LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl |
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J IMP S njg, 4 3 WILLIAM O. PAR M E R, J R.
February 26, 1982 Tra ~ e c:^aca
..o s,... e.cox v.o m-4o s a Mr. James P. O'Reilly, Regional Administrator g
U. S. Nuclear Regulatory Commission
,9 Region II O) s 101 Marietta Street, Suite 3100 g
Atlanta, Georgia 30303 3
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Re: McGuire Nuclear Station Unit 1
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Docket No. 50-369 k'/ K[
Dear Mr. O'Reilly:
Please find attached Reportable Occurrence Report R0-369/82-12. This report concerns T.S.4.7.10.1, "The Fire Suppression Water System shall be demonstrated operable:...b. at least once per 31 days by verifying that each valve (manual, power operated or automatic) in the flow path is in its correct position."
This incident was considered to be of no significance with respect to the health and safety of the public.
Very truly yours, t/
/
William O. Parker, Jr.
PBN/jfw Attachment cc: Director Records Center Office of tbnagement and Program Analysis Institute of Nuclear Power Operations U. S. Nuclear Regulatory Commission 1820 Water Place Washington, D. C.
20555 Atlanta, Georgia 30339 Mr. P. R. Bemis Senior Resident Inspector-NRC McGuire Nuclear Station 82O3180282 820226 PDR ADOCK 05000369 OFFICTAL cony S
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DUKE POWER COMPANY McGUIRE NUCLEAR STATION REPORTABLE OCCURRENCE REPORT NO. 82-12 REPORT DATE: February 26, 1982 FACILITY: McGuire Unit 1, Cornelius, NC IDENTIFICATION: Failure to Meet Surveillance Requirement For Fire Protection System DISCUSSION: The January 19, 1982, routine quality assurance audit of the periodic test, " Fire Protection System Monthly Test", found discrepancies on the surveillance documentation for November and December, 1981. The completed system line-up verification sheets indicated that three. valves were "not acces-sible".
The purpose of this periodic test is to satisfy Technical Specification 4.7.10.1.b, which insures the fire suppression water (RF) system is operable every 31 days by verifying ite valves are in their correct positions.
It provides no exception for valves inaccessible due to high radiation fields. At the time of. discovery the unit was in mode one at 50% power. During the period since the valves were last verified on October 22, 1981, the unit had been at various power levels up to and including 100%, with outages from November 15 to November 25 and from December 2 to January 2.
The valves involved are located in the " midget hole", which is a room in the Auxiliary Building that adjoins the unit one reactor building.
Radiation levels here can.be.high in some loca-tions due to the nature of various process lines present. The valves involved have the following functions: Auxiliary Building Elevation 716 feet loop isola-tion, Auxiliary Building Elevation 733 feet hose station supply isolation, and supply to room 600 sprinkler system.
The position of these valves was not verified because Safety Assistant "A", who performed the periodic test in November and December, 1981, checked with Health Physics prior to inspecting the valves and was encouraged not to enter the area unless necessary. Radiation levels present would have resulted in an external dose probably less than approximately 5 mR.
Since the valves were inaccessible as determined by the safety assistant, "not accessible" was written on the test's data sheet, but was not noted on a discrepancy sheet. The Shift Supervisor was not notified that the surveillance requirement could not be met and that appli-cable action statements would have to be observed.. These mistakes are due to a lack of understanding of periodic testing fundamentals resulting from a lack of training received by the safety group. This incident is determined to be due to Personnel Error.
Immediate corrective action consisted of verifying the valves in their correct positions as documented by the periodic test. This was completed on January 22, with the valves found in their correct position.
EVALUATION: A basic misunderstanding of the significance of Technical Specifi-cation Surveillance Requirements for the RF system played a major role in this incident. When the safety assistant performing the test in November and December was told he should not enter the room unless necessary, he assumed the valves were inaccessible. This was not the case. The term " inaccessible" in the
~s Report No. 82-12 Page 2 Technical Specifications is interpreted by the station as meaning an individual would receive an external dose greater than approximately 100 mR.
