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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:RO)
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARU-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 U-603033, Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals1998-07-20020 July 1998 Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals U-603041, Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 ML20151U1501998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 U-603023, Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 1 U-603014, Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed1998-05-28028 May 1998 Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed ML20236E7991998-05-26026 May 1998 Final Part 21 Rept Re W Dhp Circuit Breaker Auxillary Switch Operating Assembly Anomalies.Caused by Loss of Breaker Safety Function.Dhp Circuit Will Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted U-603004, Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable1998-05-15015 May 1998 Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable ML20216A9601998-05-0808 May 1998 Part 21 Rept Re Failure of 12 Volt DC Inverter Power Supply. Caused by Inadequately Sized Output Transistor Pair Combined W/Degraded Capacitors.Licensee Plans to Replace All Output Transistors & Degraded Capacitors U-602995, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts1998-05-0505 May 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts U-603006, Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 1 U-602994, Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable1998-04-29029 April 1998 Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable ML20216B1351998-04-21021 April 1998 Rev 0 to Illinois Power Co Clinton Power Station SVC Design Rept U-602979, Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable1998-04-0707 April 1998 Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable U-602976, Monthly Operating Rept for Mar 1998 for Clinton Power Station1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Clinton Power Station ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue U-602968, Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue1998-03-24024 March 1998 Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue U-602960, Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 9804111998-03-12012 March 1998 Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 980411 U-602954, Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 9805131998-03-0909 March 1998 Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 980513 1999-09-30
[Table view] |
Text
. . _ _ ,
A
.. U+01595 !
o - 2 L45 90()1 -17 ) LP _l
. 2C.220 f ILLINol8 POWER COMPANY IP CLINTON POntR STATION, P.O. BOX 678. CLINTON, ILLINOi$ 61727 l l
'l January 17, 1990 l i
10CFR50.73 -
l Docket No. 50-461 I
U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Subj ect: Clinton Power Station' Unit 1 Licensee Event Renort No. 89-041-00 l I
Dear Sir:
f Please find enclosed Licensee Event Report No. 89 041 00: '
Leakane of Refrigerant from Chiller Results in Inonerable High Pressure' -l Core Sorav System While Reactor Core Isolation Coolina System was i
- Inocerable. This report is being submitted in accordance with the {
requirements of 10CFR50.73. !
-t i
Sincerely yours, j
~
- 5) m .
D.'L. Holt'zscher '
Acting Manager . -
Licensing and Safety DAS/krm , ;
Enclosure-i cc: NRC Resident Office !
NRC Region III, Regional' Administrator ;
INPO Records Center Illinois Department of Nuclear Safety- l NRC Clinton Licensing Project Manager ..
I 9001250005 900117 PDR ADOCK 05000461
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On December 18, 1989, Clinton Power Station management determined that an event reportable pursuant to 10CFR50.73(a)(2)(1)(B) had occurred on November 22, 1989, when the plant entered 'Iechnical Specification (TS) 3.0.3 for approximately 37 minutes, llowever, due to a procedural deficiency, the Shift Supervisor did not recognize that entry into TS 3.0.3 was a reportable event. The entry into TS 3.0.3 was required because the Reactor Core Isolation Cooling (RCIC) system and the liigh Presnure Core Spray (llPCS) system were inoperable simultaneously. The RCIC system was inoperable for planned maintenance. The llPCS system became inoperable because a chiller condensing unit on the Division III Essential Switchgear lleat Removal System became inoperable. The chiller condensing unit tripped during chiller performance monitoring as a result of low refrigerant prec sure. Following the trip, the chiller was recharged with refrigerant, then started and declared operable. The cause of tha low refrigerant pressure is believed to be a result of leakage from the system. Corrective actions include developing and impicmenting a plan to investigate and correct the refrigerant leakage, briefing Shift Supervisors and training licensed operations personnel so they recognize that entry into TS 3.0.3 is a reportable event, and revising the deficient procedure.
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DESCR Z ION OF EVENT On December 18, 1989, Clinton Power Station management determined that an event reportable pursuant to 10CFR50.73(a)(2)(1)(B) had occurred on November 22, 1989.
