ML20035F353

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Insp Rept 50-482/93-03 on Stated Date.Violations Noted.Major Areas Inspected:Plant Status,Operational Safety Verification & Maint Observations
ML20035F353
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 04/13/1993
From: Johnson W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20035F345 List:
References
50-482-93-03, 50-482-93-3, NUDOCS 9304210185
Download: ML20035F353 (30)


See also: IR 05000482/1993003

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APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report:

50-482/93-03

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Operating License No.:

NPF-42

Docket:

50-482

Licensee: Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, Kansas 66839

Facility Name: Wolf Creek Generating Station

Inspection At: Coffey County, Burlington, Kansas

Inspection Conducted:

February 13 through March 27, 1993

Inspectors:

G. A. Pick, Senior Resident Inspector

L. E. Myers, Resident Inspector

P. A. Goldberg, Reactor Engineer

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R. V. Azua, Resident Inspector, Fort Calhoun Station

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Approved:

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Division ov,$hiEf, Proj'ect Section A

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Reactor Projects

Inspection Summary

Areas Inspected:

Routine, unannounced inspection including plant status,

operational safety verification, maintenance observations, surveillance

observations, reliable decay heat removal during outages, refueling

activities, followup on corrective actions for violations, other followup, and

in-office review of licensee event reports (LER).

Results:

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The inspectors identified two examples of a violation of Technical

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Specification 6.8.1.a concerning inadequate control and coordination

during clearance order implementation.

A radioactive gas release

occurred inside containment because of miscommunication during shift

turnover, and personnel placed clearances in the wrong order that

resulted in additional draining of the reactor coolant system below

midloop (Sections 2.6 and 2.13).

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Two noncited violations were identified. After discovering Technical

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Specification 3.9.4 was violated, the licensee quickly implemented

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effective actions to prevent recurrence (Section 2.8).

The licensee

determined that a personnel oversight resulted in a failure to perform an

as-found local leak rate test (Section 2.11).

A licensee investigation team determined the root cause and recommended

appropriate corrective actions in response to a containment purge

isolation. The investigation was comprehensive and demonstrated an

increased awareness by licensee management of the need to respond to

events (Section 2.6).

The licensee conducted a thorough but untimely evaluation of a reactor

protection system response time testing concern.

After the inspectors

expressed concern regarding timeliness of work group evaluations, the

licensee initiated a quality assurance surveillance (Section 2.2).

Qualified quality assurance personnel provided performance based 24-hour

coverage of the plant shutdown, and security conservatively increased the

sensitivity of metal detectors beyond that required in the security plan

(Sections 2.3 and 2.7).

The licensee implemented a good response to pressurizer temperature

transients (Section 2.4).

During a reactor coolant system drain down,

the licensee continued to drain with a level discrepancy, but the

licensee used the most negative indication as the true level

(Section 2.5).

The inspectors determined that, overall, the licensee had a good safety

program and an excellent program for controlling scaffolding

(Section 2.10).

The licensee initiated a performance improvement request (PIR) to

document that measuring and test equipment out-of-calibration evaluations

were significantly backlogged. After the inspectors expressed concern

about operability of equipment needed in Modes 5 and 6, the licensee

promptly reviewed all outstanding evaluations, determining that no

operability problems existed.

The inspectors considered the licensee

f ailure to evaluate equipment operability 4 months earlier, when quality

assurance personnel identified the deficiency, to be a weakness

(Section 3.1).

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The inspectors determined that the licensee established a well-planned,

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conservative outage schedule that ensured reliable decay heat removal and

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included availability of both onsite and offsite power supplies related

to the operable decay heat removal train (Section 5).

The inspectors determined that licensee programs assured compliance with

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refueling related Technical Specifications.

The licensee established

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strong controls for loose objects around the spent fuel pool. The

licensee thoroughly evaluated a method to perform vacuum venting of the

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reactor coolant system. The venting was determined to be necessary to

help minimize transgranular stress corrosion cracking of canopy seal

welds on spare reactor vessel head penetrations. The licensee identified

a failed fuel rod in an F-type assembly (Section 6).

Summary of Inspection Findings:

Violation 482/9301-01 was opened (Sections 2.6 and 2.13).

Violations 482/9126-02, 482/91202-01, 482/9208-01, 482/9208-02, and

482/9212-02 were closed (Section 7).

Inspection Followup Items 482/9202-01 and 482/9301-02 and a 10 CFR

Part 21 report were closed (Section 8).

Licensee Event Reports 482/91-013, 482/91-018, 482/92-001, 482/92-004,

482/92-011, and 482/92-012 were closed (Section 9).

Attachments:

Attachment 1 - Persons Contacted and Exit Meeting

Attachment 2 - Documents Reviewed

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DETAILS

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1 PLANT STATUS (71707)

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At the beginning of the inspection period, the plant operated at 100 percent

power. On March 4, 1993, the licensee began a controlled shutdown in order to

begin Refuel VI.

At the end of the inspection period, the reactor was

completely defueled.

2 OPERATIONAL SAFETY VERIFICATION

(71707)

The objectives of this inspection were to ensure that the facility was being

operated safely and in conformance with license and regulatory requirements,

and that the licensee's management control systems were effectively

discharging the licensee's responsibilities for safe operation.

The methods used to perform this inspection included direct observation of

activities and equipment, observation of control room operations, tours of the

facility, interviews and discussions with licensee personnel, independent

verification of safety system status and Technical Specifications limiting

conditions f ar operation, verification of corrective actions, and review of

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facility records.

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2.1

Loss of Offsite Notification Ability

On February 16, 1993, the licensee lost offsite power to the surrounding area

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and the emergency operations facility for a 3-hour period.

The following

afternoon, the licensee made a 1-hour 10 CFR Section E0.72 notification after

determining that six emergency plan sirens had lost power the previous day.

The licensee considered the loss of the sirens a major loss of emergency

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response capability.

The inspectors reviewed the program established for offsite agencies to notify

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the facility when emergency response sirens become inoperable.

The licensee

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had signed memorandums of agreement in 1988 specifying the notification

requirements; however, because the system had not been exercised, offsite

personnel failed to quickly recall their responsibilities.

Because of this event, the licensee conducted meetings with county personnel

to develop a plan to prevent recurrence.

The licensee signed new memorandums

of agreement and established a requirement in Procedure EPP 02-1.8, " Testing

and Maintenance of Alert and Notification System Status," Revision 7, to

remind agencies annually of their notification responsibilities for loss of

emergency response capabilities. The licensee revised Procedure ADM 01-033,

" Instructions for Evaluating, Reporting, and Documenting Potentially

Reportable Events," Revision 28, to specify that a loss of three or more

sirens for greater than I hour constitutes a major loss of the offsite

notification system and should be reported.

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2.2 Reactor Protection System Response Time Testing

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On February 28, 1993, the licensee informed the inspectors that the Technical

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Specifications surveillance tests for reactor protection system response times

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did not account for all delays assumed in the safety analysis. The licensee

reviewed this condition in response to Industry Technical Information Program

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Item 01985, " Technical Bulletin 92-03: Westinghouse Trip Protection." The

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vendor issued the letter to all plants with reactor coolant pump undervoltage

trip protection to address confusion related to response-time testing.

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vendor had determined that some plants did not include the time delays related

to the effects of back electromotive force and associated with opening of the

control rod drive mechanism gripper fingers. The licensee determined that.

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when testing the reactor coolant pump undervoltage trip response time, they

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failed to account for the back electromotive force and the gripper finger

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release time delays. Additionally, the licensee determined that they did not

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include the gripper finger release time delays in other response time tests.

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However, the licensee included the gripper finger release time during rod drop

testing, as specified in the Technical Specifications.

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On March 4, 1993, the licensee initiated PIR AN 93-0141 to ensure that the

issue would be resolved and initiated Work Request 01131-93 to ensure

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operability would be evaluated. The licensee made a 10 CFR Section 50.72

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report based on potentially being outside their design bases. This report was

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retracted on March 18, 1993. The operability evaluation for Work

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Request 01131-93 determined by a calculation that the back electromotive force

effects approximated 200 milliseconds (ms) and by review of past rod drop

tests that the gripper release time was 60 ms.

Adding 260 ms to the longest

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recorded time delay from surveillance tests (1.215 seconds) resulted in a time

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delay of 1.475 seconds, less than the acceptance criteria of 1.5 seconds.

The licensee initiated voluntary LER 482/93-001 and determined that other

reactor protection system instrumen't response times were not exceeded.

While

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reviewing the circumstances surrounding this deficiency, the licensee

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determined that:

(1) currently existing programs for assuring that they

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adhered to the safety analysis were adequate, (2) the root cause was an

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inadequate vendor definition of response time testing, and (3) sample reviews

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of other analyses would not be worthwhile. The licensee implemented or will

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implement the following additional actions:

(1) documenting the processes

used by nuclear analysis when they assumed responsibility of each safety

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analysis from the vendor, (2) determining the actions needed to resolve

problems identified in the safety analysis, and (3) addressing this generic

issue with the vendor owner's group.

