LER-1982-024, Forwards LER 82-024/03L-0.Detailed Event Analysis Encl |
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TELEPm0NE: Aata 704 Strase Pacouctiow 373-4083 Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 i
Re: McGuire Nuclear Station Unit 1 Docket No. 50-369 i
Dear Mr. O'Reilly:
Please find attached Reportable Occurrence Report R0-369/82-24. This report concerns T.S.3.4.1.4, "Two residual heat removal (RHR) loops shall be operable i
and at least one RHR loop shall be in operation". This incident was considered to be of no significance with respect to the health and safety of the public.
Although my letter of April 8, 1982 stated that this report would be submitted by April 19, in the interest of completeness it is being submitted 3 days later, We regret any inconvenience this delay may have caused.
5 Ve y truly yours
- - u.-w, W 111am O. Parker, Jr PBN/jfw Attachment.
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Director Records Center Office of Management and Program Analysis Institute of Nuclear Power Operations U. S. Nuclear. Regulatory Commission 1820 Water Place Washington, D. C.
20555 Atlanta, Georgia 30339 l
Mr.-.P. R. Bemis l
Senior Resident Inspector-NRC McGuire Nuclear Station i
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DUKE POWER COMPANY McGUIRE NUCLEAR STATION REPORTABLE OCCURRENCE REPORT NO. 82-24 REPORT DATE: April 22, 1982 FACILITY: McGuire Unit 1, Cornelius, NC IDENTIFICATION: Partial Air-Binding of Residual Heat Removal (ND) Pump 1A While the Reactor Coolant (NC) System was being Drained for Maintenance DISCUSSION: While draining Unit 1 NC System on March 2, 1982 for steam generator inspection, investigation of an ND pump low discharge pressure alarm resulted in ND pump 1A being stopped due to signs of cavitation. During the fifty minutes it was secured, no means existed for removing core residual heat because the redundant pump, IB, was out of service for maintenance. Upon restart, normal ND flow could not be maintained without signs of cavitation reappearing. The control board level gauge indicated that NC system water level was 250-270 inches above the bottom of the NC pump suction loops (175 inches is the minimum for ND operation). However, a later check of tygon tubing connected to a loop drain and vented to a RTD manifold vent indicated that level was 4 to 6 inches below that specified for ND operation.
Draining (to hot leg centerline - 175 inches on the level gauge) was being accomplished, per procedure, with a nitrogen (N ) overpressure on the Pressurizer Relief Tank (PRT) 2 and Power Operated Relief Valve (PORV) open to admit N2 to the pressurizer (PZR).
This incident resulted from inaccurate indication by the transmitter for the level sauge, due to a misapplication of the level transmitter.
EVALUATION: To insure pump 1A could be restarted safely after showing signs of cavitation, it was vented, and the fueling water storage tank supply to ND valve (a source of make-up water) opened briefly. An attempt was made to verify level at or above the RTD manifold which would have insured proper level for pump opera-tion. Water was reported present when the RTD manifold vent was opened, and the level in a tygon tube vented to the atmosphere agreed with the level gauge. Although cause for the pump's behavior could not be determined, it was returned to service as soon as possible per Technical Specification 3.4.1.4.
Pump parameters soon began to oscillate, and flow was throttled to 1,500 gpm.
Later, flow was throttled to just above 500 gpm after parameters had begun to oscillate again. After flow was throttled to 500 gpm, level was observed (using tygon tubing vented to the RTD manifold vent) below that specified for ND operation.
The operator that checked level earlier had been misled by a small amount of water present in the vent piping. The low water level was allowing air into the ND suction, causing partial air-binding of the pump, with symptoms similar to cavitation. As level was later increased, ND flow was increased, without signs of air-binding, until level was 175 inches and flow approxi-mately 3,000 gpm.
The only instrument indicating water level while draining or filling the NC system is the control board level gauge. The transmitter for this gauge is referenced to atmosphere because its desigr. function is to indicate water level during refueling.
