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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:RO)
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARU-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 U-603033, Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals1998-07-20020 July 1998 Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals U-603041, Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 ML20151U1501998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 U-603023, Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 1 U-603014, Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed1998-05-28028 May 1998 Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed ML20236E7991998-05-26026 May 1998 Final Part 21 Rept Re W Dhp Circuit Breaker Auxillary Switch Operating Assembly Anomalies.Caused by Loss of Breaker Safety Function.Dhp Circuit Will Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted U-603004, Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable1998-05-15015 May 1998 Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable ML20216A9601998-05-0808 May 1998 Part 21 Rept Re Failure of 12 Volt DC Inverter Power Supply. Caused by Inadequately Sized Output Transistor Pair Combined W/Degraded Capacitors.Licensee Plans to Replace All Output Transistors & Degraded Capacitors U-602995, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts1998-05-0505 May 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts U-603006, Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 1 U-602994, Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable1998-04-29029 April 1998 Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable ML20216B1351998-04-21021 April 1998 Rev 0 to Illinois Power Co Clinton Power Station SVC Design Rept U-602979, Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable1998-04-0707 April 1998 Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable U-602976, Monthly Operating Rept for Mar 1998 for Clinton Power Station1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Clinton Power Station ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue U-602968, Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue1998-03-24024 March 1998 Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue U-602960, Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 9804111998-03-12012 March 1998 Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 980411 U-602954, Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 9805131998-03-0909 March 1998 Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 980513 1999-09-30
[Table view] |
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CLIN 1QN POWLH ST ATION, P.O. HON 078. CLIN 10N. ILL1hOlb 617274Ki78. TI:LLl'ilON!: (2171935 8881 Februsry 20, 1991 10CTR50.73 Docket NO. 50 451 Docwnent Contcol Desk Nuclear Regulatory Commission Washin6 ton, D.C. 20555
Subject:
Clinton Power Station Unit 1 Licensee Event Report No. 91-001-00
Dear Sir:
Please find enclosed Licensee Event Report No. 91 001 00: 6D ltindnquat e System Ittpact ASItnitet of Turbine Modi f tnL[nn,_WnrJ;
[Mulj;ed in Automatic Containment Isolat ion Dut:lq,Jernonnel Error.
This report is being sobinitted in accordance with the requirements of 10CTR50.73.
Sincerol; yours
- i
%ff, F. A. Sp4 igen rg, IIW Hanager, 1.icensing and Salety STil/alh Enclosuto cc: NRC Clinton Licensing Project Manager NRC Resident Office NRC Region III, Regional Administrator Illinois Department of Nuclear Safety INPO Records Center i
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"""' An Inadequate System Impact Assessment of Turbine Modification Work Resulted in'{0Fl0 d' Autor, otic Containment Isolation Due to Personnel Error ,
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..t.c,n...,i,,.,....,,,...,,.,m...<......n.o...n.1 At approximately 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br /> on January 21, 391, during the planc's s
second refuelinB outage, while the plant was in Operationn1 condi ion 4 (COLD S!!!J1'DOWN), a Group I containment isolation signal was genersted from Condenser Low Vacuum Bypass logie resulting in automatic closure of inboard Main Stearn Isolation valves 1B21-F022 A, B, C, and D, and inhoard Main Steam Drain Line Isolation valve 1B21 F016. At approximately 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br />, the 'B' Control Room Operator (CRO) manual g tripped the main turbine logic. At approximately 1317 hours0.0152 days <br />0.366 hours <br />0.00218 weeks <br />5.011185e-4 months <br />, the 'B' CR0 reset the ,
Condenter 1.ow yacuum Bypass logic and reopened valves 1B21 F022 A, B, C, and D, and 1B21.F016. At the tinto of the event, main t arbino q modification adjustments and preparations for the reacts r vessel hydrostatic test were in progress. The cause of the evsnt was attributed to utility maintenance personnel error in that personnel did not properly tissess the iirpact to the plant of turbine modification during revisions '
> of the Maintenance Work Request (MVR) being used to implement the turbine modification. Corrective actions include: suspending turbine modification work, revising the MWR to include jobsteps to defeat the Group I containment isolation signal, training assistant maintenance supervisors on revising MWRs, and briefing appropriate personnel on this event.
