05000364/LER-1981-013-03, /03L-0:on 810505 & 06,lube Oil & Fuel Oil Leaks Found on Diesel Generator 2B.First Caused by Leaking O-ring on Lube Oil Strainer;Second by Fatigue Failure of Compression Fitting on Copper Line.Ring & Line Replaced

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/03L-0:on 810505 & 06,lube Oil & Fuel Oil Leaks Found on Diesel Generator 2B.First Caused by Leaking O-ring on Lube Oil Strainer;Second by Fatigue Failure of Compression Fitting on Copper Line.Ring & Line Replaced
ML20004F644
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/12/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004F638 List:
References
LER-81-013-03L, LER-81-13-3L, NUDOCS 8106190326
Download: ML20004F644 (2)


LER-1981-013, /03L-0:on 810505 & 06,lube Oil & Fuel Oil Leaks Found on Diesel Generator 2B.First Caused by Leaking O-ring on Lube Oil Strainer;Second by Fatigue Failure of Compression Fitting on Copper Line.Ring & Line Replaced
Event date:
Report date:
3641981013R03 - NRC Website

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LICENSEE EVENT REPORT

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(PLEA 0E FRINT OR TYPE ALL AECUlRED INFORMATION)

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lo 2l l At 1026 on 5/5/81 and 0915 on 5/6/81, Diesel Generator 2B was declared inoperable due to g 4 a e a I-1 a lube oil leak and fuel oil leak respectively. Tech. Spec. 3.8.1.1, in part, requires ;

ITITI IDG 28.to be operable. Tech. Spec. 3.8.1.1 action require =ents were met.

Health / safety l o i s I l of the public was not affected. The occurrence on 5-5-81 was the sixth failure -in the l

foTs'] I last 100 valid tests.

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g l The cause for the first e rent was a leaking "0" ring on the lube oil strainer and the "0','

PTFl ~ l ring was replaced. The cause for the cacond event was a fatigue failure, due to vibra,

j,,.,j l tion, of the compressi:n fitting on a copper line. The line was replaced.with stainless j - 1 l steel and rerouted to reduce vibration. Following a successful timed start DG 2B was i

i4i l returned to service at 1312 on 5/5/81 and 1425 on 5/6/81.

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