At 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> on November 21, 1989, the plant was in Mode 1 (POWER OPERATION) at approximately sixty one percent reactor [RCT) power. At 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br />, the Reactor Core Isolation Cooling (RCIC) system [BN) was declared inoperable in order to perform planned maintenance. At approximately 1019 hours0.0118 days <br />0.283 hours <br />0.00168 weeks <br />3.877295e-4 months <br /> on November 22, 1989, the Division III safety.
related essential switchgear [SWCR) heat removal system (VX) chiller condensing unit [CDU) IVXO6CC was started to monitor chiller performance in accordance with Clinton Power Station (CPS) Procedure 2604.01,
" Chiller Performance". However, after starting, the chiller condensing unit tripped due to low refrigerant pressure. At 1023 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br />, the chiller condensing unit was declared inoperable.
The function of chiller condensing unit IVXO6CC is to provide adequate heat removal to maintain required temperatures in the Division III safety-related switchgear area and the Division III battery.[BTRY) room following a loss of the non safety related cooling coil cabinet. As L
such, IVXO6CC provides support for the operability of the equipment in these areas. As a result of IVXO6CC becoming inoperable, the Division III battery charger [BYC) and other equipment served by this system were declared inoperable. Action "b" of Technical Specification 3.8.2.1, "DC Sources Operating", requires that, with the Division III battery and/or charger inoperable, the High Pressure Core Spray (HPCS) system [BC) be declared inoperable. Technical Specification 3.5.1, " Emergency Core Cooling System Operating", and Technical Specification 3.7.3, ' Reactor Core Isolation Cooling", do not address having the RCIC and HPCS systems inoperable simultaneously. Therefore, this condition resulted in entry into Technical Specification 3.0.3. -Entry into Technical Specification 3.0.3 constitutes a condition prohibited by the plant's Technical Specifications and is therefore reportable pursuant to 10CFR50.73(a)(2)(1)(B) (as discussed in the " Questions and Answers from the LER Workshops" section of NUREC-1022 " Licensee Event Report System",
Supplement 1).
Following recharging of the refrigerant in chiller condensing unit IVXO6CC, the chiller condensing unit was restarted. At 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on November 22, 1989, IVXO6CC was declared operable and Technical Specification 3.0.3 was exited.
At the time of this event, the Shift Supervisor did not recognize that entry into Technical Specification 3.0.3 constituted operation prohibited by the plant's Technical Specifications and hence, was reportable pursuant to 10CFR50.73(a)(2)(1)(B). As a result of determining that M'oa* ** ..... cro, i m . m . m , m n i
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entry into Technical Specification 3.0.3 on November 29, 1989 was ]
reportable (see LER 89 037 00), a review was conducted to determine whether there were previous entries into Technical Specification 3.0.3.
On December 18, 1989 CPS management determined that an entry into !
Technical Specification 3.0.3 had occurred on November 22, 1989. l' Therefore, this event is being reported within 30 days of this determination on December 18, 1989.
1 No automatic or manually initiated safety system responses were necessary !
.to place the plant in a safe and stable condition. No other equipment or 'l components were inoperable at the start of this. event such.that their inoperable condition contributed to this event.
1 CAUSE OF EVENT i
Inoperability of IVX06CC resulted in declaring the HPCS system )
inoperable. Since this condition occurred while.the RCIC system was ;
inoperable for planned maintenance, it required entry into Technical j Specification 3.0.3. The cause of the inoperability of chiller condensing unit IVXO6CC was low refrigerant pressure believed to be a ,
result of leakage of the refrigerant from the system. l At the time of this event, the Shift Supervisor did not recognize that ,
entry into Technical Specification 3.0.3 constituted operation prohibited j by the plant's Technical Specifications and was therefore reportable-pursuant to 10CFR50.73(a)(2)(1)(B). The cause of this aspect of the 1 event has been attributed to a deficient procedure. Administrative procedure 1016.04, "Clinton Power Station Licensee Event Reports (LER)"
does not identify that entry into Technical Specification 3.0.3 is a reportable event. .