Health physics estimates a dose of less than 5 mR would probably have been received while verifying these valves. L'nder extreme circumstances, it is possible a dose of 20 mR might have been received, which is not enough to justify calling the valves inaccessible. However, Technical Specification 4.7.10.1.b has no provisions for inaccessible valves. The safety assistant was relying on his memory and got this Technical Specification confused with Technical Specification 4.7.10.4.a (Fire Hose Stations).
It is important to understand the meaning of inaccessible in Technical Specifications to insure a surveillance requirement that has provi-sions for accessibility is not missed because the ALARA program discourages performing the surveillance.
Marking a particular surveillance item "not accessible" constituted changing the periodic test without initiating a procedure change form or without rewrit-ing and reapproving the test.
Discrepancies discovered in performing a periodic test must be listed on a discrepancy sheet and signed off as resolved by a station supervisory staff member within the group responsible prior to approving the procedure as completed.
Another important aspect of this incident was that the Shift Supervisor on duty when this missed surveillance was discovered was not notified to make a Techni-cal Specifications Action Items Logbook entry.
The RF system was technically inoperable because the 31 day surveillance of verifying the valves in their correct positions had not been done in approximately 90 days. The Technical Specification Action Statement requires steps to be taken at various times after the RF system is ieclared inoperable, and the mechanism to document when it is declared inoperable and when various actior.s are necessary is the Logbook. The Shift Supervisor should have been notified of the date and time the Quality Assurance Audit Group discovered the deficiencies in the periodic test. Accepted station practice dictates that the group responsible for the particular surveil-lance item is responsible for informing the Shift Supervisor.
SAFETY ANALYSIS
The valves involved were found locked open which is consistent with Technical Specifications. Thus, assuming they had not been both closed and later reopened without authorization between October 23 and January 22, the RF system was able to perform its design function if needed although the sur-veillance was not met.
It is significant that the valves are locked open.
It would take deliberate action on someone's part to close the valve because a key would have to be obtained and the lock removed before closing the valve. This eliminates the possibility that someone touring the Auxiliary Building would indiscriminately close the valve.
CORRECTIVE ACTION
Immediate corrective action was to begin performing the periodic test on January 21.
It was completed on January 22, with the valves found in their correct position. Training in the areas of Technical Specifi-cations and Station Directives requirements for periodic testing will be com-pleted by March 1.
Training coiering applicable station directives is currently being developed. Technical Specification requirements will be discussed by the station Projects and Licensing Engineer.
