system to reduce the temperature of the reactor coolant to the cold shutdown temperature at a controlled rate during the second part of normal plant cooldown and maintains this temperature until the plant is started up again.
Part of the RHR system also serves as part of the emergency core cooling system (ECCS) during the injection phase of a loss of coolant accident (LOCA).
The RHR system may be used to transfer refueling water between the refueling cavity and the refueling water storage tank at the beginning and end of the refueling operations.
The RHR system consists of two residual heat rooval exchangers, two residual heat removal pumps, and the associated pipin,, valves, and instrumentation necessary for operational control.
The suction lines to the RHR system are connected to the hot legs of two reactor coolant loops, while the return lines are connected to the cold legs of each of the reactor coolant loops.
The RHR system is designed to be isolated from the RCS whenever the RCS pressure exceeds the RHR design pressure.
The RHR system suction lines are isolated from the RCS by three normally-closed motor-operated valves in series.
The
. two normally closed isolation valves inside containment in each RHR system suction line receive power from the same Class lE source as the RHR pump in that line while the valve outside containment is powered by the opposite train.
This arrangement ensures that single failure requirements for RHR system accessibility and isolation are met.
Each discharge line is isolated from the RCS by three check valves located inside the containment and by a normally open motor-operated valve located outside the containment.
(The eneck valves and the motor-operated valve on each discharge line are not part of the RHR system; these valves are shown as part of the ECCS; Millstone Unit No. 3 FSAR, Figure 6.3-1.)
As stated above, there are three motor-operated valves in series in each of the two RHR pump suction lines from the RCS hot legs.
Two valves in series located close to the containment walls, one inside containment and one outside containment, are provided with interlocks.
The interlock features provided for the isolation valves are identical for both trains and are shown on FSAR l
Figure 7.6-1.
l Each of the two valves is interlocked so that it cannot be opened unless the RCS pressure is below approximately 375 psig.
This interlock prevents the I
valve from being oper.ed when the RCS pressure plus the RHR pump pressure would-be above the RHR system design pressure.
A second pressure interlock is provided to close the valve automatically if the RCS pressure subsequently increases to above 750 psig.
The interlocks for each train are independent and diverse, derived from signals generated by transmitters manufactured by two different vendors.
The third valve in each train is located inside containment and is closed and deenergized at the MCC during power operation. No interlocks are provided.
1 l
l l
q U.S. Nuclear Regulatory Commission B13510/Page 3 October 25, 1990 Safety Assessment i
By letter dated August 8,1989,(I) the NRC indicated that they have completed review of a topical report, WCAP-11736, " Residual Heat Removal System Auto-closure Interlock Removal Report for the Westi:' house Owners Group."
In that letter, the Staff concluded that the information in WCAP-11736 can be used to supplement plant-specific requests to remove-the ACI from the Westinghouse plants covered by the report.
WCAP-11736 provides an evaluation of the removal of the ACI from suction / isolation valves in the RHR system at four reference plants:
Salem Unit 1, Callaway Unit 1, North Anna Unit I and Shearon Harris Unit 1.
NNECO on behalf of Millstone Unit No. 3 participated in this program.
The Westinghouse Owners Group (WOG) plants participating in the program were categorized into one of four groups based on RHR system configuration and design characteristics that were similar to one of the four reference plants.
It was intended that other members of the WOG could refer-ence the applicable lead plant in the study and provide a plant-specific analysis should they desire to delete the ACI feature from the RHR system suction valves.
The basis information presented in WCAP-ll736 is applicable for use in the Millstone Unit No. 3 plant-specific effort.
It is noted that for Millstone Unit Ho. 3, the reference plant in WCAP-11736 is Callaway Unit 1.
The literature review and licensing basis remain the same for all Westinghouse plants.
The probabilistic models and data base can be utilized as a basis for the plant-specific effort.
The recommended changes to Techni-cal Specifications are also applicable.
In addition, the Staff, in their safety evaluations (2) identified five items that must be addressed on a plant-specific basis. provides responses to those five items.
A review and analysis have been performed for Millstone Unit No. 3.(see Attachment 3) to justify removal of the ACI associ-ated with the Millstone Unit No. 3 RHR system suction valves.