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The inspectors determined that the Industry Technical Information Program

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coordinator received Technical Bulletin 92-03 on June 4,1992. The Industry

Technical Information Program coordinator issued Industry Technical

Information Program Item 01985 on July 6,1992, to design engineering after

discussing the potential that back electromotive force was not included in

response time testing. On August 7, 1992, design engineering requested an

extension until February 5,1993, based on the results of the NRC Electrical

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Distribution Safety Functional Inspection conclusions on undervoltage relay

response time testing. On February 12, 1993, a preliminary evaluation-

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concluded that gripper release and back electromotive force time delays were

not included in response time testing.

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Based upon the vendor numbers for back electromotive force and gripper release

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response times, the Techn'ical Specifications required response time would be

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exceeded. The inspectors expressed concern because of the delay in evaluating

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Industry Technical Information Program Item 01985.

In response to the

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inspectors' concern, the Vice President, Nuclear Assurance initiated a quality

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assurance surveillance to evaluate the effectiveness of the initial

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evaluations of Industry Technical Information Program items upon receipt by

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the work groups.

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2.3 Ouality Assurance Surveillance Activities

During the plant shutdown from Modes 1 to 5, two quality assurance auditors,

who held or had held operator licenses at Wolf Creek, provided 24-hour

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coverage for approximately 3 days. The auditors documented their observations

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in Surveillance S-2003, " Plant Shutdown, Mode 1 to Mode 5."

The auditors

noted:

(1) outstanding control room communications among operations personnel

and among the operators and other work groups, (2) that system engineers

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actively assisted the shift supervisor in resolving problems, and (3) that

operators performed the plant shutdown in a well-controlled manner with

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heightened awareness to seismic nnitor alarms. During the surveillance, the -

auditors issued PIR OP 93-0146 that documented a failure to log into the-

control room log an instrument air bypass valve found out of position and a

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lifting relief valve. The manager of operations issued a memorandum

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specifying the need to document all problems and challenges to systems.

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Quality assurance had not accepted the response at the end of the inspection

period.

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2.4 Pressurizer

On March 8,1993, while cooling down the plant in preparation for Refuel VI,

the licensee exceeded the pressurizer cooldown rate of 200oF/ hour specified in

Technical Specification 3.4.9.2.

Approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> later, the licensee

exceeded the pressurizer heatup rate of 100oF/ hour specified in Technical Specification 3.4.9.2.

This phenomenon occurred on two occasions in 1992

during plant cooldowns (refer to NRC Inspection Report 50-482/92-02,

Section 5.14). The licensee evaluated the effects on the pressurizer of

exceeding these limits. The licensee reviewed pressurizer water temperature,

pressurizer steam space temperature, charging flows, letdown flows, and

pressurizer surge line temperatures to perform the evaluations.

The licensee determined that the excessive cooldown lasted for 8 minutes with

a temperature change of 242oF because reactor coolant system water surged into

the pressurizer.

The insurge occurred because of the charging / letdown

mismatch, and the pressurizer spray flow rate was insufficient to force flow

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from the pressurizer. After going solid in the pressurizer, the licensee

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determined that an excessive heatup rate lasted for 40 minutes with a

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temperature change of 130of as the hotter liquid volume in the upper part of

the pressurizer displaced the cooler liquid volume in the lower part of the

pressurizer.

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The inspectors determined that the licensee contacted the vendor regarding the

consequences of the pressurizer temperature transients. The vendor concurred

with the licensee's evaluation that the transients did not significantly

affect the integrity of the pressurizer walls or bottom nozzle. The

inspectors determined that a vendor owner's group insurge/outsurge evaluation

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program had an estimated completion date of December 1994.

Since the

cooldown/heatup transients experienced were less severe and occurred less

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frequently than transients in design analyses, the licensee concluded that the

accumulated fatigue usage factor for the pressurizer was within design.

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Consequently, the licensee determined that the pressurizer could be used as

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The inspectors determined that the licensee will implement changes to their

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operating procedures prior to drawing a bubble in the pressurizer to minimize

insurges and outsurges. The licensee will create / collapse the bubble at a

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higher temperature so the spray flow can be increased to ensure flow goes from

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the pressurizer to the surge line.

In the future the same methodology will be

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used to 90 solid. By operating the pressurizer in this manner, the delta

temperatures between the reactor coolant system and the pressurizer are

decreased minimizing temperature transients.

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2.5 Level Instrument Deviations

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On March 9,1993, the licensee initiated a reactor coolant system drain down

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to 18 inches below the reactor vessel flange so that the vessel head could be

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lifted, as specified in Procedure GEN 00-007, "RCS Drain Down," Revision 12.

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When draining the reactor coolant system, the licensee uses two independent

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level instruments and a tygon hose. Operations personnel verified that no

kinks, low points, or loop seals existed in the tygon hose. The individual

stationed inside the containment building to monitor the tygon hose level

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periodically communicated the level readings to the control room. Prior to

beginning the drain down, instrumentation and control technicians calibrated

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the midloop level instruments in accordance with Procedure STN IC-286, "RCS

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Midloop Level Instrumentation Calibration," Revision 0.

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The licensee established a controlled drain down process, but several delays

occurred.

For example, since the licensee added nitrogen to the reactor

coolant system to help remove fission product gases, personnel changed

nitrogen bottles when the bottle pressure decreased. Approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

into the drain down, operators stopped draining the reactor coolant system

because a 30-inch level discrepancy existed between the tygon hose and the

level transmitters. After investigating, the licensee removed a loop seal

that had developed in the tygon hose. Also, the operators stopped draining to

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perform a shift turnover.

Later, after resuming the drain down, operators

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determined that a 16-inch difference existed between the level transmitters

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and the tygon hose.

No problems were identified in the tygon hose. Draining

was continued until the water level was 18 inches below the flange, as

determined by the lowest indicating instrument.

After reducing the water level to 18 inches below the flange, the licensee

began troubleshooting the 16-inch level discrepancy.

During the

troubleshooting, the levels diverged to a maximum of approximately 30 inches.

The operators altered the charging and letdown flows to ensure that the lowest

indicated level remained higher than 3 feet below the flange to prevent

entering reduced inventory conditions.

The next day after instrumentation and

control technicians drained water from the reference leg for the level

transmitters under Work Request 01386-93, the level difference between the

transmitters and the tygon tube agreed within 1/2 inch. The licensee

determined that on March 9,1993, personnel had opened the midloop level

instrument root valves with the pressurizer level above the instrument taps,

as permitted by Procedure GEN 00-007, which prevented the reference leg from

draining. Subsequently, after the pressurizer water level decreased below the

instrument taps, the licensee drained the reference legs. The licensee

determined that the level indications diverged during the drain down because

water droplets that had adhered to the instrument tube walls slowly collected

in the reference leg tubing.

The change in relative pressures caused the

indicated level deficiency. The licensee changed Procedure Gen 00-007 to

insure the reference leg isolation valves will not be opened until the

pressurizer water level drains below the pressurizei instrument taps.

2.6 Containment Purge Isolation

On March 10, 1993, a containment purge isolation and control room ventilation

isolation occurred when gaseous activity exceeded the activation setpoint of

1.00 E-3 uCi/ml on Radiation Monitor GT RE-022, located in the containment

purge ventilation duct. As reported under 10 CFR Section 50.72, the licensee

evacuated 77 people from the containment building. The licensee determined

the root cause to be the release of gases from the pressurizer relief tank

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through the excess letdown heat exchanger drain line.

On March 11, 1993,

approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> later, Radiation Monitor GT RE-022 went into alert.

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response to the alarm, the operators manually isolated the containment purge

system before an automatic isolation occurred.

The 'nspectors reviewed

computer printouts and interviewed personnel and determined that an engineered

safety features isolation would not have occurred.

In response to these

events, the Vice President, Plant Operations established an investigation team

in accordance with Procedure ADM 01-116, " Incident Investigation," Revision 4,

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to address:

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The cause of the containment purge isolation,

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Operator actions,

Radiological consequences, and

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Lessons learned including corrective actions.

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The investigation team reviewed other ongoing activities determining that the

sequence of events that caused the gas release involved opening Valve BG V221,

excess letdown heat exchanger tube side combined drain valve.

The licensee

determined that the 9 psi gas pressure in the pressurizer relief tank applied

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against the seats of Target Rock Valves BG HV8157A and -B, excess letdown heat

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exchanger outlet to pressurizer relief tank isolations, created a flow path

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into the containment building. The investigation team identified several root

causes and specified corrective actions. The root causes included:

(1) the

design misapplication of Valves BB HV8157A and -B, (2) operations personnel

were unaware of the unidirectional properties of the solenoid vales, and

(3) the lack of timely distribution of solenoid operated valve

problem /information. Because of these deficiencies, operations personnel

inappropriately used the solenoid valves as clearance order boundary valves.