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0l0 0 l2 OF 0l5 itxi w ~. . . ==. . ma ne w,m, DESCRIPTION OF EVENT At 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br /> on January 21, 1991, with the plant in Operational Condition 4 (COLD SilUTDOWN), with the reactor [RCT) coolant temperature rt 169 degrees Fahrenheit and at atmospheric pressure, a Group I containment isolation signal was generated from Condenser [COND] Low Vacuum Bypass logic resulting in automatic closure of inboard Main Steam
[SB) Isolation Valves (MSIVs) [ISV) 1B21 F022 A, B, C, and D, and inboard Ma,in Steam Drain [DRN] Line Isolation Valve 1B21-F016.
At the time the containment isolation signal was generated, preparations for the reactor coolent boundary system leakage test wera in progren with reactor yessel ,RPV) level being raised to support the hydrostatic test. These preparations were being performed in accordance with plant technical procedure 2800.03, " Reactor Coolant System Leakage Test." The valve [V) lineup associated with this test required the inboard MSIVc to a- be open a-d the outboard MSIVs to be shut.
Concurrently but independently, plant personnel wer; implementing plant
- modification TGF008 to convert the main turbine [TRB) from full arc admission to partial arc a&nission.
Modification work'of the m'ain turbine was being controlled by Maintenance Work Request (MWR)-D09786. This modification implemented Field Engineering Change Notice (FECN; '5470 which changed $ e operating characteristics of the Turbine Control valves (TGV) {FCV). While MWR D09786-implemented a change in the operating characteristic e the TCVs, the MWR did not provide specific steps to verify TCV operav < ring the modification process. Subsequently, the assistant Control are Instrumentation maintenance (C&I) supervisor revised MWR D09786 in accordance with plant administrative procedure 1029.01, "Preparatin and Routing of Maintenance Work Requests," to incorporate steps developed from excerpts of plant surveillance procedure 9431.21, " Turbine Control and Stop Valves Scram Response Time Teut," that would allow the main turbine logic to be reset in order to verify TGV operation.
Investigation of this event revealed that this revision did not include l the nece uary piacautions, prerequisites, and limitations corresponding to the appropriate excerpts from plant surveillance procedure 9431.21
), = - used to develop jobst'ps of the MWR. AdG tionally , this revision and previous versions of the MWR did not include a system impact matrix to address the jobsteps of the MWR, since the jobsteps were assumed to be '
within the tagout boundary for the MWE.
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i The revision was > . jewed by Maintenance Planning and the Nuclear Station Engineering Department (NSED), and by the Operations Lina Assistant Shift Supervisor (LASS) and the Staff Assistant Shift Supervisior, (SASS) y rior 3 to-Operations giving the C&1 technicians permission to start work. On y January 18.-1991, the C&I. technicians began. lifting leads ta defeat main [
turbine' trips in preparation of resetting the main turbine at a later 'L time.
On January 21, 1991,-with preparations for the reactor coolant boundary system leakage test in progress, the LASS gave. permission for the y continuation of the turbine modification work that began on January 18, 4 1991. At;approximately-1305 hours, the *B' Control Room Operator (CRO)..
in accordance with MWR D09786, placed the main turbine in manual control on-the Operating Mode. switch and selected "Close Valves" on the Speed ~ Set revolutions per minuto (RPM) switch (SIS], TheB' CR0 then reset the main turbine logic by depressing the "Resot" push button, Shnrtly afterward, the 'B'-CR0 selected "800 RPM" on the Speed. Set RPM switch, and-the Turbine Stop_ Valves (TSV) 9pened in response, Openine,wf the TSVs resulted in automatic reset of the Condenser Low V , Vacuum containment. isolation logic that had previously been bypassed,
. Reset of the main turbine logic and positioning of the TSVs greater than !
