LER-1981-008, /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged |
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NRC FORM DG U. S. EdUCLEAR REGULATORY COMMISSION (F 77)
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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo121IThe unit was shut down on 7-4-81 for the 150 EFPD steam generator eddy I
lo lal l current examination.
On 7-10-81 verification of all initial eddy Current data of tubes with indication exceeding the plugging limit was completed.
Two tubes in each the "A" and "B" SG's had indicationn y
>40%.
Prior to eddy current examination a 2000 psid primary-to-g g,
, secondary and an 800 psig secondary-to-primary leak test was done.
- This,
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event is similar to others and reportable per T.S. 15.6.9.2.A.3.
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CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUSCODE SUBCODE lo_19 l l Cl Bl@ y@ WQ l Hl Tl El Xl Cl H l@ W@ W @
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CODE TYPE N O.
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- i ;o,[Three of the indications were within the crevice and are considered to g e IGA caused by caustic.
The fourth indication is 1/2" above the b
3 3 tubesheet and is believed to be a remnant of phosphate wastage.
The
,, i lfour tubes with defects have been plugged.
A crevice flush will be l
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DisCOvERv DESCRIPTION sPOwER OTHER STATUS l
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ACTIVITY CO TENT RELEASED OF RELEASE AVOUNT OF ACTIVITY LOCATION OF RELE ASE
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NUMRER l0 l 0 l 0lgl N/A 1 a 7
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ATTACHMENT TO LICENSEE EVENT REPORT NO. 81-008/0lT-0 Wisconsin Electric Power Company Point Beach Nuclear Plant, Unit 1 Docket No. 50-266 Thi July 10, 1981, verification of all initial steam generator eddy current data-for tubes with indications exceeding the plugging limit was completed.
Two tubes in the "A" steam generator and two tubes in the "B" steam generator were verified to.have degradation greater than 40%, which is the plugging limit of Technical Specification 15.6.2.A.S.
1 On July 4, 1981, Unit 1 was shut down for steam generator eddy. current inspection.
The 2000 psid primary-
.to-seconRO:y hydrostatic test condition was established while the unit sas~being cooled down.
An 800 psig secondary-to-primary leak check-was performed on July 6 and 7.
Detailed inspections of the tubesheets with remote video equipment showed a total of nine e. plosive plugs which were either wet, boric acid coated, or dripping at a s.1.ow rate-(less than one drop every one and one-half minutes).
Of the nine plugs, five had similar obser-vations ncted in previous outages.
Based upon the low leak rate before shut-down_(four gallons per day) and potential steam generator demonstration sleeving during the fall 1981 Tefueling outage, the plugs were not repaired during this outage.
The fact that weld repair of an explosive plug involves a relatively high personnel radiation exposure was also a major factor in deciding not.to repair the explosive plugs at this time.
The specific conditions noted during the leak check are noted below.
"A" Steam Generator R03C09 explosive plug, wet, less than 1 drip /2 minutes R19C33 explosive plug, wet, less than 1 drip /2 minutes R24C37 explosive plug, wet, 1 drip /1.5 minutes R33C50 explosive plug, boric acid coated R21C49 explosive plug, wet end, no drips R04C59 mechanical plug, boric acid ring, appears wet inside R08C50 mechanical plug, boric acid ring, appears wet inside "B" Steam Generator R23C53 explosive plug, wet end, no drips R29C35 explosive plug, wet, 1 drip /2 minutes R04C46 mechanical plug,-boric acid coated, appears wet inside R29C41 weld repair, boric acid coated R28C39 explosive plug, boric acid coated R29C37 explosive plug, boric acid coated - -
. Of the wet end and dripping plugs, the following have been noted in previous inspections:
R19C33 "A"
steam generator R24C37 "A"
steam generator R21C49 "A"
steam generator R23C53 "B"
steam generator R29C35 "B"
steam generator The eddy current inspection consisted of remote inspection of all-readily accessible tubes to the first tube support plate.
