LER-1981-003, Forwards LER 81-003/01T-0 |
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Wisconsin Electnc eom couem 231 W. MICHIGAN, P.O. BOX 2046. MILWAUKEE, WI 53201 June 4, 1981 Mr. James G. Keppler, Regional Director Office of Inspection and Enforcement, Region III U.
S. NUCLEAR REGULATORY COMMISSION 799 Roosevelt Road Glen Ellyn, Illinois 60137
Dear Mr. Keppler:
DOCKET NO. 50-301 POINT BEACH NUCLEAR PLANT, UNIT 2 LICENSEE EVENT REPORT NO. 81-003/0lT-0 Enclosed is Licensee Event Report No. 81-003/0lT-0 (a 14-day followup report) and an attachment which provides a description of an event reportable in accordance with Technical Specification 15.6.9.2.A.2, " Operation of the unit or affected systems when any parameter or operation subject to a limiting condition for operation is less conservative than the least conservative aspect of the limiting condition for operation established in the Technical Specification."
Very truly yours, bADJ
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C. W. Fay, Director Nuclear Power Department Enclosure Copy to NRC Resident Inspector 3107140368 810702 PDR ADOCK 05000266 S
PDR JUL.
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NHC E ORM 366 U.S NUCLE AR REGULA10RY COMMISSION (7 77)
LICENSEE EVENT REPORT CONTROL BLOCK: l l
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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lDuring normal operations at 1250 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.75625e-4 months <br />, on May 26, 1981, attempts to l
O 2 i o l3 l l cycle 2A steam generator blowdown sample isolation valve, 2CV-2 0 8 3, we re l iol4ll unsuccessful.
Failure of 2CV-2083 to close when actuated is a technicall l violation of containment integrity as defined in T.
S.
15.1.d.
This l
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15.6.9.2.A.2 as l
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15.3.6.A.a.
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33 34 35 36 Ji 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i O l Failure of 2CV-2083 to close upon actuation was due to excessive stem tol li ii ; l packing friction resulting from dried (
pa ck in g.
Followina discoverv I lof the prob'lem the packing gland was g y ed and the valve stem was I
i,l3; l lubricated.
The valve was tested satis f t2s vrily and returned to I
i, i, i loperation at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> on May 26, 1981.
At no time was the public l
safe ty endangered.
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DISCOVERY DESCRIPTION
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Fay PHONE:
NAME OF PREPARER
P ATTACHPENT TO LICENSEE EVENT REPORT NO. 81-003/OlT-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 2 Docket No. 50-301 At 1250 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.75625e-4 months <br /> on May 26, 1981, during normal power operation, Unit 2, "A" steam generator blowdown sample.
valve, 2CV-2083, failed to close upon a manual remote signal from the control operator.
The attempt to close 2CV-2083 was at the request of Chemistry Group personnel to stroke the valve.
Valve 2CV-2083 is an air-operated containment isolation valve which is required to close automatically upon actuation of containment isolation.
Inoperability of 2CV-20 83 is a technical violation of containment integrity as defined in Technical Specification 15.1.d.
This occurrence is reportable in accordance with Technical Specification 15.6.9.2. A.2 as operating in a less conservative manner than the limiting condition of operation specified in Technical Specification
- 15. 3. 6. A. a.
After an immediate investigation it was found that 2CV-2083 failed to close due to excessive stem to packing friction resulting from dried out packing.
The packing was adjusted and the valve stem lubricated.
Followirg a satis-factory operational test on 2CV-2083, it was. returned to an operable status at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> on May 26, 1981.
The automatic containment isolation function of 2CV-20 83 was installed, in accordance with NUREG-0578, during the Unit 2 refueling outage ending on May 22, 1981.
The last operability test of 2CV-2083 was conducted on May 13, 19 81, with satisfactory results.
If containment isolation was initiated while 2CV-2083 was inoperable, isolation could be provided via accessible mar.ual valves downstream of 2CV-208 3.
At no time was the public safety endange red.
