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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:RO)
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARU-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 U-603033, Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals1998-07-20020 July 1998 Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals U-603041, Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 ML20151U1501998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 U-603023, Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 1 U-603014, Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed1998-05-28028 May 1998 Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed ML20236E7991998-05-26026 May 1998 Final Part 21 Rept Re W Dhp Circuit Breaker Auxillary Switch Operating Assembly Anomalies.Caused by Loss of Breaker Safety Function.Dhp Circuit Will Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted U-603004, Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable1998-05-15015 May 1998 Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable ML20216A9601998-05-0808 May 1998 Part 21 Rept Re Failure of 12 Volt DC Inverter Power Supply. Caused by Inadequately Sized Output Transistor Pair Combined W/Degraded Capacitors.Licensee Plans to Replace All Output Transistors & Degraded Capacitors U-602995, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts1998-05-0505 May 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts U-603006, Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 1 U-602994, Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable1998-04-29029 April 1998 Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable ML20216B1351998-04-21021 April 1998 Rev 0 to Illinois Power Co Clinton Power Station SVC Design Rept U-602979, Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable1998-04-0707 April 1998 Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable U-602976, Monthly Operating Rept for Mar 1998 for Clinton Power Station1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Clinton Power Station ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue U-602968, Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue1998-03-24024 March 1998 Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue U-602960, Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 9804111998-03-12012 March 1998 Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 980411 U-602954, Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 9805131998-03-0909 March 1998 Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 980513 1999-09-30
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d U- 601657 -
L45 90(04 30)-LP 20.220 llLINDIS POWER COMPANY CLINTON POWER $TATION, P.O. BOX 678. CLINTON. ILLIN0l$ 61727 April 30, 1990 i 4 10CFR50.73
. Docket No. 50 461 U.S. Nuclear _ Regulatory Commission Document Control Desk Washington,-D.C. 20555
Subject:
Clinton Power Station : Unit 1 jfeensee-Event Reoortjlq;90-007 00
]
DeariSir:
Please find enclosed Licensee Event Report No.90-007 00:
Inadeounte Determination of Eautement Status Durine Restoration Results ittpe-energization of Nuclear Systgg Protection System Loads and-Asj;uation of Engineered Saferv Features. -This report is being submitted i in accordance with the requirements of 10CFR50.73. 3 Sincerely yours, j 0 A.,Qo F. A. SpangbrJ,u.t 1
, III Manager Licensing and S, ety TSA/csm t
Enclosure i
cc: NRC Resident Office NRC Region III, Regional Administrator INPO' Records Center Illinois Department of Nuclear Safety
. NRC Clinton Licensing Project Manager
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Inadequate Determination of Equipment Status During Restoration Results in De-energization of Nuclear System Protection System Logds and Actuation of Engineered Safety Features , ;
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On March 31, 1990, the plant was in Mode 4 (COLD SHUTDOWN). Operators were in the process of restoring Nuclear System Protection System (N5PS)
Division II to its nornal configuration following the completion of maintenance. A control room operator (CRO) requested that the 'C' area operator determine the status of the Division II NSPS Inverter. The 'C' area operator incorrectly determined that the Inverter was de energir.ed.
In accordance with section 8.1.1, "NSPS Bus Energization," of nroceduro 3509.01, " Instrument Power System", the operator opened the cir.uit breakers associated with the Division II loads. Opening the breakers de-energized the Division II NSPS loads resulting in the automatic initiation of a number of Engineered Safety Features. The cause of this -
event is attributed to personnel error. The CR0 did not consult Main Control Room indications to determine the status of the Division II NSPS Inverter. The 'C' area operator incorrectly evaluated the indications at the Inverter. Inadequacy of procedure 3509.01 contributed to the event.
The format of the proc 9 dure makes it difficult for operators to identify applicable steps. Corrective actions includa distribution of a " fact sheet" on NSPS operation, retrainin5 on the importance of monitoring equipment configuration, and revising procedure 3509.01.
