LER-1980-027, /01T-0:on 801024,while Performing Surveillance Check,Rhr Pump 2C Failed to Start Because Trip Interlock Signal Received from Pump Suction Valve M0-2-1001-7C.Caused by Incorrectly Adjusted Limit Switch.Switch Readjusted |
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e0 et occxET NUweER es. 89 EVENToArt 74 75 REPORT oArt 80 EVENT DESCRIPTION AND PROSABLE CONSEQUENCES h o 2 l While performing RHR Pump Operability Surveillance, QOS 1000-2, RHR Pump 2C failed to l start because a trip Interlock signal was received irom pump suction valve MO-2-1001-l gg o e l 7C. The 1/2 Diesel Generator was out of service for maintenance and testing was l
being performed to satisfy Technical Specification 3 9/4.9-E.1.
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34 JS 36 37 40 ' el 42 43 44 47 33 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l ioll The limit switch on valve MO-2-1001-7C had been incorrectly adlusted after the valve 1 i i l operator was replaced.
Immediate action was to block out the valve /ouno i n te rl ock I
, 2 l relay thus establishing 2C RHR Pump operabil.ity. The limit switch was re-adjusted; l
, 3 l Electrical Maintenance was retrained. More complete testing will be specified after l maintenance on safety-related valves which utilize interlocks gl for system operation.
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LER NUMBER: LER/R0 80-27/0lT-0 11.
LICENSEE NAME: Commonwealth Edison Company quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit Two IV.
DOCKET NUMBER: 050-265 V.
EVENT DESCRIPTION
On Octobe-24,1980, at 8:45 p.m. with Unit Two operating at 2092 MWt and a load of 682 MWe, RHR Pump Operability Surveillance QOS 1000-2 was being performed. The 2C RHR Pump failed to start. The 1/2. Diesel Generator was out of service for maintenance at the time and Technical Specification 3.9/4.9-E.1 required demonstration of operability of the low pressure core cooling systems and the RHR containment cooling loop associated with the operable Unit Two Diesel Generator.
Since 2C pump suction valve MO-2-1001-7C had recently had maintenance performed, a possible trip Interlock assoc!ated with the pump suction valve was suspected as the probable cause of the failure of the 2C RHR pump to start. The MO-2-1001-7C valve interlock limit switch relay Kl9B was blocked open in order to prevent the valve from further not allowing the 2C RHR Pump to start. The 2C RHR Pump was subsecuently retested and demonstrated to be operable.
Work Request q08619 was initiated to investigate the cause of the MO 1001-7C suction valve Interlock malfunction.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
The effects of this occurrence on the overall safety of the reactor and safety related systems were not adverse. The 2D RHR Pump was fully ope rable. The B Core Spray Loop and the B RHRS Containment Cooling Loop were also fully operable. Also, with normal power available the A & B RHR Pumps, the A Core Spray Loop, and the A RHRS Containment Cooling Loop were operable.
Vll. CAUSE:
I The cause of this occurrence was discovered to be a ilmit switch on the pump suction valve motor operator which had been incorrectly adjusted af ter the valve operator was replaced. This misadjustment prevented the pump from starting due to the protective valve / pump interlock system.
The position limits on the switch were incorrectly set on October 22, 1980, following Installation of a neu valve operator. The valve at that time was returned to service and stroked three times successfully. No further testing was performed at that time.
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Vill. CORRECTIVE ACTION:
The immediate corrective action was to block out the valve / pump inter-lock relay, thereby re-establishing operability of the 2C RHR Pump in order to satisfy Technical Specification requirements. The limit switch was re-adjusted and MO-2-1001-7C was tested satisfactorily. An in-vestigation is being conducted pursuant to this event. Emphasis is being given to Electrical Maintenance personnel of correct and accurate limit point settings. The Electrical Maintenance Department has since received additional training from a service representative of Limitorque Corporation, the manufacturer of the vcive operator.
Further, more complete testing will be specified af te.' maintenance is performed on safety-related valves, which utilize ?n.erlocks necessary for system operation.
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| 05000265/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001-03, /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | | | 05000254/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000254/LER-1980-002-03, /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | | | 05000265/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000265/LER-1980-002-03, /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | | | 05000265/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000265/LER-1980-003-03, /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | | | 05000254/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000254/LER-1980-003-03, /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | | | 05000254/LER-1980-004-03, /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | | | 05000254/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004-03, /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | | | 05000265/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000265/LER-1980-005-03, /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | | | 05000254/LER-1980-005-03, /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | | | 05000254/LER-1980-006-03, /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | | | 05000254/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000265/LER-1980-006-01, /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | | | 05000265/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000254/LER-1980-007-03, /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | | | 05000254/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000265/LER-1980-007-03, /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | | | 05000265/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000254/LER-1980-008-03, /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | | | 05000265/LER-1980-008-03, /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | | | 05000265/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000254/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000265/LER-1980-009-03, /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | | | 05000265/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-009-03, /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | | | 05000254/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-010-03, /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | | | 05000254/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-010-03, /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | | | 05000265/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-011-03, /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | | | 05000265/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-011-03, /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | | | 05000254/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000265/LER-1980-012-03, /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | | | 05000254/LER-1980-012-03, /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | | | 05000265/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000254/LER-1980-013-03, /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | | | 05000265/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000254/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000265/LER-1980-013-03, /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | |
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