ML19310A212

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LER 80-020/03L-0:on 800429,during Power Operation,Rcs Pressure Was Too Low Due to Stuck Pressurizer Spray Valve & Reactor Tripped on Low Steam Generator Level During Load Reduction.Caused by Loose Valve Seat.Valve Repaired
ML19310A212
Person / Time
Site: Millstone Dominion icon.png
Issue date: 05/29/1980
From: Gurney P
NORTHEAST UTILITIES
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19310A205 List:
References
LER-80-020-03L, LER-80-20-3L, NUDOCS 8006060285
Download: ML19310A212 (1)


Text

i NRC FORF.1386 U. S. NUCLEAR REGULATORY CCMAtISSION (7 771 ~

LICENSEE EVENT REPORT

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- ~ - I 7 8 60 61 COCKET NisM8ER 68 69 EVENT OATE EVENT DESCRIPTION AND PRCBA8LE CONSEQUENCES h 1 o 121 l During routine oower operation, the reactor coolant system orersure was less than l l

lo isi i that allowed by Technical Specification 3.2.6. The pressure decrease was caused by I  !

Io i4 l i the loop 1 A pressurizer spray valve sticking open. The reactor tripped on low I i o i s i t steam generator level during load reduction following discovery of the stuck valve. I io is i l There are no probable consequences since the unit was operated in accordance with I loi7i i Technical Specification 3.2.6. I I

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CAUSE DESCRIPTION AND CCRRECTIVE ACTIONS l # 3 l l The valve stuck open due to a loose valve seat. The valve was isolated for subsecuent I ii,ij istartup. During a later, unrelated outage the valve was recaired. Valve data: I i,,,, i 3 inch Fischer Controls angle valve with air operator. l 1: 131 1 I 1

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