ML20039D329

From kanterella
Jump to navigation Jump to search
IE Insp Repts 50-324/81-29 & 50-325/81-29 on 811015-1115. Noncompliance Noted:No Alarm Procedures Established for Hi & Hi Hi Flood Level in Rhr,Core Spray & HPCI Rooms as of 811007
ML20039D329
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 11/25/1981
From: Burger C, Garner L, Dante Johnson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20039D299 List:
References
TASK-1.A.1.2, TASK-1.C.2, TASK-1.C.4, TASK-3.A.1.2, TASK-TM 50-324-81-29, 50-325-81-29, NUDOCS 8112310528
Download: ML20039D329 (9)


See also: IR 05000324/1981029

Text

(

. . '

.

.

UNITED STATES

-9

g

8

NUCLEAR REGULATORY COMMISSION

o-

g

a

' REGION 11

o

101 MARIETTA ST N.W SUITE 3100

ATLANTA, GEORGIA 30303

o

.....

Report Hos. 50-324/81-29 and 50-325/81-29

Licensee: Carolina Power and Light Company

411 Fayetteville Street

Raleigh, N. C. 27602

Facility Name: Brunswick

Docket Nos. 50-324 and 50-325

License Nos. DPR-62 and DPR-71

Inspection at Brunswick site near Wilmington N. C.

Inspectors:

.b

/W

'

D. F. d6hfison, Senior Aesident inspector

Date Signed

C , W',

/(/es/81

L. W. GaKMr. Resident . Inspector

Date Signed

Approved by:

b

/kl4/M

C. Burge d Section Chief, Division of.

Date Signed

Resident and Reactor Project ' Inspection -

SUlttARY

Inspection on October 15 - November 15, 1981

Areas Inspected

This inspection in_volved 150 resident inspector-hours on site in the areas of :

operational safety verification, review of operational events, review of periodic

,

reports, followup on licensee event reports, plant tours, followup on Tit! Task

'

Action Plan items followup on previous inspection findings, review and audit of

'

onsite safety contaittee meetings, and independent inspection efforts.

Results

Of the 9 areas inspected, one violation was identified.

(Failure to establish

alann procedures per Technical Specification 6.8.1.a,. see paragraph 5.)

i-

8112310528 811223

PDR ADOCK 05000324

G

PDR.

[

. . .

.

. - -

.

- -

. -

-

-

-

- .

,.

.

.

DETAILS

1.

Persons Contacted

Licensee Employees

A. Bishop, Engineering Supervisor

G. Bishop, Project Engineer

S. Bohanan, Principal Specialist Regulatory Compliance

J. Boone, Project Engineer

J. Cook, E & RC Foreman

  • C, Dietz, General Manager, Brunswick

J. Dimette,11echanical Maintenance Supervisor

E. Enzor, I & C/ Electrical Maintenance Supervisor

  • it. Hill, flaintenance fianager

R. Knebel,flanager, Operations

it. Long, Manager, Special Projects

  • R. florgan, Plant Operations Manager
  • D. Novotny, Regulatory Specialist

G. Oliver, E & RC flanager

  • A. Padgett, Assistant to General llanager

G. Peeler, Shift Operating Supervisor

  • R. Poulk, Regulatory Specialist

W. Triplett, Administrative !!anager

  • L. Tripp, RC Supervisor
  • W. Tucker, Technical and Administrative fianager
  • V. Wagner, Director, Planning and Scheduling

Other licensee employees contacted included technicians, operators and

engineering staff personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on November 18, 1981 with

those persons indicated in Paragraph 1 above.

lieetings were also held with

senior facility management periodically during the course of this inspection

to discuss the inspection scope and findings.

3.

Reportable Occurrences

The below listed Licensee Event Reports (LER's) were reviewed to determine

if the information provided met NRC reporting requirements.

The determi-

nation included adequacy of event description and corrective action taken or

planned, existence of potential generic problems and the relative safety

significance of each event. Additional in-plant reviews and discussions

with plant personnel, as appropriate, were conducted for those reports

indicated by an asterisk.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _

__

_

_

_

_. __

_

_ _ _ -

.

.

2

Unit 1

Supplement-

.

.

1-79-104 (3L)

High Pr2ssure Cooling. Injection Turbine ' isolated due to

high steamline differential pressure.

A-81-45 (3L)

liain Steam Isolation Valve on "C" Line experienced

.-

and Supplement

Stem-Disk Separation.-

Supplement

1-81-60 (3L)

Suppression Chamber Visual Inspection not performed.

1-81-62 (3L)

Vacuum Breaker's Butterfly Valves,- 1-CAC-V17 and V16,

opened out of specification.