Of the 2,853 open tubes in the "A"
steam generator, 2,814 were inspected and 2,816 of the 2,861 open tubes in the "B"
steam generator were inspected.
The tubes that were not inspected are tubes under the eddy current fixture foot (19 in "A" and 17 in "B"),
the tubes that contain template plugs (17 in both "A" and "B",
randomly located), and tubes with restricted tube ends which prevented the insertion of a.720 probe (3 in "A" and 11 in "B").
These tubes were not inspected because of the exposure associated with moving template plugs, hand probing, and opening tube ends.
The non-inspected tubes constitute lens than 2% of the unplugged tubes, most are not located in the zone where large numbers of defects have occurred and the overall eddy current results did not indicate that it would be necessary to inspect the tubes.
Cae overall eddy current results and comparison with the December 1980 tapes are listed below:
"A" Steam Generator December 1980 Comparison With Tube Indication Reported December 1980 Tapes R15C29 43%, 21" ATE NDD 31%, small change R23C36 49%, 8" ATE NDD small change R20C20
<20%,
5" ATE NDD NDD, small change R05C07 UDI, 15" ATE NDD no change R18C37
- UDI, 8" ATE NDD small change RllC43 UDI, 18-20" ATE UDI no change R23C43
- DDI, 5-7" ATE NDD small change R25C44 UDi, 13-15" ATE UDI no change
- - R25C47 UDI, 13-18" ATE UDI no change R08C55 UDI, 17" ATE UDI nc whange R15C60 UDI, 14-18" ATE UDI no change Rl8C68 UDI, 15-17" ATE NDD small change R10C54 32%, TTS
<20%
34% in July 1980 F'3C54
<20%, 1/2" ATS 22%
34% in July 1980 ATE - Above Tube End NDD - No Defect Detected UDI - Undefinable Indication ATS - Above Tubesheet
a.
. "B" Steam Generator December 1980 Comparison With Tube Indication Reported December 1980 Tapes R03C25 80%, 17" ATE NDD small change R06C43 33%, 21" ATE NDD no change
- - R16C47 52%, 1/2" ATS NDD no change R27C30 29%, 1/2" ATS 29%
ATE - Above Tube End NDD - No Defect Detected UDI - Undefinable Indication ATS - Above Tubesheet As in the past, all indications were rmall volume.
Besides the above listed indications, a number of restrictions were encountered with the.720 eddy current probe.
In the "A" steam generator three tube ends and 23 first tube support plate restrictions were encountered.
In the "B"
steam generator 11 tube ends and 40 first tube support plate restrictions were encountered.
Most of the same restrictions were noted in the July and December 1980 inspections.
During the December 1980 inspection all but seven of the restrictions passed a.700 eddy current probe.
Based on this experience, the restricted tubes were not gauged.
Gauging of restricted tubes may be done during the refueling outage inspection.
The four cubes with indications greater than 40%
were' plugged on July 11, 1981.
In addition, tube R06C43 in the "B" steam generator was also plugged.
Correct plugging was visually' verified the same day.
A crevice flush will be performed before the unit is returned to service in an attempt to remove impurities from the tubesheet crevice.
Operation of the unit at a reduced temperature in' order to reduce the corrosion rate will continue.
However, the unit-will be returned to service at a slightly higher temperature than.that at which it has been operated since December 1979, assuming the results of the crevice flushing are satisfactory.
The NRC Resident Inspector was notified of these findings.
This event is reportable in accordance with Technical Specification 15.6.9.A.3 and is similar to others.
Unit 1 return to power is scheduled for about July 20, 1981.