Pressures other than 0 psig are possible during draining and filling because the j
system is not directly vented to atmosphere. During draining, FC is vented to the L
l Report No. 82-24 Page 2 PRT where a N2 overpressure can exist per procedure, " Draining the Reactor Coolant System".
The PRT is monitored using a 0-100 psig pressure transmitter and the computer video display (low Pressures cannot be accurately read on this 0-100 psig control board gauge) to insure no pressure deviation occurs that would significantly affect indicated level. NC pressure can differ significantly from PRT pressure if the drain or fill rate is high because the N2 must pass through a small hole in the PORV discharge line inside the PRT. When ND flow was throttled to 500 gpm, PRT pressure indicated 0 psig with the drain secured. A pressure of 2.89 psig would cause a 170 inch level to indicate 250 inches on the level gauge.
Calibration of the pressure transmitter on March 3 revealed it was within tolerance.
SAFETY ANALYSIS
In the fifty minutes ND was off, incore thermocouples indicated core coolant temperature rose from approximately 105 F to 1300F. A conservative linear extrapolation shows that ND could be shutdown almost four hours before the onset of boiling. This boiling would not be detrimental provided make-up was available (one centrifugal charging pump was operable) and any vapor generated was not released to containment (vapor would be condensed in the PRT). Public health and safety were not affected by this incident.
CORRECTIVE ACTION
Immediate corrective action was to raise level to 175 inches and resume normal ND flow. After its N2 supply was secured, the PRT was vented to containment atmosphere to insure the control board level gauge would indicate level accurately. A work request initiated to calibrate PRT pressure indication was completed on March 3.
Statements will be incorporated into the procedure " Draining the Reactor Coolant System" warning that the 5-7 psig PRT overpressure can greatly affect the levels in-dicated on the control board gauge. A modification to have the reference leg of the level transmitter connected to the PORV discharge line is planned. This avoids problems associated with a pressurizer tap and is satisfactory since a PORV is required open during draining. The modification will also entail redundant level indication and an expanded scale (s) in the normal NC level range for UD operation.
A narrow range PRT nitrogen purge pressure indication is also planned.
A limit and precaution will be added to the Equipment and Removal and Restoration Procedure stating redundant components are not to be taken out of service prior to a major plant evaluation when possible, i
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| 05000369/LER-1982-001, Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-001-01, /01T-0:on 820106,routine Review of Source Document Changes Revealed Class H Piping in Fire Protection Sys in Diesel Generator Room 1A Routed Above One Nuclear safety-related Essential Cable & Instrument Panel | /01T-0:on 820106,routine Review of Source Document Changes Revealed Class H Piping in Fire Protection Sys in Diesel Generator Room 1A Routed Above One Nuclear safety-related Essential Cable & Instrument Panel | | | 05000369/LER-1982-002-03, /03L-0:on 820101,temp Sensing Valve Position Indication Disagreed W/Alternate Position Indication & Declared Inoperable.Caused by Environ Conditions | /03L-0:on 820101,temp Sensing Valve Position Indication Disagreed W/Alternate Position Indication & Declared Inoperable.Caused by Environ Conditions | | | 05000369/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-003-03, /03L-0:on 820102,average Temp in Upper Containment Was Reduced Below Temp Requirement.Caused by Cold Weather Cooling Bldg.Temp Increased Using