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| 05000369/LER-1982-001, Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-001-01, /01T-0:on 820106,routine Review of Source Document Changes Revealed Class H Piping in Fire Protection Sys in Diesel Generator Room 1A Routed Above One Nuclear safety-related Essential Cable & Instrument Panel | /01T-0:on 820106,routine Review of Source Document Changes Revealed Class H Piping in Fire Protection Sys in Diesel Generator Room 1A Routed Above One Nuclear safety-related Essential Cable & Instrument Panel | | | 05000369/LER-1982-002-03, /03L-0:on 820101,temp Sensing Valve Position Indication Disagreed W/Alternate Position Indication & Declared Inoperable.Caused by Environ Conditions | /03L-0:on 820101,temp Sensing Valve Position Indication Disagreed W/Alternate Position Indication & Declared Inoperable.Caused by Environ Conditions | | | 05000369/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-003-03, /03L-0:on 820102,average Temp in Upper Containment Was Reduced Below Temp Requirement.Caused by Cold Weather Cooling Bldg.Temp Increased Using Dihydrogen Recombiner Heaters | /03L-0:on 820102,average Temp in Upper Containment Was Reduced Below Temp Requirement.Caused by Cold Weather Cooling Bldg.Temp Increased Using Dihydrogen Recombiner Heaters | | | 05000369/LER-1982-004-03, /03L-0:on 820103,power Operated Relief Valve NC-32 Found Leaking.Cause Unknown.Insp of Valve to Determine Exact Nature of Component Failure Not Yet Possible.Block Valve Closed & de-energized to Prevent Inadvertent Opening | /03L-0:on 820103,power Operated Relief Valve NC-32 Found Leaking.Cause Unknown.Insp of Valve to Determine Exact Nature of Component Failure Not Yet 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Remote Auxiliary Shutdown Control Panel Indicated No Flow When Corresponding Control Room Gauge Read 100 Gpm.Caused by Water Leaking Into Differential Pressure Transmitter Electronics Housing | | | 05000369/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000369/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Encl | Forwards LER 82-007/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-007-03, /03L-0:on 820111,many Instrument Lines Froze W/ Instruments Declared Inoperable Leading to Inadvertent Actuation of ESF Causing Safety Injection,Steamline Isolation & Reactor Trips.Caused by Cold Weather | /03L-0:on 820111,many Instrument Lines Froze W/ Instruments Declared Inoperable Leading to Inadvertent Actuation of ESF Causing Safety Injection,Steamline Isolation & Reactor Trips.Caused by Cold Weather | | | 05000369/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-008-03, /03L-0:on 820115,exam of Programs on Operator Computer Revealed Equipment Run Time on Fuel Pool Ventilation Sys Exceeded Tech Specs W/O Sample Being Taken from Charcoal Absorber.Caused by Lack of Procedure | /03L-0:on 820115,exam of Programs on Operator Computer Revealed Equipment Run Time on Fuel Pool Ventilation Sys Exceeded Tech Specs W/O Sample Being Taken from Charcoal Absorber.Caused by Lack of Procedure | | | 05000369/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000369/LER-1982-009-03, /03L-0:on 820116,during Review of Surveillance Documentation,Periodic Testing of Diesel Generator Battery Trains Edga & Edgb Not Performed within Test Frequency Required by Tech Specs.Caused by Personnel Error | /03L-0:on 820116,during Review of Surveillance Documentation,Periodic Testing of Diesel Generator Battery Trains Edga & Edgb Not Performed within Test Frequency Required by Tech Specs.Caused by Personnel Error | | | 05000369/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-010-03, /03L-0:on 820120,while in Mode 1,all Digital Rod Position Indications for Control Rod K-8 Lost.Caused by Cabling to Detectors Susceptible to Conductor Damage Due to Own Weight.Bulkhead Connector Cable Replaced | /03L-0:on 820120,while in Mode 1,all Digital Rod Position Indications for Control Rod K-8 Lost.Caused by Cabling to Detectors Susceptible to Conductor Damage Due to Own Weight.Bulkhead Connector Cable Replaced | | | 05000369/LER-1982-011-03, /03L-0:on 820120,maint Personnel Working on Spent Fuel Pool Cooling Sys (Kf) Heat Exchanger 1A Discharge Throttle Bypass Relief Valve Discovered That Kf Mechanical Snubber Was Removed