The investigation team determined h contributing cause was the implementing

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order of work activities within the outage window, which included work on the

reactor coolant drain tank.

The licensee measured the exposure from the thermoluminescent dosimeters of.

the last two individuals who left containment. The licensee calculated the

highest potential skin and whole body exposures to be 15 and 12 mrem,

respectively. From review of radiation monitor data, the licensee determined

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the maximum gas activity to be 1.45 E-3 uCi/ml and leveled at 4.33 E-4 uCi/ml.

The licensee determined that for future events the actuation setpoint will be

1.0 E-2 uCi/ml to be consistent with the Offsite Dose Calculation Manual for

Shutdown Conditions. The licensee determined that the containment evacuation

generally went well.

Following the containment purge and control room ventilation isolations, the

manager of operations directed that Clearance Order 93-0435-BG be changed to

restore the reactor coolant drain tank to allow depressurizing and draining

the pressurizer relief tank in accordance with Procedure SYS BB-202,

" Pressurizer Relief Tank Operation," Revision 16, to remove the gases.

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day shift personnel did not develop the changes to Clearance Order 93-0435-BG,

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but the night shift personnel did develop the necessary changes in accordance

with the turnover information provided. However, during the turnover to night

shift personnel, day shift personnel did not adequately stress the need to

keep Valve BG V221 closed and not place the associated five clearance order

tags. Consequently, personnel inadvertently took the original set of

clearance order tags and the change clearance order tags to the field and

reopened Valve BG V221 without the cognizance of the shift

supervisor / supervising operator.

Approximately 10 minutes after personnel opened Valve BG V221, Radiation

Monitor GT RE-022 alarmed at the alert setpoint. The failure of operations

personnel to perform an adequate turnover indicated a weakness in control and

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coordination of clearance orders that could have resulted in an unnecessary

engineered safety features actuation. Also, the inspectors determined that

the licensee had no formalized method to control tags that are not placed as

intended.

Procedure ADM 02-100, " Clearance Order Procedure," Revision 27,

Step 7.1.3.4, specified that, "After the clearance and tags have been prepared

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and approved, the shift supervisor / supervising operator shall review the

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tagging arrangement and reverify that the clearance will not adversely affect

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the plant." This is the first example of a violation of Technical

Specification 6.8.1.a (482/9303-01) involving failure to properly coordinate

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clearance orders.

Corrective actions included:

(1) evaluating the appropriate time to

depressurize the pressurizer relief tank during outages, (2) changing

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Procedure ADM 02-100 to prohibit the use of Target Rock Solenoid valves as

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clearance order boundaries, (3) including the unidirectional characteristics

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of solenoid operated valves in operator training, and (4) evaluating

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enhancements to the operating experience program. The licensee intends to

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evaluate improvements to information specified in night orders and

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improvements in turnover communications in response to the second release.

Night orders provide specific infermation to the operating crew from

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operations management. The licensee will report this event as LER 482/93-002

2.7 Metal Detector Calibration

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Because of concerns with the sensitivity of the metal detectors and the

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security plan calibration requirements, the inspectors reviewed the licensee's

process for calibrating the metal detectors.

On March 13, 1993, the

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inspectors observed an instrumentation and control technician check the metal

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detector calibration with the specifie f security plan calibration standard.

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The technician performed the calibration in accordance with

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Procedure INC C-3314, " Portal Metal Detectors Preventive Maintenance,"

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Revision 4.

Following calibration of the detector, the technician increased

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the detector sensitivity of the detector until the monitor could detect a

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second standard that contained less metal.

The. inspectors considered this

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enhancement to plant security to be proactive.

2.8 Failure to Maintain Containment Integrity

On March 14, 1993, following restoration from a local leak rate test, test

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personnel questioned the control room operators about the required position

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for Valve EF V085, Essential Service Water B to containment vent. As

operations personnel evaluated the required position of Valve EF V085, the

operators determined that Procedure SYS EF-420, "ESW A(B) Train Drain,"

Revision 0, left several Essential Service Water B return header vent valves

open and some containment cooler -vent valves open. Additionally, Clearance

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Order 93-0540-EF tagged the following containment penetration isolation valves

open and daenergized:

EF HV032, essential se,rvice water / containment air

cooling containment isolation; EF HV034, Essential Service Water B to

containment air coolers; EF HV046, Essential Service Water B from containment

air coolers, and EF HV048, . essential service water / containment air cooling

containment isolation.

With the vent valves and containment isolation valves open, a direct path from

the containment building to the auxiliary building existed that violated

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Technical Specification 3.9.4.

The licensee immediately established

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containment integrity by closing the containment isolation valves. The

licensee determined the root cause to be failure to assure the procedure could

be implemented as written under the existing plant conditions. The licensee

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initiated PIR OP 93-0190 to ensure that corrective actions would be

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implemented and initiated Reportability Evaluation Request 93-007 to evaluate

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reportability. The licensee corrected the Essential Service Water A procedure

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prior to draining Train A and stated they would review similar system

operating procedures for those systems that go into the containment. This

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violation of Technical Specification 3.9.4 will not be cited because the

criteria specified in paragraph VII.B.2 of the NRC Enforcement Policy were

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satisfied. The licensee appropriately identified the root cause and initiated

actions to prevent recurrence. The licensee will report this event as

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LER 482/93-003.

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2.9 Loss of Instrument Air

On March 16, 1993, while in Mode 6, the plant experienced a loss of the

instrument air system with the reactor parJ1v defueled. The spent fuel pool

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cooling system continued to operate properly.

Ine shutdown cooling flow

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increased to 3600 gpm because air-operated flow control valves failed open.

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The licensee dispatched personnel to the air dryers / compressors to investigate

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the cause of the event.

Licensee personnel determined that solenoid valves

for the Train B instrument air dryer failed. The Train A air dryer was tagged

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out of service for maintenance.

The licensee replaced five solenoid valves

and declared the system operable after performing appropriate postmaintenance

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tests.

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The affected valves included two three-way and one four-way solenoid valves

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located on Train A and two four-way solenoid valves located on Train B.

Preliminarily, the licensee determined that sticking of the four-way solenoid

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valves contributed to this event because the four-way valve blew down instead

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of flowing to the air system. The licensee determined that the faulty four-

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way solenoid valves were unique to the air dryer system. The licensee

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initiated a hardware failure analysis to determine the root cause and

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corrective actions for these solenoid valve failures, prior to startup.

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2.10 Plant Safet_y Tours

The inspectors toured the plant accompanied by the safety coordinator to

assess:

(1) the safety condition of the plant, (2) the adequacy of plant

safety equipment, and (3) general work practices of licensee and contract

personnel. The inspectors determined the licensee maintained good

housekeeping considering the amount of maintenance activities being performed.

The inspectors inspected a number of slings in use and determined the sling

conditions met the acceptance criteria of the licensee's safety manual,

including current inspection' tags. The inspectors found personnel to be

knowledgeable concerning the use of slings. The inspectors considered the

construction and control of scaffolding to be superior, with scaffold permits

hanging at the access point. of all the scaffolds inspected. The inspectors

identified two deficiencies during the turbine building tour:

(1) a grinding

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wheel had a concave groove on the grinding wheel surface, and (2) an air hose

was connected to the service air system without a cotter pin to secure the

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hose fitting. The licensee promptly corrected both deficiencies.

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The inspectors reviewed the licensee's Occupational Safety and Health

Administration 200 Log, " Survey of Occupational Injury and Illness," noting

,

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that five logable events were recorded during 1993.

The inspectors reviewed

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the licensee's actions related to one of the recordable injuries and found the

actions to be thorough and comprehensive.

The safety coordinator stated that

I

hand injuries constitute the bulk of the injuries experiencad at Wolf Creek

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Generating Station. Consequently, the licensee took actions to minimize

injuries by heightening personnel awareness.

For example, the licensee issued

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a pamphlet to all personnel that provided useful information on proper work

practices in a comic book style, increasing the chances that it would be read.

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2.11

Failure to Perform local Leak Rate Test

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On March 23, 1993, licensee personnel determined that the actuator for

Motor-0perated Valve (MOV) BG HV8105, charging pump to regenerative heat

exchanger containment isolation, was removed prior to performing an as-found

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local leak rate test as required by Technical Specification 4.6.1.2 and ANSI

Standard N45.4-1972, " Leakage Rate Testing of Containment Structures for

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Nuclear Reactors," Step 4.2.

Without taking the as-found leakage rate, the

licensee could not determine whether leakage through the valve had changed

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from the leak rate measured in December 1991. The licensee initiated

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PIR TS 93-0228 to investigate the actions leading to the event and to ensure

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corrective actions would be implemented. The licensee will report this event

as LER 482/93-005.