Dihydrogen Recombiner Heaters | /03L-0:on 820102,average Temp in Upper Containment Was Reduced Below Temp Requirement.Caused by Cold Weather Cooling Bldg.Temp Increased Using Dihydrogen Recombiner Heaters | | | 05000369/LER-1982-004-03, /03L-0:on 820103,power Operated Relief Valve NC-32 Found Leaking.Cause Unknown.Insp of Valve to Determine Exact Nature of Component Failure Not Yet Possible.Block Valve Closed & de-energized to Prevent Inadvertent Opening | /03L-0:on 820103,power Operated Relief Valve NC-32 Found Leaking.Cause Unknown.Insp of Valve to Determine Exact Nature of Component Failure Not Yet Possible.Block Valve Closed & de-energized to Prevent Inadvertent Opening | | | 05000369/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | | 05000369/LER-1982-005-03, /03L-0:on 820105,during Mode 1 Power Escalation, Small Seal on Lower Personnel Air Lock Auxiliary Bldg Failed to Open.Caused by Design Oversight by Door Manufacturer.Seal Replaced & Successfully Passed Leak Rate Test | /03L-0:on 820105,during Mode 1 Power Escalation, Small Seal on Lower Personnel Air Lock Auxiliary Bldg Failed to Open.Caused by Design Oversight by Door Manufacturer.Seal Replaced & Successfully Passed Leak Rate Test | | | 05000369/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000369/LER-1982-006-03, /03L-0:on 820106,flow Gauge on Remote Auxiliary Shutdown Control Panel Indicated No Flow When Corresponding Control Room Gauge Read 100 Gpm.Caused by Water Leaking Into Differential Pressure Transmitter Electronics Housing | /03L-0:on 820106,flow Gauge on Remote Auxiliary Shutdown Control Panel Indicated No Flow When Corresponding Control Room Gauge Read 100 Gpm.Caused by Water Leaking Into Differential Pressure Transmitter Electronics Housing | | | 05000369/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000369/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Encl | Forwards LER 82-007/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-007-03, /03L-0:on 820111,many Instrument Lines Froze W/ Instruments Declared Inoperable Leading to Inadvertent Actuation of ESF Causing Safety Injection,Steamline Isolation & Reactor Trips.Caused by Cold Weather | /03L-0:on 820111,many Instrument Lines Froze W/ Instruments Declared Inoperable Leading to Inadvertent Actuation of ESF Causing Safety Injection,Steamline Isolation & Reactor Trips.Caused by Cold Weather | | | 05000369/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-008-03, /03L-0:on 820115,exam of Programs on Operator Computer Revealed Equipment Run Time on Fuel Pool Ventilation Sys Exceeded Tech Specs W/O Sample Being Taken from Charcoal Absorber.Caused by Lack of Procedure | /03L-0:on 820115,exam of Programs on Operator Computer Revealed Equipment Run Time on Fuel Pool Ventilation Sys Exceeded Tech Specs W/O Sample Being Taken from Charcoal Absorber.Caused by Lack of Procedure | | | 05000369/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000369/LER-1982-009-03, /03L-0:on 820116,during Review of Surveillance Documentation,Periodic Testing of Diesel Generator Battery Trains Edga & Edgb Not Performed within Test Frequency Required by Tech Specs.Caused by Personnel Error | /03L-0:on 820116,during Review of Surveillance Documentation,Periodic Testing of Diesel Generator Battery Trains Edga & Edgb Not Performed within Test Frequency Required by Tech Specs.Caused by Personnel Error | | | 05000369/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-010-03, /03L-0:on 820120,while in Mode 1,all Digital Rod Position Indications for Control Rod K-8 Lost.Caused by Cabling to Detectors Susceptible to Conductor Damage Due to Own Weight.Bulkhead Connector Cable Replaced | /03L-0:on 820120,while in Mode 1,all Digital Rod Position Indications for Control Rod K-8 Lost.Caused by Cabling to Detectors Susceptible to Conductor Damage