1-81-63-(3L)

Failed Reed Switch in Position Indicator Probe of

Control Rods 26-31 and 02-31

1-81-65 (3L)

One-half Group I Isolation Signal received due to

initiation of High Flow Signal from "C" Main Steamline

High Flow Instrument,1-B21-PDT-N008C.

1-81-66 (3L)

HPCI System Auxiliary 011 Pump uncoupled from T10 tor due

to broken Pump-Motor coupling.

1-81-67 (3L)

~

Drywell Airlock Exterior Door Leakage Rate Excee'ded

specifications.

1-81-68 (3L)

Defective Rod Position Indication Probe Reed Switch on

Control Rod 14-43.

1-81-69 (3L)

Primary Containment Atmospheric Monitor 1-CAC-ATH-1259

tripped.

1-81-70 (3L)

Suppression Chamber Water Level Recorder,1-CAC-LR-2602,

out of calibration.

1-81-71 (3L)

One-half of a Group I isolation signal received due

to low pressure signal from "B" main steam line low

pressure instrument, 1-B21-PS-N0158.

Unit 2

2-80-37 (3L)

11etal bracing fell on Intermediate Range lionitor "B"

separating it from its electrical connector.

  • 2-81-C06 (3L)

liain Steamline Valve Stem-Disk separation on Valve

and Supplement

F028C.

.

r

~

.

.

3

2-81-72 (3L)

High Pressure Coolant Injection Differential Temperature

Switch 2-E51-DTS-N604D, out of calibration.

  • 2-81-83

(3L)

Reactor Core Isolation Cooling System automatically

and Supplement

isolated.

2-81-93 (3L)

Rod B1ock fionitor Channel "A" would not "INOP".

2-81-95 (3L)

IbactorLow Water level Ins trument, 2-B21-LIS-N0428,

out of calibration.

2-81-98 (3L)

Switch No.1 of "A" Core Spray Differential Pressure

Instrument 2-E21-DPIS-N004A, would not actuate.

2-81-99 (3L)

Failure to sample Reactor Coolant following notifi-

cation of power increase.

2-81-100 (3L)

RCIC isolated due to corroded Microswitches of Turbine

Exhaust Diaphram pressure Switch 2-E51-PS-N012C.

2-81-102 (3L)

Fire Hose Station, SW-1, inoperable due to bent hose

reel.

2-81-103 (3L)

Primary Containment Atmospheric 0xygen Analyzer,

2-CAC-AT-1259-2, showed upscale indication of Torus

Oxygen concentration.

2-81-107 (3L)

Suppression Chamber Water Level Recorder, 2-CAC-LR-2602,

showed downscale indication.

2-81-113 (3L)

Power supply fuse to Drywell Floor Drain and Drywell

Equipment Drain integrators, and Drywell Equipment Drain

tank temperature indicators, blew causing lo! . of

indications.

2-81-111 (3L)

The "A" RHRSW pumps unable to start due to pump

suction header low pressure lockout signal from switch

2-SW-PS-1175.

2-81-114 (3L)

Primary Containment Atmospheric 0xygen Analyzer,

2-CAC-AT-1259-2, erroneous indications due to moisture

buildup in torus sample line.

4.

THI Task Action Plan Requirements

a.

Item I.A.1.2, Shift Supervisor Responsibilities

Administrative Procedure 2.0 " Organization and Responsibility",

Revision 051, dated September 30, 1981, establishes duties and

responsibilities of the shift supervisor for safe operation of the

-

-

.

.

.

4

facility under all conditions on his shift and clearly. establishes his-

'

command duties.

Administrative Procedure 2.0%1so includes duties, responsibilities and

authorities of other control room personnel, and establishes a definite

line of command in the absence of the shift supervisor.

The 'above procedure appears to satisfy the requirements of NUREG-0578,

Section 2.2.1.a. and Position I.C.3, Shift Supervisor Responsibilities.

This item is closed.

b.

Item I.C.2, Shift and Relief Turnover Procedures

Operating Instruction 01-2, " Shift Turnover Checklist", Revision 5,

dated Setpbember 30, 1981, has been revised to include the

reconnendations stated in NUREG-0578, Section 2.2.1.c.

The inspectors

verified by direct observation that the above procedure is being

implemented including the utilization of checklists for on-coming and

off-going shifts.

The inspector noted, however, during observation of. certain shift

turnovers, that all items on tae checklists are not being signed off

prior to taking over the shif t and that some turnovers are extremely

brief.

In addition, review of Procedure 01-2 resulted in the following

comments.