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| 05000301/LER-1981-001-03, /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | | | 05000301/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000266/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000266/LER-1981-001-01, /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested | /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested | | | 05000301/LER-1981-002, Forwards Results of Metallographic Insp & Exam of Steam Generator Tube R15C73,as Committed to in LER 81-002/01T-01. Also Forwards Addl Rept on Evaluation of Apr 1981 Eddy Current Insp Results & Eddy Current Insp Maps | Forwards Results of Metallographic Insp & Exam of Steam Generator Tube R15C73,as Committed to in LER 81-002/01T-01. Also Forwards Addl Rept on Evaluation of Apr 1981 Eddy Current Insp Results & Eddy Current Insp Maps | | | 05000266/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000266/LER-1981-002-03, /03L-0:on 810113,post Acceptance Review of Annual Test Results from 04-80,for Control Room Emergency Filtration Sys,Showed 1980 Annual Test Incomplete.Caused by Personnel Failing to Determine Sys Velocity & Flow Info | /03L-0:on 810113,post Acceptance Review of Annual Test Results from 04-80,for Control Room Emergency Filtration Sys,Showed 1980 Annual Test Incomplete.Caused by Personnel Failing to Determine Sys Velocity & Flow Info | | | 05000301/LER-1981-002-01, /01T-0:on 810420,leaking Plug Detected in Steam Generator a & Degraded & Defective Tubes Found in Each Steam Generator During Eddy Current Exam of First Support Plate on 810426.Cause Not Stated.Eddy Current Insp Results Encl | /01T-0:on 810420,leaking Plug Detected in Steam Generator a & Degraded & Defective Tubes Found in Each Steam Generator During Eddy Current Exam of First Support Plate on 810426.Cause Not Stated.Eddy Current Insp Results Encl | | | 05000301/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000266/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000301/LER-1981-003-01, /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated | /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated | | | 05000266/LER-1981-003-03, /03L-0:on 810328,3D Diesel Generator Dc Power Failure Alarm Actuated.Caused by Failure of Field Failure Voltage (Ffv) Relay Coil.Ffv Relay Coil Replaced & Generator Returned to Svc | /03L-0:on 810328,3D Diesel Generator Dc Power Failure Alarm Actuated.Caused by Failure of Field Failure Voltage (Ffv) Relay Coil.Ffv Relay Coil Replaced & Generator Returned to Svc | | | 05000266/LER-1981-004-03, /03L-0:on 810425,during Inservice Testing of Containment Spray Valves (IT-50),Valve 1-860D Failed to Open.Caused by Maladjusted Closing Torque Switch.Switch Adjusted & Valve Retested & Returned to Svc | /03L-0:on 810425,during Inservice Testing of Containment Spray Valves (IT-50),Valve 1-860D Failed to Open.Caused by Maladjusted Closing Torque Switch.Switch Adjusted & Valve Retested & Returned to Svc | | | 05000266/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000301/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000301/LER-1981-004-01, /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | | | 05000266/LER-1981-005-03, /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | | | 05000266/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005-03, /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | | | 05000301/LER-1981-006-03, /03L-0:on 810803,during Routine Calibr Check of Pressurizer Level Instrumentation,One Channel Found Outside Tech Spec Range.Caused by Zero Drift of Level Transmitter Calibr.Instrument Adjusted.New Calibr Procedure Formalized | /03L-0:on 810803,during Routine Calibr Check of Pressurizer Level Instrumentation,One Channel Found Outside Tech Spec Range.Caused by Zero Drift of Level Transmitter Calibr.Instrument Adjusted.New Calibr Procedure Formalized | | | 05000266/LER-1981-006-01, /01T-0:on 810621,spray Additive Isolation Valve 1-831A Found Shut.Caused by Failure of Operator to Position Valve Correctly After Surveillance Testing.Valve Repositioned & Locked Open | /01T-0:on 810621,spray Additive Isolation Valve 1-831A Found Shut.Caused by Failure of Operator to Position Valve Correctly After Surveillance Testing.Valve Repositioned & Locked Open | | | 05000266/LER-1981-006, Forwards LER 81-006/01T-0 | Forwards LER 