LER-1981-001, /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested |
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LICENSEE EVENT REPORT (v.
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8 60 68 OOCKET NUMSE R 88 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h 10121 l At 0139 hours0.00161 days <br />0.0386 hours <br />2.29828e-4 weeks <br />5.28895e-5 months <br /> on 01-02-81 the supply breaker for safeguards motor I
iO i3i l control center 1B42 tripped while performing a monthly ventilation l
10 l 41 l system test.
The unit was at about 70% steady state power at the time. l _
i O i s i l The loss of 1B42 resulted in a loss of the lYO4 instrument bus.
The l
10 is I l loss of the lYO4 bus resulted in a momentary violation of the minimum l
l0l2l l degree of redundancy required by Technical Specifications and is l
1 O t8 i i reportable IAW Tech. Spec. 15.6.9.2.A.2.
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O S SC E COMPONENT CODE SU8 0'E S
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9 to il 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION L
EVENTVEAR REPORT NO.
CODE TYPE NO.
@,a=E R'ROl 811l l-l 1010 l11 l/l 10111 lT l L-J LO_]
,, 21 22 23 24 26 27 28 29 30 31 32 TAK N AC O P NT HOURS S8 i FOR b 8.
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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h li l O I l The lYO4 instrument bus was shifted to its alternate power supply at I
ii ii i l 0140 hours0.00162 days <br />0.0389 hours <br />2.314815e-4 weeks <br />5.327e-5 months <br /> and power was restored to 1B42 at 0141 the same day.
The I
g i cause of the breaker trip was found to be dust in the instantaneous I
g l trip valve on the breaker.
The Westinghouse type DB-50 breaker was l
l cleaned, tested, and returned-to-service.
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ACTIVITY CO TENT RELEASE @D OF RELEASE @l N/A l
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AMOUNT OF ACTIVITv LOCATION OF RELEASE 1 6 PERSONNEL EXPOS ES y l 010 l 0 lhlTvPE@lDESCRiPT ON@
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' PERSONNEt iN;u' dies NUM9ER
DESCRIPTION
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NAME OF PREPARER
.t ATTACHMENT TO LICENSEE EVENT REPORT NO. 81-001/0lT-0 Wisconsin Electric Power Company Point Beach Nuclear Plant, Unit 1 Docket No. 50-266 During normal operation at 0139 hours0.00161 days <br />0.0386 hours <br />2.29828e-4 weeks <br />5.28895e-5 months <br /> on January 2, 1981 with Unit 1 operating at approximately 70% power, the supply breaker for safeguards motor control center 1B42 tripped.
The breaker tripped during a monthly ventilation system test.
Loss of the motor control center rasulted in a loss of the lYO4 instrument bus for a short period of time.
A turbine runback was also initiated by the loss of the lYO4 instrument bus from a power level of 70% to approximately 50%.
The 1YO4 instrument bus was shifted to its alt:ernate power supply at 0140 hours0.00162 days <br />0.0389 hours <br />2.314815e-4 weeks <br />5.327e-5 months <br /> and power was restored to the 1B42 motor control center within two minutes of the event by resetting the supply breaker.
Unit 2 was not affected by this event.
Unit 1 was returned to 70% power at 0511 hours0.00591 days <br />0.142 hours <br />8.449074e-4 weeks <br />1.944355e-4 months <br /> on January 2, 1981.
The momentary loss (approximately one minute) of the lYO4 instrument bus constituted a violation of the minimun degree of redundancy required by the Technical Specifications for contain-ment spray actuation and steam line isolation.
Containment pressure channel PC-950 is powered by lYO4 and requires power to generate a high-high pressure trip signal.
The loads on 1B42 which were de-energized for approximately two minutes are shown on the attached list.
The breaker trip was caused by dust on the instantaneous trip valve seat which lowered the current required to trip the valve.
During the ventilation system surveillance testing, the starting current for the additional equipment caused the breaker to trip.
The Westinghouse type DB-50 breaker was cleaned, tested, and returned-to-service later the same day.
There have been no previous events related to DB-50 breakers due to this cause.
This event is being reported in accordance with Technical Specification 15.6.9.2.A.2.