The checklists do not specifically designate those-item that must

--

be performed prior to assuiaing shift duties and responsibilities;

.the requirements for the use of the turnover checklist are not

--

clearly defined.

,

!

The licensee concurred with the inspector's comments and committed to

t

revise Procedure 01-2 and the turnover checklists by December 1,1981

with respect to the above concerns.

f

This is an inspector follow item (50-324/81-29-02 and 50-325/81-29-02).

c.-

Item I.C.4, Control Room Access

!

Administrative Procedure " Conduct of Operations", Section 4.1.11,

l

establishes 'the authority and responsibility'of the person in charge of

the control-room to limit access if the presence of any individual

(

interferes with operations or may compromise plant safety.

The Emergency Plan, Section 3.0, " Emergency Response Organization",-

L

clearly establishes a line of authority and responsibility in the

control room in the event of an emergency,-including plant mangement

personnel not in direct command of operations.

L

!

r----

- - - - - - -

- - - - - - -

.-

.

.

5

The above procedures appear to meet the requirements of NUREG-0578,

Section 2.2.2.a.

This item is closed,

d.

Item III. A.1.2.1.a, Upgrade Emergency Support Facilities

The licensee has established an onsite technical support center

separate from and in close proximity to the control room, that has the

capability to transmit plant status tu those individuals who are

knowledgeable of and responsible for engineering and management support

of reactor operations in the event of accident.

The licensee's

emergency plan has been revised to incorporate the role and location of

the technical support center.

In addition, the inspector witnessed the

manning and operability of the technical support center during various

emergency drills conducted during the year, including the designated

onsite operational support center.

Based on the above, Position III.A.1.2.1. appears satisfied.

This item is closed.

5.

Failure to have Annunciator Procedures

On October 20, 1981, the inspector observed control room RTGB annunciatur

window 2-2, North RHR Flood Level Hi, on panel 2-UA-12 lit. Operatinq

lbnual Volume XVI, Book 2 - Annunciator Procedures - Unit 2, was found to

contain a procedure entitled 'RX BLOG FIRE SYSTEM PRESS LOW' for this

window. Discussion with the Shift Foreman revealed that information

necessary to write the procedure had been requested from engineering

approximately two weeks earlier and operations had received a reply on

October 20, 1981. He indicated that annunciator procedures were also in

preparation for the Hi and Hi Hi flood level annunciators for core spray,

HPCI and south RHR rooms.

The alarms had been installed as part of plant modification 79-061 and

79-062. The equipment had been turned over to operations in October 1980.

Prior to that time, another plant modification had moved the fire protection

alarms to the fire protection panel.

Failure to have procedures for these annunciators is a violation of

Technical Specification Section 6.8.1.a (324/81-29-0? and 325/81-29-01).

6.

Plant Transients

On November 2,1981. at 1431 hours0.0166 days <br />0.398 hours <br />0.00237 weeks <br />5.444955e-4 months <br />, Unit 2 reactor scrammed from 77% power.

Investigation revealed that a malfunctioning moisture separator reheater

high level trip switch number 2-MD-LSHMS-2 had initiated a turbine trip.

The turbine stop valve closure above 30% power resulted in a reactor scram.

No ECCS actuation occurred. The HSIV's did close, but were immediately

reopened. Probable cause for the Group I was movement of the mode switch

- - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-

-

.

6

from 'Run' to ' Shutdown' prior to steam flow decreasing below 40% of rated

fl ow.

On November 3,1981 at 0308, hours, Unit 2 reactor scramed from 7% power

while in startup mode. A flux spike caused by cold water injection resulted

in an APRM 15% high flux reactor protection system trip.

Prior to the trip,

vessel level had decreased to approximately 175".

The 2A reactor feed pump

increased speed, thereby causing a sudden increase of cold water flow.

Investigation indicated that sticking of the 2A RFP mechanical linkage

between the hydraulic actuators and the control valves had resulted in feed

flow temporarily not following demand. A large demand subsequently freed

the mechanism and allowed a slug of cold water to be added to the vessel.

The linkage has been lubricated and verified to be operating smoothly.

On October 29,1981, at 1631 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.205955e-4 months <br />, Unit I reactor scramed on low water

level.

Prior to the protective circuit trip, the unit was at 100% power,

low condensate booster pump suction alarms had been received at 1627 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.190735e-4 months <br />

and reactor feed pump 1A had tripped with a reactor recirculation pump

runback at 1631 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.205955e-4 months <br />. Loss of the feed pump and shrinkage from the power

reduction resulted in vessel level decreasing to the trip point. At 1655

hours, low condenser vacuum initiated closure of the itSIV's. At 1703 hours0.0197 days <br />0.473 hours <br />0.00282 weeks <br />6.479915e-4 months <br />,

a reactor high pressure trip was received.