CORRECTIVE ACTIONS J 5
Chiller condensing unit IVX06CC was recharged with refrigerant and I restored to OPERABLE status at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on November 22, 1989, i Illinois Power has developed a plan to investigate and correct the loss of refrigerant problem and any other equipment problems which may affect 3 the operability of the VX system. -]
1 In accordance with this plan, a leak check will be performed on each i division of the VX system by January 31, 1990. System leaks will be i corrected on a priority basis consistent with parts availability and as l permitted by plant conditions.
Additionally, VX system equipment history will be reviewed to identify system problems. Maintenance personnel will provide input on problems identified. For problems which are not associated with leakage of 801C p@ies pesa 'U.S. Gros 190 9-5 20- 589 > 90010 C 43)
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Further, a preventive maintenance task has been generated to run the condensing units of the three divisions on a weekly basis. During these runs, operating data will be obtained and then trended. The frequency of running the condensing units will be reassessed and revised accordingly after sufficient weekly runs have been completed.
Shift Supervisors will be briefed so they recognize that entry into Technical Specification 3.0,.3 constitutes operation prohibited by the plant's Technical Specifications and hence, is reportable pursuant to 10CFR50.73(a)(2)(1)(B). This briefing is scheduled to be completed by January 31, 1990.
Procedure 1016.04 will be revised to identify that entry into Technical Specification 3.0.3 is an event reportable under the provisions of 10CFR50.73(a)(2)(1)(B). This revision is scheduled to be completed by April 30, 1990.
Additionally, reportability of plant entry into Technical Specification 3.0.3 will be reviewed with licensed operations personnel during requalification training for 1990. This training is scheduled to be completed by June 4, 1990.
ANALYSIS OF EVENT Upon failure of the RCIC and HPCS systems to function properly following a small break loss of coolant accident, the automatic depressurization system (ADS) automatically causes depressurization of the reactor so that flow from the low pressure Emergency Core Cooling Systems (ECCS) can enter the core in time to limit fuel cladding temperature to less than 2200 degrees F. At the time of this event, the ADS, as well as the four low pressure ECCS trains were operable.
Each division of the switchgear heat removal system consists of two -
independent switchgear heat removal coil cabinets connected to a common supply duct [ DUCT) system. Each switchgear heat removal coil cabinet (CAB) consists of a filter [FLT), cooling coil [CCL), and fan [ FAN). One switchgear heat removal coil cabinet is non safety related and has a chilled water coil fed from the plant chilled water system [KM). This i non-safety related coil cabinet is utilized for cooling during normal station operating conditions. The other switchgear heat removal coil cabinet is safety related and has a refrigerant evaporator coil fed from a water cooled condensing unit located within the switchgear room. The condenser heat is removed by shutdown service water'[BI) or plant service' water [KG)'. This safety related coil is aligned in standby and is utilized during abnormal operating conditions or upon failure of the non-g ,.... ~
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safety related coil cabinet. Under normal. operating conditions, makeup !
air to the VX system is provided by the auxiliary' building HVAC supply system [VF). Under abnormal operating conditions, provision is made for !
outside air to be inducted to the switchgear room to make up for the j battery room exhaust requirements. Therefore, cooling to the areas l served by IVXO6CC was not lost during this event. ]
Additionally, the low refrigerant pressure condition ~of IVXO6CC was - I discovered during the routine chiller performance of CPS Procedure {
2604.01. Therefore, this condition would not have gone undetected. Upon _;
identification of this condition, the appropriate Technical Specification !
Actions were entered. Once identified, had this condition persisted for i longer than allowed by the Technical Specifications, action would have !'
'oeen taken to place the plant in the shutdown condition, thereby mitigating the consequences of this event. Based upon the above assessment, this event is not considered to be nuclear safety significant. ;
-l The VX and HPCS systems were inoperable from 1023 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br /> to 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on' -
November 22, 1989. The RCIC system was inoperable from 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> on.
November 21, 1989 until 1440 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.4792e-4 months <br /> on November 22, 1989.
ADDITIONAL INFORMATION ;
The chiller condensing unit IVX06CC which failed is a Model SF40 >
manufactured by Carrier Corporation. l No events have been previously reported which' identified entry into Technical Specification 3.0.3 as a result of the failure of the essential l switchgear heat removal system.
For further information regarding this event, contact D. R. Morris, Director - Plant Operations at (217) 935 8881, extension 3205.
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