MOTOR CONTROL CENTER 1B42 LOADS j
'MOV-850B Containment sump "B"
isolation MOV-852B Reactor vessel injection isolation MOV-866B Safety injection hot leg isolation MOV-860B Containment spray isolation
- - MOV-8968 "B" safety injection pump suction isolation MOV-878C Safety injection loop " A" isolation MOV-878B Safety injection loop "B" isolation MOV-860D Containment spray isolation MOV-851B Containment sump "B" isolation MOV-856B Residual heat removal pump "B"
suction MOV-870B Spray pump "B" suction MOV-871B' Containment spray pump "B" recirc line MOV-825B Safety injection header to refueling water storage tank isolation MOV-841B Accumulator "B" isolation MOV-738B Cooling to residual heat removal heat exchanger "B"
MOV-701 Residual heat removal to loop " A" MOV-5 9 9 Loop "B" drain _
MOV-826 A Boric acid supply to safety injection pump MOV-826B Boric acid supply to safety injection pump MOV-35 0 Emergency boration MOV-719 Containment cooling MOV-1298 Charging line isolation MOV-427 Letdown line isolation MOV-596 Pressurizer relief tank drain MOV-516 Power-operated relief isolation P12B Spent fuel pool cire pump l
MOV-4021 Auxiliary feed pump P38B discnarge i
MOV-4006 Service water to turbine driven auxiliary - feed pump Boric acid heat tracing transformer 1GYO4 Instrument bus AC M-G set Diesel generator G01 starting air compressor W12C Diesel room supply fan 1
MOV-2908 Service water from containment vent coolers
_MOV-2880 Service water to spent fuel pit heat exchanger MOV-29 30 Spent fuel cooling service water supply MOV-3931-Fuel oil to Diesel day tank "B" W21A Auxiliary building stack vent fan
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| 05000301/LER-1981-001-03, /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | | | 05000301/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000266/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000266/LER-1981-001-01, /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested | /01T-0:on 810102,while Performing Monthly Ventilation Sys Test,Supply Breaker for Safeguards Motor Control Ctr 1B42 Tripped.Caused by Dust in Instantaneous Trip Valve on Breaker.Breaker Cleaned & Tested | | | 05000301/LER-1981-002, Forwards Results of Metallographic Insp & Exam of Steam Generator Tube R15C73,as Committed to in LER 81-002/01T-01. Also Forwards Addl Rept on Evaluation of Apr 1981 Eddy Current Insp Results & Eddy Current Insp Maps | Forwards Results of Metallographic Insp & Exam of Steam Generator Tube R15C73,as Committed to in LER 81-002/01T-01. Also Forwards Addl Rept on Evaluation of Apr 1981 Eddy Current Insp Results & Eddy Current Insp Maps | | | 05000266/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000266/LER-1981-002-03, /03L-0:on 810113,post Acceptance Review of Annual Test Results from 04-80,for Control Room Emergency Filtration Sys,Showed 1980 Annual Test Incomplete.Caused by Personnel Failing to Determine Sys Velocity & Flow Info | /03L-0:on 810113,post Acceptance Review of Annual Test Results from 04-80,for Control Room Emergency Filtration Sys,Showed 1980 Annual Test Incomplete.Caused by Personnel Failing to Determine Sys Velocity & Flow Info | | | 05000301/LER-1981-002-01, /01T-0:on 810420,leaking Plug Detected in Steam Generator a & Degraded & Defective Tubes Found in Each Steam Generator During Eddy Current Exam of First Support Plate on 810426.Cause Not Stated.Eddy Current Insp Results Encl | /01T-0:on 810420,leaking Plug Detected in Steam Generator a & Degraded & Defective Tubes Found in Each Steam Generator During Eddy Current Exam of First Support Plate on 810426.Cause Not Stated.Eddy Current Insp Results Encl | | | 05000301/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000266/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000301/LER-1981-003-01, /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated | /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated | | | 05000266/LER-1981-003-03, /03L-0:on 810328,3D Diesel Generator Dc Power Failure Alarm Actuated.Caused by Failure of Field Failure Voltage (Ffv) Relay Coil.Ffv Relay Coil Replaced & Generator Returned to Svc | /03L-0:on 810328,3D Diesel Generator Dc Power Failure Alarm Actuated.Caused by Failure of Field Failure Voltage (Ffv) Relay Coil.Ffv Relay Coil Replaced & Generator Returned to Svc | | | 05000266/LER-1981-004-03, /03L-0:on 810425,during Inservice Testing of Containment Spray Valves (IT-50),Valve 1-860D Failed to Open.Caused by Maladjusted Closing Torque Switch.Switch Adjusted & Valve Retested & Returned to Svc | /03L-0:on 810425,during Inservice Testing of Containment Spray Valves (IT-50),Valve 1-860D Failed to Open.Caused by Maladjusted Closing Torque Switch.Switch Adjusted & Valve Retested & Returned to Svc | | | 05000266/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000301/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000301/LER-1981-004-01, /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | | | 05000266/LER-1981-005-03, /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | | | 05000266/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005-03, /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | | | 05000301/LER-1981-006-03, /03L-0:on 810803,during Routine Calibr Check of Pressurizer Level Instrumentation,One Channel Found Outside Tech Spec