05000333/LER-1981-053-03, /03L-0:on 810625,mgt Review Revealed That Electric & Diesel Fire Pump Flow & Pressure Tests Per Tech Specs Were Not Conducted within Required Time Period.Caused by Failure to Place Surveillance Tests on Schedule.Tests Perfor

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/03L-0:on 810625,mgt Review Revealed That Electric & Diesel Fire Pump Flow & Pressure Tests Per Tech Specs Were Not Conducted within Required Time Period.Caused by Failure to Place Surveillance Tests on Schedule.Tests Performed
ML20009D659
Person / Time
Site: FitzPatrick 
Issue date: 07/10/1981
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009D656 List:
References
LER-81-053-03L, LER-81-53-3L, NUDOCS 8107240258
Download: ML20009D659 (1)


LER-1981-053, /03L-0:on 810625,mgt Review Revealed That Electric & Diesel Fire Pump Flow & Pressure Tests Per Tech Specs Were Not Conducted within Required Time Period.Caused by Failure to Place Surveillance Tests on Schedule.Tests Performed
Event date:
Report date:
3331981053R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 77)

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60 61 DOCKET NUVBER 68 6'J EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h o 2 1 During normal operation, as a result of management review, it was found that

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