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On March 31, 1990, the plant was in Mode 4 (COLD SHUTDOWN) and the reactor.[RCT) was at atmospheric pressure and approximately 132 degrees Fahrenheit. The Division II emergency diesel generator (EDG) [DG) was E out of service for maintenance. The Reactor Protection System (RPS) (JC) s was in a tripped condition and the Control Rod Drive (CRD) [AA) Charging Water lleader. Isolation Valve [ISV), IC11F034, was in the closed position c to allow the performance of maintenance on the Instrument Air (IA) system
[LD).
s At 0054 hours6.25e-4 days <br />0.015 hours <br />8.928571e-5 weeks <br />2.0547e-5 months <br />, a non licensed utility operator, in attempting to restore the Nuclear System Protection System (NSPS) [JE] to its.normab configuration, following the completion of maintonance, de energized the Division II NSPS loads causing the actuation of a number of Engineered y Safety foatures (ESFe),
g Each division of NSPS is normally supplied power via an internal solid state inverter which converts 125 voir direct current (VDC) '[EJ) to 125 volt alternating current (VAC) [ED). Alternate power to the-inverter is provided by a 120 VAC bus [BU). A static transfer switch [HS) automatically switches the Invertor povar supply from its normal to its ,
alternate source upon inverter failure. The static transfer switch can be used to manually transfer the Inverter power supply. Indicating *l lights on the Inverter are enar;ized when the Inverter is receiving power from its normal source. ;
On March 30, 1990, Electrical Maintenance personnel begu. performing maintenance in accordance with Maintenance Work Roquest (MWR) D15009. '
This MWR provided directions for the replacement of the variable resistor s in the Division II NSPS Inverter (IvVT). S To allow installation of the variable resistor in the Division II Inverter, at 2245 hours0.026 days <br />0.624 hours <br />0.00371 weeks <br />8.542225e-4 months <br />, Operations potsonnel transferred the Inverter power supply from its normal to its alternate source using the internal -
static transfer switch. Use of the static transfer switch is an electronic method of alternating power supplies. The manual transfer L switch on the Inverter theref,cre remained in the Normal / Inverter position.
At 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />, following completion of shift briefings and turnover, the
, "mid shift" Oparations crew assumed control of plant operations. ,
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NRC rey Je4A i U.S. NuCLEA:n 7E!ULitoRY Coussissegg LICENSEE EVENT REPCRT (LER) TEXT CONTINUATION Amoveo oMn No. am-om i (APtRES: $/31/95 e Aciuty haut t,t i pocast NUMDLR (2p 4th NUM0ER 163 PACI (3) vsea "20' I.*6 n $ ?,7; Clinton Power Station ]
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l On March 31, 1990, at 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />, Electrical Maintent.nce notified Operations personnti that they had completed replacement of the variable resistor. A licensed control room operator (CRO) dispatched a non-licensed utility 'C' area operator to the Division II NSPS Inverter to detatnine its status and to restore NSPS to its normal configuration.
s The G'O was unsure of the status of the Inverter and did not review the indications in the Main Control Room or discuss the status with the Shift Superviso rs .
The 'C' area operator reviewed the status of the meters [MTR), switches, and indicating lights [IL) at the NSPS Inverter and incorrectly determined that the Division II NSPS bus was de energized. This .
determination was based upon the de energized indicating light 1*or the *
, static transfor switch end the incorrect belief that the output frequency
!. and voltage meters had ofailed as is". The indicating light was !
de energized because the Inverter was receiving power from its alvornite source. Since the indicating light was de energized the operator .
l believed the meters had " failed as is". although they indicated normal- '
l frequency and voltage. The operator did not inspect the position of the
- internal static transfer switch.
The 'C' crea operator informed the CR0 that the Division II USPS Inverter 6 was c'a energized. Tho operators determined that the appropriate portion E
et Clinton Power Station (CPS) procedure 3509.01, " Instrument Power System", to be utilized to restore NSPS to its normal configuration was-i section 8.1.1, "NSPS Bua Energirstion" rather than section 8.1,14, l " Energizing Inverter With the Bus Energized."
At 0051 hours5.902778e-4 days <br />0.0142 hours <br />8.43254e-5 weeks <br />1.94055e-5 months <br />, in acc.ordance with section 8.1.1, the 'C' area operator
.de energized the Division II NSPS loads by opening the following circuit breakers [BKR): Leak Detection [IJ) 1H13 P642; NSPS Division II Logic Test and Transmitter Power Supply 1H13 P662 and Scram Discharge Volume '
Controls and indication H13-P662; Power and Startup Range Neutron Monitoring and Process Radiation Monitoring [IL) 1H13-P670; Loss of Coolant Accident Bypass Relays [RLY) Division II 1H13-P851; and tNuclear Steam Supply Shutoff System Valves [V). Loss of these loads resulted in the actuation of the following signals: a Reactor Water Low Level signal; High Drywell Pressure , signal;'a Main Steam [MB) Line High Radiation signal: and a Leak Detection, safety signal. These' signals' resulted in the automatic initiation of a number of Engineered Safety Features. Di/ision II of the Neatron Monitoring System tripped. A Reactor Core Isolation Cooling (RCIC) [BN) system initiation signal initiated causing the RCIC gland seal compreosor [ CMP) to start, i However, since the-plant was shutdown the low pressure RCIC isolation s signal prevented system injection. The 'A' Reactor Water Cleanup System
[CE) pump [P) tripped. Valves 1E12 F034B and 1E12-F0340, the Low Pressure Coolant Injection (LPCI) [BO) isolation valves opened, however, since the plant was in Node 4 no water was injected. The Drywell Cooling N!C FORM $364 *
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,y I Clinton Power Station 0 [t, l0 l 0 l o l4 l 6]1 9l0 0l0l7 0]O 0l4 or 0l5 stxi ca ne, sou, a o e.m. e., ema.nne re,,, anu n un System (VB) chilled water pump tripped. High level trip signals were .