!

The licensee determined that maintenance personnel overlooked the work

instructions that required performing an as-found local leak rate test in Work

Request 04447-93 because of personnel oversight.

,

The individual failed to perform Special Work Instruction Step 01 that

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required personnel to verify that an as-found local leak rate test was

performed. The licensee counseled the individual on the importance of

attention to detail. Also, the licensee will implement " positive discipline"

by requiring the individual to discuss the circumstances related to this

deficiency with his peers. The failure to perform the local leak rate test is

a violation of Technical Specification 4.6.1.2.

However, the violation will

not be cited because the criteria specified in paragraph VII.B.2 of the NRC

Enforcement Policy were satisfied.

Licensee personnel determined the test was

not performed. The licensee initiated an LER as required and implemented

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actions to prevent recurrence.

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2.12 High Thrust Bearing Temperature

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On March 23, 1993, following overhaul of Emergency Diesel Generator B, the

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licensee started the emergency diesel engine to perform the 24-hour

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postmaintenance test. After loading Emergency Diesel Generator B to 1600 kW,

the licenseo received a high thrust bearing temperature alarm. The

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annunciator alarms at temperatures greater than 190 F, and the licensee

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determined that the bearing temperature reached approximately 350 F.

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Operators stopped the emergency diesel generator after being notified by

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personnel who were in the room. The licensee initiated disassembly,

inspection, and reassembly of the thrust bearing in accordance with Work

Request 01784-93. The licensee determined that the inner thrust bearing was

wiped. The journal surface on the crankshaft had two bandr of deposited

bearing material 360o around the shaft and the journal surface was slightly

tempered.

Preliminarily, the licensee suspected that a loss of oil or low oil

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flow allowed the bearing surface to overheat. However, testing indicated that

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lubricating oil flowed to the bearing. The licensee determined that the

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bearing had shifted slightly around the shaft but had stopped after contacting

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the locating dowel.

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The licensee contacted an expert in hardware failure analysis to help

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determine the root cause. The licensee initiated Hardware failure

Analysis NP 93-008 to document the root cause and corrective actions. As part

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of the hardware failure analysis, the licensee will evaluate other affected

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components such as the main bearing and the bull gear. Also, the licensee

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contacted the vendor and a shaft-machining expert to help remove the tempering

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damage to the emergency diesel generator crankshaft.

From initial

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evaluations, the licensee determined the crankshaft would require machining

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until the metal was at the required hardness of 30 Rockwell C.

As documented

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in the engineering disposition to Work Request 01893-93, the licensee could

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machine the

haft by 1.5 mm initially. A hardness test will be initiated, and

,

if the required hardness is not met, the licensee will machine the shaft in

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0.5 mm increments until a total depth of 2.5 mm.

If additional machining is

necessary, another evaluation will be performed.

The inspectors will continue

,

to follow licensee activities in the next inspection period.

2.13 Clearance Order 1ssues

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On March 21, 1993, with the reactor vessel defueled, Mode E, the licensee

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di ained the reactor coolant system to half pipe to perform maintenance on

otherwise inaccessible valves. The operators performed the drain down in

accordance with Procedure SYS BB-212, " Draining the RCS to Midloop Level and

Below, fuel Off-loaaed," Revision 4.

After stabilizing the water level to

ensure the steam generator U-tubes were drained, operators noticed that the

reactor coolant system level continued to decrease. The licensee investigated

this deficiency, determining that miscoordination of Clearance

Orders 93-0651-EJ and 93-0618-EJ occurred.

Personnel should have established

Clearance Order 93-0618-EJ prior to Clearance Order 93-0651-EJ; however,

personnel established Clearance Order 93-0618-EJ first.

The inspectors determined that the implementation of the half-pipe clearance

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orders required close coordination.

Previously, the licensee established a

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single clearance order that removed all systems from service; however, to

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minimize the impact of MOV testing on clearance orders, the licensee

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specifically developed some clearance orders to support MOV testing. The

licensee issued PIR OP 93-0248 in response to this event. The PIR documented

i

that the tagging group failed to ensure that the shift crews understood the

i

significance of placing the half-pipe clearance orders in the correct order.

Also, the inspectors determined that Clearance Order 93-0651-EJ cautioned that

certain valves could be spened so long as they do not conflict with existing

clearances.

Procedure ADM 02-100 Step 7.1.3.4, specified that, "After the

clearance and tags have been prepared and approved, the shift

supervisor / supervising operator shall review the tagging arrangement and

,

reverify that the clearance will not adversely affect the plant." This is the

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second example of a violation of Technical Specification 6.8.1.a (482/9303-01)

involving failure to properly coordinate clearance orders.

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On March 25, 1993, control room operators noticed that the indicating lights

for MOV EJ HV88098, residual heat removal to Accumulator Injection Loops 3 and

4 isolation valve, were illuminated even though the handswitch had a Do Not

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Operate tag on the switch. Upon investigating, the licensee determined that

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electrical maintenance personnel requested that Clearance Order 93-0596-EJ be

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removed and a Human Do Not Operate control be established to allow local valve

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operation for troubleshooting. The Human Do'Not Operate control is an

individual stationed at a control device to prevent damage to equipment or

personnel injury. The individual places a placard at the control device

designating a Human Do Not Operate control is in effect.

The licensee

)

determined that a contract worker believed that a Human Do Not Operate control

could override Do Not Operate tags. Consequently, the individual disregarded

,

Clearance Order 93-0587-EJ. The licensee had the individual turn off the

breaker and counseled the individual on the proper use and significance of Do

Not Operate tags. The licensee initiated a procedure change for

Procedure ADM 02-100 to strengthen the issuance of Human Do Not Operate

controls and Do Not Operate tags. The changes specified that:

(1) equipment

will not be operated under any circumstances with a Do Not Operate tag

attached, (2) individuals must go to the control room and sign a newly created

attachment explaining the responsibilities of Human Do Not Operate controls,

and (3) possession of a Human Do Not Operate control does not give permission

to operate / change position of equipment with a Do Not Operate tag on it.

The

inspectors reviewed Procedure ADM 02-100, determining that the changes

strengthened the clearance order controls and the new attachment clearly

specified the responsibilities and limitations of a Human Do Not Operate

control.

On March 26, 1993, a worker removing MOV SJ HV127, reactor coolant system

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liquid sample outer containment isolation bypass, and MOV SJ HV005, reactor

coolant system liquid sample inner containment isolation, was sprayed with

reactor coolant fluid because the system was pressurized. The licensee

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determined that special instructions on Clearance Order 93-0377-SJ stated that

the local leak rate test performed prior to placing the clearance order would

drain the system. The licensee performed the local leak rate test for the

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affected penetration on March 13, 1993, and personnel established Clearance

Order 93-0377-SJ on March 24, 1993.

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The inspectors determined that, as originally planned, Clearance

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Order 93-0377-SJ would be placed in conjunction with the local leak rate test.

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The licensee completed the local leak rate test during defueling, but the

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licensee decided to place the clearance order following defueling. However,

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no thought was given to ensuring the system was drained. The licensee

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immediately added vent and drain valves to Clearance Order 93-0377-EJ and

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drained the affected piping. The licensee removed low levels of contamination

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from the individual determining the skin dose to be 1.13 mrem, and a whole

body count identified no internal contamination.

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Following the second significant clearance or6er coordination problem in

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2 days, the Vice President, Plant Operations established an investigation team

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on March 26, 1993, in accordance with Procedure ADM 01-116. The investigation

team was chartered with reviewing several clearance order problems occurring

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since the beginning of Refuel VI. The investigation team was to determine

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common causal factors and a root cause, if possible, so that corrective

actions to eliminate the problem could be implemented. The inspectors will

continue their inspections of these deficiencies in the next inspection

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period.

2.14 Conclusions

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The licensee implemented good corrective actions in response to a loss of

a

offsite emergency preparedness notification ability. The licensee failed to

.

evaluate in a timely manner whether they met Technical Specifications during

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reactor protection system response time testing.

In response to NRC concerns,

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the licensee initiated a quality assurance surveillance to determine the

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extent of the untimely initial evaluations of. Industry Technical Information

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Program items. .The implementation of 24-hour quality assurance auditor

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coverage for 3 days during the plant shutdown demonstrated a proactive quality

assurance organization. While going solid in the reactor coolant system, the

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licensee exceeded the pressurizer cooldown and heatup rates specified in

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Technical Specifications. To prevent recurrence of the temperature

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transients, the licensee will change operating procedures prior to drawing a

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bubble. During the reactor coolant system drain down, the licenset identified

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level discrepancies between the tygon hose and the midloop level

2

instrumentation. The licensee did not stop the drain down but continued using

the lowest reading instrument as the actual level. The licensee decision to

form an investigation team to evaluate gas releases inside containment was

a

commendable.