ninety percent' open resulted, by design, in the generation of a Group I _
containment isolation signal'due to Condenser Low Vacuum-Bypase._ logic. ,
This unplanned isolation signal caused'automaH.c closure of isolation
= valves 1B21-F022 A,-B, C, and D,' and.1B21 F0' At app'roximately 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br />,.the main turbine Logic was-manually tripped by.the 'B' CRO, At 1317 hours0.0152 days <br />0.366 hours <br />0.00218 weeks <br />5.011185e-4 months <br />, the 'B' CR0 completed th Automatic
- Isolation. Checklist, and satisfactorily varified -aL complete Group 1 i
isolauion. Tne Condenser Low Vacuum bypass logic-was reset and: isolation
- valves 1B21.F022 _A, - B, J. and D,- and 1B21 F016 = were reopened. _ Turbine- - 1' modification and work under MWR-D0978_6 was suspended pending further investigation and determination uf root cause, No other automatic or_ manually initiated safety' system responses were-
- necessary to place the plant in a safe and stable condition. No other-equipment or'coeponents were inoperabic at the-start of this event such that:their inoperable condition-contributed to this event,
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-CAUSE OF THE EVENT The cause of this event is attributed to personnel error. The assistant C&T supervisor, a utility member, did not properly evaluate and identify all potential impacts on other plant systems when revising MWR D09786.
The assistant C&I supervisor was relatively new in hic ;osition and had not revised many MWRs. He determ!ned that a system impact matrix was not required for the revisions to the MWR, since the added jobsteps were assumed to be within the tagout boundary for the MWR. Required reading of plant administrative procedure 1029.01 was the extent of his training for revising MWRs.
Additionally, plant administrativo procedure 1029.01, section 8.6,
" Revision of MWRs," does not address including the necessary precautions,
. prerequisites, and limitations when using procedure excerpts within the jobsteps of revised MWRs; however, this is addressed in section 8.2,
" Maintenance Planning: Processing of Routine Maintenance Work Requests."
Investigation determined that the precas, lons, prerequisites, and limitations of plaat surveillance procedt to 9431.21 did correctly address the required plant conditions to perform :he test; however, the excerpts of this procedure used as jobsteps for K.R D09786 did not include the necessary precautions, prurcquisites, and limitations from this prccedure prior to this event.
CORRECTIVE ACTION The assistant C&I supervisor recognized his error associated with this event. He has readily admitted the error associated with this' event and
.has been counselled on the-requirements for evaluating and identifying
~ potential impacts on other plant systems when revising MWRs and performing maintenance activities.
MWR D09786 was revised to include.jobsteps for li.' ting leads to defeat a
. Group I containment isolation- . A syster impact matrix for-each TSV end L4 TGVL and for lif ting leads was completed Dr WD D09786.
' Training will'be provided to assistant maintenance supervisors, who have not been previously assigned to maintenance planning, on the requirements
- .evising MWRs. Thi's training will include information on system
- . impact matrix preparation and when a system impact matrix is required, l
This training-.is-scheduled to be completed by August 20,~ 1991, Plant admin.strative procedure.1029.01,- section 8.6, will be revised to-
-include- a statement that plant piocedure excerpts used in jobsteps of revised MWRs chall include precautions. prerequisites,-and limitations-from the edure when necessary. This procedure revision-is scheduled torbe comy.,ted by May 1, 199L g ,..M o. . u . . .. .- a
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' Appropriate C&I and NSED personnel will be briefed on this event. These
- briefings are scheduled to be completed by March 20, 1991.
ANALYSIS OF EVFET This event is reportable under 10CFR50.73(a)(2)(iv) due to an automatic actuation of an Engineered Safety Feature. This event occurred while the plant was shutdown and' did not tesult in a condition significant to the safe operation of Clinton Power Station. Because main turbino admission modifications are performed only when the reactor is shutdown, this event '
would not occur during other modes of operation. Reactor vessel pressure '
monitoring instruments (PI) in place to support the primary coolant leakage test showed-no increase in reactor pressure as a result of this incident.
ADDITIONAL INFORMATION -
.All systems associated with this event responded as designed and no '
components failed during this event.
LER 86-024 00 discusses automatic closure of Group-I containment isolation valves due to Condenser Low Vacuum Bypass logic caused by utility personnel error.
For further information regarding this event, contact S. E. Rasor, Director - Plant Maintenance at 217 935 8881, Ext. 3204.
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