Rendering Snubber Inoperable | /03L-0:on 820120,maint Personnel Working on Spent Fuel Pool Cooling Sys (Kf) Heat Exchanger 1A Discharge Throttle Bypass Relief Valve Discovered That Kf Mechanical Snubber Was Removed Rendering Snubber Inoperable | | | 05000369/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000369/LER-1982-012-03, /03L-0:on 820119,routine QA Audit of Fire Protection Sys Test Found Three Valves Marked Not Accessible & Had Not Been Checked.Caused by Personnel Error.Periodic Test Performed & Valves Found in Correct Position | /03L-0:on 820119,routine QA Audit of Fire Protection Sys Test Found Three Valves Marked Not Accessible & Had Not Been Checked.Caused by Personnel Error.Periodic Test Performed & Valves Found in Correct Position | | | 05000369/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-013-03, /03L-0:on 820126,two Upper Head Injection Train a Accumulator Tank Level Switches Miscalibr,Rendering Isolation Valves Inoperable.Caused by Faulty Data Programmed Into Computer Memory.Program Corrected | /03L-0:on 820126,two Upper Head Injection Train a Accumulator Tank Level Switches Miscalibr,Rendering Isolation Valves Inoperable.Caused by Faulty Data Programmed Into Computer Memory.Program Corrected | | | 05000369/LER-1982-014-03, /03L-0:on 820128,process Monitoring Sys Containment Gas Monitor EMF-39(L) Declared Inoperable Due to Scale Low Indication & Loss of Indication.Caused by Failure of Quality Bnn Connector.Sys Repaired | /03L-0:on 820128,process Monitoring Sys Containment Gas Monitor EMF-39(L) Declared Inoperable Due to Scale Low Indication & Loss of Indication.Caused by Failure of Quality Bnn Connector.Sys Repaired | | | 05000369/LER-1982-014, Forwards LER 82-014/03L-0 | Forwards LER 82-014/03L-0 | | | 05000369/LER-1982-015, Forwards LER 82-015/01T-0.Detailed Event Analysis Encl | Forwards LER 82-015/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-015-01, /01T-0:on 820212,both Centrifugal Charging Pumps (CCP) Declared Inoperable When Hydrogen from Reciprocating Charging Pump Suction Dampeners Entered CCP Suction,Causing Cavitation | /01T-0:on 820212,both Centrifugal Charging Pumps (CCP) Declared Inoperable When Hydrogen from Reciprocating Charging Pump Suction Dampeners Entered CCP Suction,Causing Cavitation | | | 05000369/LER-1982-016-03, /03L-0:on 820211,discovered Pivot Pin Missing from safety-related Hanger Located in Centrifugal Charging Pump 1B Room Supporting Pump 4-inch Discharge Line Rendering Hanger Inoperable.Cause Undetermined.New Pin Installed | /03L-0:on 820211,discovered Pivot Pin Missing from safety-related Hanger Located in Centrifugal Charging Pump 1B Room Supporting Pump 4-inch Discharge Line Rendering Hanger Inoperable.Cause Undetermined.New Pin Installed | | | 05000369/LER-1982-016, Forwards LER 82-016/03L-0 | Forwards LER 82-016/03L-0 | | | 05000369/LER-1982-017-03, /03L-0:on 820212,control Room Alarms Indicated Closing of 4 Accumulator Discharge Isolation Valves, Rendering Upper Head Injection Portion of ECCS Inoperable. Cause Probably Due to Installation Deficiency | /03L-0:on 820212,control Room Alarms Indicated Closing of 4 Accumulator Discharge Isolation Valves, Rendering Upper Head Injection Portion of ECCS Inoperable. Cause Probably Due to Installation Deficiency | | | 05000369/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-018-03, /03L-0:on 820218,control Room Annunciators Indicated Reactor Coolant Loop B Overtemp & Overpower Delta T Alarms.Caused by Faulty Lead/Lag Amplifier Card in Loop B Delta T Section of 7300 Control Sys Cabinets | /03L-0:on 820218,control Room Annunciators Indicated Reactor Coolant Loop B Overtemp & Overpower Delta T Alarms.Caused by Faulty Lead/Lag Amplifier Card in Loop B Delta T Section of 7300 Control Sys Cabinets | | | 05000369/LER-1982-018, Forwards LER 82-018/03L-0 | Forwards LER 82-018/03L-0 | | | 05000369/LER-1982-019-03, /03L-0:on 820228,during Mode 4,performance of RCS Pressure Isolation Valve Leak Rate Test Determined That 3 Valves Failed Test.Caused by Failure of Valves to Seat Properly.Valves Disassembled & Repaired | /03L-0:on 820228,during Mode 4,performance of RCS Pressure Isolation Valve Leak Rate Test Determined That 3 Valves Failed Test.Caused by Failure of Valves to Seat Properly.Valves Disassembled & Repaired | | | 05000369/LER-1982-020-03, /03L-0:on 820304,during Mode 5,operator-trainee Attempted to Address Status of Fire Zone Through Honeywell Fire Detection Sys Operator Terminal & Mistakenly Dumped Central Processing Unit Memory.Caused by Personnel Error | /03L-0:on 820304,during Mode 5,operator-trainee Attempted to Address Status of Fire Zone Through Honeywell Fire Detection Sys Operator Terminal & Mistakenly Dumped Central Processing Unit Memory.Caused by Personnel Error | | | 05000369/LER-1982-020, Forwards LER 82-020/03L-0 | Forwards LER 82-020/03L-0 | | | 05000369/LER-1982-021-03, /03L-0:on 820309,discovered Cold Leg Injection Accumulator Isolation Valves Not Periodically Tested for Correct Response to P-11 Interlock Signal.Caused by Procedural Deficiency.Tests Performed on 820312 | /03L-0:on 820309,discovered Cold Leg Injection Accumulator Isolation Valves Not Periodically Tested for Correct Response to P-11 Interlock Signal.Caused by Procedural Deficiency.Tests Performed on 820312 | | | 05000369/LER-1982-021, Forwards LER 82-021/03L-0 | Forwards LER 82-021/03L-0 | | | 05000369/LER-1982-022-03, /03L-0:on 820310,while in Mode 5,procedure Review Revealed Pressurizer 1 Power Operated Relief Valve (PORV) Had Not Been Timed.Procedure Change on 800915 Failed to Include PORV for Time Test.Procedure Changed | /03L-0:on 820310,while in Mode 5,procedure Review Revealed Pressurizer 1 Power Operated Relief Valve (PORV) Had Not Been Timed.Procedure Change on 800915 Failed to Include PORV for Time Test.Procedure Changed | | | 05000369/LER-1982-022, Forwards LER 82-022/03L-0 | Forwards LER 82-022/03L-0 | | | 05000369/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-023-03, /03L-0:on 820312,after Filling & Venting of RCS, Sample Indicated Boron Concentration at 1,025 Ppm.Caused by Procedural Deficiency Due to Operating Boric Acid Blender W/O Concentration Verification During Addition to RCS | /03L-0:on 820312,after Filling & Venting of RCS, Sample Indicated Boron Concentration at 1,025 Ppm.Caused by Procedural Deficiency Due to Operating Boric Acid Blender W/O Concentration Verification During Addition to RCS | | | 05000369/LER-1982-024, Forwards LER 82-024/03L-0.Detailed Event Analysis Encl | Forwards LER 82-024/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1982-024-03, /03L-0:on 820302,while Draining RCS for Insp,Rhr Pump Low Discharge Pressure Alarm Sounded.Caused by Inaccurate Indication of RCS Water Level Due to Misapplication of Control Board Level Gauge Transmitter | /03L-0:on 820302,while Draining RCS for Insp,Rhr Pump Low Discharge Pressure Alarm Sounded.Caused by Inaccurate Indication of RCS Water Level Due to Misapplication of Control Board Level Gauge Transmitter | | | 05000369/LER-1982-025, Forwards LER 82-025/03L-0 | Forwards LER 82-025/03L-0 | | | 05000369/LER-1982-025-03, /03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency | /03L-0:on 820318,vol Control Tank Makeup Frequency Increased & Containment Floor & Equipment Sump 1A Level Increased During RCS Leak Test.Caused by Failure to Verify Isolation Valves Closed Due to Procedural Deficiency | | | 05000369/LER-1982-026, Forwards LER 82-026/03L-0 | Forwards LER 82-026/03L-0 | |
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