Personnel implemented an extensive and thoroug!, evaluation

identifying the root cause and recommending corrective actions.

Increasing

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the metal detector sensitivity demonstrated the licensee's proactive attitude

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in security. The licensee failed to maintain containment closure as required

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by Technical Specification 3.9.4 when operators performed a procedure in a

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mode other than intended that resulted in a noncited violation. The

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inspectors considered the licensee attitudes about personnel safety to be

proactive.

Housekeeping was found to be good with the licensee maintaining

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excellent control of plant scaffolding. During this period, licensee

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personnel failed to perform an as-found local leak rate test as specified in

Technical Specification 4.6.1.2 that resulted in a noncited violation.

The

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inspectors identified a violation with two examples of improperly coordinated

clearance orders.

The licensee had a second gas release in containment

because of improper turnover, and the licensee continued to drain down the

reactor coolant system in Mode E because clearance orders were not placed in

the correct order.

The licensee initiated an investigation team to identify

causal factors and a common root cause of several clearance order issues that

occurred over a 3-week period.

3 MAINTENANCE OBSERVATIONS (62703,62700)

The purpose of inspections in this area was to ascertain whether maintenance

activities on safety-related systems and components were conducted in

accordance with approved procedures and Technical Specifications. Methods

used in this inspection included direct observations of maintenance

activities, personnel interviews, and records review.

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3.1 Out-of-Calibration Measuring and Test Equipment

The licensee generated PIR 93-0151, dated March 6, 1993, that identified

93 out-of-calibration measuring and test equipment evaluations that were

significantly backlogged. The inspectors expressed concern because of the

quantity and age of the backlogged out-of-calibration evaluations, and the

inspectors questioned the operability of safety-related equipment required in

Mode 6.

The licensee determined that 62 out-of-calibration evaluations

affected safety-related components, with some dating back over 1 year.

The

immediate corrective actions included prioritizing the backlogged evaluations

and applying maintenance support resources during Refuel VI to decrease the

backlog.

Long-term corrective actions included determining acceptable backlog

levels, identifying the number of personnel needed to maintain these levels,

providing maintenance management with monthly backlog aging reports, and

generating guidance for performing evaluations.

The inspectors reviewed Procedure ADM 08-210, " Calibration and Control of

Maintenance and Modification Measure and Test Equipment (M&TE)," Revision 11.

This procedure specified the steps to be taken when personnel identified

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measuring and test equipment out of tolerance during recalibration. The

inspectors noted that the procedure did not specify a time limit for

evaluating the effects of the out-of-calibration measuring and test equipment.

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The inspectors determined that the licensee generated eight work requests from

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the evaluations of the safety-related uses of measuring and test equipment

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found out of calibration.

The licensee stated that they had reviewed all the

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nonsafety out-of-calibration applications and determined that none affected

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plant safety. During the discussion, the licensee stated that the long-term

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corrective actions to control the backlog will be determined and possibly in

place by the end of the current refueling outage.

The licensee completed

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their reviews of the nonsafety applications related to out-of-calibration

evaluations by March 27, 1993.

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The inspectors reviewed the licensee dispositions for the eight work requests

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generated from the out-of-calibration measuring and test equipment

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evaluations. The inspectors determined that the licensee appropriately

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dispositioned six of the work requests "use as is."

Work Request 01465-93

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concerned the potential overtorquing of the housing bolts for a reactor

coolant pump bearing oil filter. The system engineer determined that the

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cover bolts were torqued beyond their allowable stress values and would be

repl aced. The inspectors agreed with the engineering disposition. Work

Request 01467-93 concerned the potential overtorquing of the bonnet bolts for

the Containment Spray Pump A to containment spray nozzles check valve. The

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system engineer calculated that the bolting was potentially overstressed.

The

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inspectors concurred with the engineering disposition that required all of the

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bonnet bolts to be replaced during Refuel VI.

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The inspectors determined from discussions with quality assurance personnel

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that they identified that the out-of-calibration maintenance and test

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equipment backlog could affect equipment operability in November 1992.

In the

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executive summary of the audit report, quality assurance identified the

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timeliness of technical evaluations by maintenance support to be poor. The

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licensee stated that the ASME program quality assurance audit scheduled for

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the fall of 1993 will review the maintenance department measuring and test

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equipment backlogs.

Also, the licensee stated that they might perform a

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surveillance of measuring and test equipment backlogs this year. The

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inspectors considered the licensee's failure to act on the quality assurance

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department recommendations a weakness.

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3.2 Main Steam Safety Valve Testing

On March 3, 1993, the inspectors observed vendor personnel perform a trevitest

on Main Steam Safety Valve AB V057. The trevitest method uses hydraulics to

begin the valve lift that is completed by main steam pressure.

From the data

collected, the technicians calculated the steam pressure that would have

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lifted the safety valve. The inspectors observed a sixth and second

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consecutive successful test of Main Steam Safety Valve AB V057 with the

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acceptance criteria being two consecutive valve lifts within the specified

setpoints. Because this valve was a test failure (the first two valve lifts

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failed), the licensee increased their test sample by four predetermined

valves. During this outage, the licensee tested ten main steam safety valves

with only one test failure. The inspectors verified that the vendor personnel

performed the testing in accordance with their procedures, that the test

equipment was within calibration and properly connected, and that two

consecutive valve lifts occurred prior to declaring an acceptable test.

The engineering disposition for Work Request 01097-93 determined that, since

Main Steam Safety Valve AB V057 lifted at 1236 psi, which was well within the

designed rating for the main steam lines of 1303 psi, the valve would still

have performed its designed function of preventing the main steam line from

overpressurizing.

Further, the licensee determined that complete failure of

this valve would have limited the ability of the main steans safety valves to

release 80 percent instead of the required 81.3 percent.

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3.3 Conclusions

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The inspectors determined that the licensee had a significant backlog of

measuring and test equipment out-of-calibration data sheets awaiting

!

evaluation. After the inspectors expressed concern because of the potential

effects on equipment operability, the licensee increased their evaluation

efforts, determining that no out-of-calibration evaluations affected equipment

operability. The inspectors considered the failure of the maintenance

,

organization to respond to quality assurance audit observations 4 months

earlier to be a weakness. The licensee determined that one out of 10 main

steam safety valves failed to lift at the required setpoint during insitu

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trevitesting. The licensee determined that no consequences to the plant would

occur had the relief valve been required to actuate.

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4 SURVEILLANCE OBSERVATIONS (61726)

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The inspectors reviewed this area to ascertain whether surveillance of safety-

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related systems and components was conducted in accordance with Technical

Specifications and approved procedures.

4.1 Reactor Coolant Drain Tank Flow T-ansmitter Calibration

On March 9, 1993, the inspectors observed instrumentation and control

technicians perform a calibration of Flow Transmitter HB FT-1009, reactor

coolant drain tank pump discharge flow. The technician performed the

calibration in accordance with Procedure INC C-1003, " Calibration of

Transmitters," Revision 4.

For the field calibration, the technicians used a

,

data sheet that specified the required outputs for a given input, including

the instrument accuracy. The technicians properly connected and utilized

calibrated test equipment.

The technicians did not have the procedure present since the area was

contaminated.

From review of the procedure, the inspectors determined that

the calibration was performed in accordance with the procedure.

The procedure

specified shift supervisor approval prior to starting, recording of test

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instruments, instrument accuracy, and acceptance criteria.

The procedure

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specified that technicians may vary the zero, span, and linearity, as

j

necessary, to bring the instrument into calibration.

4.2 Pressure Transmitter Calibration

On Mard 12, 1993, the inspectors observed an instrumentation and control

technician perform Procedure STS 10-530B, " Channel Calibration RCS Wide Range

Pressure Transmitter," Revision 5.

The technicians maintained good

communications with the personnel at the pressure instrument.

Concurrent with

the surveillance, the inspectors determined that the operators were confused

because their temperature indications became erratic.

The procedure required the tecnnician to place various bistables in test,

removing the respective functions from the circuit. When the technicians

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placed Card 861, BS-1 bistable in test, the wide range temperature being

monitored in the control room became erratic.

The inspectors determined that

this response was normal because the computer point no longer received

temperature data from the field sensor. The inspectors interviewed personnel

and learned that, previously, the operators did not use the computer to

monitor the temperature.

Temperature indicators that did not receive computer

inputs remained constant. The installation of the new computer, 2 years

earlier, enabled the licensee to diversify their monitoring capability. The

licensee initiated PIR.TS 93-0192 to correct the problem and determined that

the temperature instrument input to the computer could remain in service

during future surveillances.

4.3 Conclusions

The inspectors determined that instrumentation and control technicians

maintained excellent coordination during surveillance tests. The technicians

performed testing in accordance with procedures and used calibrated test

equipment.

