LER-1982-067, Forwards LER 82-067/03L-0.Detailed Event Analysis Encl |
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DUKE POWER GOMPAN ~dNRC PEG!TN :
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s o.nox sanno CitAMI,oTTI:. N.C. 28242 II AI. II. TUCKEH TER_EPHONE 32 sea 17 P l: $ 3 (70-1) 373-4 Nil vua.mensorst September 10, 1982 Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 Re: McGuire Nuclear Station Unit 1 Docket No. 50-369
Dear Mr. O'Reilly:
Please find attached Reportable Occurrence Report R0-369/82-67. This report concerns T.S.3.3.2, "The Engineered Safety Feature Actuation System (ESFAS) instrumentation channels and interlocks shown in Table 3.3-3 shall be operable with their trip setpoints set consistent with the values shown in the trip setpoint column of Table 3.3-4...".
This incident was considered to be of no significance with respect to the health and safety of the public.
Very truly yours,
.g':d flal B. Tucker PBN/jfw Attachment cc: Director Records Center Office of Management and Program Analysis Institute of Nuclear Power Operations U. S. Nuclear Regulatory Commission 1820 Water Place Washington, D. C.
20555 Atlanta, Georgia 30339 Mr. P. R. Bemis Senior Resident Inspector McGuire Nuclear Station
- ed 8209210;y/y fp
t DUKE POWER COMPANY McGUIRE NUCLEAR STATION REPORTABLE OCCURRENCE REPORT NO. 82-67 REPORT DATE: September 10, 1982 FACILITY: McGuire Unit 1, Cornelius, NC IDENTIFICATION: Failure of Train A Auxiliary Feedwater Pump Turbine (AFPT)
Low Suction Pressure Switches
DESCRIPTION
On August 13, 1982, with Unit 1 at 50% power, two AFPT low suction pressure switches were declared inoperable pursuant to Technical Specification 3.3.2.
The switches failed to perform properly during performance of the " Auxiliary Feedwater Low Suction Functional Test".
This incident is attributed to Component Failure / Malfunction. The pressure switches were recalibrated and the functional test was successfully completed.
On August 26, 1982, while reviewing past work requests on the pressure switches as part of the incident investigation, a discrepancy between setpoints was noted.
The presence of a water leg not included in the August 13, 1982 calibration was verified. Technicians recalibrated the pressure switches 'r include the water leg and verified operability. Due to the incorrect calibration of August 13, 1982, the pressure switches were inoperable for an additional 13 days. This event was a result of Personnel Error.
EVALUATION; The purpose of the pressure switches is to provide 'A' train Nuclear Service Water to the Auxiliary Feedwater Pump Turbine on low suction pressure (loss i
of water supply). When the technicians isolated and vented the switches during the performance of the functional test on August 13, 1982, the decrease to zero psig pressure failed to open a valve (via switch actuation) as required. The technicians manually operated the pressure switches and the valve opened, indicating that one or both pressure switches had failed to actuate during the test.
No mechanical problems were observed on either switch, but the switches were out of calibration.
Although this may have resulted from instrument drift, the setpoints appeared to have been misadjusted. A technician obtained the setpoints from the Mechanical Instrument List and the pressure switches were calibrated to 2 psig decreasing.
A replacement was obtained for one of the switches and it was bench calibrated to expedite return to service (the removed pressu-switch was later tested, set to 2 psig decreasing, and verified functional).
On August 26, 1982, a review of previous calibrations revealed a setpoint of 5 psig, decreasing, for the switches. This setpoint included 2 psig for the process plus 3 psig to compensate for an 80 inch water column between the suction piping center-line (instrument tap) and the lower elevation of the pressure switches. This water leg could account for both of the pressure switches being found apparently misad-justed on August 13, 1982. The effective setpoint (relative to the process) of the August 13 calibration was 2 psig minus the 3 psig water leg, or -1 psig. This violated the allowable value of > 1 psig (Technical Specification Table 3.3-4, item 7.f.) and would have inhibited swap over to 'A' train Nuclear Service Water. The pressure switches were recalibrated to 5 psig decreasing.
Report No. 82-67 Page 2 It is probable that the failure of August 13, 1982 was limited to only one pressure switch since both switches must actuate to open the valve. The pressure switches are United Electric Type J302 (Model 552 -refers to range). Type J302 pressure switches have a good service history.
The inadvertant omission of water leg compensation was a personnel error directly attributable to a lack of training in the use of setpoints obtained from the Mechanical Instrument List. Unbalanced water legs must be identified, measured, and, if necessary, added to the process setpoint (or range) obtained from the list.
Although training at the Technical Training Center includes the effect of water legs on instrumentation, newer technicians are not fully aware that water legs are normally not included in the Mechanical Instrument List.
Many procedures are generic and do not include setpoints (this is the case with the
" Calibration Procedure for Electric Pressure Switch Type J302), thereby requiring proper use of the Mechanical Instrument List.