Due to Own Weight.Bulkhead Connector Cable Replaced | | | 05000369/LER-1982-011-03, /03L-0:on 820120,maint Personnel Working on Spent Fuel Pool Cooling Sys (Kf) Heat Exchanger 1A Discharge Throttle Bypass Relief Valve Discovered That Kf Mechanical Snubber Was Removed Rendering Snubber Inoperable | /03L-0:on 820120,maint Personnel Working on Spent Fuel Pool Cooling Sys (Kf) Heat Exchanger 1A Discharge Throttle Bypass Relief Valve Discovered That Kf Mechanical Snubber Was Removed Rendering Snubber Inoperable | | | 05000369/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000369/LER-1982-012-03, /03L-0:on 820119,routine QA Audit of Fire Protection Sys Test Found Three Valves Marked Not Accessible & Had Not Been Checked.Caused by Personnel Error.Periodic Test Performed & Valves Found in Correct Position | /03L-0:on 820119,routine QA Audit of Fire Protection Sys Test Found Three Valves Marked Not Accessible & Had Not Been Checked.Caused by Personnel Error.Periodic Test Performed & Valves Found in Correct Position | | | 05000369/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-013-03, /03L-0:on 820126,two Upper Head Injection Train a Accumulator Tank Level Switches Miscalibr,Rendering Isolation Valves Inoperable.Caused by Faulty Data Programmed Into Computer Memory.Program Corrected | /03L-0:on 820126,two Upper Head Injection Train a Accumulator Tank Level Switches Miscalibr,Rendering Isolation Valves Inoperable.Caused by Faulty Data Programmed Into Computer Memory.Program Corrected | | | 05000369/LER-1982-014-03, /03L-0:on 820128,process Monitoring Sys Containment Gas Monitor EMF-39(L) Declared Inoperable Due to Scale Low Indication & Loss of Indication.Caused by Failure of Quality Bnn Connector.Sys Repaired | /03L-0:on 820128,process Monitoring Sys Containment Gas Monitor EMF-39(L) Declared Inoperable Due to Scale Low Indication & Loss of Indication.Caused by Failure of Quality Bnn Connector.Sys Repaired | | | 05000369/LER-1982-014, Forwards LER 82-014/03L-0 | Forwards LER 82-014/03L-0 | | | 05000369/LER-1982-015, Forwards LER 82-015/01T-0.Detailed Event Analysis Encl | Forwards LER 82-015/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-015-01, /01T-0:on 820212,both Centrifugal Charging Pumps (CCP) Declared Inoperable When Hydrogen from Reciprocating Charging Pump Suction Dampeners Entered CCP Suction,Causing Cavitation | /01T-0:on 820212,both Centrifugal Charging Pumps (CCP) Declared Inoperable When Hydrogen from Reciprocating Charging Pump Suction Dampeners Entered CCP Suction,Causing Cavitation | | | 05000369/LER-1982-016-03, /03L-0:on 820211,discovered Pivot Pin Missing from safety-related Hanger Located in Centrifugal Charging Pump 1B Room Supporting Pump 4-inch Discharge Line Rendering Hanger Inoperable.Cause Undetermined.New Pin Installed | /03L-0:on 820211,discovered Pivot Pin Missing from safety-related Hanger Located in Centrifugal Charging Pump 1B Room Supporting Pump 4-inch Discharge Line Rendering Hanger Inoperable.Cause Undetermined.New Pin Installed | | | 05000369/LER-1982-016, Forwards LER 82-016/03L-0 | Forwards LER 82-016/03L-0 | | | 05000369/LER-1982-017-03, /03L-0:on 820212,control Room Alarms Indicated Closing of 4 Accumulator Discharge Isolation Valves, Rendering Upper Head Injection Portion of ECCS Inoperable. Cause Probably Due to Installation Deficiency | /03L-0:on 820212,control Room Alarms Indicated Closing of 4 Accumulator Discharge Isolation Valves, Rendering Upper Head Injection Portion of ECCS Inoperable. Cause Probably Due to Installation Deficiency | | | 05000369/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-018-03, /03L-0:on 820218,control Room Annunciators Indicated Reactor Coolant Loop B Overtemp & Overpower Delta T Alarms.Caused by Faulty Lead/Lag Amplifier Card in Loop B Delta T Section of 7300 Control Sys