5 RELIABLE DECAY HEAT REMOVAL DURING OUTAGES (2515/113)

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The inspectors evaluated licensee activities for assuring that decay heat

removal was available as required during the outage.

5.1

Inspection

The inspectors reviewed the outage schedule and interviewed personnel,

determining that the licensee ensured that one or both of the residual heat

removal systems were available at all times. Also, the licensee ensured that

for the inservice train of residual heat removal both onsite and offsite power

sources were available.

The licensee conducted a shutdown risk assessment in accordance with

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Procedure ADM 01-249, " Outage Risk Management," Revision 0, and developed

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contingency plans for periods of high risk based upon the outage schedule.

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The licensee developed the outage schedule in a manner to assure maximum

availability of decay heat removal and electrical power.

During the risk

'

evaluation, the licensee ensured that one train of residual heat removal was

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available whenever fuel was in the vessel and that two offsite and one onsite

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power source was available. Also, the licensee established a contingency plan

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to place flagmen in the switchyard during switchyard maintenance.

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The licensee does not use natural circulation as a normal, planned method to

assure core cooling.

Procedure OFN EJ-015, " Loss of RHR During Decreased RCS

Inventory or Refueling," Revision 0, and Procedure OFN BB-031, " Shutdown

Emergency," Revision 0, specify conditions required to be monitored to assure

natural circulation is taking place, if required.

The inspectors verified

that two offsite power sources and an emergency diesel generator were

available at all times when residual heat removal was required. When the

licensee performed battery testing and maintenance, the licensee powered the

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affected DC bus from a backup battery charger.

The licensee trained operators

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on Procedure EMG E-0, " Reactor Trip or Safety Injection," Revision 3.

This

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procedure specified the appropriate sequence for adding safety-related

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equipment whenever the equipment fails to load automatically.

The inspectors verified that the licensee considers the emergency diesel

generators to be inoperable when the field flashing source is removed from

service. The licensee has proceduralized their nonstandard electrical lineups

for each type of bus (i.e., 4160 kV, 480 V, etc.).

The procedures specify

that the maximum load to be carried during the lineup shall not exceed the

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maximum load of either bus.

The inspectors reviewed the safety evaluations

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for a temporary modification during Refuel IV that was proceduralized for this

outage. The inspectors determined that the evaluation was properly conducted.

5.2 Conclusions

The inspectors determined that the licensee implemented conservative actions

during Refuel VI to assure they maintained reliable decay haat removal.

The

licensee assessed shutdown risk and developed contingency plans for periods of

high risk. Also, the licensee minimized the unavailability of electrical

power.

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6 REFUELING ACTIVITIES (60710,86700)

The inspectors reviewed licensee activities during the refueling outage to

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verify that their performance met regulatory requirements. The inspectors

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reviewed numerous documents during review of this area as listed in

Attachment 2.

6.1 Refueling Activities

The inspectors determined that the licensee established surveillance

requirements for verifying:

boron concentration, refueling crane interlocks,

operability of ventilation and filters, communications, fuel pool levels,

injection flow paths, and containment integrity. The inspectors verified that

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the required Technical Specifications surveillances were completed within the

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appropriate time frames prior to CORE ALTERATIONS. The inspectors verified

that the licensee performed the required daily and weekly Technical

Specifications surveillances.

The inspectors verified that the licensee maintained proper staffing in the

control room and on the refueling floor.

Also, the inspectors verified that

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qualified contractor personnel performed the fuel movement and vessel

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di sassembly. The inspectors determined that the contractor's training program

provided good guidance and that the licensee verified the adequacy of the

training provided. The inspectors determined that the licensee established

and enforced good housekeeping and loose object control in the refueling and

spent fuel pool areas.

The data below indicates the licensee's readiness to implement Refuel VI work

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activities at the beginning of the outage and at the end of the inspection

period. The information in the table is listed in percent.

3/4/93

3/27/93

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Plant Modification Requests:

Complete

--

62

Ready to Work

74

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Package Preparation

12

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Hold Parts

9

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Other

5

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MOV Plant Modification Requests:

Ready to Work

64

100

Package Preparation

8

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Hold Parts

28

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Work Requests:

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Complete

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Ready to Work

73

61

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Package Preparation

17.5

19

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Hold Parts

7.1

3

.

Other

2.4

2

The inspectors determined that the licensee made significant progress to get

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ready for Refuel VI from February 13 to March 4,1993 (refer to NRC Inspection

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Report 482/93-01).

From discussions with personnel, the inspectors determined

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that packages not yet ready to work were for upcoming outage windows.

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6.2 Spent Fuel Pool Activities

The inspectors reviewed licensee activities related to a potentially damaged

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rod control cluster assembly. While inserting Rod Control Cluster

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Assembly RSIO into the spent fuel pool, the assembly stopped prior to entering

the storage rack. The licensee attempted a second insertion without . success.

The licensee determined that a hole in the insert plate over the storage rack

was not drilled. The licensee moved the rod control cluster assembly into a

different storage location and will remove the defective plate following the

outage. The licensee visually inspected the rod control cluster assembly to

ensure that welded connections were intact, the condition of the end plug and

the rod, and overall visual appearance of the rod control cluster assembly.

The licensee determined the rod control cluster assembly could be used as is.

The inspectors monitored licensee activities related to fuel movement.

During

the fuel shuffle of the burnable poison rod assemblies, the inspectors noted

that mechanical stops prevented the overhead crane from passing over fuel

storage positions. The inspectors determined that the licensee maintained

spent fuel pool level above the minimum requirement, as noted by visual

inspection of the spent fuel pool level indication. The licensee maintained

spent fuel pool temperature at 100oF. The inspectors considered overall

housekeeping in the area to be good with no items that would interfere with

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the proper operation of the fuel handling machine nor that could fall into the

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spent fuel pool.

Licensee personnel operating the fuel handling equipment

were knowledgeable of their responsibilities.

The inspectors verified that -

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the procedures used to perform the burnable poison rod fuel assembly shuffle

were properly reviewed and approved.

In addition, the inspectors verified

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that personnel maintained an accurate record of the shuffle.

6.3 Reactor Coolant System Vacuum Venting

The inspectors reviewed the licensee activities performed to prepare for the

vacuum venting of the reactor coolant system since this will be the licensee's

first attempt using this method. The licensee established a procedure that

uses an eductor to pull a vacuum in the reactor coolant system. The

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eductor:

(1) vents the reactor coolant system in 2 to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> instead of the

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6 to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> needed without a vacuum, (2) extends the life of reactor coolant

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pump motors and seals by decreasing the number of pump starts needed to remove

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air from steam generator tubes, and (3) decreases the potential for

transgranular stress corrosion cracking in spare reactor vessel head

penetrations. The licensee functionally tested the vacuum vent system on

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February 26, 1993.

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The licensee determined the required reactor coolant system temperature and

water level, components required to be isolated, and components that should

remain in service. After the vacuum pressure remains constant for

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150 minutes, the operators will increase reactor coolant system water level at

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60-80 gpm.

Chemistry personnel will sample the reactor coolant for dissolved

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oxygen prior to vacuum venting and prior to the primary becoming solid to

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evaluate the ability of the system to remove dissolved oxygen.

Previously, the procedure for venting of the reactor coolant system required

filling and pressurizing the reactor coolant system to approximately 400 psi,

bumping a reactor coolant pump to remove air from the associated steam

generator tubes, reducing reactor coolant system pressure to 50 psi, and

venting the reactor coolant system. This process of pressurizing, reactor

coolant pump bumping, depressurizing and venting was repeated several times

with the remaining reactor coolant pumps. The vacuum vent system will remove

air and noncondensibles from the vessel, steam generator tubes, and the

pressurizer within 2 to 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> with reduced reactor coolant pump starts,

which will minimize equipment maintenance costs.

In February 1992 the licensee repaired spare Reactor Vessel Head

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Penetrations 24 and 25 because of leaking canopy seal welds. During this

outage, the licensee determined that spare Reactor Vessel Head Penetration 29

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will require repair because of canopy seal weld cracking. The licensee

determined the postulated cause to be transgranular stress corrosion cracking

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at the canopy seal weld. Trapped oxygen could not be vented through the head

vent because the air pocket is higher than the head vent. After plant heatup,

the reactor coolant system pressure and temperature adds the other two

components required to initiate stress corrosion cracking.

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The inspectors reviewed the 10 CFR Section 50.59 evaluation and Configuration

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Change Package CC00246 and determined that system engineering had developed a

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detailed method of vacuum venting the reactor coolant system. The evaluation

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reviewed the effects on all primary system components and specified in detail

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the method to be followed.

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6.4 Failed Fuel Rod

On March 16, 1993, as personnel lifted fuel Assembly H10 in Location H-7

during defueling, the spotter noticed that a fuel rod piece was bridging the

fuel assemblies between Locations H-6 and H-7.