SAFETY ANALYSIS
The purpose of the Auxiliary Feedwater System is to provide a backup to the Main Feedwater system to insure adequate dissipation of energy from the Reactor Coolant System when the main heat sinks (turbine generator or steam dump and main feedwater) are unavailable. At no time during the event did a loss of the assured supply (nuclear service water) to the Auxiliary Feedwater Pump Turbine occur. Although the pressure switch failures prevented 'A' train Nuclear Service Water from being available in the event of an emergency, 'B' train Nuclear Service Water was available.
Additionally, both 'A' and 'B' trains of Nuclear Service Water were available to the Motor Driven Auxiliary Feedwater Pumps.
Therefore, the health and safety of the public were unaffected by this incident.
CORRECTIVE ACTION
The action taken to correct the switch malfunction was to calibrate the two pressure switches. Proper operation of the switches was verified August 26, 1982 by successfully completing the calibration at the appropriate set-point.
Since United Electric Type J302 pressure switches have given reliable service and it is probable that only one pressure switch actually malfunctioned, this action is sufficient.
To prevent future instances of incorrect calibration management will notify all technicians, ir, crew meetings, of the necessity to identify and, if necessary, add water legs to satpoints and ranges obtained from the Mechanical Instrument List.
This information vill also be incorporated into the Orientation training program conducted for new technicians.
Additionally, management will review the efficiency of the present method of obtaining setpoints and ranges that are corrected to water legs.
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| 05000369/LER-1982-001, Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-001-01, /01T-0:on 820106,routine Review of Source Document Changes Revealed Class H Piping in Fire Protection Sys in Diesel Generator Room 1A Routed Above One Nuclear safety-related Essential Cable & Instrument Panel | /01T-0:on 820106,routine Review of Source Document Changes Revealed Class H Piping in Fire Protection Sys in Diesel Generator Room 1A Routed Above One Nuclear safety-related Essential Cable & Instrument Panel | | | 05000369/LER-1982-002-03, /03L-0:on 820101,temp Sensing Valve Position Indication Disagreed W/Alternate Position Indication & Declared Inoperable.Caused by Environ Conditions | /03L-0:on 820101,temp Sensing Valve Position Indication Disagreed W/Alternate Position Indication & Declared Inoperable.Caused by Environ Conditions | | | 05000369/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-003-03, /03L-0:on 820102,average Temp in Upper Containment Was Reduced Below Temp Requirement.Caused by Cold Weather Cooling Bldg.Temp Increased Using Dihydrogen Recombiner Heaters | /03L-0:on 820102,average Temp in Upper Containment Was Reduced Below Temp Requirement.Caused by Cold Weather Cooling Bldg.Temp Increased Using Dihydrogen Recombiner Heaters | | | 05000369/LER-1982-004-03, /03L-0:on 820103,power Operated Relief Valve NC-32 Found Leaking.Cause Unknown.Insp of Valve to Determine Exact Nature of Component Failure Not Yet Possible.Block Valve Closed & de-energized to Prevent Inadvertent Opening | /03L-0:on 820103,power Operated Relief Valve NC-32 Found Leaking.Cause Unknown.Insp of Valve to Determine Exact Nature of Component Failure Not Yet 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| | 05000369/LER-1982-008-03, /03L-0:on 820115,exam of Programs on Operator Computer Revealed Equipment Run Time on Fuel Pool Ventilation Sys Exceeded Tech Specs W/O Sample Being Taken from Charcoal Absorber.Caused by Lack of Procedure | /03L-0:on 820115,exam of Programs on Operator Computer Revealed Equipment Run Time on Fuel Pool Ventilation Sys Exceeded Tech Specs W/O Sample Being Taken from Charcoal Absorber.Caused by Lack of Procedure | | | 05000369/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000369/LER-1982-009-03, /03L-0:on 820116,during Review of Surveillance Documentation,Periodic Testing of Diesel Generator Battery Trains Edga & Edgb Not Performed within Test Frequency Required by Tech Specs.Caused by Personnel Error | /03L-0:on 820116,during Review of Surveillance Documentation,Periodic Testing of Diesel Generator Battery Trains Edga & Edgb Not Performed within Test Frequency Required by Tech Specs.Caused by Personnel Error | | | 05000369/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-010-03, /03L-0:on 820120,while in Mode 1,all Digital Rod Position Indications for Control Rod K-8 Lost.Caused by Cabling to Detectors Susceptible to Conductor Damage Due to Own Weight.Bulkhead Connector Cable Replaced | /03L-0:on 820120,while in Mode 1,all Digital Rod Position Indications for Control Rod K-8 Lost.Caused by Cabling to Detectors Susceptible to Conductor Damage Due to Own Weight.Bulkhead Connector Cable Replaced | | | 05000369/LER-1982-011-03, /03L-0:on 820120,maint Personnel Working on Spent Fuel Pool Cooling Sys (Kf) Heat Exchanger 1A Discharge Throttle Bypass Relief Valve Discovered That Kf Mechanical Snubber Was Removed Rendering Snubber Inoperable | /03L-0:on 820120,maint Personnel Working on Spent Fuel Pool Cooling Sys (Kf) Heat Exchanger 1A Discharge Throttle Bypass Relief Valve Discovered That Kf Mechanical 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820212,control Room Alarms Indicated Closing of 4 Accumulator Discharge Isolation Valves, Rendering Upper Head Injection Portion of ECCS Inoperable. 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