81-006/01T-0 | | | 05000301/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000301/LER-1981-007-03, /03L-0:on 810902,boric Acid Heat Trace Circuit P131 Found Inoperative.Caused by Failed Fuse Holder.Fuse Holder Replaced & Boric Acid Heat Trace Circuit Returned to Svc | /03L-0:on 810902,boric Acid Heat Trace Circuit P131 Found Inoperative.Caused by Failed Fuse Holder.Fuse Holder Replaced & Boric Acid Heat Trace Circuit Returned to Svc | | | 05000301/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000266/LER-1981-007, Forwards LER 81-007/01T-0 | Forwards LER 81-007/01T-0 | | | 05000266/LER-1981-007-01, /01T-0:on 810626,during Normal Operation,Unit Tripped from Approx 80% Power Due to Loss of Instrument Bus. Caused by Performance of Backfitting Mods.Plant Contractors Reinstructed | /01T-0:on 810626,during Normal Operation,Unit Tripped from Approx 80% Power Due to Loss of Instrument Bus. Caused by Performance of Backfitting Mods.Plant Contractors Reinstructed | | | 05000301/LER-1981-008-01, /01T-0:on 811022,valve 2SI-866A,high Head a SI Pump Discharge Valve,Indicated Shut Position.Possibly Caused by Operator Inattentiveness During Replacement of Ready Status Light.Operators Cautioned | /01T-0:on 811022,valve 2SI-866A,high Head a SI Pump Discharge Valve,Indicated Shut Position.Possibly Caused by Operator Inattentiveness During Replacement of Ready Status Light.Operators Cautioned | | | 05000301/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000266/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000266/LER-1981-008-01, /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged | /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged | | | 05000266/LER-1981-009, Forwards LER 81-009/01T-0 | Forwards LER 81-009/01T-0 | | | 05000266/LER-1981-009-01, /01T-0:on 810714,per IE Bulletin 80-11 Analyses, Contractor Reported That Four Control Room & Two Battery Room Walls Did Not Meet Revised Criteria for Seismic Event. Caused by Reanalysis Per Revisions.Supports Installed | /01T-0:on 810714,per IE Bulletin 80-11 Analyses, Contractor Reported That Four Control Room & Two Battery Room Walls Did Not Meet Revised Criteria for Seismic Event. Caused by Reanalysis Per Revisions.Supports Installed | | | 05000266/LER-1981-010-01, /01T-0:on 810716,check Valves 1-853C & D Were Opened Up & Found Stuck in Full Open Position During Testing.Caused by Interference Between Disc Wire & Valve Body.Disc Wires Replaced W/Cotter Pins | /01T-0:on 810716,check Valves 1-853C & D Were Opened Up & Found Stuck in Full Open Position During Testing.Caused by Interference Between Disc Wire & Valve Body.Disc Wires Replaced W/Cotter Pins | | | 05000266/LER-1981-010, Forwards LER 81-010/01T-0 | Forwards LER 81-010/01T-0 | | | 05000266/LER-1981-011-03, /03L-0:on 810721,during Biweekly Safeguards Sys Logic Periodic Testing,Unit 1 Test Switch PC-950A Failed. Probably Caused by Dirty Contacts.New Rees Contact Block Installed | /03L-0:on 810721,during Biweekly Safeguards Sys Logic Periodic Testing,Unit 1 Test Switch PC-950A Failed. Probably Caused by Dirty Contacts.New Rees Contact Block Installed | | | 05000266/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000266/LER-1981-012, Forwards LER 81-012/01T-0 | Forwards LER 81-012/01T-0 | | | 05000266/LER-1981-012-01, /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | | | 05000266/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000266/LER-1981-013-03, /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | | | 05000266/LER-1981-014, Forwards LER 81-014/01T-1 | Forwards LER 81-014/01T-1 | | | 05000266/LER-1981-014-01, /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | | | 05000266/LER-1981-015-01, /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | | | 05000266/LER-1981-015, Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. Affected Line Flushed & 1-853C Retested | Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. Affected Line Flushed & 1-853C Retested | | | 05000266/LER-1981-016, Forwards LER 81-016/01T-0 | Forwards LER 81-016/01T-0 | | | 05000266/LER-1981-016-01, /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | | | 05000266/LER-1981-017, Forwards LER 81-017/01T-0 | Forwards LER 81-017/01T-0 | | | 05000266/LER-1981-017-01, /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | |
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