The refueling personnel

stopped the defueling with Assembly H10 in location H-7 lifted approximately

71/2 inches vertical and 3 inches away from Assembly F67 in Location H-6.

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The licensee used an underwater camera to determine that the fuel rod piece

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came from Assembly F67.

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The licensee developed a plan to use remote, pneumatic operated vice grips to

latch onto the fuel rod piece. The licensee placed a 2 by 5 foot catch pan

under the raised assembly to catch the fuel rod piece if it fell. When

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personnel attempted to capture the fuel rod piece in the vise _ grips, the fuel

rod piece fell below the core plate. The licensee moved Assembly F67 into the

spent fuel pool. After defueling the reactor, the licensee implemented a

foreign object search and retrieval effort and recovered the fuel rod piece.

After recovering the fuel rod piece, personnel used a vacuum to clean and

remove all small particles possible. The licensee determined the fuel rod

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piece was 12 inches long.

The licensee reviewed films of the failed fuel rod

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sections and inspected the vessel interior.

Since the licensee identified no

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loose pellets during the foreign object search and retrieval effort, the

licensee had some confidence that all pellets were accounted for.

The

licensee reported this issue in accordance with 10 CFR Section 50.72 and will

issue LER 482/93-004.

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The licensee identified three fuel assemblies. Assemblies F43, F54, and F67,

that had fuel clad failures in 14 fuel rods. The licensee discharged all the

fuel assemblies. During the previous outage, the licensee had identified a

similar fuel rod failure.

All the F-type assemblies manufactured on the same

fixture were discharged (refer to LER 91-019 and NRC Inspection

Report 50-482/91-31).

Preliminary evaluations indicated that the f ailure

mechanisms could be similar. The NRC and licensee personnel will meet in the

near future to discuss these additional failures.

6.5 Conclusions

The inspectors determined that the licensee programs for conduct of Technical

Specifications surveillances assured that the applicable Technical

Specifications for refueling were met. The licensee had excellent procedures

for controlling the refueling. The licensee implemented the outage in a

controlled manner that ensured maintenance and modifications could be

implemented. The licensee identified that they had a failed fuel rod, but a

root cause had not yet been determined.

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7 FOLLOWUP ON CORRECTIVE ACTION FOR VIOLATIONS (92702)

7.1

(Closed) Violation (482/9126-02):

Containment Purge Isolation and

Control Room Ventilation Caused by High Gaseous Activit_y Durinq

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Containment Purge

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On October 2, 1991, after initiation of a containment purge, the containment

purge and control room ventilation systems isolated because of high gaseous

activity in the containment purge system.

The licensee determined that

operators failed to use Procedure 0FN 00-019 " Loss of Instrument Air,"

Revision 8, earlier that day when restoring from a loss of instrument air to

the containment building. After initiating the containment purge, the

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operator noticed that Damper GT HZ-8, containment purge exhaust, was closed.

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When the operator opened the damper, a containment purge isolation signal was

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received. The operators restored from the containment purge and control room

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ventilation system isolations. The licensee sampled the containment air,

determining that no airborne activity existed inside the containment building.

Because of a previous, similar occurrence, the licensee evaluated alternate

methods for venting the reactor coolant system.

The inspectors verified that the licensee established an alternate method for

venting the reactor coolant system in Procedure GEN 00-007. Additionally, the

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inspectors determined that the licensee was completing a review of all

components inside containment serviced by instrument air. The licensee

intends to issue a controlled document that lists the instrument air loads

located in each building to aid operators during restoration of components

serviced by instrument air.

7.2

(Closed) Violation (482/91202-01):

Inadeouate Procedure

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NRC issued this violation because Procedure ALR 00-128C, "TDAFP BRG Oil Temp

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Hi," Revision 3, incorrectly referenced instrumentation to be used in

determining intermediate and long-term operator actions when operators

responded to high turbine-driven auxiliary feedwater pump lube oil

temperatures.

The procedure referenced bearing temperatures and not the lube

oil temperature.

Also, the procedure did not describe that lube oil cooler

outlet temperatures could only be monitored locally.

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The inspectors verified that the licensee modified Procedure ALR 00-128C.

The

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licensee implemented a program to improve their alarm response procedures as

required by Management Action Plan Issue V.

The licensee transferred the

procedure upgrades to Performance Enhancement Program Action Plan 3.3.2.

The

inspectors determined that the alarm response procedure upgrades should be

completed by September 30, 1993. The licensee reviewed the alarm response

procedures to ensure that existing guidance was usable and technically

correct. The procedure upgrade group corrected identified deficiencies such

as improper numbering, alarm windows without response procedures, and alarm

procedures written for nonexistent windows. Approximately 20 minor

deficiencies remain to be corrected.

The licensee should correct the

deficiencies by April 30, 1993.

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The inspectors determined that out of 1400 alarm response procedures,

personnel had drafted 683 procedures and had placed 100 procedures in the

review / approval process. The inspectors determined that the licensee

implemented a well-controlled, detailed process for upgrading the alarm

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response procedures.

The inspectors walked through the development of two

alarm response procedures and determined that the licensee used good

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verification and validation techniques.

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7.3 (Closed) Violation 482/9208-01:

Inadvertent Release of Radioactive

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Gaseous Waste Due to inadeauate Procedures

On April 23, 1992, as a radwaste operator placed Waste Gas Decay Tank 4 in

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service, an inadvertent release of radioactive gas occurred because of

inadequate procedures.

The licensee determined that Procedure SYS HA-200,

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" Waste Gas System Startup and Shutdown," required the inlet pressure control

valve to be in manual, which immediately pressurized the hydrogen recombiner.

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Prior to overhauling the compressors, the licensee operated the system

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manually to compensate for the poor discharge pressure. After installing new

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compressor internals, the licensee failed to change the system operation to

automatic. Consequently, Procedure SYS HA-200 did not provide sufficient

steps to prevent the rapid pressure rise.

Additionally, with the recombiner

sample isolation valves open, as specified by Procedure SYS HA-205, " Gaseous

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Radwaste System Gas Analyzer Racks (HA-161/HA-162) and Catalytic Hydrogen

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Recombiners (SHA01A/SHA01B) Operations," a direct path existed for release of

waste gas into the radwaste building ventilation.

The licensee implemented actions to preclude future violations. The licensee

revised Procedure SYS HA-200 to ensure that the waste gas system pressure

control valve is in automatic to prevent rapid pressurization. Additionally,

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the licensee revised Procedure SYS HA-205 to ensure the analyzer rack

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instrument sample isolation valves remain closed until the system is

recirculating and all parameters are stable. The inspectors found the

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corrective actions to be acceptable.

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7.4

(Closed) Violation 482/9208-02:

Performance of Maintenance Activities on

Boric Acid Filter Drain Valve BG V322 Without an Appropriate Work Reauest

On May 21, 1992, the licensee identified a decrease in boric acid tank levels

because Valve BG V322, boric acid filter drain, was not fully closed. The

licensee determined that a bolt on the valve-to-reach rod attachment contacted

a support, preventing full closure of Valve BG V322.

Subsequently, mechanical

maintenance personnel adjusted the bolt on the reach rod attachment without an

appropriate work request.

The licensee attributed the root cause of this event to be a personnel error

for failing to follow Procedure ADM 01-057, " Work Request," which required

issuance of a work request to document and control work performed on plant

systems.

In addition, the licensee determined that the postmaintenance

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testing specified on Work Request 02652-92 was not effective.

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The licensee completed a review session on the use of Procedure ADM 01-057 and

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the work request process with the involved mechanical maintenance personnel.

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Additionally, the postmaintenance testing requirements as specified in

Procedure ADM 01-057 were revised. The postmaintenance test block on the work

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request form was changed to require more specific information on the test,

including test description, responsible group, acceptance criteria, and

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results. Maintenance management and supervision plan to continue monitoring

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the effectiveness of postmaintenance testing.

7.5 (Closed) Violation 482/9212-02:

Failure to Meet Technical Specifications

Surveillance Schedule Reauirements for Emergency Diesel Generator B and

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Containment Airlocks

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On June 8,1992, while performing the Technical Specifications operability

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test for Emergency Diesel Generator B, operators stopped the emergency diesel

generator because of high oil and bearing temperatures. This was the fifth

valid failure experienced by this emergency diesel generator within the last

100 tests. On June 26, 1992, the licensee determined that they failed to

increase the surveillance testing to once per 7 days as required by Technical

Specifications. On July 7, 1992, the licensee noted that

Procedure STS PE-14A, " Containment Air Locks Test (Personnel Hatch)," and

Procedure STS PE-14B, " Containment Air Locks Test (Emergency Hatch)," were

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performed past their assigned due date.