Range.Caused by Zero Drift of Level Transmitter Calibr.Instrument Adjusted.New Calibr Procedure Formalized | /03L-0:on 810803,during Routine Calibr Check of Pressurizer Level Instrumentation,One Channel Found Outside Tech Spec Range.Caused by Zero Drift of Level Transmitter Calibr.Instrument Adjusted.New Calibr Procedure Formalized | | | 05000266/LER-1981-006-01, /01T-0:on 810621,spray Additive Isolation Valve 1-831A Found Shut.Caused by Failure of Operator to Position Valve Correctly After Surveillance Testing.Valve Repositioned & Locked Open | /01T-0:on 810621,spray Additive Isolation Valve 1-831A Found Shut.Caused by Failure of Operator to Position Valve Correctly After Surveillance Testing.Valve Repositioned & Locked Open | | | 05000266/LER-1981-006, Forwards LER 81-006/01T-0 | Forwards LER 81-006/01T-0 | | | 05000301/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000301/LER-1981-007-03, /03L-0:on 810902,boric Acid Heat Trace Circuit P131 Found Inoperative.Caused by Failed Fuse Holder.Fuse Holder Replaced & Boric Acid Heat Trace Circuit Returned to Svc | /03L-0:on 810902,boric Acid Heat Trace Circuit P131 Found Inoperative.Caused by Failed Fuse Holder.Fuse Holder Replaced & Boric Acid Heat Trace Circuit Returned to Svc | | | 05000301/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000266/LER-1981-007, Forwards LER 81-007/01T-0 | Forwards LER 81-007/01T-0 | | | 05000266/LER-1981-007-01, /01T-0:on 810626,during Normal Operation,Unit Tripped from Approx 80% Power Due to Loss of Instrument Bus. Caused by Performance of Backfitting Mods.Plant Contractors Reinstructed | /01T-0:on 810626,during Normal Operation,Unit Tripped from Approx 80% Power Due to Loss of Instrument Bus. Caused by Performance of Backfitting Mods.Plant Contractors Reinstructed | | | 05000301/LER-1981-008-01, /01T-0:on 811022,valve 2SI-866A,high Head a SI Pump Discharge Valve,Indicated Shut Position.Possibly Caused by Operator Inattentiveness During Replacement of Ready Status Light.Operators Cautioned | /01T-0:on 811022,valve 2SI-866A,high Head a SI Pump Discharge Valve,Indicated Shut Position.Possibly Caused by Operator Inattentiveness During Replacement of Ready Status Light.Operators Cautioned | | | 05000301/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000266/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000266/LER-1981-008-01, /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged | /01T-0:on 810710,four Tubes in Steam Generators Were Verified to Have Degradation Greater than 40% Which Exceeds Plugging Limit of Tech Specs.Caused by Intergranular Attack Due to Caustic.Defective Tubes Plugged | | | 05000266/LER-1981-009, Forwards LER 81-009/01T-0 | Forwards LER 81-009/01T-0 | | | 05000266/LER-1981-009-01, /01T-0:on 810714,per IE Bulletin 80-11 Analyses, Contractor Reported That Four Control Room & Two Battery Room Walls Did Not Meet Revised Criteria for Seismic Event. Caused by Reanalysis Per Revisions.Supports Installed | /01T-0:on 810714,per IE Bulletin 80-11 Analyses, Contractor Reported That Four Control Room & Two Battery Room Walls Did Not Meet Revised Criteria for Seismic Event. Caused by Reanalysis Per Revisions.Supports Installed | | | 05000266/LER-1981-010-01, /01T-0:on 810716,check Valves 1-853C & D Were Opened Up & Found Stuck in Full Open Position During Testing.Caused by Interference Between Disc Wire & Valve Body.Disc Wires Replaced W/Cotter Pins | /01T-0:on 810716,check Valves 1-853C & D Were Opened Up & Found Stuck in Full Open Position During Testing.Caused by Interference Between Disc Wire & Valve Body.Disc Wires Replaced W/Cotter Pins | | | 05000266/LER-1981-010, Forwards LER 81-010/01T-0 | Forwards LER 81-010/01T-0 | | | 05000266/LER-1981-011-03, /03L-0:on 810721,during Biweekly Safeguards Sys Logic Periodic Testing,Unit 1 Test Switch PC-950A Failed. Probably Caused by Dirty Contacts.New Rees Contact Block Installed | /03L-0:on 810721,during Biweekly Safeguards Sys Logic Periodic Testing,Unit 1 Test Switch PC-950A Failed. Probably Caused by Dirty Contacts.New Rees Contact Block Installed | | | 05000266/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000266/LER-1981-012, Forwards LER 81-012/01T-0 | Forwards LER 81-012/01T-0 | | | 05000266/LER-1981-012-01, /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | | | 05000266/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000266/LER-1981-013-03, /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | | | 05000266/LER-1981-014, Forwards LER 81-014/01T-1 | Forwards LER 81-014/01T-1 | | | 05000266/LER-1981-014-01, /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | | | 05000266/LER-1981-015-01, /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | | | 05000266/LER-1981-015, Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. Affected Line Flushed & 1-853C Retested | Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. Affected Line Flushed & 1-853C Retested | | | 05000266/LER-1981-016, Forwards LER 81-016/01T-0 | Forwards LER 81-016/01T-0 | | | 05000266/LER-1981-016-01, /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | | | 05000266/LER-1981-017, Forwards LER 81-017/01T-0 | Forwards LER 81-017/01T-0 | | | 05000266/LER-1981-017-01, /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | |
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