05000321/LER-1981-050-03, /03L-0:on 810612,while Performing RHR Valve Operability,Containment Spray Isolation Valve B Found Inoperative.Caused by Incorrect Installation of Motor Pinion Gear.Motor Pinion Gear Reinstalled

From kanterella
(Redirected from ML20009F566)
Jump to navigation Jump to search
/03L-0:on 810612,while Performing RHR Valve Operability,Containment Spray Isolation Valve B Found Inoperative.Caused by Incorrect Installation of Motor Pinion Gear.Motor Pinion Gear Reinstalled
ML20009F566
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 06/30/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F562 List:
References
LER-81-050-03L-01, LER-81-50-3L-1, NUDOCS 8107310309
Download: ML20009F566 (2)


LER-1981-050, /03L-0:on 810612,while Performing RHR Valve Operability,Containment Spray Isolation Valve B Found Inoperative.Caused by Incorrect Installation of Motor Pinion Gear.Motor Pinion Gear Reinstalled
Event date:
Report date:
3211981050R03 - NRC Website

text

(7 77)

LICENSEE EVENT REPORT CONTROL BLOCCt: l l

l l

l l

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

l0 l1l lG l A lE II lH l1 l@l010l-l0l0l0lOl0l-lOl0l@l4l1l1]1l1l@l l

l@

7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25

.15 LICENSE TYPE JO 57 CAT 58 COM*T l0lil 3a,,,lL}@l0151010 10 13 l2 l1 l@l0l6l1l2l8l1l@l 0l6l3l0l8l1l@

"EP0 8

60 61 DOCKET NUMBER 68 69 EVENT DAT2 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l O ; 21 l With the reactor in the start-up and hot standby mode, while performina l

RHR Valve Operability due to HPCI being inoperable, "B" Containment Spray 1

10;3; l 1014i l Isolation Valve was found to be inoperative.

Limiting conditions for l

IO 1si l operations wera implemented per Tech Spec 3.5.D.3.

There were no effects i

10 te 1 I upon public health and safety due to this event. This is a non-repetitive I

l o 171 I event.

I I

10181l 80 E

CODE SUSCO E COMPONENT CODE SUSC DE SU E

Q l Cl Fl@ l El@ l B l@ lV l A lL lV 10 lP l@ l Xi@ Q @

i 7 8

9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R RO EVENT YEAR R EPORT NO.

CODE TYPE N O.

l8 l1 l l-l l015l0l l/l l 01 3l l L]

l-l l 01

@ REQE 4

RT

_ 21 22 23 24 26 27 28 29 30 31 32 TK N AC ON ON P NT M

HOURS S8 1 D

FOR b B.

SUPPLIE MAN FACTURER l B l@l A l@

lZl@

lZl@

l0101010l

(_yj @

l Nl@

l N l@

lLl210l0l@

34 35 36 31 40 41 42 43 44 47 JJ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11 10 I I This event can be attributed tn norennnel prene in the installatinn of I

it iii i motor ninion gear.

This permitted the meshina of pinion aear and motor i

l i i 21 1 drive intermediate gear to be out of alignment.

Motor pinion gear was I

i, i3i l reinstalled correctly and valve was-proven operable.

1 I

I1 14 II 80 7

8 9 l

STA

% POWER OTHER STATUS 15 O RY DISCOVERY DESCRIPTION l1 Is l l Cl@ l 0 l 0 l 0 l@l NA l

d @l Surveillance Testina l

l CO# TENT aC nvlTY R2 LEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE i l1 le l l Zl @ l Z l@l NA l

l NA I

PERSONNEL EXPOS ES NUMBER TYPE

DESCRIPTION

li 171 l 0l 01 Ol@l Zl@l NA l

PERSONNEL INJURIES NOUSER

DESCRIPTION

li,iaiiOiOiOlgl NA l

80

'7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY i

TYPE

DESCRIPTION

li 19 l l Zl@l NA l

i 80

, 7 8 9 10 NRC WE ONW ISSUED @ DESCRIPTION h 8107310309 810630 y

l PDR ADOCK 05000321 l

lllllllllllll2 a o S

PDR 68 69 80.

7 8 9 to 912-367-7781 2

R. T. Nix, Supt. Of Maint.

pggyg:

NAME OF PREPARER

-~._.

LER No.: 50-321/1981-50 Licensee: Georgia Power Company Facility: Edwin I. Hatch Docket No. : 50-321

Narrative

Report for LER 50-321/1981-050.

i -

On June 5, 1981, with the reactor in the start-up and hot standby mode HNP-1-3162, RHR Valve Operability Test, was being performed.

During this test, IE11-F0288, Containment Spray Isolation Valve, failed to operate.

Due to HPCI being inoperable, Tech Spec 13.5.D.2 requires this valve to be operable. There were no effects upon public health and safety due to this event.

This is a non-repetitive event.

An investigation revealed the valve failed to operate due to improper

. Since the gear had been installation of the motor pinion drive gear.

improperly installed, it would not mesh with the valve drive gear, thus not allowing the valve to operate.

The motor pinion drive gear was re-moved and re-installed correctly.

RHR valve operability was then performed with all results satisfactory and RHR returned to service.

A generic review revealed no int.erent problems.

J r

1 u