Safety relief valve F013D was

manually actuated for approximately 2 minutes resulting in lowering vessel

pressu re.

The Group I isolation was reset and the f1SIV's were reopened at

1711 hours0.0198 days <br />0.475 hours <br />0.00283 weeks <br />6.510355e-4 months <br />. The reactor system was stabilized and normal cooldown

commenced.

Investigation revealed that a sudden increase in tube leakage in

feedwater heater SA resulted in feedwater being diverted from the vessel to

the condenser via the feedwater heater drain subsystem. This bypass flow

plus normal vessel flow exceeded the amount that could be delivered by

condensate booster pumps 1A and 18.

Therefore, low suction pressure

resulted at the reactor feed pumps. Condensate booster pump 1C was not

available for service at the time.

Feedwater heater 4A and 5A will be kept

out of service until repairs can be made during the next outage of

sufficient length to allow the work to be accomplished.

During the three events, all safety systems which were required to actuate

performed as designed. The inspector has no further questions at this time.

7.

Review of Periodic Reports

The inspector reviewed the following Licensee Report.

--

Brunswick Steam Electric Plant, Units Nos.1 and 2, !1onthly Operation

Report for September,1981.

The inspector verified that the information reported by the licensee is

technically adequate and satisfies applicable reporting requirements

established in 10 CFR 50, and Technical Specifications.

The inspector had no further questions in this area.

No violations were

identified.

.

_ _ _ _ _ _ _ _ _

_ _ _ _ .

_ _ _ _ _

_

_

_ _ _

_

__

_ _ _ _ _ _ _ _ _ _ _ _ _ _

_

_ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _

.

7

8.

Onsite Review Committees

The inspector attended several special PNSC meetings conducted during the

period of October 15 through Novermber 15, 1981.

The inspector verified the following items:

fleetings were conducted in accordance with Technical Specification

--

requirements regarding quoroum membership, reitiew process frequency and

personnel qualification;

ficeting minutes were reviewed to confirm that decision /recomendations

--

were reflected and follow-up of corrective actions were completed.

No violations were identified.

9.

Review of Plant Operations

The inspector reviewed plant operations through direct inspections and

a.

observations throughout the reporting period.

The following areas were

inspected.

(1) Control Room

(2) Service Building

(3) Reactor Buildings

(4) Diesel Generator Rooms

(5) Control Points

(6) Site Perimeter

(7) Service Water Building

(8) Turbine Building

b.

The following deteminatians were made:

Monitoring instrumentation. The inspector verified that selected

--

instr"ments were functional and demonstrated parameters within

Technical Specification limits.

Valve positions. The inspector verified that selected valves were

--

in the position or condition required by Technical Specifications

for the applicable plant mode. This verificationincluded control

board indication and field observation of valve position -

(Safeguard Systems).

--

Radiation Controls. The inspector verif ud by observation that

control point procedures and posting requirements were being

followed.

The inspector identified no failure to properly post

radiation and high radiation areas.

Plart housekeeping conditions. Unit I core spray "B" pump room

--

was found to have wooden boards stacked on the floor. The

licensee has removed these items.

._

..:.

8

Fluid leaks. No fluid leaks were observed which had not been

--

identified by station personnel.

Safety-Related Snubber 1E21-25SS96, was found corroded.

It has

--

been repaired.

Initial investigation indicates that sea water

apparently came in contact with the snubber during recent

maintenance on the overhead roon cooler. A similar event was

report in I & E Inspection Report 81-24.

The apparent failure of

personnel to adequately protect safety-related equipment during

maintenance as indicated by this item is an Unresolved Item

(325/81-29-03). Unresolved Item-(325/81-24-02), is now

incorporated into this new item and thus (325/81-24-02), is

closed.

Control room annunciators.

Selected lit annunciators were

--

discussed with control room operators to verify that the reasons

for them were understood and corrective action, if required, was

being taken.

By observation during the inspection period, the inspector

--

verified the control roon manning requirements of 10 CFR 50.54(k)

and the Technical Specifications were being met.

In addition, the

inspector observed shift turnovers to verify that continuity of

system status was maintained. The inspector periodically

questioned shift personnel relative to their awareness of plant

conditions.

Technical Specifications. Through log review and direct

--

observation during tours, the inspector verified compliance with

selected Technical Specifications Limiting Conditions for

Operation.

Security. During the course of these inspectians, observations

--

relative to protected and vital area security were made, including

access controls, boundary integrity, search, escort, and badging.

No unsatisfactory conditions were identified, except the unresolved item

noted in paragraph 9.b above.