Removal of the RHR ACI function addresses industry and NRC concerns regarding t:,s potential
'for failure of the ACI circuitry to cause inadvertent isolation of the RHR system and subsequent loss of RHR capability during-cold shutdown and refuel-ing cperations.
The purpose of the analysis provided in Attachment 3 is to investigate the risk impact of removing the ACI from the RHR system suction valves 3RHS*MV8701 A & B and 3RHS*MV8702 A & B at Millstone Unit No. 3 and adding a control room alarm to alert the operator that a suction / isolation valve is not fully closed when the RCS pressure is above the alarm setpoint.
The plant-specific report for Millstone Unit No. 3 justifies removal of the ACI based on a safety evaluation of the effect of ACI removal on low temperature overpressure protection, RHR system reliability and interfacing system LOCA potential.
l-(1)
A. Thadani letter to R. A. Newton, Chairman WOG, Acceptance for Reference WCAP-11736, Rev. O, " Residual Heat Removal System, Auto Closure Interlock (ACI) Removal Report" in Plant Specific Submittals, dated August 8,1989.
l (2)
Ibid.
l l
1
U.S. Nuclear Regulatory Commission B13510/Page 4 October 25, 1990 This report recommends the deletion of the autoclosure interlock of the RHR system suction / isolation valves during shutdown.
The installation of a control room alarm is recommended to warn the operator that a
suction / isolation valve (s) is not fully closed when RCS pressure is above the alarm setpoint.
The results of the intersystem LOCA analysis show that the i
frequency of the Event V decreases (approximately 2.3%) with the removal of the ACI feature.
Removal of the ACI features will reduce the RHR short-term unavailability by 12% from 1.64E-2 to 1.45E-2.
Further, removal of the ACI features significantly reduces the long-term RHR unavailability (approximately 70%) from 3.94E-2 to 1.19E-2.
It is also concluded that the removal of the RHR ACI has no significant impact on the overpressure transient due to a) adequata capacity of RHR relief valves, b) adequate capacity of pressurizer power operated relief valves and c) the plant procedure that directs the inadvertent safety injection actuated charging flow to the refueling water storage tank, rather than to the RCS.
In addition, the fluid system review of this proposed modification has deter-mined that RHR ACI removal would not adversely impact the capability of the RHR system to perform its safety function.
The electrical and control system review indicates that removal of the RHR ACI feature does not degrade the capability of the remaining plant protection logic to perform its safety function.
Description of the Proposed Chanae The proposed Technical Specification change will delete the surveillance requirements (Section 4.5.2.d.1) associated with the RHR ACI concurrent with the removal of the ACI circuitry planned for the third refueling outage.
Surveillance Requirements 4.5.2.d.1 of the Millstone Unit No. 3 Technical Specifications requires that the automatic isolation and interlock function of the RHR inlet isolation valves be demonstrated operable on an 18-month inter-val.
However, with the ACI function removed, there is no longer a need to retain this surveillance requirement within the Technical Specifications.
Sianificant Hazards Consideration In accordance with 10CFR50.92, NNEC0 has reviewed the attached proposed change and has: concluded that it-does not involve a significant hazards considera-tion.
The basis for this conclusion is that the three criteria of 10CFR50.92(c) are not compromised.
The proposed change does not involve a significant hazards considerations because the change would not:
1.
Involve a significant increase in the probability or consequences of an accident previously evaluated.
The removal of the RHR ACI was analyzed generically in WCAP-ll736 in terms of the frequency of an interfacing LOCA, the availability of the RHR system and the effect on overpressure transients.
This generic analysis has been supplemented by the plant-specific submittal (Attachment 2) for Millstone Unit No. 3.
With the removal of the ACI and addition of a control room alarm, the analysis predicts a decrease in interfacing LOCA frequency of approximately 2.3%.
Further, removal of the ACI feature significantly reduces the long-term m
l U.S. Nuclear Regulatory Commission B13510/Page 5 October 25, 1990 RHR unavailability (approximately 70%) from 3.94E-2 to 1.19E-2.
- Finally, removing the RHR ACI has no significant impact on the overpressure transient.