received on Source Range Monitor 'B', Intermediate Range Monitors 'B' and
'F', Av w .ge Power Range Monitor 'B', and the Main Steam Line Radiation Monitors. The Division II EDG received a start signal but since the'EDG was removed from service it did not start.
At 0152 hours0.00176 days <br />0.0422 hours <br />2.513228e-4 weeks <br />5.7836e-5 months <br />, after verifying that all valves affected by the ESF actuations were in the expected positions, in accordance with CPS ;
l procedure 4001.020001, " Automatic Isolation Checklist," operators re- '
energized and restored NSPS to its normal configuration.
By 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br />, the systems and components affected by the de energization of the Division II NSPS loads were restored to their previous configuration.
l No automatic or manually initiated safety system responses wer. necessary to place the plant in a safe and stable condition. No other equipment or components were inoperable at the start of this event such that their inoperable condition contributed to this event.
CAUSE OF EVENT I
p The cause of this event is attributed to personnel error by utility operators. The CR0 failed to utilize available Main Control Room indications.to determine the status of the Division II NSPS Inverter. ,
Additionally, although the status of the Inverter was discussed at shift turnover, the CR0 failed to consult with other members of the t.hift crew when unsure of its status. The 'C' area operator incorrectly determined that the Division II NSPS Inverter was de energized. The operator believed that the voltage and frequency meters at the NSPS Inverter had
" failed as is" although they indicated normal voltage and frequency. The indicating light for the static transfer switch was not energized since
,the Inverter was receiving power from its alternate source. The 'C' area operator did not verify the position of the static transfer switch.
Contributing to this event was the inadequacy of procedure 3509,01. This procedure is a generic procedure for NSPS. Uninterruptible Power Supplies
[EF), and Reactor Protection !iystem Scram Solenoid (SOL) power distribution systems. Currently this procedure is divided into two sections, 8.1, Normal Operation and 8.2, Abnormal Operation. The subsections for energization, deenergization and transfer of loads for j each of the types of power supplies are distributed among each of these i
two sections. This format makes it difficuir for operators to identify the applicable subsections.
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UCENSEE EVENT REPORT (LER) TEXT CONTINUATION w aovtoowowo.v u.eios (XP AES: SWm iAcetsty naut us u n gg nyuggn m vtAh Clinton Power Station sw wm. .,m e=w =.,nomenw nc m wnn CORRECTIVE ACTIONS Operations shif t personnel were provic'ed with a " fact sheetr that described this event and pertinent details on NSPS power supply operation.
Each shift crew has been retrained on the importance of closely monitoring equipment configuration and performing thorough equipment status checks during shift turnovers.
During the in progress requalification training cycle, active licensed operators will perform a job performance meacure to demonstrate their understanding of NSPS indications and operation. This action is expected to be completed by July 15, 1990.
Procedure 3509.01 will be revised to separate the steps for each type of power supply into sections. Then distinct sections will enable the operators to more easily determine which steps are applicable. This action is expected to be completed by July 30, 1990.
ANALYSIS OF EVENT This event is reportable in accordance with the provisions of 10CrR50.73(a)(2)(iv) due to the actuation of various Engineered Safety Features.
Analysis of the nucicar safety significance and consequences of this event indicates that this event was not significant under these or any other operating conditions. All equipment and components responded as designed, placing the plant in a safe and stable condition, upon the de energizstion of the Division II NSPF loads. If this event had
,securred at power it is possible injection into the reactor would have
, occurred. This possibility is analyzed in Chapter 15 of the Updated Safety Analysis Report, ADDITIONAL INFORMATION No Engineered Safety Feature actuations have previously occurred as a result of inadequate determination of equipment status by utility operators.
No components failed to perform as designed during this event.
For further information regarding this event contact D. R. Morris, Director Plant Operations at (217)935-8881, extension 3205.
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