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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20024H2731991-05-23023 May 1991 Ro:Vital Fire Suppression Water Sys Equipment Not Available for Greater than Seven Days.Caused by Prolonged Preventive Maint.Diesel Driven Fire Pump Was Declared Operable on 910503 ML19318D0481980-06-25025 June 1980 Suppl 1 to RO 79-25/1T:concurs W/Conclusions of Encl GE Proprietary Info on Loose Parts Analysis That Water Rod Lower End Plug Would Wear & Cause Shank to Break.Ge Info Withheld (Ref 10CFR2.790) ML19318C2961980-06-25025 June 1980 RO 79-205/1T,Suppl 1:encl GE Loose Parts Analysis Addresses Possibility That Water Rod Lower End Plug Could Wear to Extent That Shank Would Break.Licensee Concurs W/Conclusion That Generation of Loose Part Is Unexpected.W/O Encl 1991-05-23
[Table view] Category:LER)
MONTHYEARML20024H2731991-05-23023 May 1991 Ro:Vital Fire Suppression Water Sys Equipment Not Available for Greater than Seven Days.Caused by Prolonged Preventive Maint.Diesel Driven Fire Pump Was Declared Operable on 910503 ML19318D0481980-06-25025 June 1980 Suppl 1 to RO 79-25/1T:concurs W/Conclusions of Encl GE Proprietary Info on Loose Parts Analysis That Water Rod Lower End Plug Would Wear & Cause Shank to Break.Ge Info Withheld (Ref 10CFR2.790) ML19318C2961980-06-25025 June 1980 RO 79-205/1T,Suppl 1:encl GE Loose Parts Analysis Addresses Possibility That Water Rod Lower End Plug Could Wear to Extent That Shank Would Break.Licensee Concurs W/Conclusion That Generation of Loose Part Is Unexpected.W/O Encl 1991-05-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8831999-10-21021 October 1999 Safety Evaluation Supporting Proposed Alternatives to Code Requirements Described in RR-V17 & RR-V18 ML20217G2041999-10-13013 October 1999 Safety Evaluation Supporting Amend 179 to License DPR-28 BVY-99-127, Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With ML20212C2551999-09-17017 September 1999 Safety Evaluation Supporting Amend 175 to License DPR-28 BVY-99-112, Monthly Operating Rept for Aug 1999 for Vermont Yankee.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Vermont Yankee.With BVY-99-109, Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 9908311999-08-19019 August 1999 Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 990831 BVY-99-102, Monthly Operating Rept for July 1999 for Vermont Yankee. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Vermont Yankee. with ML20209J0081999-07-14014 July 1999 Special Rept:On 990615,diesel Driven Fire Pump Failed to Achieve Rated Flow of 2500 Gallons Per Minute.Pump Was Inoperable for Greater than 7 Days.Corrective Maint Was Performed to Reset Pump Lift Setting BVY-99-090, Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With ML20196G5071999-06-23023 June 1999 Vynp Assessment of On-Site Disposal of Contaminated Soil by Land Spreading BVY-99-077, Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With BVY-99-068, Monthly Operating Rept for Apr 1999 for Vynp.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Vynp.With ML20206E8741999-04-29029 April 1999 SER Determined That Flaw Evaluation Meets Rules of ASME Code & Assumed Crack Growth Rate Adequate for Application ML20206D9301999-04-27027 April 1999 1999 Emergency Preparedness Exercise 990427 Exercise Manual (Plume Portion) ML20205S4211999-04-16016 April 1999 Non-proprietary Version of Revised Page 4-3 of HI-981932 Technical Rept for Vermont Yankee Spent Fuel Pool Storage Expansion ML20205K7581999-04-0707 April 1999 Safety Evaluation Supporting Alternative Proposal for Reexamination of Circumferential Welds with Detected Flaw Indications in Plant RPV BVY-99-046, Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With ML20205F6631999-03-0404 March 1999 Jet Pump Riser Weld Leakage Evaluation BVY-99-035, Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With ML20205P8241999-02-28028 February 1999 Rev 2 to Vermont Yankee Cycle 20 Colr ML20203H9881999-02-18018 February 1999 SER Accepting Alternative to 10CFR50.55a(g)(6)(ii)(A) Augmented Reactor Vessel Exam at Vermont Yankee Nuclear Power Station.Technical Ltr Rept Encl ML20203A6951999-02-0404 February 1999 Revised Rev 2,App B to Vermont Yankee Operational QA Manual (Voqam) ML20199K7151999-01-21021 January 1999 Corrected Safety Evaluation Supporting Amend 163 Issued to FOL DPR-28.Pages 2 & 3 Required Correction & Clarification ML20199K6991999-01-20020 January 1999 Safety Evaluation Concluding That Request to Use YAEC-1339, Yankee Atomic Electric Co Application of FIBWR2 Core Hydraulics Code to BWR Reload Analysis, at Vermont Yankee Acceptable ML20199L5951999-01-14014 January 1999 Safety Evaluation Accepting Licensee Proposed Alternative to Code Requirement,Described in Rev 2 to Pump Relief Request RR-P10 Pursuant to 10CFR50.55a(a)(3)(i) BVY-99-071, Corp 1998 Annual Rept. with1998-12-31031 December 1998 Corp 1998 Annual Rept. with BVY-99-001, Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station ML20198H5481998-12-23023 December 1998 Rev 2 to Vermont Operational QA Manual,Voqam ML20196H8641998-12-0101 December 1998 Cycle 19 Operating Rept BVY-98-163, Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With ML20195C4161998-11-0909 November 1998 SER Accepting Request That NRC Approve ASME Code Case N-560, Alternative Exam Requirement for Class 1,Category B-J Piping Welds BVY-98-154, Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With ML20155B6471998-10-26026 October 1998 Safety Evaluation Accepting Jet Pump Riser Insp Results & Flaw Evaluation,Conducted During 1998 Refueling Outage ML20154N0891998-10-16016 October 1998 Rev 1 to Vermont Operational QA Program Manual (Voqam) ML20154B6951998-10-0101 October 1998 SER Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Vermont Yankee Nuclear Power Station BVY-98-149, Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With ML20239A1361998-09-0202 September 1998 SER Re License Request for NRC Review & Concurrence W/Changes to NRC-approved Fire Protection Program BVY-98-135, Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With ML20151U0361998-08-28028 August 1998 Non-proprietary Rev 1 to Holtec Rept HI-981932, Vermont Yankee Nuclear Power Station Spent Storage Expansion Project ML20237E9221998-08-20020 August 1998 Vynp 1998 Form NIS-1 Owners Summary Rept for ISI, 961103-980603 BVY-98-122, Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station ML20205F6491998-07-31031 July 1998 Rev 1 to GE-NE-B13-01935-02, Jet Pump Assembly Welds Flaw Evaluation Handbook for Vermont Yankee ML20236G0011998-06-30030 June 1998 Individual Plant Exam External Events BVY-98-098, Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station ML20248C5081998-05-31031 May 1998 Rev 2 to 24A5416, Supplemental Reload Licensing Rept for Vermont Yankee Nuclear Power Station Reload 19 Cycle 20 ML20248C4951998-05-31031 May 1998 Rev 1 to Vermont Yankee Nuclear Power Station Cycle 20 Colr BVY-98-081, Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station ML20247J8341998-05-31031 May 1998 Peak Suppression Pool Temp Analyses for Large Break LOCA Scenarios, for May 1998 ML20247G4001998-05-12012 May 1998 Interview Rept of Ej Massey ML20247E6351998-04-30030 April 1998 Rev 1 to GE-NE-B13-01935-LTR, Jet Pump Riser Welds Allowable Flaw Sizes Ltr Rept for Vermont Yankee 1999-09-30
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VERMONT YANKEE NUCLEAR POWER CORPORATION
. n, [ Ferry Road, Brattleboro. vT 05301-7002 yh yg ENGINEERING OrnCE se ,.4.m .
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May 23,1991 U.S. Nuclear Regulatory Commission
- Washington,_ D.C. 20555 Attn: Document Control Desk
Reference:
a) Operating License DPR 28 (Docket No. 50 271)
Dear Sir:
Subject:
Report of Inoperable Equipment in the Vital Fire Suppression Water System l In accordance with Vermont Yankee Technical Specifications Section
! 3.13.B.2, this report is submitted as notification that the required Vital Fire Suppression Water system equipment was not available for greater than seven days. The diesel doven fire pump was out of service for seventeen days.
The diesel driven fire pump was removed from service on Tuesday, April 16, 1991 for preventive maintenance. The scope of the work undertaken i included disassembly, inspection, refurbishing, and restoration to service. These l activities did not reveal any_ condition which could have immediately affected the
!- operability of the pump prior to the performance of the work. The diesel driven l fire pump was declared operable on Friday, May 3,1991.
During the period when the diesel driven fire pump was unavailable, alternate provisions were made to supply the Vital Fire . Suppression Water System. These provisions are detailed in Attachment A to this letter.
Very truly yours, Vermont Yankee Nuclear Power Corporation y &
Vw[dy M Warren P. Murphy Senior Vice President, Operations I
/dm l cc: USNRC Regional Administrator, Region i USNRC Resident inspector, VYNPS USNRC Project Manager, VYNPS <
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ATTACHMENT A Provisions for Vital Fire Suppression Water System Based on the results of preventive maintenance performed on the four station service water pumps, maintenance personnel recommended that the diesel driven fire pump undergo similar preventive maintenance measures. Corrosion product build-up and impeller wear was noted in the service water pumps.
Based on _ these findings, it was determined that the diesel driven fire pump should also be inspected.
To ensure that the ?reventive maintenance work was completed in an expeditious manner, the fol;owing actions were taken;
- 1) Appropriate procedures, manuals, and repair documents were identified and made ava!!able.
- 2) Repair personnel were dedicated to the fire pump maintenance activities.
- 3) Support equipment required for the removal and installation of the fire pump was scheduled and reserved for the project.
- 4) Anticipated replacement parts were identified, located, and verified as available.
Tech Spec Section 3.13.B.1 specifies the minimum equipment requirements for an operable Vital Fire Suppression Water System. Section 3.13.B.1.a requires that two fire pumps are operable and lined up to the fire suppression loop. Since the diesel oriven fire pump preventive maintenance work placed this pump out of service, the following compensatory measures were established;
- 1) The electrically driven fire pump remained operable as the primary Vital Fire Suppression Water supply pump.
- 2) The plant service water system, which can be cross connected to the fire l water main, was utilized as the secondary source for the Vital Fire Suppression Water system.
- 3) The four plant service water pumps were verified as operable prior to the l start of work on the diesel driven fire pump. During the work effort, the four plant service water pumps remained operable.
l These actions ensured that an adequate Vital Fire Suppression Water system was maintained and that an independent water source was available at all times to supply all fire suppression systems within the plant. Based on this information, the preventive maintenance activities associated with the diesel driven fire pump did not significantly impact the operability of the Vital Fire Suppression Water system.
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