With removal of the ACI feature on the RHR suction / isolation j
valves, as stated above, the control room alarm and administrative i
procedures would be capable of ensuring that the low pressure RHR system is isolated from the high pressure RCS, when the RCS operating pressure 1
exceeds the alarm setpoint.
The current system relies on RHR suction relief valves (440 psig set pressure) and the cold overpressure protec-tion system (COPPS), to limit the pressure rise during a transient.
The RHR relief valves and COPPS will remain available per Technical Specifi-cation 3.4.9.3 to mitigate a pressure transient.
Therefore, the proposed change would not increase the consequences of an accident previously
- analyzed, i
.2.
Create the possibility of a new or different kind of accident from any previously evaluated.
The effect of an overpressure transient at cold shutdown conditions will not be altered by removal of the RHR ACI fur.c-tion. With or without the ACI function, the RHR system could be scbject to overpressure for which the RHR relief valves must be relied upon to limit pressure to within RHR design parameters.
While it is true that the ACI initiates an automatic closure of the RHR suction / isolation valves on high RCS pressure, overpressure protection of the RHR system is l
provided by the RHR system relief valves and not by the slow acting suction / isolation valves that isolate the RHR system from the RCS.
Since relief valves prevent overpressurization of the RHR system during shut-down conditions and procedures are in place to ensure that the RHR system is isolated from the RCS during normal plant conditions, removal of the ACI does not create the possibility of a new or different kind of acci-dent from any accident previously evaluated.
l 3.
Involve a significant reduction in safety margin.
The RHR ACI function is not a consideration in a margin of safety in the basis for any Tech-nical Specification.
- However, since the probabilistic analysis of WCAP-ll736 and the Millstone Unit No. 3 plant-specific analysis indicates that the availability of the RHR system is increased with removal of the i
ACI, implementation of the modification (addition of a control room alarm) and the procedural changes will produce an increase in overall
- safety, l-
~
Moreover, the Commission has provided guidance concerning the application of-standards in 10CFR50.92 by providing certain examples (51FR7751, March 6, 1986) of ~ amendments that are considered not likely to involve a significant hazards consideration.
Although the proposed change is not enveloped by a specific example, the proposed change would not involve a significant increase in the probability or consequences of an accident previously analyzed.
With the removal of the ACI-and addition of a control room alarm, the Millstone Unit No. 3 plant-specific analysis predicts a decrease in interfacing LOCA 1
frequency of approximately 2.3%.
Further, removal of the ACI features signif-l icantly reduces the long-term RHR unavailability from 3.94E-2 to 1.19 E-2.
l Finally, removing the RHR ACI has no significant impact on the overpressure transient.
l 1
l'
R U.S. Nuclear Regulatory Commission B13510/Page 6 October 25, 1990 Based upon the information contained in this submittal and the environmental assessment for Millstone Unit No. 3, there are no radiological or nonradio-logical impacts associated with the proposed change and the proposed license amendment will not have a significant effect on the quality of the human environment.
The Millstone Unit No. 3 Nuclear Review Board has reviewed and approved the attached proposed revisions and has concurred with the above determinations.
To allow for implementation of the design change related to this technical specification change during the third refueling outage, scheduled to start in 1
February 1991, your timely review and approval of the proposed license amend-ment is requested, in accordance with 10CFR50.91(b), we are providing the State of Connecticut with a copy of this proposed amendment.
Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY E. E)froczka v
Seniof' Vice President cc:
T. T. Martin, Region I Administrator D. H. Jaffe, NRC Project Manager, Millstone Unit No. 3 W. J. Raymond, Senior Resident inspector, Millstone Unit Nos.1, 2, and 3 Mr. Kevin McCarthy
. Director, Radiation Control Unit Department of Environmental Protection Hartford, CT 06116 STATE OF CONNECTICUT)
) ss. Berlin COUNTY OF HARTFORD )
Then personally appeared before nie, E. J. Mroczka, who being duly sworn, did state that he is Senior Vice President of Northeast Nuclear Energy Company, a Licensee herein, that he is authorized to execute and file the foregoing information in the name and on behalf of the Licensee herein, and that the statements contained in said information are true and correct to the best of his knowledge and belief.
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