Cabinets | /03L-0:on 820218,control Room Annunciators Indicated Reactor Coolant Loop B Overtemp & Overpower Delta T Alarms.Caused by Faulty Lead/Lag Amplifier Card in Loop B Delta T Section of 7300 Control Sys Cabinets | | | 05000369/LER-1982-018, Forwards LER 82-018/03L-0 | Forwards LER 82-018/03L-0 | | | 05000369/LER-1982-019-03, /03L-0:on 820228,during Mode 4,performance of RCS Pressure Isolation Valve Leak Rate Test Determined That 3 Valves Failed Test.Caused by Failure of Valves to Seat Properly.Valves Disassembled & Repaired | /03L-0:on 820228,during Mode 4,performance of RCS Pressure Isolation Valve Leak Rate Test Determined That 3 Valves Failed Test.Caused by Failure of Valves to Seat Properly.Valves Disassembled & Repaired | | | 05000369/LER-1982-020-03, /03L-0:on 820304,during Mode 5,operator-trainee Attempted to Address Status of Fire Zone Through Honeywell Fire Detection Sys Operator Terminal & Mistakenly Dumped Central Processing Unit Memory.Caused by Personnel Error | /03L-0:on 820304,during Mode 5,operator-trainee Attempted to Address Status of Fire Zone Through Honeywell Fire Detection Sys Operator Terminal & Mistakenly Dumped Central Processing Unit Memory.Caused by Personnel Error | | | 05000369/LER-1982-020, Forwards LER 82-020/03L-0 | Forwards LER 82-020/03L-0 | | | 05000369/LER-1982-021-03, /03L-0:on 820309,discovered Cold Leg Injection Accumulator Isolation Valves Not Periodically Tested for Correct Response to P-11 Interlock Signal.Caused by Procedural Deficiency.Tests Performed on 820312 | /03L-0:on 820309,discovered Cold Leg Injection Accumulator Isolation Valves Not Periodically Tested for Correct Response to P-11 Interlock Signal.Caused by Procedural Deficiency.Tests Performed on 820312 | | | 05000369/LER-1982-021, Forwards LER 82-021/03L-0 | Forwards LER 82-021/03L-0 | | | 05000369/LER-1982-022-03, /03L-0:on 820310,while in Mode 5,procedure Review Revealed Pressurizer 1 Power Operated Relief Valve (PORV) Had Not Been Timed.Procedure Change on 800915 Failed to Include PORV for Time Test.Procedure Changed | /03L-0:on 820310,while in Mode 5,procedure Review Revealed Pressurizer 1 Power Operated Relief Valve (PORV) Had Not Been Timed.Procedure Change on 800915 Failed to Include PORV for Time Test.Procedure Changed | | | 05000369/LER-1982-022, Forwards LER 82-022/03L-0 | Forwards LER 82-022/03L-0 | | | 05000369/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-023-03, /03L-0:on 820312,after Filling & Venting of RCS, Sample Indicated Boron Concentration at 1,025 Ppm.Caused by Procedural Deficiency Due to Operating Boric Acid Blender W/O Concentration Verification During Addition to RCS | /03L-0:on 820312,after Filling & Venting of RCS, Sample Indicated Boron Concentration at 1,025 Ppm.Caused by Procedural Deficiency Due to Operating Boric Acid Blender W/O Concentration Verification During Addition to RCS | | | 05000369/LER-1982-024, Forwards LER 82-024/03L-0.Detailed Event Analysis Encl | Forwards LER 82-024/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-024-03, /03L-0:on 820302,while Draining RCS for Insp,Rhr Pump Low Discharge Pressure Alarm Sounded.Caused by Inaccurate Indication of RCS Water Level Due to Misapplication of Control Board Level Gauge Transmitter | /03L-0:on 820302,while Draining RCS for Insp,Rhr Pump Low Discharge Pressure Alarm Sounded.Caused by Inaccurate Indication of RCS Water Level Due to Misapplication of Control Board Level Gauge Transmitter | | | 05000369/LER-1982-025, Forwards LER 82-025/03L-0 | Forwards LER 82-025/03L-0 | | | 05000369/LER-1982-025-03, /03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency | /03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency | | | 05000369/LER-1982-026, Forwards LER 82-026/03L-0 | Forwards LER 82-026/03L-0 | |
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