The nameplate data for 2CV-2083 is as follows:
Manufacturer:
Copes Vulcan Body Size:
3/4" Pressure Rating:
600 psig Type:
D-100-60 9
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| 05000301/LER-1981-001-03, /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | | | 05000301/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000266/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000266/LER-1981-001-01, /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested | /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested | | | 05000301/LER-1981-002, Forwards Results of Metallographic Insp & Exam of Steam Generator Tube R15C73,as Committed to in LER 81-002/01T-01. Also Forwards Addl Rept on Evaluation of Apr 1981 Eddy Current Insp Results & Eddy Current Insp Maps | Forwards Results of Metallographic Insp & Exam of Steam Generator Tube R15C73,as Committed to in LER 81-002/01T-01. Also Forwards Addl Rept on Evaluation of Apr 1981 Eddy Current Insp Results & Eddy Current Insp Maps | | | 05000266/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000266/LER-1981-002-03, /03L-0:on 810113,post Acceptance Review of Annual Test Results from 04-80,for Control Room Emergency Filtration Sys,Showed 1980 Annual Test Incomplete.Caused by Personnel Failing to Determine Sys Velocity & Flow Info | /03L-0:on 810113,post Acceptance Review of Annual Test Results from 04-80,for Control Room Emergency Filtration Sys,Showed 1980 Annual Test Incomplete.Caused by Personnel Failing to Determine Sys Velocity & Flow Info | | | 05000301/LER-1981-002-01, /01T-0:on 810420,leaking Plug Detected in Steam Generator a & Degraded & Defective Tubes Found in Each Steam Generator During Eddy Current Exam of First Support Plate on 810426.Cause Not Stated.Eddy Current Insp Results Encl | /01T-0:on 810420,leaking Plug Detected in Steam Generator a & Degraded & Defective Tubes Found in Each Steam Generator During Eddy Current Exam of First Support Plate on 810426.Cause Not Stated.Eddy Current Insp Results Encl | | | 05000301/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000266/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000301/LER-1981-003-01, /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated | /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated | | | 05000266/LER-1981-003-03, /03L-0:on 810328,3D Diesel Generator Dc Power Failure Alarm Actuated.Caused by Failure of Field Failure Voltage (Ffv) Relay Coil.Ffv Relay Coil Replaced & Generator Returned to Svc | /03L-0:on 810328,3D Diesel Generator Dc Power Failure Alarm Actuated.Caused by Failure of Field Failure Voltage (Ffv) Relay Coil.Ffv Relay Coil Replaced & Generator Returned to Svc | | | 05000266/LER-1981-004-03, /03L-0:on 810425,during Inservice Testing of Containment Spray Valves (IT-50),Valve 1-860D Failed to Open.Caused by Maladjusted Closing Torque Switch.Switch Adjusted & Valve Retested & Returned to Svc | /03L-0:on 810425,during Inservice Testing of Containment Spray Valves (IT-50),Valve 1-860D Failed to Open.Caused by Maladjusted Closing Torque Switch.Switch Adjusted & Valve Retested & Returned to Svc | | | 05000266/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000301/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000301/LER-1981-004-01, /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | | | 05000266/LER-1981-005-03, /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | | | 05000266/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005-03, /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | | | 05000301/LER-1981-006-03, /03L-0:on 810803,during Routine Calibr Check of Pressurizer Level Instrumentation,One Channel Found Outside Tech Spec Range.Caused by Zero Drift of Level Transmitter Calibr.Instrument Adjusted.New Calibr Procedure Formalized | /03L-0:on 810803,during Routine Calibr Check of Pressurizer Level Instrumentation,One Channel Found Outside Tech Spec Range.Caused by Zero Drift of Level Transmitter Calibr.Instrument Adjusted.New Calibr Procedure Formalized | | | 05000266/LER-1981-006-01, /01T-0:on 810621,spray Additive Isolation Valve 1-831A Found Shut.Caused by Failure of Operator to Position Valve Correctly After Surveillance Testing.Valve Repositioned & Locked Open | /01T-0:on 810621,spray Additive Isolation Valve 1-831A Found Shut.Caused by Failure of Operator to Position Valve Correctly After Surveillance Testing.Valve Repositioned & Locked Open | | | 05000266/LER-1981-006, Forwards LER 81-006/01T-0 | Forwards LER 81-006/01T-0 | | | 05000301/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000301/LER-1981-007-03, /03L-0:on 810902,boric Acid Heat Trace Circuit P131 Found Inoperative.Caused by Failed Fuse Holder.Fuse Holder Replaced & Boric Acid Heat Trace Circuit Returned to Svc | /03L-0:on 810902,boric Acid Heat Trace Circuit P131 Found Inoperative.Caused by Failed Fuse Holder.Fuse Holder Replaced & Boric Acid Heat Trace Circuit Returned to Svc | | | 05000301/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000266/LER-1981-007, Forwards LER 81-007/01T-0 | Forwards LER 81-007/01T-0 | | | 05000266/LER-1981-007-01, /01T-0:on 810626,during Normal Operation,Unit Tripped from Approx 80% Power Due to Loss of Instrument Bus. Caused by Performance of Backfitting Mods.Plant Contractors Reinstructed | /01T-0:on 810626,during Normal Operation,Unit Tripped from Approx 80% Power Due to Loss of Instrument Bus. Caused by Performance of Backfitting Mods.Plant Contractors Reinstructed | | | 05000301/LER-1981-008-01, /01T-0:on 811022,valve 2SI-866A,high Head a SI Pump Discharge Valve,Indicated Shut Position.Possibly Caused by Operator Inattentiveness During Replacement of Ready Status Light.Operators Cautioned | /01T-0:on 811022,valve 2SI-866A,high Head a SI Pump Discharge Valve,Indicated Shut Position.Possibly Caused by Operator Inattentiveness During Replacement of Ready Status Light.Operators Cautioned | | | 05000301/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000266/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000266/LER-1981-008-01, /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged | /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged | | | 05000266/LER-1981-009, Forwards LER 81-009/01T-0 | Forwards LER 81-009/01T-0 | | | 05000266/LER-1981-009-01, /01T-0:on 810714,per IE Bulletin 80-11 Analyses, Contractor Reported That Four Control Room & Two Battery Room Walls Did Not Meet Revised Criteria for Seismic Event. Caused by Reanalysis Per Revisions.Supports Installed | /01T-0:on 810714,per IE Bulletin 80-11 Analyses, Contractor Reported That Four Control Room & Two Battery Room Walls Did Not Meet Revised Criteria for Seismic Event. Caused by Reanalysis Per Revisions.Supports Installed | | | 05000266/LER-1981-010-01, /01T-0:on 810716,check Valves 1-853C & D Were Opened Up & Found Stuck in Full Open Position During Testing.Caused by Interference Between Disc Wire & Valve Body.Disc Wires Replaced W/Cotter Pins | /01T-0:on 810716,check Valves 1-853C & D Were Opened Up & Found Stuck in Full Open Position During Testing.Caused by Interference Between Disc Wire & Valve Body.Disc Wires Replaced W/Cotter Pins | | | 05000266/LER-1981-010, Forwards LER 81-010/01T-0 | Forwards LER 81-010/01T-0 | | | 05000266/LER-1981-011-03, /03L-0:on 810721,during Biweekly Safeguards Sys Logic Periodic Testing,Unit 1 Test Switch PC-950A Failed. Probably Caused by Dirty Contacts.New Rees Contact Block Installed | /03L-0:on 810721,during Biweekly Safeguards Sys Logic Periodic Testing,Unit 1 Test Switch PC-950A Failed. Probably Caused by Dirty Contacts.New Rees Contact Block Installed | | | 05000266/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000266/LER-1981-012, Forwards LER 81-012/01T-0 | Forwards LER 81-012/01T-0 | | | 05000266/LER-1981-012-01, /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | | | 05000266/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000266/LER-1981-013-03, /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | | | 05000266/LER-1981-014, Forwards LER 81-014/01T-1 | Forwards LER 81-014/01T-1 | | | 05000266/LER-1981-014-01, /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | | | 05000266/LER-1981-015-01, /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | | | 05000266/LER-1981-015, Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. Affected Line Flushed & 1-853C Retested | Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. Affected Line Flushed & 1-853C Retested | | | 05000266/LER-1981-016, Forwards LER 81-016/01T-0 | Forwards LER 81-016/01T-0 | | | 05000266/LER-1981-016-01, /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | | | 05000266/LER-1981-017, Forwards LER 81-017/01T-0 | Forwards LER 81-017/01T-0 | | | 05000266/LER-1981-017-01, /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | |
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