The licensee determined that they failed to meet Technical Specifications

surveillance schedule requirements for Emergency Diesel Generator B because of

cognitive personnel error and procedural weakness. A licensee engineer failed

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to formally review the number of failures in the last 20 and 100 valid tests

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immediately following the valid failure on June 8,1992. Also,

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Procedure ADM 01-0244, "EDG Reliability Monitoring Program," required the

number of failures in the last 20 valid tests to be listed on a form for all

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valid failures.

Procedure ADM 01-244 did not list the failures in the last

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100 valid tests since it was not developed to verify compliance with Technical

Specifications

The licensee determined that a change to the computerized scheduling program

resulted in a failure to meet Technical Specifications surveillance schedule

requirements for the containment airlock tests. The licensee determined that,

upon altering the surveillance scheduler program to eliminate the

3.25 surveillance test limit that was removed from Technical Specifications,

they added a 25 percent extension to the containment airlock test due dates.

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Consequently, the scheduler automatically calculated the next late date

inappropriately since the 25 percent extension is not applicable to

Procedures STS PE-014A and -B.

The licensee revised Procedure ADM 01-244 on August 19, 1992, to monitor

Technical Specifications Table 4.8-1 failures and provided requirements to

complete the form within 5 days. This should ensure the 7-day testing

frequency is met if accelerated testing is required. Also, the licensee

modified the form to document all valid tests to maintain a better awareness

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of the failures. A computer program was written to be used on the

computerized scheduling database for modifying production data.

In addition,

a quarterly comparison will be made of the information currently in the

surveillance database compared to what was in the database the previous

quarter.

8 FOLLOWUP (92701)

8.1

Inspection Followup Items

8.1.1

(Closed) Inspection Followup Item 482/9202-01:

Permanent Cavity

Seal Ring

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During a forced outage in March 1992, the licensee determined that borated

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polyethylene from within the permanent cavity seal was deposited on the

reactor coolant system piping.

Investigation into why the barated

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polyethylene melted determined that the heat source was inleakage of air at

the corners of the vertical and horizontal insulation.

As corrective actions,

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the licensee filled the corner gap with additional insulation, placed

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insulation between the reactor vessel and the permanent cavity seal ring,

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redistributed the air flow to enhance cooling, and placed stainless steel

sheets over reactor coolant system piping to preclude the borated polyethylene

from dropping on the piping.

The inspectors reviewed the results of the inspections performed during

Refuel VI and interviewed licensee personnel, determining that the borated

polyethylene did not flow from the permanent cavity seal. Throughout the

operating cycle, the inspectors verified that health physics radiation surveys

indicated no increasing trend of radiation levels above the permanent cavity

seal that would indicate the borated polyethylene was melting.

The radiation

surveys indicated that radiation levels were reduced more by the permanent

cavity seal than they had been by the removable cavity seal.

The licensee implemented Temporary Modification 93-007-BB during Refuel VI to

install dosimeters that will monitor the relative radiation levels above and

below the permanent cavity seal. The licensee installed four additional

dosimeters at various locations to determine radiation levels over one

operating cycle. The licensee expects the monitors to verify that the

radiation levels have decreased inside containment. This should increase the

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lifetime of environmentally qualified equipment.

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8.1.2

(Closed) Inspection Followup Item 482/9301-02:

Differential Relay

Testing

The licensee had identified jumpers installed from Phase C to ground on a

terminal board for the Emergency Diesel Generator B differential current

relay. The inspectors initiated this open item to follow the licensee's

activities to inspect other safety-related breaker cubicles for installed

jumpers. During the Refuel VI Train B 4160 kV bus outage, the licensee

inspected each of the 4160 kV breaker cubicles. Additionally, the licensee

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initiated Work Request 01684-93 to inspect terminal boards in the 4160 kV

Train A breaker cubicles.

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8.2 10 CFR 21 Report

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(Closed) 10 CFR 21 Report:

Limitorque Part 21 Notification Dated December 11,

1990:

SMB-00 Torque Switch Roll Pin f ailures During Declutching Operations

The inspectors reviewed this issue in NRC Inspection Report 50-482/92-31,

Section 3.3.

The licensee will replace the torque switches in the affected

valves by the end of Refuel VI.

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9 IN-0FFICE REVIEW OF LICENSEE EVENT REPORTS (90712)

The inspectors reviewed the following LERs to determine that the corrective

actions discussed in the report were appropriate and completed.

9.1

(Closed) LER 482/91-013:

Inadequate Electrical Separation

9.2 (Closed) LER 482/91-018:

Containment Purge Isolation and Control Room

Ventilation Caused by High Gaseous Activity During Containment Purge

9.3

(Closed) LER 482/92-001:

Failure to follow Procedures Could Have Caused

Both Intermediate Range Channels to be Inoperable During Physics Testinq

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9.4

(Closed) LER 482/92-004:

Feedwater Isolation Signal Actuation Resulting

From a Lead to a Logic Card in the Solid State Protection System

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inadvertently Remaking Contact

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9.5 (Closed) LER 482/92-011:

Personnel Error in not Increasing Emergency

Diesel Generator Testing Frequency Following a Valid Failure Results in a

Technical Specifications Violation

9.6 (Closed) LER 482/92-012:

Error in Surveillance Database Results in a

Failure to Meet Technical Specifications Surveillance Requirements

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ATTACHMENT 1

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1 PERSONS CONTACTED

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P. D. Adams, Supervisor, Reactor Engineering

R. S. Benedict, Manager, Quality Control

V. J. Canales, Supervisor, Maintenance Support

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T. F. Deddens, Manager, Outage

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M. E. Dingler, Manager, Nuclear Plant Engineering Systems, Support

C. W. Fowler, Manager, Maintenance and Modifications

R. B. Flannigan, Manager, Nuclear Safety Engineering

D. E. Gerrelts, Manager, Instrumentation and Control

N. W. Hoadley, Manager, Equipment Engineering

J. W. Johnson, Manager, Security

R. L. Logsdon, Manager, Chemistry

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0. L. Maynard, Vice President, Plant Operations

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R. A. Meister, Senior Engineer Specialist, Licensing

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K. J. Moles, Manager, Regulatory Services

T. S. Morrill, Manager, Radiation and Protection

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C. E. Parry, Director, Performance Enhancement Program

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G. J. Pendergrass, Supervisor, Inservice Testing

L. D. Ratzliff, Supervisor, System Engineering

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F. T. Rhodes, Vice President, Engineering

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C. E. Rich, Jr., Supervisor, Electrical Maintenance

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T. L. Riley, Supervisor, Regulatory Compliance

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B. B. Smith, Manager, Modifications

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C. M. Sprout, Manager, System Engineering

J. D. Stamm, Manager, Plant Design Engineering

M. G. Williams, Manager, Plant Support

The above licensee personnel attended the exit meeting.

In addition to the

personnel listed above, the inspectors contacted other personnel during this

inspection period.

2 EXIT MEETING

An exit meeting was conducted on April 1, 1993. During this meeting, the

inspectors reviewed the scope and findings of the report. The licensee did

not identify as proprietary any information provided to, or reviewed by, the

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inspectors.

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ATTACHMENT 2

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Documents Reviewed

ADM 01-108, " Outage Planning and Implementation," Revision 8

ADM 01-248, " Conduct of Infrequently Performed Tests or Evaluations,"

Revision 0

ADM 01-249, " Outage Risk Management," Revision 0

FHP 02-001, " Refueling Procedure," Revision 12

FHP 02-004, " Refueling Cavity Exclusion Area," Revision 1

FHP 02-011, " Fuel Siiuffle and Position Verification," Revision 13

FHP 03-006, " Fuel Transfer System Operating Instructions," Revision 4

FHP 03-007, " Spent Fuel Pool Bridge Crane Operating Instructions and

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Daily Checks," Revision 15

CEN 00-007, "RCS Drain Down," Revision 17

MGE TP-004, " Temporary Power For NB02 Maintenance Bus Outage,"

Revision 0

ML TRN-001, " Fueling Operations Personnel Qualifications," Revision 4

OFN BB-031, " Shutdown Emergency," Revision 0

OFN EJ-015, " Loss of RHR During Decreased RCS Inventory or Refueling,"

Revision 0

OFN KE-018, " Fuel Handling Accident," Revision 0

Special Order 12, " Fuel Handling Equipment Qualifications," Revision 6

Standing Order 21, " Control of Switchyard Maintenance," Revision 7

STS BB-Oll, " Reactor Coolant System and Pressurizer Heatup/Cooldown

Surveillance," Revision 10

STS CR-002, " Shift Log for Modes 4, 5 and 6," Revision 16

STS PE-023, " Fuel Building Negative Pressure Test," Revision 4.

(Train A performed in February 1993 on an 18-month frequency as

specified by Technical Specification 4.9.13.g.2.)

SYS BB-212, " Draining the RCS to Midloop Level and Below Fuel

Offloaded," Revision 4

Technical Specification Interpretation 010-89, " Tech Specs Application

with No Fuel in the Vessel"

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